LER-1980-006, /01T-0:on 800617,during Safeguards Logic Test W/ One Emergency Diesel Generator Out of Svc,Auto Containment Spray Pump Actuation Threatened During Loss of Ac & high- High Containment Pressure.Caused by Personnel Error |
| Event date: |
|
|---|
| Report date: |
|
|---|
| 3011980006R01 - NRC Website |
|
text
tUL%CJCO'
~
U. S. NUCLEA~J i.EOULATCRY COMMISSION (7 77)
LICENSEE EVENT REPORT
) CONTROL BLOCK: l l
l l
l l lh (PLEASE PRINT CR TYPE ALL CEQUITED INFOIMATl!NI i
j s
6 [oTi1 I w I I I P I a i n 12 I@l 0 l 0 l-I O 1010 l o l 01 - 10 l 0 I@i 411 l 1 l1 l 1 I@l l
lg 7
8 9 LfCENSEE CODE 14 tS LICENSE NUMBER 25 26 LICENSE Type JO
$7 CAT $8 CON'T l o l Lj l L ]@l 0 l 5 l 0 l 0 l 0 l 3 l 0 l1 ]@l 016 l 1l 7 I 8 l 0 l@l 0 l 6 l 3 l 0 l 8 l 0 l@
$O RCE F
8 60 64 DOCKET NUM8ER 68 69 EVtNT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROB A8LE CONSEQUENCES h 10121 l On 06-17-80, a routine safeguards logic test was conducted with one l
[ o l a l l emergency Diesel generator out of service for maintenance.
On the morn-l Iing of 06-18-80, it was discovered that fully performing this test l
o 4 l o i s t l could have defeated automatic containment spray pump actuation during a l 1oisl l loss of AC and a high-high containment pressure.
Spray pump automatic l
lO lil f actuation was defeated for only about one minute during the test.
This l 1018i l event is reportable per Technical Specification 15.6.9.2. A.6.
l 7
8 9 80 OE CODE SU8C E COMPONENT CODE SUSCODE SU E
l0l9l lS lB l@ @@ l Xl@ lI lN lS lT lR lU l@ gg l Zl@
7 s
9 10 11 12 13 18 19 20 SEOUENTIAL OCCURRENCE REPORT REVISION
_EVENTYEAR R EPOR T NO.
CODE TYPE NO.
@ g(ga on 18 10 l I-I 101016l l/l 10111 ITl l-l 10 1 gr
_ 21 22 23 24 26 27 28 29 30 31 J2 TATE 4 ftO ON PLANT V T HOURS 22 58 iT FOR 8.
SU #LI R MANUFACTURER i X JglJ4Hj@
l Z ] g l36Zl@ 10 l 0 l 0 lU l lYlg lNlg lNlg lWlIl2l0lg JJ JS 34 43 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h li t o i l The event was caused by personnel error in that a technician failed to l
L'i'J l verify that both Diesels were operable before performing the test.
Pet r,-j r; y 21 l sonnel have been instructed to verify precautions on test procedures i
g l before performing any test.
All routine testing of the inservice j
l Diesel safeguards train will be deferred when the other is inoperable.
l i 4 7
8 9 80 ST S
% POWER OTHER STATUS Dis O RY DISCOVERY DESCRIPTION E [E j@ l 1 l 0 l 0 l@l N/A l
g gl Test Review l
'8 RELEASE AMOUNT OF ACTIVITY LOCATIO'N OF RELEASE W I Z l @D OF RELEASF[Z_j@lN/A l
l N/A l
PERSONNEL EXPOS ES oESCR, TION @
~ UMBER TY,E 10 l0 l 0 l@W@l N /A l
1 7 P E R SO~ ~ El',~,u'J, E S DESCRIPTION @
NuM8ER l0l0l0j@l N/A l
t a 7
8 9 11 12 80
'S*E
^"' ion '*'*@
T ESC PT l Z l@l N/A l
1 9 7
8 9 to 80 ISSUE @ DESCRIPTION lN/A l
l__l_ l l l l l l l l l l l $
2 o 7
8 9 to 68 69 80 3 C. W.
Fay 414/277-2811 2
NAME OF PREPARER Phot <E:
sootu0349
.h 7
2 ATTACHMENT -TO LICENSEE EVENT REPORT NO. 80-006/OlT i Wisconsin Electric Power Company Point Beach Nuclear Plant Unit 2 Docket No. 50-301 4
- - At 0805 hours0.00932 days <br />0.224 hours <br />0.00133 weeks <br />3.063025e-4 months <br /> on June 18, 1980 it was discovered that a routine safeguards logic test was conducted on June 17 with one. diesel.out-of-service for annual maintenance.
To perform this test, certain safeguards signals must be rendered ineffective so the logic test.can be conducted.
Signals. tested j
include "A" and "B" steam line low pressure, primary system low pressure, containment high pressure, and containment high-high pressure.
The.first four signals are for initiation of safety injection and any one of them will initiate safety injection.
{
As discussed in the Technical Specifications, there is an inherent redundancy between.these four signals in that a loss-of-coolant accident will cause both low primary system pressure and high containment pressure.
A steam line break will cause a low steam
~line pressure, a low primary system pressure, and also a high containment pressure if the steam line break is within containment.
The containment high-high pressure signal is for initiation of containment spray.
Curing logic testing, each one of these signals
)
is defeated one at a time for about one minute each.
With the 3D emergency diesel generator out-of-service, the "A" train is rendered ineffective during a loss of AC accident.
With the "A" train. ineffective, the associated safety injection train and containment spray pump will not start upon I
receiving' a start signal since there is no power to the train.
]
The "B" train, however, would ~be energized Dy the 4D diesel during i
a' loss of AC.
The associated safety injection train would have started on a LOCA or steam line break even if one of the four t
j associated signals was defeated because of the redundancy.
- However, i
the "B" train containment spray pump would not have started if the j
containment high-high pressure signal was defeated.
This would 1
i mean that neither spray pump would have operated automatically, although two containment fan coolers would have been energized upon a safety injection signal.
The spray pump, however, can be manually started.upon or before a containment high-high pressure
- - alarm.
Also, the spray pump would have started automatically upon unblocking the high-high pressure signal if such a condition existed during and subsequent-to testing of that signal logic.
l To cope.with a' loss-of-coolant. accident, the FFDSAR assumes availability of two' fan coolers and one spray pump.
The analysis assumes the spray pump and fans are started 60 seconds (vs. 10 and.30 seconds respectively in the safety injection
' sequence) after occurrence of a LOCA.
A taximum pressure of 52
)
to 53 psig is predicted vs. a containment. design pressure of 60-psig.
.i i
- - 1_
.+
.a
.. - - Based on this' fact, rendering the high-high containment pressure signal ineffective for about one minute would yield a sequence of events very similar to that analyzed in the FFDSAR.
l The eveet was caused by personnel error.
A technician failed to verify that both emergency diesel generators were operable before performing'the test.
The test procedure contains a precaution stating that if one diesel is out-of-service, the safeguards train associated with the in-service diesel should not be tested.
To prevent recurrence of this event, personnel have been instructed to verify all precautions on test procedures prior to performing any test.
Also, all routine testing of the in-service emergency diesel generator safeguards train will be deferred when the other diesel is inoperable.
l l
This event is reportable in accordance with Technical Specification 15.6.9.2.A.6 in that personnel error could have prevented initiation of containment spray for the short time the containment high-high pressure signal was defeated.
The unit was at 100% power at the time the test was conducted.
The NRC Resident Inspector was notified of the event at about 0830 hours0.00961 days <br />0.231 hours <br />0.00137 weeks <br />3.15815e-4 months <br /> on June 18 7.nd the " red phone" notification was made at about 0902 hours0.0104 days <br />0.251 hours <br />0.00149 weeks <br />3.43211e-4 months <br /> ene same day.
i :
4 t
4
|
|---|
|
|
| | | Reporting criterion |
|---|
| 05000266/LER-1980-001-01, /01T-0:on 800202,during Routine Calibr of Pressure Transmitters for Motor Driven Auxiliary Feed Pumps, Transmitter Isolation Block Valves Discovered Closed.Caused by Inadvertent Closing of Isolation Valves.Snubbers Added | /01T-0:on 800202,during Routine Calibr of Pressure Transmitters for Motor Driven Auxiliary Feed Pumps, Transmitter Isolation Block Valves Discovered Closed.Caused by Inadvertent Closing of Isolation Valves.Snubbers Added | | | 05000266/LER-1980-001, Forwards LER 80-001/01T-0 | Forwards LER 80-001/01T-0 | | | 05000301/LER-1980-001-01, /01T-0:on 800221,during Full Power Operation, Momentary Loss of Red Instrument Bus Occurred,Resulting in Power Range Channel N41 Failing Low.Caused by Faulty Capacitor in 2DY01 Power Supply.Capacitor Replaced | /01T-0:on 800221,during Full Power Operation, Momentary Loss of Red Instrument Bus Occurred,Resulting in Power Range Channel N41 Failing Low.Caused by Faulty Capacitor in 2DY01 Power Supply.Capacitor Replaced | | | 05000301/LER-1980-001, Forwards LER 80-001/01T-0 | Forwards LER 80-001/01T-0 | | | 05000301/LER-1980-002-01, /01T-0:on 800227,primary-to-secondary Leak Was Identified in Steam Generator a Resulting in Shutdown of Unit.Caused by Leaking Tube at Position R18C37.Six Defective Tubes Found in Steam Generator a | /01T-0:on 800227,primary-to-secondary Leak Was Identified in Steam Generator a Resulting in Shutdown of Unit.Caused by Leaking Tube at Position R18C37.Six Defective Tubes Found in Steam Generator a | | | 05000266/LER-1980-002, Updated LER 80-002/01T-01:on 800311,during 800 Psi Secondary to Primary Hydrostatic Leak Test,Tubes R23C44 & R8C37 & Plug End R23C50 Found Leaking.Eddy Current Insp Performed.Tube Holes & Leaking Explosive Plugs Were Plug Welde | Updated LER 80-002/01T-01:on 800311,during 800 Psi Secondary to Primary Hydrostatic Leak Test,Tubes R23C44 & R8C37 & Plug End R23C50 Found Leaking.Eddy Current Insp Performed.Tube Holes & Leaking Explosive Plugs Were Plug Welded | | | 05000266/LER-1980-002-01, /01T-0:on 800311,during shutdown,800 Psi secondary-to-primary Hydrostatic Leak Test of B Steam Generator Revealed Tube R23C44 Leaking,Tube R8C37 Wet & Plug End R23C50 Wet.Tube Holes Will Be Weld Plugged | /01T-0:on 800311,during shutdown,800 Psi secondary-to-primary Hydrostatic Leak Test of B Steam Generator Revealed Tube R23C44 Leaking,Tube R8C37 Wet & Plug End R23C50 Wet.Tube Holes Will Be Weld Plugged | | | 05000301/LER-1980-002, Updated LER 80-002/01T-1:on 800227,during Normal Operation, Indication of Increasing primary-to-secondary Leak in a Steam Generator Noted.Caused by Leaking Tube in a Steam Generator Position R18C37 | Updated LER 80-002/01T-1:on 800227,during Normal Operation, Indication of Increasing primary-to-secondary Leak in a Steam Generator Noted.Caused by Leaking Tube in a Steam Generator Position R18C37 | | | 05000266/LER-1980-003, Forwards LER 80-003/03T-0 | Forwards LER 80-003/03T-0 | | | 05000301/LER-1980-003, Forwards LER 80-003/01T-0 | Forwards LER 80-003/01T-0 | | | 05000266/LER-1980-003-03, /03T-0:on 800318,during post-mod Testing of Containment Spray Sys,Relay 1CSB Would Not Latch.Caused by Latching Mechanism Misalignment.Latch Adjusted & Proper Operation Verified on 800318.Similar Relay Bench Tested | /03T-0:on 800318,during post-mod Testing of Containment Spray Sys,Relay 1CSB Would Not Latch.Caused by Latching Mechanism Misalignment.Latch Adjusted & Proper Operation Verified on 800318.Similar Relay Bench Tested | | | 05000301/LER-1980-003-01, /01T-0:on 800408,while Testing Pressurizer Logic Channels,Pressurizer Level Channel 427 Was Momentarily Failed Low by Instrumentation & Control Technicians.Caused by Personnel Error.Event Discussed W/Personnel | /01T-0:on 800408,while Testing Pressurizer Logic Channels,Pressurizer Level Channel 427 Was Momentarily Failed Low by Instrumentation & Control Technicians.Caused by Personnel Error.Event Discussed W/Personnel | | | 05000266/LER-1980-004, Forwards LER 80-004/03L-0 | Forwards LER 80-004/03L-0 | | | 05000301/LER-1980-004-03, /03L-0:on 800417,during Seismic Analysis of as-built safety-related Sys Per IE Bulletin 79-14, Discovered Overstressed Condition in Component Cooling Sys Piping.Caused by Lack of Support Upstream of Juncture | /03L-0:on 800417,during Seismic Analysis of as-built safety-related Sys Per IE Bulletin 79-14, Discovered Overstressed Condition in Component Cooling Sys Piping.Caused by Lack of Support Upstream of Juncture | | | 05000301/LER-1980-004, Forwards LER 80-004/03L-0 | Forwards LER 80-004/03L-0 | | | 05000266/LER-1980-004-03, /03L-0:on 800409,w/plant at Normal Steady State, Emergency Diesel Generator Failed to Start During Routine Surveillance Test.Second Attempt Unsuccessful.Caused by Broken Vane in Starting Air Motor.Air Motor Replaced | /03L-0:on 800409,w/plant at Normal Steady State, Emergency Diesel Generator Failed to Start During Routine Surveillance Test.Second Attempt Unsuccessful.Caused by Broken Vane in Starting Air Motor.Air Motor Replaced | | | 05000266/LER-1980-005, Forwards LER 80-005/03L-0 | Forwards LER 80-005/03L-0 | | | 05000266/LER-1980-005-03, /03L-0:on 800417,during Normal Operation,Review of Security Logs Revealed That Designated Fire Brigade Was Below Min Supervision Requirements on Three Occasions.Caused by Operations Personnel Designation Error | /03L-0:on 800417,during Normal Operation,Review of Security Logs Revealed That Designated Fire Brigade Was Below Min Supervision Requirements on Three Occasions.Caused by Operations Personnel Designation Error | | | 05000301/LER-1980-005-03, /03L-0:on 800609,during Training Walkdown of Safeguards Electrical Supply Cabinets,Noted That Tie Breaker Between AO5 & AO6 Safeguards Buses Was Shut.Probably Caused by Improper Electrical Lineup After Loss of Ac Test | /03L-0:on 800609,during Training Walkdown of Safeguards Electrical Supply Cabinets,Noted That Tie Breaker Between AO5 & AO6 Safeguards Buses Was Shut.Probably Caused by Improper Electrical Lineup After Loss of Ac Test | | | 05000301/LER-1980-005, Forwards LER 80-005/03L-0 | Forwards LER 80-005/03L-0 | | | 05000266/LER-1980-006-03, /03L-0:on 800417,during Analysis of as-built safety-related Piping Sys Per IE Bulletin 79-14,overstressed Condition Discovered in Cooling Sys Piping.Caused by Lack of Support Between Valves Upstream of Juncture | /03L-0:on 800417,during Analysis of as-built safety-related Piping Sys Per IE Bulletin 79-14,overstressed Condition Discovered in Cooling Sys Piping.Caused by Lack of Support Between Valves Upstream of Juncture | | | 05000301/LER-1980-006-01, /01T-0:on 800617,during Safeguards Logic Test W/ One Emergency Diesel Generator Out of Svc,Auto Containment Spray Pump Actuation Threatened During Loss of Ac & high- High Containment Pressure.Caused by Personnel Error | /01T-0:on 800617,during Safeguards Logic Test W/ One Emergency Diesel Generator Out of Svc,Auto Containment Spray Pump Actuation Threatened During Loss of Ac & high- High Containment Pressure.Caused by Personnel Error | | | 05000301/LER-1980-006, Forwards LER 80-006/01T-0 | Forwards LER 80-006/01T-0 | | | 05000266/LER-1980-006, Forwards LER 80-006/03L-0 | Forwards LER 80-006/03L-0 | | | 05000301/LER-1980-007-01, /01T-0:on 800619,at Full Power,Test IT-04 Was Performed W/Emergency Diesel Generator 3D Out of Svc. Emergency Safeguards Train Equipment Would Have Been Inoperable on Loss of Ac Power.Caused by Personnel Error | /01T-0:on 800619,at Full Power,Test IT-04 Was Performed W/Emergency Diesel Generator 3D Out of Svc. Emergency Safeguards Train Equipment Would Have Been Inoperable on Loss of Ac Power.Caused by Personnel Error | | | 05000266/LER-1980-007, Forwards LER 80-007/01T-0 | Forwards LER 80-007/01T-0 | | | 05000266/LER-1980-007-01, /01T-0:on 800611,blue Instrument Bus 1Y02 Was de-energized,resulting in de-energization of 3 Containment Pressure Channels.Caused by Personnel Error.Power Restored & Instrumentation Returned to Normal | /01T-0:on 800611,blue Instrument Bus 1Y02 Was de-energized,resulting in de-energization of 3 Containment Pressure Channels.Caused by Personnel Error.Power Restored & Instrumentation Returned to Normal | | | 05000301/LER-1980-007, Forwards LER 80-007/01T-0 | Forwards LER 80-007/01T-0 | | | 05000266/LER-1980-008, Forwards LER 80-008/03L-0 | Forwards LER 80-008/03L-0 | | | 05000266/LER-1980-008-03, /03L-0:on 800606,during Normal Operation,Testing Revealed That Relay 1-247/AO2X in Train B Would Not Drop Out to Initiate Undervoltage Trip Function.Cause Not Determined. Relay Replaced & Tested Satisfactorily | /03L-0:on 800606,during Normal Operation,Testing Revealed That Relay 1-247/AO2X in Train B Would Not Drop Out to Initiate Undervoltage Trip Function.Cause Not Determined. Relay Replaced & Tested Satisfactorily | | | 05000301/LER-1980-008, Forwards LER 80-008/01T-0 | Forwards LER 80-008/01T-0 | | | 05000301/LER-1980-008-01, /01T-0:on 800912,following Trip from Full Power, Main Steam Stop Valve B Failed to Close Upon Receiving Close Signal.Caused by Deposit Buildup on Valve Shaft &/Or Hardening of Gland Packing | /01T-0:on 800912,following Trip from Full Power, Main Steam Stop Valve B Failed to Close Upon Receiving Close Signal.Caused by Deposit Buildup on Valve Shaft &/Or Hardening of Gland Packing | | | 05000301/LER-1980-009, Forwards LER 80-009/03L-0 | Forwards LER 80-009/03L-0 | | | 05000301/LER-1980-009-03, /03L-0:on 801101,during Normal Operation, Performance of ICP 2.14 Found P8 Permissive Bistable from Channel N44 to Be Set at 50.5%.Caused by Instrument Drift. Bistable Adjusted & Tested Satisfactorily | /03L-0:on 801101,during Normal Operation, Performance of ICP 2.14 Found P8 Permissive Bistable from Channel N44 to Be Set at 50.5%.Caused by Instrument Drift. Bistable Adjusted & Tested Satisfactorily | | | 05000266/LER-1980-009, Forwards LER 80-009/01T-0 | Forwards LER 80-009/01T-0 | | | 05000266/LER-1980-009-01, /01T-0:on 800728 While in Cold Shutdown & During Hydrostatic Leak Test of Steam Generators,Two Dripping Explosive Plugs & Two Wet End Plugs Noted.Cause Not Stated. Dripping Plugs Weld Repaired | /01T-0:on 800728 While in Cold Shutdown & During Hydrostatic Leak Test of Steam Generators,Two Dripping Explosive Plugs & Two Wet End Plugs Noted.Cause Not Stated. Dripping Plugs Weld Repaired | | | 05000266/LER-1980-010-03, /03L-0:on 800827,during Normal Operation,After Redundant Containment Spray Pump Recirculation Phase Suction Valve Maint,Operability Test Was Not Performed.Caused by Personnel Failure to Fully Comprehend Maint Procedures | /03L-0:on 800827,during Normal Operation,After Redundant Containment Spray Pump Recirculation Phase Suction Valve Maint,Operability Test Was Not Performed.Caused by Personnel Failure to Fully Comprehend Maint Procedures | | | 05000266/LER-1980-010, Forwards LER 80-010/03L-0 | Forwards LER 80-010/03L-0 | | | 05000301/LER-1980-010, Forwards LER 80-010/03L-0 | Forwards LER 80-010/03L-0 | | | 05000301/LER-1980-010-03, /03L-0:on 801117,safety Injection Pump 2P15A Motor & Pump Shaft to Coupling Keys Found to Be Sheared.Cause Undetermined.Pump & Motor Checked for Damage,Keys Replaced & Pump Operability Verified | /03L-0:on 801117,safety Injection Pump 2P15A Motor & Pump Shaft to Coupling Keys Found to Be Sheared.Cause Undetermined.Pump & Motor Checked for Damage,Keys Replaced & Pump Operability Verified | | | 05000301/LER-1980-011-03, /03L-0:on 801118,axial Flux Difference Deviated from Target Band.Caused by Improper Interpretation of Tech Specs Resulting in Failure to Lower High Neutron Flux Setpoint.Instruction Clarified | /03L-0:on 801118,axial Flux Difference Deviated from Target Band.Caused by Improper Interpretation of Tech Specs Resulting in Failure to Lower High Neutron Flux Setpoint.Instruction Clarified | | | 05000301/LER-1980-011, Forwards LER 80-011/03L-0 | Forwards LER 80-011/03L-0 | | | 05000266/LER-1980-011, Forwards LER 80-011/03L-0 | Forwards LER 80-011/03L-0 | | | 05000266/LER-1980-011-03, /03L-0:on 800926,found That,Aug 1977-Sept 1980, Containment Spray Sys Spray Additive Valves Were Tested Per ASME Program Requirements Instead of Per Tech Specs.Caused by Administrative Error Re NRC | /03L-0:on 800926,found That,Aug 1977-Sept 1980, Containment Spray Sys Spray Additive Valves Were Tested Per ASME Program Requirements Instead of Per Tech Specs.Caused by Administrative Error Re NRC | | | 05000266/LER-1980-012, Forwards LER 80-012/03L-0 | Forwards LER 80-012/03L-0 | | | 05000266/LER-1980-012-03, /03L-0:on 801005,logs Showed Decrease in Holdup Tank Pressure During 801002-05.Evaluation Showed Leak on Compression Fitting on Inlet to Valve IPCV-1022C.Caused by Improper Reinstallation of Valve After Cleaning | /03L-0:on 801005,logs Showed Decrease in Holdup Tank Pressure During 801002-05.Evaluation Showed Leak on Compression Fitting on Inlet to Valve IPCV-1022C.Caused by Improper Reinstallation of Valve After Cleaning | | | 05000301/LER-1980-012, Forwards LER 80-012/03L-0 | Forwards LER 80-012/03L-0 | | | 05000301/LER-1980-012-03, /03L-0:on 801202,slippage Found in Shaft Driven Seal Water Pump Impeller Resulting in Overheating of Throttle Bushing.Caused by Reduced Seal Water Flow Due to Loosening of Pumping Ring.Shaft Sleeve & Bushing Replaced | /03L-0:on 801202,slippage Found in Shaft Driven Seal Water Pump Impeller Resulting in Overheating of Throttle Bushing.Caused by Reduced Seal Water Flow Due to Loosening of Pumping Ring.Shaft Sleeve & Bushing Replaced | | | 05000266/LER-1980-013, Forwards LER 80-013/01T-0 | Forwards LER 80-013/01T-0 | | | 05000266/LER-1980-013-01, /01T-0:on 801113,suction to 1P4B Boric Acid Transfer Pump Isolated,Rendering Pump Inoperable.Probably Caused by Personnel Error in Returning Valve Lineup to Normal Following Recirculation & Sampling | /01T-0:on 801113,suction to 1P4B Boric Acid Transfer Pump Isolated,Rendering Pump Inoperable.Probably Caused by Personnel Error in Returning Valve Lineup to Normal Following Recirculation & Sampling | |
|