05000302/LER-1978-011-03, /03L-0:on 780201,during Mode 3 Operation,Primary Containment Integrity Not Maintained When Nitrogen Valve NGV-81 Open for 3-h 42 Minutes.Caused by Oversight of Tech Spec 3.6.1 1 Requirements.Personnel Instructed

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/03L-0:on 780201,during Mode 3 Operation,Primary Containment Integrity Not Maintained When Nitrogen Valve NGV-81 Open for 3-h 42 Minutes.Caused by Oversight of Tech Spec 3.6.1 1 Requirements.Personnel Instructed
ML19317G311
Person / Time
Site: Crystal River Duke Energy icon.png
Issue date: 02/22/1978
From: Cooper J
FLORIDA POWER CORP.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19317G307 List:
References
LER-78-011-03L, LER-78-11-3L, NUDOCS 8002280923
Download: ML19317G311 (2)


LER-1978-011, /03L-0:on 780201,during Mode 3 Operation,Primary Containment Integrity Not Maintained When Nitrogen Valve NGV-81 Open for 3-h 42 Minutes.Caused by Oversight of Tech Spec 3.6.1 1 Requirements.Personnel Instructed
Event date:
Report date:
3021978011R03 - NRC Website

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,o,2, l During a preplanned outage, Mode 3 operation, nitrogen valve NGV-81 was 1

g, open for a period of 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> and 42 minutes. Primary Containment Integrity, i,,,,iwas not maintained contrary to Tech Spec 3.6.1.1.

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Valve NGV-81 was immediately closed and I i, g, i lockeds First occurrence of an event of this type.

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SUPPLEMENTARY INFORMATION 1

tore No.:

50-302/78-011/03L-0 v

2.

Facility:

Crystal River Unit #3 3.

Report Date:

22 February 1978 4.

Occurrence Date:

1 February 1978 5.

Identification of Occurrence:

Primary Contahnt Integrity was not maintained as prescribed by Technical Specifica-tion 3.6.1.1. in that Nitrogen Valve NGv-81 was opened in Mode 3 operation.

6.

Conditions Prior to Occurrence:

Mode 3 operation.

7.

Description of Occurrence:

At 1027, it was discovered that nitrogen valve NGV-81 was in the open position.

Further investigation revealed that NGV-81 had been opened at 0645 during the previous shift, by i

Operations personnel to provide a source of nitrogen to aid in the calibration of instru-.

mentation located in the Reactor Building.

During this ti:na frame, due to a pre-planned outage, the plant was in Mode 3 operation and the Technical Specification requirement for this valve to be closed was overlooked. Upon discovery, Valve NG7-81 was i= mediately closed and locked in the closed position..The valve was in the open position for 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> and 42 :tinutes.

S.wassignation of Apparent Cause:

This event was due to an oversight of Operations personnel of the Tech Spec requirements.

This oversight could have been attributed to the large nu=ber of outage functions in progress.

9.

Analysis of Occurrence:

The safety 1:rplications of this occurrence were minisal.

10.

Corrective Action

Operations Supervisory personnel have been instructed as to the proper method for hand-ling manual isolation valves while in applicable operational nodes. Discrepancy F4 port

  1. C-00823 has been submitted to further point out the consequences of this event and document corrective action taken.

11.

Failure Data:

f This is the first occurrence. of an event of this type.

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