ML19317G311

From kanterella
Jump to navigation Jump to search
LER 78-011/03L-0:on 780201,during Mode 3 Operation,Primary Containment Integrity Not Maintained When Nitrogen Valve NGV-81 Open for 3-h 42 Minutes.Caused by Oversight of Tech Spec 3.6.1 1 Requirements.Personnel Instructed
ML19317G311
Person / Time
Site: Crystal River Duke Energy icon.png
Issue date: 02/22/1978
From: Cooper J
FLORIDA POWER CORP.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19317G307 List:
References
LER-78-011-03L, LER-78-11-3L, NUDOCS 8002280923
Download: ML19317G311 (2)


Text

_ _ _ _ . _ _ _ _ _ _ _ _ _ - - _ _ _ _ _ _ _ _ _-

'.i

.- .}

' ~

h ac FOAM JC6 . U.S NUCLEAR a(cukAfortY CoMM 534cM

] LICENSEE EVENT REPORT EXHIBIT A Co=Taot stoCx: 1,

! I I I I .I@ trttAst ranst on tves ALL atousato issomu4Trous

  • lo Ii el l, F i LI Q R\ Fj 3 Jgl 0 ( 0 l- OfOOt i Og0 l ;0 g 0( g g 4,; 1,1 ;l ; 1 ; g g ,gg usau4acoo4 i. u . vcau. ~,.v.e a a :. 6.ca .a v .. a uw

' Con r loIil l'*y @l 0 i 510; -!0 3 310 r 2 @i o f ZIO I 117 I 8 a@l0 ! 21212 I 7181@

> . u .. coe.u w. ,u. - u a. = :us a ai car aare sa EVENT otscasPrioN ANo paCSA8LE CoNSEcvCNCES h

,o,2, l During a preplanned outage, Mode 3 operation, nitrogen valve NGV-81 was ,

1 g , open for a period of 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> and 42 minutes. Primary Containment Integrity, i,,,,iwas not maintained contrary to Tech Spec 3.6.1.1. Redundancy NA. No i f o 6,i I safety hazard to olant or oublic. Valve NGV-81 was immediately closed and I i, g , i lockeds First occurrence of an event of this type. ,

lo tit I f t o is I !  !

';rr' c a :

+

sfor g {'"';g ,c,'"!,{g ; ziz z e zi z i c=., s m e==, ,J.;;;.

rg gig @i, n '

r io i i i

$ 8cyt NTial.

,, ,. i, u .g g; gyt%7vtam a gaom? NC.

OCCJsst. t . a t.a n y sgy,1,cq t C3:,E

  • vat go

@ ,a(a'o ;g; oc I 7 i8 l

_a

[-J u

l oi1111 y iOI 3I I Il 8 @

.: . .. 2, ., ., u v u W2: WER at':Sr ';GtW -ou., S 'i','%D' ,;.'?.h 'C.VY: t',?;"',.

\ [H_jgg. @ lz!@ @@ l0t01011 u . . .. 2 .:

lN[g W@ [ zi 9 91 9 fg <

CAuse otsCaierion Aso ComarCm e Ac iC..s @ ,

, , , o i l The cause of this event was an oversig.c of Tech Spec requirements attribut9d j

, , , , , , to the large number of outage functions in progress. Concerned personnel ,

, , , ,., have been instructed as to proper control of manual isolation valves and ,

, , , , ,, ; Discrepancy Report f1C-00823 submitted to point out the consequences of this, i .iti  ! * *** *

  • r

's s  %*; nae cTwtasyarts h E,$3 f a3  : s n. g m, gg:.... ,.,

i.6,t dl@ l0fOfQ@l NA l Igigj Operator observatica

' l

+ J,,u ,., d?.n, i ', = =>-

  • n

,,g;]'g'g;

'"v"'TfO g l NA '" " * " ' ' '" b  ;

....o,c.i , m,, " ,, - a a 1, .

iii 1 I 0;s.d.a @[ z,r@[:u ... n %n.A _, g i . . . . , "

i , i . i I O! O .d., ',srJ,.o,: ....se NA r s 7 i Ore!

o I:

[

80

'. eg pgg ,.

Ir ' I >al ,[__zl@ls2 NA l

.<t.  : . 8 *t CN N' N 7*I #

I:i<lL,It61 8 8 'J NA  ! Ii i i! : : iii! .

g\ es it sJ d Cooper

% A..g

. Or am(sans a 8-CNE (90 0 795- 6436 e )o.

~

seos i8o D 3 i

,. , , , . , . . - , . . . _ . , , n n. , e ,G,. -

SUPPLEMENTARY INFORMATION 1 tore No.: 50-302/78-011/03L-0 2.

v Facility: Crystal River Unit #3

3. Report Date: 22 February 1978
4. Occurrence Date: 1 February 1978
5. Identification of Occurrence:

Primary Contahnt Integrity was not maintained as prescribed by Technical Specifica-tion 3.6.1.1. in that Nitrogen Valve NGv-81 was opened in Mode 3 operation.

6. Conditions Prior to Occurrence:

Mode 3 operation. 1

7. Description of Occurrence:

At 1027, it was discovered that nitrogen valve NGV-81 was in the open position. Further investigation revealed that NGV-81 had been opened at 0645 during the previous shift, by i Operations personnel to provide a source of nitrogen to aid in the calibration of instru- . "

mentation located in the Reactor Building. During this ti:na frame, due to a pre-planned outage, the plant was in Mode 3 operation and the Technical Specification requirement for this valve to be closed was overlooked. Upon discovery, Valve NG7-81 was i= mediately closed and locked in the closed position. .The valve was in the open position for 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> and 42 :tinutes.

S.wassignation of Apparent Cause:

This event was due to an oversight of Operations personnel of the Tech Spec requirements.

This oversight could have been attributed to the large nu=ber of outage functions in progress.

9. Analysis of Occurrence:

The safety 1:rplications of this occurrence were minisal.

10. Corrective Action:

Operations Supervisory personnel have been instructed as to the proper method for hand-ling manual isolation valves while in applicable operational nodes. Discrepancy F4 port

  1. C-00823 has been submitted to further point out the consequences of this event and document corrective action taken.
11. Failure Data:

f This is the first occurrence. of an event of this type.

Om

- - - - . -- ._. ,