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Category:NOTICE OF VIOLATION OF A REGULATION
MONTHYEARML20211K9431997-09-26026 September 1997 Notice of Violation from Insp on 970721-26.Violation Noted: Licensee Failed to Follow Procedures for Security Badges & Access Control of Facility ML20210S0391997-08-27027 August 1997 Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $330,000.Violation Noted:Between 970501-02,w/ Fuel in Oconee Unit 3 Core & RCS Temp Greater than 350 F, Licensee Failed to Maintain HPI Sys Operable as Required ML20134D2581991-06-0404 June 1991 Notice of Violation from Insp on 910312-15.Violations Noted:Station Was Not Maintained According to Main Procedure MP/0/A/1800/105,Section 6.5,which Clearly Identified That Flange Was to Be Installed on Valve 3LP19 ML20207T5431987-03-12012 March 1987 Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $25,000.Noncompliance Noted:Measures Not Established to Assure That Regulatory Requirements & Design Bases Correctly Translated Into Specs,Drawings & Procedures ML20211A4991987-02-11011 February 1987 Notice of Violation from Insps on 870112-16 ML20210U3211987-02-0505 February 1987 Notice of Violation from Insp on 861015-1110.Violation Noted:For Periods in 1978,1981 & 1986 When Lake Keowee Elevation Less than 792 Ft,Emergency Condenser Cooling Water Sys Inoperable & Unable to Provide Sustained Siphon Flow ML20211A0871987-02-0303 February 1987 Notice of Violation from Insp on 870105-08 ML20212F5511986-12-24024 December 1986 Notice of Violation from Insp on 861103-12 ML20199H4661986-03-27027 March 1986 Notice of Violation from Insp on 860224-28 ML20210H3741986-03-21021 March 1986 Notice of Violation from Insp on 860114-0210 ML20214D7201986-02-19019 February 1986 Notice of Violation from Insp on 851216-20 ML20137U5261986-02-12012 February 1986 Notice of Violation from Insp on 851210-860113 ML20137E3821985-11-22022 November 1985 Notice of Violation from Insp on 851008-1111 ML20133C7351985-10-0101 October 1985 Notice of Violation from Insp on 850903-06 IR 05000813/20090091985-09-16016 September 1985 Notice of Violation from Insp on 850813-0909 ML20132C1851985-09-13013 September 1985 Notice of Violation from Insp on 850729-0802 ML20135D5841985-08-28028 August 1985 Notice of Violation from Insp on 850709-0812 ML20125B5471985-06-0606 June 1985 Notice of Violation from Insp on 850211-0310 IR 05000411/20050131985-06-0303 June 1985 Notice of Violation from Insp on 850411-0513 ML20127N7301985-05-20020 May 1985 Notice of Violation from Insp on 850422-26 ML20127F1021985-04-0909 April 1985 Notice of Violation from Insp on 850318-21 ML20132B0651985-01-23023 January 1985 Notice of Violation from Insp on 841126-30 ML20129H3211984-11-23023 November 1984 Notice of Violation from Insp on 840910-14 ML20024F6531983-07-27027 July 1983 Notice of Violation from Insp on 830628-0701 ML20024A7401983-06-0202 June 1983 Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $180,000.Noncompliance Noted:Inadequate Procedures to Ensure That Air Lock Sys Restored to Operability After Maint ML20058H5731982-06-16016 June 1982 Notice of Violation from Insp on 820510-14 ML20054K3371982-05-0303 May 1982 Notice of Violation from Insp on 820310-0410 ML20053E2571982-04-0202 April 1982 Notice of Violation from Insp on 820210-0310 ML20050H8151982-03-0505 March 1982 Notice of Violation from Insp on 820110-0210 ML19347F5441981-04-0303 April 1981 Notice of Violation from Insp on 810311-13 ML19345G6641981-02-24024 February 1981 Notice of Violation from Insp on 810102-31 ML19350C0031981-02-11011 February 1981 Notice of Violation from Insp on 801201-31 ML19350C0451981-02-10010 February 1981 Notice of Violation from Insp on 801215-18 & 810105-08 ML20003D8251981-02-0909 February 1981 Notice of Violation from Insp on 810106-09 ML19341D6671981-02-0505 February 1981 Notice of Violation from Insp on 801208-12 ML20008F3331981-01-0808 January 1981 Notice of Violation from Health Physics Appraisal on 800908-19 ML20003A6061980-11-26026 November 1980 Notice of Violation from Insp on 801001-31 ML19339B0051980-09-0404 September 1980 Notice of Violation from Insp on 800701-31 ML19337A8851980-07-28028 July 1980 Notice of Violation from Insp on 800602-30 ML19337A9761980-06-20020 June 1980 Notice of Violation from Insp on 800501-30 ML19332A1291980-05-23023 May 1980 Notice of Violation from Insp on 800401-30 ML19332A6391980-05-15015 May 1980 Notice of Violation from Insp on 800415-17 & 21-23 ML19323E2281980-04-0202 April 1980 Notice of Violation from Insp on 800201-29 ML19305B1301980-01-30030 January 1980 Notice of Violation from Insp on 791218 ML19322E3531980-01-28028 January 1980 Notice of Violation from Insp on 791127-30 ML19305E2771980-01-11011 January 1980 Notice of Violation from Insp on 791203-10 ML19344D3751979-11-21021 November 1979 Notice of Violation from Insp on 791009-12 ML19257D6491979-10-24024 October 1979 Notice of Violation from Insp on 790904-28 ML19250A7101979-09-10010 September 1979 Notice of Violation from Insp on 790806-10 ML19250C4601979-07-13013 July 1979 Notice of Violation from Insp on 790627-29 1997-09-26
[Table view] Category:TEXT-INSPECTION & AUDIT & I&E CIRCULARS
MONTHYEARPNO-II-97-065, on 971228,initiated Controlled Shutdown of Unit Due to Exceeding TS Leakage Limit of 150 Gpd.Licensee Continuing W/Plant Depressurization & Cooldown & Outage Planned of Several Days to Investigate & Repair SG1997-12-29029 December 1997 PNO-II-97-065:on 971228,initiated Controlled Shutdown of Unit Due to Exceeding TS Leakage Limit of 150 Gpd.Licensee Continuing W/Plant Depressurization & Cooldown & Outage Planned of Several Days to Investigate & Repair SG ML20211K9431997-09-26026 September 1997 Notice of Violation from Insp on 970721-26.Violation Noted: Licensee Failed to Follow Procedures for Security Badges & Access Control of Facility ML20210S0391997-08-27027 August 1997 Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $330,000.Violation Noted:Between 970501-02,w/ Fuel in Oconee Unit 3 Core & RCS Temp Greater than 350 F, Licensee Failed to Maintain HPI Sys Operable as Required PNO-II-97-034, on 970613,extended Shutdown to Meet CAL 2-97-03 Commitments to Shutdown Unit 1 No Later than 970614 & to Implement Actions Re HPI Sys.Nrc Resident Inspector Will Followup on Unit 1 Shutdown & Recovery Activities1997-06-13013 June 1997 PNO-II-97-034:on 970613,extended Shutdown to Meet CAL 2-97-03 Commitments to Shutdown Unit 1 No Later than 970614 & to Implement Actions Re HPI Sys.Nrc Resident Inspector Will Followup on Unit 1 Shutdown & Recovery Activities IR 05000269/19930321994-01-0606 January 1994 Insp Repts 50-269/93-32,50-270/93-32,50-287/93-32, 50-369/93-31,50-370/93-31,50-413/93-35 & 50-414,respectively on 931213-17.Violations Noted.Major Areas Inpected:Licensee Safeguards Info Program to folow-up on Licensee Repts PNO-II-93-039, on 930823,reactor Trip Occurred Due to Loss of Power to Vital Panelboard.Investigation Team Dispatched to Site to Review Root Cause & Plant Response.State & Local Authorities Notified1993-08-24024 August 1993 PNO-II-93-039:on 930823,reactor Trip Occurred Due to Loss of Power to Vital Panelboard.Investigation Team Dispatched to Site to Review Root Cause & Plant Response.State & Local Authorities Notified IR 05000269/19930181993-06-13013 June 1993 Insp Repts 50-269/93-18,50-270/93-18 & 50-287/93-18 on 930614-17.No Violations Noted.Major Areas Inspected:Annual Emergency Preparedness Exercise IR 05000269/19930101993-04-16016 April 1993 Insp Repts 50-269/93-10,50-270/93-10 & 50-287/93-10 on 930315-19.No Violations or Deviations Noted.Major Areas Inspected:Radiological Effluents,Process & Effluent Radiation Monitoring Instrumentation & Water Chemistry IR 05000269/19930061993-03-22022 March 1993 Partially Withheld Insp Repts 50-269/93-06,50-270/93-06 & 50-287/93-06 on 930222-25 (Ref 10CFR73.21).No Violations or Deviations Noted.Major Areas Inspected:Licensee Physical Security Program for Power Reactors IR 05000269/19933001993-02-23023 February 1993 Initial Exam Rept 50-269/93-300 Administered During Wk of 930125.Exam Results:Seven Senior Reactor Operators Passed Both Written Exams & Operating Tests ML20034E9571993-02-19019 February 1993 Insp Repts 50-269/93-03,50-270/93-03 & 50-287/93-03 on 930103-30.Violations Noted.Major Areas Inspected:Plant Operations,Surveillance Testing,Maint Activities,Keowee Issues & Insp of Open Items IR 05000269/19930011993-02-0101 February 1993 Safeguards Insp Repts 50-269/93-01,50-270/93-01 & 50-287/93-01 on 930104-07.No Violations Noted.Major Areas Inspected:Physical Security Program.Details Withheld (Ref 10CFR73.21) IR 05000269/19920251992-12-0303 December 1992 Insp Repts 50-269/92-25,50-270/92-25 & 50-287/92-25 on 921102-06.No Violations or Deviations Noted.Major Areas Inspected:Physical Security Program for Power Reactors, Audits,Protected & Vital Area Barriers.Details Withheld PNO-II-92-070A, on 921019,AIT Dispatched to Facility Following Reactor Trip Due to Loss of Ac Power Followed by Degraded Emergency Power Supply.Following Implementation of Corrective Actions,Facility Restarted on 9210261992-10-28028 October 1992 PNO-II-92-070A:on 921019,AIT Dispatched to Facility Following Reactor Trip Due to Loss of Ac Power Followed by Degraded Emergency Power Supply.Following Implementation of Corrective Actions,Facility Restarted on 921026 PNO-II-92-070, on 921019,several Circuit Breakers Failed in 230KV Switchyard to Open Position for Unknown Reasons. Licensee Has Inititated Investigation to Review Event to Determine Cause & Determine Why Certain Equipment Failed1992-10-20020 October 1992 PNO-II-92-070:on 921019,several Circuit Breakers Failed in 230KV Switchyard to Open Position for Unknown Reasons. Licensee Has Inititated Investigation to Review Event to Determine Cause & Determine Why Certain Equipment Failed PNO-II-91-074B, on 911123,unit Remained in Cold Shutdown,Per Declaration of Alert at 0214 Due to Leak in Rcs.As of 911126,total of 7,800 Gallons of Treated Water Released from Plant to Lake Hartwell1991-11-26026 November 1991 PNO-II-91-074B:on 911123,unit Remained in Cold Shutdown,Per Declaration of Alert at 0214 Due to Leak in Rcs.As of 911126,total of 7,800 Gallons of Treated Water Released from Plant to Lake Hartwell ML20134D2581991-06-0404 June 1991 Notice of Violation from Insp on 910312-15.Violations Noted:Station Was Not Maintained According to Main Procedure MP/0/A/1800/105,Section 6.5,which Clearly Identified That Flange Was to Be Installed on Valve 3LP19 IR 05000269/19910081991-04-10010 April 1991 Insp Repts 50-269/91-08,50-270/91-08 & 50-287/91-08 on 910312-15.violations Noted.Major Areas Inspected:Maint, Control Room Operation,Planning & Scheduling Activities, Training & Procedures,Plant Physical Condition & Mgmt PNO-II-91-006A, on 910308,augmented Insp Team Dispatched to Followup on Loss of Decay Heat Capability Event.Team Will Arrive on-site & Begin Insp on 9103121991-03-11011 March 1991 PNO-II-91-006A:on 910308,augmented Insp Team Dispatched to Followup on Loss of Decay Heat Capability Event.Team Will Arrive on-site & Begin Insp on 910312 PNO-II-91-006, on 910308,during Draining of RCS & Borated Water Storage Tank,Loss of DHR Occurred.Caused by Securing LPI Pump 3A Due to Pump Cavitation.Suction Valves from Borated Water Tank Opened to Recover Rx Vessel Level1991-03-0808 March 1991 PNO-II-91-006:on 910308,during Draining of RCS & Borated Water Storage Tank,Loss of DHR Occurred.Caused by Securing LPI Pump 3A Due to Pump Cavitation.Suction Valves from Borated Water Tank Opened to Recover Rx Vessel Level PNO-II-90-070, on 901108,unit Commenced Controlled Shutdown from 60% Power Due to Tube Leak in Steam Generator a1990-11-0808 November 1990 PNO-II-90-070:on 901108,unit Commenced Controlled Shutdown from 60% Power Due to Tube Leak in Steam Generator a IR 05000269/19900321990-11-0505 November 1990 Partially Withheld Insp Repts 50-269/90-32,50-270/90-32 & 50-287/90-32 on 901015-19.No Violations Noted.Major Areas Inspected:Physical Security Program Plans,Mgt Support, Security Program Plans & Protected & Vital Area Barriers IR 05000269/19900241990-10-0202 October 1990 SALP Repts 50-269/90-24,50-270/90-24,50-287/90-24 & 72-0004/90-24 for Feb 1989 - Jul 1990 IR 05000269/19900221990-07-24024 July 1990 Partially Withheld Safeguard Insp Repts 50-269/90-22, 5-270/90-22 & 50-287/90-22 on 900625-29.No Violations or Deviation Noted.Major Areas Inspected:Core Insp Program for Power Reactors & Safeguards Contingency Plan Implementation IR 05000269/19900181990-06-21021 June 1990 Partially Withheld Insp Repts 50-269/90-18,50-270/90-18 & 50-287/90-18 on 900604-08 (Ref 10CFR2.790 & 73.21).No Violations Noted.Major Areas Inspected:Security Program Audit,Detection & Assessment Aids & Key Control PNO-II-90-024, on 900517,plant Operators in Unit 1 & 2 Control Room Break Area Noted Water Coming Down Wall.Water Being Pumped to Spent Fuel Pool Due to Out of Sequence Valve Alignment Which Caused Overfilling.No Personnel Injured1990-05-18018 May 1990 PNO-II-90-024:on 900517,plant Operators in Unit 1 & 2 Control Room Break Area Noted Water Coming Down Wall.Water Being Pumped to Spent Fuel Pool Due to Out of Sequence Valve Alignment Which Caused Overfilling.No Personnel Injured IR 05000269/19900061990-03-19019 March 1990 Partially Withheld Insp Repts 50-269/90-06 & 50-270/90-06 & 50-287/90-06 on 900212-16 (Ref 10CFR2.790(d) & 73.21). Violations Noted.Major Areas Inspected:Physical Security Program for Power Reactors,Specifically Mgt & Barriers IR 05000269/19890391990-02-22022 February 1990 Insp Repts 50-269/89-39,50-270/89-39 & 50-287/89-39 on 891212-15 & 18-20.No Violations or Deviations Noted.Major Areas inspected:post-refueling Startup Tests of Unit 3 & Core Performance Surveillances on Units 1 & 2 IR 05000269/19890321989-11-20020 November 1989 Partially Withheld Insp Repts 50-269/89-32,50-270/89-32 & 50-287/89-32 on 891002-04 (Ref 10CFR2.790 & 73.21).Major Areas Inspected:Physical Security Program for Power Reactors IR 05000269/19890331989-11-15015 November 1989 Insp Repts 50-269/89-33,50-270/89-33 & 50-287/89-33 on 890930.No Violations or Deviations Noted.Major Areas Inspected:Physical Protection of Shipment of Irradiated Reactor Fuel IR 05000269/19890301989-11-0707 November 1989 Partially Withheld Insp Repts 50-269/89-30,50-270/89-30 & 50-287/89-30 on 890918-22 (Ref 10CFR2.790 & 73.21).One non- Cited Violation Noted.Major Areas Inspected:Physical Security Program for Power Reactors & Mgt Effectiveness IR 05000269/19890201989-07-25025 July 1989 Partially Withheld Insp Repts 50-269/89-20,50-270/89-20 & 50-287/89-20 on 890626-30 (Ref 10CFR2.790.(d) & 73.21). Violations Noted.Major Areas Inspected:Physical Security Program for Power Reactors & Security Audit IR 05000269/19890101989-05-19019 May 1989 Partially Withheld Insp Repts 50-269/89-10,50-270/89-10 & 50-287/89-10 on 890410-14 (Ref 10CFR2.790 & 73.21). Violations Noted.Major Areas Inspected:Mgt Support,Security Program Plans & Audits & Protected & Vital Area Barriers IR 05000269/19890091989-04-10010 April 1989 Insp Repts 50-269/89-09,50-270/89-09 & 50-287/89-09 on 890306-10.No Violations Noted.Weaknesses Noted Re Data Base Used to Prepare computer-generated Work Requests.Major Areas Inspected:Design Control,Mods & Open Items IR 05000269/19890071989-03-10010 March 1989 Insp Repts 50-269/89-07,50-270/89-07 & 50-287/89-07 on 890213-17.Deviation Noted.Major Areas Inspected:Conformance to Reg Guide 1.97 Re Instrumentation for light-water-cooled Plants to Assess Conditions During & Following Accident IR 05000269/19880051988-03-21021 March 1988 Insp Repts 50-269/88-05,50-270/88-05 & 50-287/88-05 on 880217-0316.No Violations Noted.Major Areas Inspected:Maint, Operations,Surveillance,Physical Security & Design Changes PNO-II-88-013, on 880211,two Workers Slightly Contaminated W/ Radioactive Water.Caused by Approx 1,000 Gallon Leak of Radioactive Water Occurring During Maint on Valve.Workers Showered to Remove Contamination1988-02-12012 February 1988 PNO-II-88-013:on 880211,two Workers Slightly Contaminated W/ Radioactive Water.Caused by Approx 1,000 Gallon Leak of Radioactive Water Occurring During Maint on Valve.Workers Showered to Remove Contamination ML20237B2261987-12-15015 December 1987 EN-87-017A:informs That 870309 Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $25,000 Withdrawn Due to Determination That Violation Did Not Occur. Violation Based on Failure of Emergency Feedwater Pumps ML20235T5821987-09-18018 September 1987 Exam Rept 50-269/OL-87-02 on 870713-23.Exam Results:Seven of Ten Reactor Operator (RO) & Eight of Nine Senior Reactor Operator (SRO) Candidates Passed Written Exam.All RO & SRO Candidates Passed Operating Exam ML20238F7081987-09-0909 September 1987 Exam Rept 50-269/OL-87-01 for Units 1,2 & 3 on 870713-17. Exam results:7 of 10 Reactor Operators & 3 of 6 Senior Reactor Operators Passed ML20236E5111987-07-14014 July 1987 EN-86-056:on 870717,notice of Violation & Proposed Imposition of Civil Penalty in Amount of $25,000 Will Be Issued to Licensee.Action Based on Failure to Properly Implement Startup Procedure Causing Trains to Fail IR 05000269/19870101987-03-17017 March 1987 Insp Repts 50-269/87-10,50-270/87-10 & 50-287/87-10 on 870210-0309.No Violations or Deviations Noted.Major Areas Inspected:Areas of Operations,Surveillance,Maint,Followup of Events & Verification of ESF Lineups IR 05000269/19870091987-03-17017 March 1987 Insp Repts 50-269/87-09,50-270/87-09 & 50-287/87-09 on 870209-13.No Violations Noted.Major Areas Inspected:Onsite Review of Liquid & Gaseous Radwaste Programs & Review of TMI Action Items II.B.3 & II.F.1.2 ML20207T5431987-03-12012 March 1987 Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $25,000.Noncompliance Noted:Measures Not Established to Assure That Regulatory Requirements & Design Bases Correctly Translated Into Specs,Drawings & Procedures ML20207R4851987-03-0909 March 1987 EN-87-017:on 870312,notice of Violation & Proposed Imposition of Civil Penalty in Amount of $25,000 Will Be Issued to Util Based on Failure to Provide Adequate Design Control to Ensure Emergency Feedwater Pump Operability IR 05000269/19870061987-03-0909 March 1987 Insp Repts 50-269/87-06,50-270/87-06 & 50-287/87-06 on 870126-30.No Violations or Deviations Noted.Major Areas Inspected:Inservice Insp,Ongoing Repairs in Reactor Coolant Pumps & Maint & Welding Activities IR 05000269/19870041987-02-17017 February 1987 Insp Repts 50-269/87-04,50-270/87-04 & 50-287/87-04 on 870113-0209.No Violation or Deviation Noted.Major Areas Inspected:Operations,Surveillance,Maint,Verification of ESF Linups,Followup of Events & Shutdown Work in Progress ML20211A4991987-02-11011 February 1987 Notice of Violation from Insps on 870112-16 IR 05000269/19870021987-02-11011 February 1987 Partially Withheld Insp Repts 50-269/87-02,50-270/87-02 & 50-287/87-02 on 870126-30 (Ref 10CFR2.790).Violation Noted Re Inadequate App R Circuit Analysis IR 05000269/19870031987-02-10010 February 1987 Insp Repts 50-269/87-03,50-270/87-03 & 50-287/87-03 on 870112-16.Violation Noted:Failure to Adequately Evaluate Radiological Hazards 1997-09-26
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APPENDIX A NOTICE OF VIOLATION Duke Power Company License Nos. DPR-47 Based on the results of the NRC inspection conducted on May 9-12, 1978, it appears that certain of your activities were not conducted in full compliance with NRC requirements as indicated below. These items have been categorized as described in our correspondence to you dated December 31, 1974.
10 CFR 20.203(c) statas in part: "(2) Each entrance or access point to a high radiation area shall be:
(1) Equipped with a control device which shall cause the level of radiation to be reduced...;
or (ii) Equipped with a control device which shall energize a conspicuous visible or audible alarm signal... ; or maintained locked except during period when access to the area is required, with positive control over each individual entry.... (4) In the case of a high radiation area established for a period of 30 days or less, direct surveillance to prevent unauthorized entry may be substituted for the control required by subparagraph (2) of this paragraph."
w Contrary to the above, a high radiation area surrounding a de-watered resin cask, located outside the Unit 2 auxiliary building was not under direct surveillance from 11:00 a.m. on May 9,1978 to 12:00 p.m. on May 11, 1978 nor was the area locked or alarmed.
This is an infraction.
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h RII RIpert N:s. 50-269/78-12, 50-270/78-11 and 50-287/78-11 I-1 DETAILS I Prepared by:
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W R6~actfr Infpector Date Nuc1 ar,pport Section No. 2 Reactor Operations and Nuclear Support Branch Dates of Inspection:,y.
9-12, 978 I
if 8gY Reviewed by:
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/Date Nuc ea Support Section No. 2 Reactor Operations and Nuclear Support Branch 1.
Persons Contacted J. E. Smith, Plant Manager
- R. C. Adams, I&E Engineer M. Alexander, Technical Support Engineer R. T. Bond, Project License Engineer
- W. A. Brown, Staff Chemist C. Burns, I&E Foreman
- R. M. Koehler, Superintendent Technical Services
- J. M. Davis, Maintenance Superintendent
- C. T. Yongue, Health Physics Supervisor
- J. N. Pope, Operations Supervisor Five instrument technicians and two plant operators were also contacted.
- Denoted those attending exit interview.
2.
Licensee Action on Previous Inspection Findings Not inspected.
3.
Unresolved Items Unresolved items are matters about which more informaticn is required in ceder to ascertain whether they are acceptable items, items of noncompliance or deviations. One unresolved item disclosed during the inspection is discussed in paragraph 6.
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RII Report Nos. 50-269/78-12, 50-270/78-11 and 50-287/78-11 I-2 4.
Exit Interview The inspectors met with licensee representatives (denoted in paragraph 1) at the conclusion of the inspection on, May 12, 1978. The inspectors summarized the scope and findings of the inspection as discussed in paragraphs 5, 6, 7, 8 and 9.
The licensee acknowledged the item of noncompliance and indicated a review of responsibilities between departments would be conducted.
5.
Surveillance (Periodic) Test Procedure and Results Verification The inspectors conducted a review of test procedures and results and witnessed testing as follows:
(Procedures and Results)
IPO O A 0310 07A, ES Logic Subsystem 1 HPI CH.1 PT-0 A 0110 01, Spent Fuel Pool Ventilation Test PT 0 A 0200 46, Reactor Coolant System Leak Rate Test PT 0 A 020212, HP Injection System ES Test PT 0 A 029'
..a stop Valve Closure Time Test PT 0 A 060015, CRD Movement Test PT 0 A 060017, Group 7 Control CRD Withdrawal PT 0 A 0620 09, Keowee Hydro Emergency Start Test PT 1 A 025104, LP Borated Water Pump Performance Test PT 2 A 060011, Emergency Feedwater System IP 3 A 0340 15, CRD Position Indication Tube Alignment The inspectors used one or more of the following acceptance criteria for the above items:
I DPC0 Topical Report - 17.2.11 - Test Control I
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i RII Report Nos. 50-269/78-12, 50-270/78-11 and 50-287/78-11 I-3 Technical Specification - Section 4.0 ANSI N45.2-1971 ANSI N18.7-1972 Inspector Judgement Quality Assurance Program The test procedures and test results were reviewed to verify:
Test prerequisites and plant conditions were specified, and reviewed, and approvals had been performed.
Technical contents of the procedure were correct, and the test was performed on schedule.
Test instruments were listed in the procedure and the instruments used identified in the test results.
Test results were recorded and compared with acceptance criteria, and return of equipment to service was veritied upon t;&;'-tion of test.
Within the areas inspected no items of noncompliance or ieviations were identified.
(Test Witnessed)
PT 2 A 6001/1 - Periodic Instrupc3t Surveillance (Encle sure 13.1)
PT 3 A-305/3A - RPS - CH. A Functional Verification Surveillance tests were witnessed to verify:
Correct procedure was being used for testing and that technicians and operators understood equipment being tested.
Data was correctly recorded and verified.
Calibrated test equipment was in use where requi ed.
Verification of return of equipment to service and removal of test equipment was done, u-)
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RII Report Nos. 50-269/78-12, 50-270/78-11 and 50-287/78-11 1-4 i
Within the areas inspected no items of noncompliance or deviations were identified.
6.
Instrumentation Calibration Program Verification The inspector conducted a review of the following calibration procedures and test results:
1 P 0 A 0150 O1G, Reactor Building Temperature Recorded Calibration IP 0 A 020010, RC Pressure Instrument Calibration IP 0 A 020101A, CF Tank Pressure Instrument Calibration IP OA 020101 B, CF Tank Pressure Instrument Calibration IP 0 A 030103D, NI 4 Calibration (Annual)
IP 0 A 0.$05 01 M, RPS CH. A Pressure Calibration IP 0 A 0305 05 H, RPS CH. A RB High Pressure Trip IP 0 A 0305 05 D, Pressure Trip RPS CH. D RB High IP 0 A 0310 05B, ES Analog CH. 3 RC Pressure IP 1 A 0305 01I, RCS Ch. A Flow Calibration IP 1 A 0305 01E, RPS Ch. A Temperature Calibration IP 2 A 0305 011, RPS Ch. "A" Flow Calibration IP 3 A 0305 01 H, RPS Temperature Calibration IP 0 A 0202 01 D, Emergency HP Injection Flow Instrument Calibration IP 0 A 0202 01F, LST Level Instrument Calibration IP O A 0203 01 A, BWST Level Instrument Calibration IP O A 0203 01 A, RB Emergency Sump Level Instrument Calibration IP 0 A 0231 07, CS Concentrated Boric Acid Storage Tank Level and Temperature
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RII Report Nos. 50-269/78-12, 50-270/78-11 and 50-287/78-11 I-5 IP 1 A 0340 04, Absolute Position Indicator Calibration IP 0 A 036101 A, Monitor System Calibration IP 0 A 0210 04, Auto Gas Analyzer Instrument Calibration The procedures and calibration results were reviewed to verify:
Reviews and approvals were being conducted, and data was recorded and evaluated.
Test instruments were listed and identified in test results.
Adherence to Technical Specifications requirements and limiting conditions for operations.
Technical contents were correct and verification of return of equipment to service and removal of test equipment was being done.
The inspectors conducted an inspection of the following measuring and
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test equipment storage facilities and records:
Instrumentation and control standards laboratory.
Measuring and test tool storage and issuing room.
These facilities were inspected to verify:
That standard test instruments were labeled and included in the calibration program.
Instruments were being calibrated on schedule and labeled with cal.bration status.
Storage facilities were proper for protecting the equipment.
Certification and calibration records were available and being maintained for test equipment.
The inspectors used one or more of the following acceptance criteria i
for evaluating the above items in the calibration program:
VEPCO Topical Report - 17.2.12 Control of measuring and Test Equipment
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RII Report Nos. 50-269/78-12, 50-270/78-11 and 50-287/78-11 I-6 ANSI N45.2-1971 ANSI N18.7-1972 Inspector Judgement Quality Assurance Program Within the areas inspected no items of noncompliance or deviations were identified.
In one area inspected the inspectors found resistance decade boxes not under quality assurance control as required by Section 13 of ANSI N45.2 (1971). The licensee reported that this equipment was regularly calibrated, but had been inadequately left out of the regular l
calibration program for instruments used for safety-related systems.
The licensee will place this equipment under safety system's instrument calibration control and NRC will verify this at a subsequent inspection.
This item will remain unresolved pending the incorporation of the decade boxes into the calibration program.
I (269/78-12-01,270/78-11-01,287/78-11-01) 7.
Inspection of Chemistry Laboratory 4
An inspection of the chemistry laboratory and associated equipment was j
conducted by the inspector to verify that procedures and equipment were
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available for determining coolant chemical concentrations and status j
as required by Technical Specifications. The method of preparation and verification of shelf life of chemical standards were also reviewed.
The inspector used the requirements of 'the Technical Specifications for conducting this inspection.
Within the areas inspected no items of noncompliance or deviations were identified.
8.
Inspection of Control Room Operations The inspector toured the control room and reviewed the plant status and operations in progress with the operators. During this inspection Unit No. I operators were conducting a pressurization test on the steam generators to check for leaks following tube plugging.
The inspector used the requirements of the Technical Specifications for performing this inspection and review.
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RII Report Nos. 50-269/78-12, 50-270/78-11 and 50-287/78-11 I-7 Within the areas inspected no items of noncompliance or deviations were i
identified.
9.
Control of High Radiation Areas During a tour of the facility the inspector noted a dewatered resin cask outside the Unit 2 auxiliary building. Discussions with licensee personnel indicated the cask had been moved from auxiliary building on May 9, 1978.
A survey conducted at 11:00 a.m. on May 9, indicated general area readings of 100 mrad /hr., cask bottom 1,000 mrad /hr., cask side 200 mrad /hr. A radiation control boundary was established around the cask. The cask was then left in a unsupervised condition until about noon on May 11, 1978. At that time the cask was placed under the direct surveillance of a security guard.
10 CFR 20.203 requires, in part, that high radiation areas either be directly surveilled to prevent unauthorized entry or be locked and ala rmed. The absense of either direct surveillance or locks and alarms constitutes an item of noncompliance with 10 CFR 20.203.
This item (270/78-11-02)is an infracti< 1.
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RII Report Nos. 50-269/78-12, 50-270/78-11 and 50-287/78-11 II-1 l
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DETAILS I_
Prepared by:
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D. R. McGuire, Physical Security Date i
Specialist Security and Investigation Section Safeguards Branch CLt (c ll &
C. L. Davis, Physical Security Date Intern l
Security and Investigation Section Safeguards Branch I
Dates of Insp tio:1: Ma 1 -12, 1978 Approved by:
W-l,b [
C.E.Miderson,ActingChief Date Security and Investigation Section Safeguards Branch 1.
Persons Contacted R. Koehler, Supervisor of Technical Services (Acting Station Manager) l J. Suffick, Contract Services Supervisor Capt. G. Cooper, Southern Security Guard 2.
Followup on Immediate Action Letter f
The inspectors conducted a followup of the Immediate Action Letter l
sent to Duke Power Company by Region II on March 17, 1978. Wile on site the inspectors walked through the facility and observed access controls, protected area barriers, and guard personnel.
The inspectors were informed that Duke Power Compatiy had recently concluded a QA audit of Oconee's security program. The audit was conducted from April 3, 1978 through May 8, 1978 and required 885 manhours by four licenree auditors.
The findings of the audit were to be issued by DPC on May 12, 1978. The audit findings and correc-tive actions will be reviewed during future inspections.
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