ML19312D513

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LER 80-017/03L-0:on 800222,while Manually Starting Turbine Driven Auxiliary Feedwater Pump,Turbine Tripped on Overspeed.Caused by Limit Switch Being Out of Adjustment. Limit Switch Adjusted & Feedwater Pump Returned to Svc
ML19312D513
Person / Time
Site: Farley Southern Nuclear icon.png
Issue date: 03/14/1980
From: Hairston W
ALABAMA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19312D498 List:
References
LER-80-017-03L, LER-80-17-3L, NUDOCS 8003240528
Download: ML19312D513 (1)


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'I & t,4 68 EVENT CESCniPTION A?40 PA04 A3LE CC'4SECUE'.OES FTTTl I uhile manually starting the Turbine Driven Auxiliary Feedwater Punp. the turbine trippec)

TTTT) ] on overspeed. The TDAniP was declared inoperabic at 0600 on 2/22/80. Tech. Spec. l TTTT] l 3.7.1.2 requires the TDARIP to be operable. T/S 3.7.1.2 action statement requirementsg t o i s t t were met.

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} s io l lThe overspeeding of the TDAniP was caused by a limit switch nn the turbine steam t ,,.,; ] supply valve being out of adjustment. The limit switch allowed the ramp signal in y j the governor control circuit to demand full opening of 'the governor valve prior to g

!- m (opening the steam supply valve. The limit switch was adjusted and the TDARiP returned ;

3 4  ; to service at 1300 on 2/22/80 af ter satisfactory completion of FNP-1-STP-22.0, TDARIP p so a sOperability Test. PETwoO o8 PSTAT.r3 AOtO.TY 4 POWER CTMEM5rATuS D:5CQvE9Y OtSC.OVERY DESCniPTso e 32 lYIll l C I@ l Of 1161@l NA I IA!@lOperatorobservation l

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Oil level restored to the proper level, and the surveillance test successfully completed. The pump was returned to service at 2130 on 2/15/80.

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