05000348/LER-1980-017-03, /03L-0:on 800222,while Manually Starting Turbine Driven Auxiliary Feedwater Pump,Turbine Tripped on Overspeed.Caused by Limit Switch Being Out of Adjustment. Limit Switch Adjusted & Feedwater Pump Returned to Svc

From kanterella
(Redirected from ML19312D513)
Jump to navigation Jump to search
/03L-0:on 800222,while Manually Starting Turbine Driven Auxiliary Feedwater Pump,Turbine Tripped on Overspeed.Caused by Limit Switch Being Out of Adjustment. Limit Switch Adjusted & Feedwater Pump Returned to Svc
ML19312D513
Person / Time
Site: Farley 
Issue date: 03/14/1980
From: Hairston W
ALABAMA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19312D498 List:
References
LER-80-017-03L, LER-80-17-3L, NUDOCS 8003240528
Download: ML19312D513 (1)


LER-1980-017, /03L-0:on 800222,while Manually Starting Turbine Driven Auxiliary Feedwater Pump,Turbine Tripped on Overspeed.Caused by Limit Switch Being Out of Adjustment. Limit Switch Adjusted & Feedwater Pump Returned to Svc
Event date:
Report date:
3481980017R03 - NRC Website

text

_ _

n.m.

LICENSEE E'.'ENT REPORT CONTROL DLCtK. l

}

l l

l' l

fh VI.E ASE PRINT OR TYPE alt. REQUIRED INFO %4TIONI i

.s 30 !0 l-1010 l@l 41 1l 1 { 1l 1l@]

l

[ p-

@ l A I f, !.1 I M l F i 1 [@l 0 l 0 l- ! 0 10 10 m.a

,y,,

u

,, m u 4

i ucto.a wot

.A a

.uw.s, 2,

a Cc. r 104-1 i"M 11. J@l 0 ! 5 : 0 l'0 ! 0 ! 3 5 4 18 '@! 01 21 21 21 81 0@l0 l 3l1 l 4 1

'I t,4 68 c%,.E T W.* J 18-el L'. L*.! OAi4

'. 8 76 RE'OR T CATE 20 EVENT CESCniPTION A?40 PA04 A3LE CC'4SECUE'.OES FTTTl I uhile manually starting the Turbine Driven Auxiliary Feedwater Punp. the turbine trippec)

TTTT) ] on overspeed. The TDAniP was declared inoperabic at 0600 on 2/22/80. Tech. Spec.

l TTTT] l 3.7.1.2 requires the TDARIP to be operable. T/S 3.7.1.2 action statement requirementsg The health and safety of the public were not af fected by this occurrence.

g t o i s t t were met.

g (c f s l f l

I307ll I

l e ta l i e4 SYSTiu cAutt CAL 23 co4**.

VALvt Coot CccE susccci CovPONENTCCDE S;accos susCoog

!TITl l u t c l@ (Pj@ I A !@ 11131 S I T ! a t u l@ s c t@ g @

7 8

9 10 55 32 1J IJ l'J 20 SE0VE%TIAL C00Un ett.ct pgpcRr

  • EVISlo'*

(gg no IVENT Ygag P E PO R T *.3.

CODE rYPE ho.

- @,=,m I a l 01 I-I I o! H 71 Ld IOI3i Ltd L-1 toI

,,,,. 2 3 72 13 25 23 2')

Jo 31 J;

ACTION FUTUAt EF8f0?

Sut"0CT.N A TTACMitNT N P

  • t-4 P'4tVI CO"P.

COUPCni1NT TAMEN A0 Tron Oas*LANT VET-c3

    • OURS sus % f fiD FCR M :n.d.

$UPPLIER waNUF.ACTURER LE_J@l zl@

I zi@

I z "@

.I o f o !

I W@

lNj,g lAlg

}1l0l7l5 g

~

3J 34 3a

.d 44 4.

42 4J as og CAUSE DESCRIPTION A?;D CCREECmE ACT;O?iS 'd,.

} s io l lThe overspeeding of the TDAniP was caused by a limit switch nn the turbine steam g

t,,.,; ] supply valve being out of adjustment. The limit switch allowed the ramp signal in y j the governor control circuit to demand full opening of 'the governor valve prior to g

!- m (opening the steam supply valve. The limit switch was adjusted and the TDARiP returned ;

to service at 1300 on 2/22/80 af ter satisfactory completion of FNP-1-STP-22.0, TDARIP p

3 4 so a sOperability Test.

PETwoO o8 P AOtO.TY STAT.r3 4 POWER CTMEM5rATuS D:5CQvE9Y OtSC.OVERY DESCniPTso e 32 NA I

IA!@lOperatorobservation l

lYIll l C I@ l Of 1161@l 80

",.t.or s, AcT,vir, @ I sce u

.,,,u A, @

ACTIVtfY CO TENT aruAno o aium NA l

NA l

FMI I z l@ I zt@l I

4 9 TJ 11 da 46 gg PtRSCN*.4L ExPosunf &

.I NOV9944 TYPE O!!CW?p't:1te 09 r

FiTT1101010 GI z!@t NA q

an3 7

8' 1!

12 u

D qqD D

f PERCut L tNJuHvis cuCn.n.or.O, A

nu m N

_ }(

( J l

101010l@l f

~

LCS".05 04 CA:.tAGE TO FACst.?v Q Twt eu:,,Pr.n

. I

  • 1 o f 1 z C.El NA l

.. 2

,o muQEca,Pim@.

80082 4 o *h3 l

ll[]i9;;;ti;J!

"acuse ont<

1 O?iliNIgr NA sai sa s,

?

8

_S

.54 i

(205) 599-5156 y

U. G. Hairston. III g op py,g

. ~.

+

Oil level restored to the proper level, and the surveillance test successfully completed. The pump was returned to service at 2130 on 2/15/80.

Y me

.m_.