Ro:On 800520,while Performing Routine Pulses,One of Five Pulses Produced Peak Power & Measured Fuel Temp Beyond Expectation for 2.55 Dollar Reactivity Insertion. Apparently Caused by 2.75 Dollar Reactivity InsertationML19310A386 |
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Oregon State University |
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Issue date: |
06/03/1980 |
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From: |
Ringle J Oregon State University, CORVALLIS, OR |
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To: |
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References |
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NUDOCS 8006110183 |
Download: ML19310A386 (4) |
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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO
MONTHYEARML20029A7541991-02-25025 February 1991 Followup RO Per 910215 Telcon:On 910215,water Level in Reactor Tank Lower than Normal.Caused by Water Running Out from Under Concrete Block Shield Surrounding Demineralizer Tank.Barrier Dam Constructed Across HX Room ML20003G2551981-04-17017 April 1981 Ro:On 810414,continuous Control Rod Withdrawal Occurred, Resulting in Net Insertion of 80 Cents Reactivity Worth. Caused by Failure of Safety Rod Up Switch.Operations Instructions Bulletin Written Re Possible Recurrence ML19340D3771980-12-19019 December 1980 Ro:On 801212,reactor Operated for Approx 1-h W/ Nonfuctioning Air Pump on Reactor Top Continuous Air Particulate Radiation Monitor.Caused by Loosely Fitting Power Plug &/Or Loose Fuse Holder Connection ML19310A3861980-06-0303 June 1980 Ro:On 800520,while Performing Routine Pulses,One of Five Pulses Produced Peak Power & Measured Fuel Temp Beyond Expectation for 2.55 Dollar Reactivity Insertion. Apparently Caused by 2.75 Dollar Reactivity Insertation 1991-02-25
[Table view] Category:LER)
MONTHYEARML20029A7541991-02-25025 February 1991 Followup RO Per 910215 Telcon:On 910215,water Level in Reactor Tank Lower than Normal.Caused by Water Running Out from Under Concrete Block Shield Surrounding Demineralizer Tank.Barrier Dam Constructed Across HX Room ML20003G2551981-04-17017 April 1981 Ro:On 810414,continuous Control Rod Withdrawal Occurred, Resulting in Net Insertion of 80 Cents Reactivity Worth. Caused by Failure of Safety Rod Up Switch.Operations Instructions Bulletin Written Re Possible Recurrence ML19340D3771980-12-19019 December 1980 Ro:On 801212,reactor Operated for Approx 1-h W/ Nonfuctioning Air Pump on Reactor Top Continuous Air Particulate Radiation Monitor.Caused by Loosely Fitting Power Plug &/Or Loose Fuse Holder Connection ML19310A3861980-06-0303 June 1980 Ro:On 800520,while Performing Routine Pulses,One of Five Pulses Produced Peak Power & Measured Fuel Temp Beyond Expectation for 2.55 Dollar Reactivity Insertion. Apparently Caused by 2.75 Dollar Reactivity Insertation 1991-02-25
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20195B6691998-11-10010 November 1998 Safety Evaluation Supporting Amend 17 to License R-106 ML20155E8121998-06-30030 June 1998 Annual Rept of Oregon State Univ Radiation Center & Triga Reactor for 970701-980630 ML20203K5281998-03-0202 March 1998 RO 33732:on 980217,OSTR Failed to Shut Down When Console Manual Scram Button Was Pushed.Caused by Spring Return Switch Failed to Return Completely to Operate Position. Console Key Switch Cleaned & Relubricated ML20236K7251998-02-20020 February 1998 RO 33732:on 980217,manual Scram Failure Occurred.Caused by Spring Return Key Switch Failing to Return Completely to Operate Position & Wiring Change Difference.Removed & Cleaned Switch & Performed Encl 10CFR50.59 Evaluation ML20236K7301998-02-20020 February 1998 Osu Triga Reactor (OSTR) Changes,Tests & Experiments Evaluated Under Provisions of 10CFR50.59 ML20199G0331998-01-28028 January 1998 Safety Evaluation Supporting Amend 16 to License R-106 ML20217A7451997-09-0505 September 1997 Ro:On 970812,questioned Whether OSTR Matl Balance Rept Date of 970728 Was Date Completed or Date Not to Be Exceeded. Caused by Reactor Administrator'S Pressure of Work Load. Completed OSTR Matl Balance Rept ML20236F4761997-06-30030 June 1997 Corrected Table V.B.2 for 1996-1997: Monthly Summary of Gaseous Effluent Releases to Annual Rept of or State Univ Radiation Ctr & Triga Reactor for Period July 1996 - June 1997 ML20212D4531997-06-30030 June 1997 Annual Rept of Oregon State Univ Radiation Ctr & Triga Reactor,960701-970630 ML20138G7651996-12-23023 December 1996 Ro:On 961203,staff Performed Irradiations W/O Following Procedural Controls.On 961216,staff Prepared Shipment of Irradiated Fission Track Samples W/O Following Procedures. Caused by Staff Error.Staff Counseled ML20134E4181996-06-30030 June 1996 Annual Rept of Oregon State Univ Radiation Ctr & Triga Reactor for Period 950701-960630 ML20093M9851995-06-30030 June 1995 Annual Rept of Oregon State Univ Radiation Ctr & Triga Reactor June 1994-June 1995 ML20094B3621995-06-30030 June 1995 Annual Rept of Changes,Tests & Experiments Performed Per 10CFR50.59 for Period Jul 1994 - June 1995 ML20078C1511994-06-30030 June 1994 Annual Rept of or State Univ Radiation Ctr & Triga Reactor, 930701-940630 ML20059C4431993-06-30030 June 1993 Annual Rept of or State Univ Radiation Ctr & Triga Reactor,920701-930630 ML20059H5841993-06-30030 June 1993 Annual Rept of Changes,Tests & Experiments Performed Under 10CFR50.59 for 920701-930630 ML20128G9901993-02-0101 February 1993 Ro:Discovered That Reactor Not Pulsed Semiannually to Compare Fuel Temp Measurements & Peak Power Levels W/Levels of Previous Pulses of Same Reactivity Value.Chart Listing Semiannual Surveillance & Maint Items Encl ML20116J2381992-06-30030 June 1992 Annual Rept of Changes,Tests & Experiments Performed Under Provisions of 10CFR50.59 for Oregon State University Triga Reactor (Ostr) ML20116D0111992-06-30030 June 1992 Annual Rept of Oregon State Univ Radiation Center & Triga Reactor for Jul 1991 - June 1992 ML20079P0261991-11-0404 November 1991 Annual Rept of Changes,Tests & Experiments Performed Under Provisions of 10CFR50.59 for Oregon State Univ Triga Reactor for Jul 1990-June 1991 ML20085L0731991-06-30030 June 1991 Annual Rept of Oregon State Univ Radiation Ctr & Triga Reactor,Jul 1990-June 1991 ML20029A7541991-02-25025 February 1991 Followup RO Per 910215 Telcon:On 910215,water Level in Reactor Tank Lower than Normal.Caused by Water Running Out from Under Concrete Block Shield Surrounding Demineralizer Tank.Barrier Dam Constructed Across HX Room ML20062H7911990-11-27027 November 1990 Annual Rept of Changes,Tests & Experiments for Jul 1989 - June 1990 Under 10CFR50.59 ML20058F2241990-06-30030 June 1990 Annual Rept of Oregon State Univ Radiation Ctr & Triga Reactor, for Jul 1989 - June 1990 ML19327C0421989-10-31031 October 1989 Amend 5 to, SAR for Oregon State Triga Reactor (Ostr). ML19325C7001989-10-0202 October 1989 Annual Rept of Changes,Tests & Experiments Performed Under Provisions of 10CFR50.59 for Triga Reactor,For Jul 1988 - June 1989 ML20246D1071989-08-15015 August 1989 Safety Evaluation Supporting Amend 10 to License R-106 ML20012A0901989-06-30030 June 1989 Annual Rept of Oregon State Univ Radiation Ctr & Triga Reactor Jul 1988 - June 1989. ML20005D6031989-06-30030 June 1989 Annual Rept of Oregon State Univ Radiation Ctr & Triga Reactor Jul 1988 - June 1989. ML20245B3461989-04-17017 April 1989 Ro:On 890406,during Routine Pulsing Operation,Blue Pen Which Records Linear & Peak Power Went off-scale.Caused by Omission of 100-ohm Resistor Normally Placed Across Console Terminals.Operators Reprimanded & Procedures Changed ML20204G1161988-09-30030 September 1988 Annual Rept of Changes,Tests & Experiments for Oregon State Univ Triga Reactor for Jul 1987 - June 1988 ML20235D0601988-06-30030 June 1988 Annual Rept of Oregon State Univ Radiation Ctr & Triga Reactor Jul 1987 - June 1988 ML20154J2511988-05-17017 May 1988 RO Re Jan 1988 Event in Which Procedures Consistent W/New NRC Policy Used Rather than Exact Written Procedures.Reactor Operations Committee Meeting on 880513 Preceeded Info for Review.Staff Instructed to Use Exact Procedures ML20150C8761988-03-15015 March 1988 Requalification Program for Licensed Operators of Oregon State Univ Triga Reactor (Ostr) ML20149M7101988-02-11011 February 1988 Safety Evaluation Supporting Amend 9 to License R-106 ML20235R1021987-09-28028 September 1987 Annual Rept of Changes,Tests & Experiments Performed Under Provisions of 10CFR50.59 for Oregon State Univ Triga Reactor (Ostr), for Jul 1986 - June 1987 ML20235E7421987-06-30030 June 1987 Oregon State Univ Triga Reactor Annual Rept ML20197B2941986-10-0303 October 1986 Annual Rept of Changes,Tests & Experiments for Jul 1985 - June 1986,per 10CFR50.59 ML20138J9471985-10-0404 October 1985 Changes to Facility,To Facility Procedures & to Reactor Experiments for Jul 1984 - June 1985 ML20133N3991985-06-30030 June 1985 Oregon State Univ Triga Reactor Annual Rept, for Reporting Period Jul 1984 - June 1985 ML20080L2971983-09-19019 September 1983 Annual Rept of Changes,Tests & Experiments Made Under 10CFR50.59 for Triga Reactor,Jul 1982 - June 1983 ML20071N4021983-05-25025 May 1983 Ro:On 830523,discovered Insp of Transient Control Rod Not Conducted Since 810317.Caused by Misinterpretation of Tech Specs.Surveillance Time Intervals Will Be Modified Per Ansi/Ans 15.1-1982 Guidelines ML20003G2551981-04-17017 April 1981 Ro:On 810414,continuous Control Rod Withdrawal Occurred, Resulting in Net Insertion of 80 Cents Reactivity Worth. Caused by Failure of Safety Rod Up Switch.Operations Instructions Bulletin Written Re Possible Recurrence ML19340D3771980-12-19019 December 1980 Ro:On 801212,reactor Operated for Approx 1-h W/ Nonfuctioning Air Pump on Reactor Top Continuous Air Particulate Radiation Monitor.Caused by Loosely Fitting Power Plug &/Or Loose Fuse Holder Connection ML19337A7821980-08-31031 August 1980 or State Univ Triga Reactor Annual Rept for Jul 1979-June 1980 ML19310A3861980-06-0303 June 1980 Ro:On 800520,while Performing Routine Pulses,One of Five Pulses Produced Peak Power & Measured Fuel Temp Beyond Expectation for 2.55 Dollar Reactivity Insertion. Apparently Caused by 2.75 Dollar Reactivity Insertation ML20125C5651979-12-18018 December 1979 Safety Evaluation Supporting Amend 4 to License R-106 ML19290A0801979-06-30030 June 1979 Annual Operating Rept for Jul 1978-June 1979 1998-06-30
[Table view] |
Text
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Radiation Center We".
University Corvallis, Oregon 97331 : sos) 754 234:
w J June 3,1980 U.S. Nuclear Regulatory Commission Region V Office of Inspection & Enforcement 1990 N California Blvd.
Walnut Creek Plaza, Suite 202 Walnut Creek, CA 94596
Reference:
Docket No. 50-243, License No. R-106 Gentlemen:
On May 20, 1980 we apparently inserted approximately $2.75 in a reactivity pulse, exceeding the limit of $2.55 in Part 3.3 of our Technical Specifications. This was reported to your office by telephone on May 21, 1980, as required by Part 6.7a of our Technical Specifications.
This written report, as required by Part 6.7b of our Technical Specifica-tions, provides more details of the incident and the corrective action
., we have taken to prevent, hopefully, this incident from happening again.
Incident On May 20, 1980 we were performing routine pulses for an experimentor.
All of the pulses involved reactivity insertions of $2.55, inserted by means of our transient rod. The first three pulses that day produced peak powers which varied from 3050 MW to 3200 MW, and measured fuel temperatures which varied from 397*C to 405'C. These were all within the normal range of variability we have observed for a $2.55 insertion.
The fourth pulse produced a peak power of 3900 MW and a measured fuel temperature of 440*C. These values were higher than any we have encountered for a $2.55 insertion. A fifth pulse was then performed to see if our pulsing instrumentation and circuitry were working properly.
This resulted in a 3040 MW pulse with a temperature of 390'C, again for a $2.55 insertion--well within the normally expected range.
The conclusion seemed to be that the fourth pulse that day was produced by a reactivity insertion greater than $2.55. If the reactivity insertion had been about $2.75 rather than $2.55, we would expect a peak power and a measured fuel temperature corresponding to the observed values.
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Oregon State University is an Allitmative Action / Equal Opportunity Employer 80 06110/33 J . . _ _ _ . _ _ . . _ _ _ . . _ _
U.S. flRC Page Two June 3, 1980 Background Information and Safety Implications 4 Having concluded that the fourth pulse on May 20, 1980 was probably genuine and that it came about from a reactivity insertion of about-$2.75, we then attempted to ascertain how this reactivity could have been introduced. The transient rod has a mechanical stop which limits the pulse reactivity insertion of this rod to $2.55. This stop was in place and functioning properly.
Thus, at most we could have gotten $2.55 from the transient rod.
The additional $0.20 must have come from one of the other rods, and' the regulating (reg) rod was the most logical candidate since the servo system moves this rod automatically in the AUTOMATIC or SQUARE-WAVE mode.
By carefully examining the switching sequence for pulsing, we discovered the following sequence which could have given an extra $0.20 of reactivity to a pulse:
- 1. Bring reactor critical at a low power in the AUTOMATIC mode.
- 2. Switch the mode switch to SQUARE-WAVE (one position beyond STEADY-STATE). The reactor is now operating as in the AUTOMATIC mode with the servo system controlling the reg rod position.
- 3. Switch the range switch to 1 MW, in preparation for the pulse.
! The servo system now starts driving out the reg rod in an attempt to bring the reactor up to the new, higher power level that is demanded.
- 4. ' Switch the mode switch to PULSE (HIGH or LOW). The reg rod now i stops driving out. It -is further out, however, than its critical -
position of step #1, and some positive reactivity has been added to the previously critical reactor. The reactor is now on a positive period.
- 5. Fire the transient rod. The reactivity value of the transient rod is now added to the positive reactivity from the reg rod
- withdrawal.
If the sequence had been followed, the reg rod would have only i .had to move out about 30 units to add an additional $0.20 of reactivity, and it would have taken .it less than 2 seconds to move those 30 units.
We feel this is' a plausible explanation of how the $2.75 reac.tfvity insertion might have occurred. The reactor operator on the console at .
the time this incident occurred agreed that this switching error could 1 ~certainly have happened. He could not verify that it did happen, only 3 tha: -it was a possibility and an explanation for the occurrence.
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U.S. NRC Page Three June 3, 1980 f
1 An operator performing a pulse using the sequence just described is not following the proper sequence in our Oregon State TRIGA Reactor j Operating Procedures (OSTROP), Chapter 4 (Reactor Operation Procedures)..
i This approved procedure is identical to the sequence just described
- except that Step #2 says to switch 'the mode switch to STEADY-STATE, not
, SQUARE-WAVE. If the proper procedure is followed, the reg rod will f not drive out and the only reactivity inserted will be from the transient rod. Since the STEADY-STATE and SQUARE-WAVE positions are next to
~
each other on the mode switch, it is certainly possible that an error of this type could be made.
Such a switching error is apparently quite rare, however. We have performed 2,172 pulses in the past 13 years, and this is the first time we have observed that an error of this type might have happened. We are also personally not aware of such an incident happening at any other TRIGA reactor facility.
E The measured fuel temperature that occurred during this apparent reactivity insertion of $2.75 was 440*C, well below the 510*C temperature which is our Limiting Safety System Setting (LSSS) for
' fuel temperature. Hence, the maximum fuel temperature was also well
- below the fuel temperature safety limit.
To examine the potential safety implications of such an incident,
- one can postulate the worst situation
- the reg rod drives out entirely, then the transient rod is fired. The reg rod is normally somewhat more than half out when the reactor is brought to a critical condition-at low power prior to a pulse. For our reactor, the reg rod has a total worth of $2.62, and in the critical configuration prior to
- pulsing, about $1.18 of worth remains in the rod. Theoretically, then, one could add about $1.18 of positive reactivity ~from the reg rod in addition to the $2.55 from thn transient rod, making the total reactivity insertion about $3.73. This is not physically possible, however.
4 Our reactor has an interlock set at a power-Tevel of 1 kW; if the-reactor power exceeds 1 kW, this interlock prevents firing of the transient rod. Thus, the maximum reactivity that can be added from the reg rod during such an incident is that amount that can be added before the power -level reaches 1 kW and trips the interlock. - Our 4
analysis has shown that if the reg rod drives out at its maximum speed, it will take about 6.3-6.4 seconds for the reactor power to increase I to l' kW. In this time interval, the reg rod has driven out about 115 units and the corresponding reactivity insertion is about $0.63.
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U.S. NRC Page Four June 3, 1980 Thus, the maximum possible reactivity insertion that we could experience during such an incident is about $3.18 ($0.63 + $2.55).
The measured fuel temperature expected for a $3.18 insertion is about 550*C. This temperature is about 40 C above our LSSS temperature of 510 C, but the maximum fuel temperature would still be 150-160*C below the fuel temperature safety limit. Thus, no fuel melting or fuel cladding failures would be expected.
Corrective Action The Reactor Operations Committee (ROC) met on May 23, 1980 to discuss and review this incident. The ROC concurred with the reactor staff findings that safety of the reactor and integrity of the fuel had not been compromised. The ROC also agreed that had the " worst case" scenario described above happened, the fuel te.nperature safety limit would not have been exceeded or even approached very closely.
The ROC did express concern that such an incident could occur, however. They agreed that the existing OSTROP procedures for pulsing, if they are followed, should prevent such an incident. The ROC voted to amend these procedures, however, to include an additional step just prior to firing the transient rod for a pulse. This additional step calls for the operator to verify that the reg rod has not moved from its critical configuration. This step should provide a final check on the amount of reactivity to be added and verify that the operator has performed the switching sequence in the proper order. This change had been implemented on an interim basis by the operations staff on May 21, 1980. Upon approval by the R0C, it immediately became a part of the OSTROP pulsing procedures.
The ROC felt that no other corrective action was necessary or justified at this time.
If you have any questions or desire any further information about this incident, please contact us.
Sincerely, b
J hn C. Rin le sistant Reactor Administrator JCR/rk cc: USNRC Office of Inspection & Enforcement, Mshington, D.C.
USNRC Document Management Branch, Washington, D.C.
Oregon Department of Energy C.H. khng, Reactor Administrator. OSU A.G. Johnson, Senior Health physicist, OSU T.V. Anderson, Reactor Supervisor, OSU