ML19309A112
| ML19309A112 | |
| Person / Time | |
|---|---|
| Site: | Crane |
| Issue date: | 03/14/1980 |
| From: | Grier B NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| To: | Arnold R METROPOLITAN EDISON CO. |
| References | |
| NUDOCS 8003260037 | |
| Download: ML19309A112 (1) | |
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UNITED STATES
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KING oF PRUSSIA, PENNSYLVANIA 19406 Docket Nos. 50-289 50-320 Metropolitan Edison Company ATTN:
Mr. R. C. Arnold Senior Vice President 100 Interpace Parkway Parsippany, New Jersey 07054 Gentlemen:
The enclosed IE Circular No. 80-04, " Securing of Threaded Locking Devices on Safety-Related Equipment," is forwarded to you for information.
No written response is required. If you desire additional information regarding this matter, please contact this office.
Sincerely, e
f W
Boyce H. Grier
- Director
Enclosures:
1.
IE Cirtular No. 80-04 2.
List or Recently Issued IE Circulars CONTACT:
L E. Tripp (315-337-5282) cc w/encls.
J. G. Herbcin, Vice President Nuclear Operations E. G. Wallage, Licensing Manager R. J. Tool.s Manager, TMI-1 W. E. Potts Radiological Controls Manager, TMI-1 R. W. Heward, Radiological Controls Manager, TMI-2 J. J. Colit;t, Plant Engineering Manager, TMI-1 J. J. Barton, Manager Site Operations, TMI-2 B. Elam, Plant Engineering Manager, TMI-2 L. W. Harding, Supervisor of Licensing R. F. Wilson, Director, TMI-2 I. R. Finfrock, Jr.
I R. W. Conrad J. B. Lieberman, Esquire G. F. Trowbridge, Esquire Ms. Mary V. Southard, Chairperson, Citizens for a Safe Environment 8003260~037 l
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ENCLOSURE 1 SSINS NO. 6830 Accession No.:
UNITED STATES 7912190662 NUCLEAR REGULATORY COMMISSION
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[7)jy OFFICE OF INSPECTION AND ENFORCEMENT WASHINGTON, D.C.
20555 J
IE Circular No. 80-04 Date:
March 14, 1980 Page 1 of 3 l
SECURING OF THREADED LOCKING DEVICES ON SAFETY-RELATED EQUIPMENT Description of Circumstances:
In recent months, several licensee event reports have been submitted that address the inoperability of safety-related equipment caused by loosened threaded locking devices.
Some of the events are listed below:
I.
MAIN STEAM CHECK VALVE HEX NUT LOCKING DEVICES, TURKEY POINT NO. 3 REPORTABLE OCCURRENCE 250-79-31 (Oct. 22, 1979)
During a planned outage of Turkey Point Unit No. 3 on October 7, 1979, a two-inch internal diameter hex nut was discovered in the internals of a steam supply valve for a moisture separator reheater.
Investigation revealed that the nut was missing from the disc stud of the 3A main steam check valve.
The disc and disc stud were in the proper position and the valve was fully operable.
The 3B and 3C main steam check valves were inspected and the disc stud, nut and locking washer were in place although some distress was noted on the 3C locking washer in that the tack welds on the locking pin had separated.
The licensee installed an improved locking device on the disc stud on each of the three main steam check valves.
The locking device consists of a tab washer that is prevented from' rotating by a pin and by fingers that extended on either side of the valve arm; the tabs are bent up against two faces of the hex nut.
The main steam isolation valves (MSIV) have the same type of hex nut locking device.
The valves are Schutte and Koerting SK Type 828.
II.
SLIPPAGE AND MISALIGNMENT OF VALVE LINKAGES, DAVIS-BESSE LICENSEE EVENT REPORT NOS78-101 (Nov. 1, 1978),78-126 (Jan. 26, 1979),79-068 (July 19, 1979), and 79-098 (Oct. 30, 1979)
These reports involve the inoperability of two service water system valves and one component cooling water system valve.
The valves were declared inoperable because the nut on the actuator linkage was either missing or had loosened to the point where there was slippage and misalign-ment of the valve linkage.
These valves were provided by Hammel-Dahl.
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The supplier has provided the licensee with an addendum to the instruction manual that defines the torque requirements for the cap screw that is used to retain the actuator link arm to the valve disc arm.
IE Circular No. 80-04 Date:
March 14, ?980 Page 2 of 3 III. ECCS SUBSYSTEM INOPERABLE - NO. 12 SAFETY INJECTION PUMP IMPELLER LCCKNUTS LOOSE, SALEM NO. 1 LICENSEE EVENT REPORT NO. 79-68 (Dec. 20, 1979).
The AC supply breaker tripped when No. 12 Safety Injection (SI) Pump was started, to fill the accumulators on October 18, 1979.
When the rotor could not be turned by hand, the upper casing was removed for an inspec-tion of the pump internals.
The radial and thrust locknuts were found loosened to the extent that they could be removed by hand.
The impeller spacer sleeves were worn and the impeller shaft was slightly bent.
The pump was reworked, tested and returned to service on November 2, 1979.
The locknuts on the three other Unit 1 and Unit 2 Safety Injection (SI)
Pumps were inspected and two pump impeller locknuts were found loose, and one pump impeller locknut was found secured with setscrews that had been installed by mistake at the manufacturing facility and the impeller was sent back to the manufacturer for rework.
The locknuts on all of the SI pumps were secured using Locktite compound per Public Service Engineering Department recommendation and the pump manufacturer's concurrence.
The pumps are horizontal, centrifugal, ten stage units manufactured by Pacific Pumps, Inc.
IV.
TARGET ROCK MOTOR OPERATED GLOBE VALVES - BUSHING NOT STAKED, ANO NO. 2 LICENSEE EVENT REPORT 79-93 (FEB. 14, 1980)
While investigating the failure of a High Pressure Safety Injection (HPSI) header shut off valve at Arkansas Nuclear One, Unit 2, the threaded bushing was found loose.
The bushing was not staked or otherwise secured to prevent movement.
This bushing is part of the mechanism which converts the valve stem rotation to linear travel of the disk.
The full open limit switch is gear driven by the valve operator and movement of the bushing can alter the relationship between stem rotation and linear travel such that valve travel in the open direction may be terminated prematurely by the limit switch.
The HPSI header shut-off valves at ANO-2 are Target Rock 2-inch 1500# ANSI Motor Operated Globe Valves.
Arkansas Power & Light found that a similar problem exists with the Low Pressure Safety Injection (LPSI) header shut off valves which are Target Rock 6-inch 1500# ANSI Motor Operated Globe Valves.
Target Rock has provided Arkansas Power & Light Company with a procedure for staking the bushing nuts.
V.
OTHER EVENTS Loose locking devices were also identified in one of the I & E Bulletins and two of the I & E Circulars issued in 1979:
IE Circular 79-04 Loose Locking Nut on Limitorque Valve Operators, IE Circular 79-19 Loose Locking Devices on Ingersoll-Rand Pumps, IE Bulletin 79-15 Deep Draft Pumps.
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IE Circular No. 80-04 Date:
March 14, 1980 Page 3 of 3 Recommended Action for Licensees Consideration:
It is recommended that licensees of operating power reactors and holders of construction permits review the specific items presented in the " Description of Circumstances" for applicability at their facilities and review their installation and maintenance procedures to determine that whether securing of locking devices has been addressed in these procedures.
It is further recommended that installation and maintenance procedures for all safety-related components be reviewed to be sure the securing of locking devices is adequately covered.
No written response to this Circul
's required.
If you require additional information regarding these mattert, contact the Director of the appropriate NRC Regional Office.
l
ENCLOSURE 2 IE Circular No. 80-04 Date:
March 14, 1980 Page 1 of 1 RECENTLY ISSUED IE CIRCULARS Circular Subject First Date Issued To No.
of Issue 79-18 Proper Installation of 9/10/79 All Power Reactor Target Rock Safety-L.icensees with an Relief Valves Operating License (OL) or Construction Permit (CP) 79-19 Loose Locking Devices 9/13/79 All Power Reactor Licensees on Ingersoll-Rand Pumps with an OL or CP 79-20 Failure of GTE Sylvania 9/24/79 All Power Reactor Licensees Relay, Type PM Bulletin with an OL or CP 7305, Catalog SU12-11-AC with a 120V AC Coil 79-21 Prevention of Unplanned 10/19/79 All Power Reactor Licensees Releases of Radioactivity with an OL or CP 79-22 Stroke Times for Power 11/16/79 All Power Reactor Licensees Operated Relief Valves with an OL or CP 79-23 Motor Starters and Con-11/26/79 All Power Reactor Licensees tactors Failed to Op-with an OL or CP erate 79-24 Proper Installation and 11/26/79 All Power Reactor Calibration of Core Facilities with an OL or Spray Pipe Break CP Detection Equipment on BWRs 80-01 Service Advice for GE 1/17/80 All Power Reactor Faci-Induction Disc Relays lities with an OL or CP 80-02 Nuclear Power Plant 2/1/80 All Power and Research Staff Work Hours Reactors with an OL or CP 80-03 Protection from Toxic 3/6/80 All Power Reactor Facil-Gas Hazards ities with an OL i
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