ML19308D274

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RO-77-29:on 770416,cooldown Rate in Excess of Tech Spec Limit Occurred During Reactor Shutdown Remote from from Control Ctr.Caused by Pressure Transmitter Out of Calibr. Transmitter Calibr & Trip Feed Pump Procedure Revised
ML19308D274
Person / Time
Site: Crystal River Duke Energy icon.png
Issue date: 04/21/1977
From: Stewart W
FLORIDA POWER CORP.
To:
Shared Package
ML19308D270 List:
References
NUDOCS 8002270721
Download: ML19308D274 (3)


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@l During the performance of Reactor shutdown remote from the Control Center, an excessive l

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[o] l The cause of this occurrence was,the overfilling of the OTSG due to out-of-calibration l,

1 09 00 Qjl pressure transmitter not causing start-up feedwater' valves WV-39 and 40 to fully close.

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SUPPLENENTARY INFORMATION I

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Report No.

50-302/77-29

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2.

Facility:

Crystal River Unit #3 3.

Report Date:

21 April 1977 4.

Occurrence Date:

16 April 1977 i

l S.

Identification of occurrence:

During the process of performing Reactor shutdown remote from the Con-

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trol Center, an excessive cooldown rate contrary to Technical Specifi-cation 3.4.9.1 was experienced in that the cooldown rate was approximately 101 F. in 20 minutes. This was primarily caused by overfilling of the i

steam generators contrary to Technical Specification,3.4.5 to a level above 360 inches.

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6.

Conditions Prior to Occurrence:

Plant was in Mode 3 during test of shutdown from outside the Control Room.

Reactor had tripped.

J 7.

Description of Occurrence:

At approximately 0815, during remote shutdown test, overfilling of the OTSG's past the high level limits was experienced.

It was determined that start-up feedwater valves FWV-39 and 40 were not fully seated causing j

the overfill. An attempt wat made to throttle the FWP discharge to no avail. The steam generator drains and atmospheric dump valves were opened i

and excessive cooldown rate was experienced.

Reactor coolant temperature i

. decreased 1010 F. in 20 minutes.

l 8.

Designation of Apparent Cause of Occurrence:

The cause of this occurrence was the overfilling of the OTSG due to out-of-calibration pressure transmitter not causing start-up feedwater valves' FWV-39 and 40 to fully close.

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9.

Analysis of Occurrence:

I At all times, the Reactor coolant temperature / pressure parameters remained within the region of acceptable operation set forth in Technical Specifica-tion 3.4.9.1, Figure 3.4.3.

Prior to start-up and power operation, an engineering evaluation was performed to determine the effects of the cool-down on the fracture toughness properties of the R coolant system.

It x

was determined that the RCS remained acceptable for continued operation.

We have been informed by Babcock & Wilcox that the cooldown transient

. which occurred on 2 March 1977 (LER-77-20) "was found to cause no derroga-tory effects". That transient was more severe than the one occurring on 16 April 1977. Therefore, it is determined that this transient did not endanger the safety of the plant.'

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.Sup'plementary Information (Cont'd.)

10.

Corrective Action:

i The pressure transmitter has been recalibrated to assure closure of the start-up feedwater valves.

In addition, the test and operating procedures have been revised to incorporate tripping of the main 4

feedwater pump at the appropriate time to prevent overfilling of' the steam generators.

^

11.

Failure Data:

This is the second occurrence of cooldown in excess of 100 F. in one hour (LER-77-20).

It is the first occurrence from these causes.

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