05000348/LER-1980-008-03, /03L-0:on 800203,during Hydraulic Snubber Visual Surveillance Test,Component Cooling Water Snubber CW4-R121 Was Declared Inoperable Due to Disconnection of Reservoir Line.Caused by Personnel Error.Reservoir Line Reconnected

From kanterella
(Redirected from ML19296D142)
Jump to navigation Jump to search
/03L-0:on 800203,during Hydraulic Snubber Visual Surveillance Test,Component Cooling Water Snubber CW4-R121 Was Declared Inoperable Due to Disconnection of Reservoir Line.Caused by Personnel Error.Reservoir Line Reconnected
ML19296D142
Person / Time
Site: Farley Southern Nuclear icon.png
Issue date: 02/25/1980
From: Hairston W
ALABAMA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19296D139 List:
References
LER-80-008-03L, LER-80-8-3L, NUDOCS 8002290401
Download: ML19296D142 (2)


LER-1980-008, /03L-0:on 800203,during Hydraulic Snubber Visual Surveillance Test,Component Cooling Water Snubber CW4-R121 Was Declared Inoperable Due to Disconnection of Reservoir Line.Caused by Personnel Error.Reservoir Line Reconnected
Event date:
Report date:
3481980008R03 - NRC Website

text

,~ ' ".,

f lCEftSEE EVENT REPORT ccNTnot stock: l l

l l

l I

s@

l IPteAss earnT OR Tves Att atou RED INFORilATIO.*4 e

lei'l.IA1T !J!MlFl1lhl010l-i0 IO l0 !OI01-lOIOl@[4l!!1[1IIl@

I l@

3

<h 9

LICEr.5ILE CODE 14

S UCENn r..a!.tuire 25 h

t h M T(PL JJ 53 C,1. i ad c-.-

Fo m ' l.,3 LoAj@loISloioio13I4 18 l@i o! 21 of 31 si oGI of 2121 si si ol@

2 4

couff a-.,5R

.w c,

E m roArt ra REPcRToATE o

EVENT DESCRIPTION AND PROB 3LE CONSE%ENCES h l o ;; J [ At 0045 on 2-3-80, during the performance of surveillance test FNP-1-STP-610.2 (Hydrau}ic

a;3g ; Snubber Visual Test), component cooling water snubber CW4-R121 was declared inoperableg g, l,ygdue to the reservoir line being disconnected. Tech. Spec. 3.7.9.1, in part, requires g g., g s j g snubber CW4-R121 to be operable.

Tech. Spec. 3.7.9.1 action statement requirements y

Iwere met.

Health and safety of the public were not affected.

9 e+-

- of-l

[

ana 1 1

7 9 9 80 SYSTEV

CAUSE

CAA."SE COP.tp.

vatvg CCDE CODE SL3OO3E CO*?PoNENT CDo6 e ar"M SUSCCCE eni l x i x lO LA_l@ ic l@ I S i u i r i o t a l T IS W@ LE @

7 s

9 10 11 Fi 13 sa 3h 2.,

SEovENTI AL CCCUR4fNCt PEFORT REVISION Lf EVENTytspr

  1. =?.70RT wo.

Cocf TYPE N O.

@,aj,'R Ro18 lo i 1I I o I o f 81 lel Ioi3I it I l-1 Ioi jj" 28 22 34

.A-25 21 23 7.3 X

33 32 ACTIC4 FUTURS EFFTCT 3= UTO 7?"J ATT ACD */? NT

";P90-4 f' RIVE CO*>*.

CCAt*CNENT TAKEN ACTION ON P*.-NT V t Tra O3 MOURS SU99JTT!O Foq u W5.

SUP*U ta WaNUKACTURER LxjgiH ig i zig iz I@

j o ! 04 I

llj@

LNjg

{Ajg l Gl 2 ( 5 l 5 lg 33 J,

35

.o 40 44 42 41 as 67 CAUSE DESCRIPTION ANC CORRECTIVE ACTIC?:S h Q lSee Attachment.

[

FTO 1 1

1

- l s

_Ll.1.? I I I

FG'I'l 1 I

7 e s sa STA

% PoveER oTHER 5raTUS 15 V R DiSCCVf*v 0ESCRIPTICFe d [0,,jh l0I010lh!

NA La,J@l Performance of surveillhnce test I

7 8

12 13 44 db 44 80 M -luAsto or muAstJ @ (2.,j h I A.,Cu m o,,c m m @ l ucu,c,, o,,,Eu,sf @

m

.,,J NA l

NA l

n==Nn E Posses oEsCR,.7,o,@

^

l

~Uo.ER Tm G'F'1 1 o 1 o I o f@l z l@f NA co,scNNE L iN2u'4 Es oEsCRmioN@

=wa E.

NA [MnifDII) kl[DM(,3,N $

ITT-il I o I o I o l@l J

LOSSOFC84O AGE TO FACJLaTY Q TYPE OESCRt* TION

%./

M ((z_,,@.}

NA l

7 km "J

iJ 30 M te(3fy h ]$ttc% LESCRtPT8o~ "'

8 0 02 2904M wt NQ!

NA l {}((11[l l[tIl}

a

= s m

i,4 s,

as -.

(205) 899-5156 78AME OF PREPARER Phot':!:

ATTAC1 DENT LICENSEE EVENT REPORT LER 80-008/03L-0 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS The reservoir line was not reconrected when the snubber was

~

reinstalled following functional testing in the summer of 1979.

(While the snubber was removed for functional testing, the reservoir outlet was capped.) Due to the reservoir line/ snubber configuration (reservoir contained adequate fluid and reservoir line was placed next to reservoir connector such that it appeared to be connected), confirmation of

~~

.__ operability by visual inspection was erroneously made following the testing.

Personnel involved in snubber inspections have been reinstructed. The snubber was purged and vented, the line to the reservoir reconnected and the snubber was declared operable following functional testing at 1035 on 2-5-80.

O eme m.

.-e-.~

wee ee,