ML19291B985
| ML19291B985 | |
| Person / Time | |
|---|---|
| Site: | Comanche Peak |
| Issue date: | 11/30/1979 |
| From: | Seyfrit K NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV) |
| To: | Gary R TEXAS UTILITIES ELECTRIC CO. (TU ELECTRIC) |
| References | |
| NUDOCS 7912190193 | |
| Download: ML19291B985 (1) | |
Text
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7 -.L c ana UNITED STATES
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G11 RYAN PL AZA DRIVE SUITE 10C0 U
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AHLINGTON, TEX AS 76012 g
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November 30, 1979 4.,,
In Reply Refer To:
RIV Docket Nos.
50-445/IE Bulletin No. 79-27 50-446/IE Bulletin No. 79-27 Texas Utilities Generating Company ATTN:
Mr. R. J. Gary, Executive Vice President and General Manager 2001 Bryan Tower Dallas, Texas 75201 Gentlemen:
The enclosed IE Bulletin No. 72-27, is forwarded to you for information.
these concerns will be Although no written response is required at this time, addressed as part of the licensing process for your plant.
If you desire additional information regarding this matter, please contact this office.
Sincerely,
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Karl V. Seyfrit
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Director
Enclosures:
1.
List of Recently Issued IE Bulletin i790'512 ro121oo /93
... _ ~........
UNITED STATES SSINS No.: 6820 NUCLEAR REGULATORY COMMISSION Accession No.:
OFFICE OF INSPECTION MD ENFORCEMENT 7910250499 WASHINGTON, D.C.
20555 IE Bulletin No. 79-27 Date: November 30, 1979 Page 1 of 3 LOSS OF NON-CLASS 1-E INSTRUMENTATION AND CONTROL POWER SYSTEM BUS DURING OPERATION Description of Circumstances:
On November 10, 1979, an event occurred at the Oconee Power Station, Unit 3, that resulted in loss of power to a non-class 1-E 120 Vac single phase power panel that supplied power to the Integrated Control System (ICS) and the Non-Nuclear Instrumentation (NNI) System. This loss of power resulted in control system malfunctions and significant loss of information to the control room operator.
Specifically, at 3: 16 p.m., with Unit 3 at 100 percent power, the main condensate pumps tripped, apparently as a result of a technician performing maintenance on the hotwell level control system. This led to reduced feedwater flow to the steam generators, which resulted in a reactor trip due to high coolant syste.,
pressure and simultaneous turbine trip at 3:16:57 p.m.
At 3:17:15 p.m., the non-class 1-E inverter power supply feeding all power to the integrated control system (which provides proper coordination of the reactor, steam generator feedwater control, and turbine) and to one NNI channel tripped and failed to automatically transfer its loads from the DC power source to the regulated AC power source.
The inverter tripped due to blown fuses.
Loss of power to the NNI rendered control room indicators and recorders for the reactor coolant system (except for one wide-range RCS pressure recorder) and most of the secondary plant systems inoperable, causing loss of indication for systems used for decay heat removal and water addition to the reactor vessel and steam generators. Upon loss of power, all valves controlled by the ICS assumed their respective failure positions. The loss of power existed for approximately three minutes, until an operator could reach the equipment room and manually switch the inverter to the regulated AC source.
The above event was discussed in IE Information Notice No. 79-29, issued November 16, 1979.
NUREG 0600 " Investigation into the March 28, 1979 TMI Accident" also discusses TMI LER 78-021-03L whereby the RCS de ressurized and Safet In~ection occurred on loss of a vital bus due to invert Actions to Be Taken by Licensees DUPLICATE DOCUMENT For all power reactor facilities witt Entire document previously completion of cgnstruction (North Anr entered into system under:
Sequoyah, and Zimmer):
ANO No. of pa9es:
090 M3