05000302/LER-1979-012-03, /03L-0 on 790214:during Safeguards Test, RB-3GP-2 Light Did Not Illuminate.Caused by Burr on Relay Shaft.Relay Cleaned & Burr Removed

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/03L-0 on 790214:during Safeguards Test, RB-3GP-2 Light Did Not Illuminate.Caused by Burr on Relay Shaft.Relay Cleaned & Burr Removed
ML19282B167
Person / Time
Site: Crystal River Duke Energy icon.png
Issue date: 02/27/1979
From: Stewart W
FLORIDA POWER CORP.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19282B166 List:
References
LER-79-012-03L, LER-79-12-3L, NUDOCS 7903090187
Download: ML19282B167 (2)


LER-1979-012, /03L-0 on 790214:during Safeguards Test, RB-3GP-2 Light Did Not Illuminate.Caused by Burr on Relay Shaft.Relay Cleaned & Burr Removed
Event date:
Report date:
3021979012R03 - NRC Website

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- es' 7903090137 EE ATTACHED SUPPLEMENTARY INFO. fATION SHEET)

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SUPPLEMENTARY INFORMATION Report No.:

50-302/79-012/03L-0 Facility:

Crystal River Unit #3 Report Date:

27 February 1979 Occurrence Date: 14 February 1979 Identification of Occurrence:

One inoperable engineered safety feature actuation system instrument channel contrary to Technical Specification 3.3.2.1.

Conditions Prior to Occurrence:

Mode 1 power operation (99%)

Description of Occurrence:

At 1000 while performing engineered safeguards Monthly Functional Test, SP-130, the Reactor Building channel three group 2 (RB-3-GP-2) indicating light did not illuminate.

Investigation revealed that relay 6322E/L was " hanging up".

Entered action statement 9.

Failure of this relay would have prevented channel 3 actuation of "D" Reactor Coolant Pump cooling water valves SWV-81 and SWV-85 in a 2 out of 3 coincidence network.

Designation ' Apparent Cause:

The esase of this event was found to be a burr on the relay shaf t (relay 63Z2E/L)

Analysis of Occurrence:

There was no hazard to plant or general public as the affected channel was placed in the tripped condition.

The two remaining channels were operable.

Corrective Action

The relay was cleaned, the burr removed.

Operability was restored after satisfactory completion of applicable section of SP-130.

That section of SP-130, affecting relay 63Z2E/L will be accomplished as a special one time test prior to the next scheduled system test.

This test is to assure component integrity and reliability as a result of corrective actions.

Failure Data:

12 previous occurrences reported under this Technical Specification.

Fourth. occurrence concerning ES cabinet relays.

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