ML19276G906

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LER 79-024/03L-0 on 790731:safety Injection Pump Test Sp 1088 Was Not Completed During Hot Shutdown as Required. Caused by Personnel Error
ML19276G906
Person / Time
Site: Prairie Island Xcel Energy icon.png
Issue date: 08/24/1979
From: Hunstad A
NORTHERN STATES POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML19276G903 List:
References
LER-79-024-03L, LER-79-24-3L, NUDOCS 7908280591
Download: ML19276G906 (1)


Text

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[5TT] l During a review of plant status on August 2nd at hot shutdown, it was discovered that o 3 [SP 1088, Safety Injection Pumps Test, had not been done prior to leaving cold shutdown; o 4 l on July 31st. The test was done on August 2nd and was acceptable, so there is reason j _ _ , ,

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