LER-1979-015, /01T-0 on 790327:during Inservice Insp,Linear Svc Indications Found on ECCS Line to Loops 1 & 2 Cold Legs & Loop 3 Hot Leg.Caused During Handling.Two Corrective Actions Proposed:Cut Out & Replace or Grind Out |
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inspection on L. nit 1 of FNP, linear surface [5'[T} Lon 3-17-79 uhile performing inservice k'hile performing the I found on the 2" ECCS line to Loop 1 cold leg.
Q W [ indications were the 2" ECCS lines to Loop 21 found on idi) Lexpanded examination additional indications were lines are stainless steel 304 schedule 160.
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ALABAMA POWER COMPANY JOSEPil M. FARLEY NUCLEAR PLANT DOCKET No. 50-348 ATTACllMENT TO LER 79-015/0lT-0 Facility: Joseph M. Farley Unit 1 Report Date:
4/10/79 Event Date:
3/27/79 Identification of Event On 3/27/79 while performing inservice inspection on Unit 1 of FNP, linear surface indications were found on the 2" ECCS line to Loop 1 cold leg.
Subsecuent investigation revealed additional indications on the 2" ECCS lines to Loop 2 cold leg and Loop 3 hot leg.
With the exception of the above, no additional indications were found on 153 welds examined.
Conditions Prior to Event
The unit was in mode 6 (refueling).
Description of Event
On 3/27/79 while performing inservice inspection on Unit 1 of FNP, linear surface indications were found on the 2" ECCS line to Loop 1 cold leg.
While performing the expanded examination, additional indications were found on the 2" ECCS lines to Loop 2 cold leg and Loop 3 hot leg.
These indications are reportable under the potential applicability of Tech. Spec. section 6.9.1.8(i).
Designation of Apparent Cause Based on an engineering evaluation the subject indications probably were caused during handling, fabrication, installation or manufacture of the piping.
A_na l y s i t. of Event on March 27, 1979, while performing inservice inspection on Unit 1 of FNP, five linear surface indications were found during P. T.
examination on the 2" ECCS line to Loop 1 cold leg.
All but one of the five indications were outside the heat affected zone of a weld.
Subsequent U. T. examination revealed that no indication was detected greater than.030" in depth.
On March 28, 1979, eleven linear surface indications were found during P. T. examination on the 2" ECCS line to Loop 2 cold Icg.
All but one of these indications were outside the heat affected zone of a weld.
Subsequent U. T. examination revealed no discontinuities.
79-015/01T-0 On March 30, 1979, one linear surface indication was found during P. T. examination on the 2" ECCS line to Loop 3 hot leg.
This indication sas inside the heat affected zone of a weld.
Effect on Plant This occurrence had no significant effect on plant operation.
Corrective Action
The design organization has provided two corrective action alternatives i.e. cut out and replace piping or grind out subject inlications.
These alternatives are being reviewed by APCo.
A follow-up report will be issued upon completion af the appropriate corrective action.
Failure Data None.
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| 05000348/LER-1979-001-03, /03L-0 on 790109:electronic Switching Sys B1G Sequencer Failed to Meet Time Requirements for Picking Up Step 2.Caused by Agastat Timer Setpoint Drift | /03L-0 on 790109:electronic Switching Sys B1G Sequencer Failed to Meet Time Requirements for Picking Up Step 2.Caused by Agastat Timer Setpoint Drift | | | 05000348/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000348/LER-1979-002-03, /03L-0 on 790116:120V Vital AC Bus 1B Was Deenergized When Inverter 1B Tripped Due to Components Failure.Capacitor,Air Core Choke,Resistor & Fuse Were Replaced & Inverter Returned to Svc | /03L-0 on 790116:120V Vital AC Bus 1B Was Deenergized When Inverter 1B Tripped Due to Components Failure.Capacitor,Air Core Choke,Resistor & Fuse Were Replaced & Inverter Returned to Svc | | | 05000348/LER-1979-003-03, /03L-0 on 790116:following Reactor Trip,Turbine Driven Auxiliary Feedwater Pump Failed to Start.Caused by Trip/Throttle Valve Which Tripped Shut | /03L-0 on 790116:following Reactor Trip,Turbine Driven Auxiliary Feedwater Pump Failed to Start.Caused by Trip/Throttle Valve Which Tripped Shut | | | 05000348/LER-1979-004-03, /03L-0 on 790123:containment Atmosphere Particulate Radioactivity Monitoring Sys Inoperable;Filter Paper Was Not Advancing.Caused by Replacement Paper Being Thicker That That Originally Supplied | /03L-0 on 790123:containment Atmosphere Particulate Radioactivity Monitoring Sys Inoperable;Filter Paper Was Not Advancing.Caused by Replacement Paper Being Thicker That That Originally Supplied | | | 05000348/LER-1979-005, /03L-0 on 790123:during Maint on Boron Injection Tank Inlet Valve Q1E21VO16B,boron Concentration Fell Below Tech Spec Requirements.Caused by Leakage Through Opened Valve During Troubleshooting Per LER 79-005/03L-0 | /03L-0 on 790123:during Maint on Boron Injection Tank Inlet Valve Q1E21VO16B,boron Concentration Fell Below Tech Spec Requirements.Caused by Leakage Through Opened Valve During Troubleshooting Per LER 79-005/03L-0 | | | 05000348/LER-1979-005-03, /03L-0 on 790123:during Surveillance Test on Boron Injection Tank Inlet Valve Q1E32V016B,valve Failed to Operate Electrically.Cause Undetermined,Since Subsequent Troubleshooting Failed to Duplicate Problem | /03L-0 on 790123:during Surveillance Test on Boron Injection Tank Inlet Valve Q1E32V016B,valve Failed to Operate Electrically.Cause Undetermined,Since Subsequent Troubleshooting Failed to Duplicate Problem | | | 05000348/LER-1979-007-03, /03L-0 on 790212:during Review of Surveillance Test Data,Noted That RCS Leakage Test (FNP-1-STP-9.0) Had Not Been Done within Time Specified.Caused by Personnel Failure.Supervisors Instructed Re Matter | /03L-0 on 790212:during Review of Surveillance Test Data,Noted That RCS Leakage Test (FNP-1-STP-9.0) Had Not Been Done within Time Specified.Caused by Personnel Failure.Supervisors Instructed Re Matter | | | 05000348/LER-1979-007, Forwards LER 79-007/03L-0,LER 79-008/03L-0,LER 79-009/03L-0, LER 79-010/03L-0, & 79-011/03L-0 | Forwards LER 79-007/03L-0,LER 79-008/03L-0,LER 79-009/03L-0, LER 79-010/03L-0, & 79-011/03L-0 | | | 05000348/LER-1979-008-03, /03L-0 on 790216:during Review of Surveillance Test FNP-1-STP-15.0,containment Main Personnel & Emergency Air Leak Outer Doors Failed to Meet Acceptance Criteria. Leakage Probably Caused by Dirty Door Seals &/Or Seal Set | /03L-0 on 790216:during Review of Surveillance Test FNP-1-STP-15.0,containment Main Personnel & Emergency Air Leak Outer Doors Failed to Meet Acceptance Criteria. Leakage Probably Caused by Dirty Door Seals &/Or Seal Set | | | 05000348/LER-1979-009-03, /03L-0 on 790216:during Plant Startup W/Reactor & Steam Generator Controls Manual & Steam Dumps in Automatic, Steam Dumps Occurred.Temp Average Reduced to 538 F.Personnel Reinstructed | /03L-0 on 790216:during Plant Startup W/Reactor & Steam Generator Controls Manual & Steam Dumps in Automatic, Steam Dumps Occurred.Temp Average Reduced to 538 F.Personnel Reinstructed | | | 05000348/LER-1979-010-03, /03L-0 on 790218:while Doing FNP-1-STP-215.1B, Steam Flow/Feed Flow Bistable (FB478A)failed to Meet Table 2-1 Trip Setpoint Valve.Caused by Bistable Setpoint Drift Below That Specified in Surveillance Test.Bistable Adjusted | /03L-0 on 790218:while Doing FNP-1-STP-215.1B, Steam Flow/Feed Flow Bistable (FB478A)failed to Meet Table 2-1 Trip Setpoint Valve.Caused by Bistable Setpoint Drift Below That Specified in Surveillance Test.Bistable Adjusted | | | 05000348/LER-1979-011-03, /03L-0 on 790221:while Doing FNP-1-STP-28.7,LOSP B1F Sequencer Failed to Meet Time Requirement for Picking Up Step 6.Caused by Agastat Timer Setpoint Drift.Agastat Timer Adjusted & Satisfactorily Retested | /03L-0 on 790221:while Doing FNP-1-STP-28.7,LOSP B1F Sequencer Failed to Meet Time Requirement for Picking Up Step 6.Caused by Agastat Timer Setpoint Drift.Agastat Timer Adjusted & Satisfactorily Retested | | | 05000348/LER-1979-012-03, /03L-0 on 790214:review of Solid State Protective Sys Train A/B Operability Test Indicated That Portion of Program Did Not Verify Spray Test Actuation Logic.Caused by Sys Train Design Change.Procedure Modified | /03L-0 on 790214:review of Solid State Protective Sys Train A/B Operability Test Indicated That Portion of Program Did Not Verify Spray Test Actuation Logic.Caused by Sys Train Design Change.Procedure Modified | | | 05000348/LER-1979-012, Forwards LER 79-012/03L-0 | Forwards LER 79-012/03L-0 | | | 05000348/LER-1979-013, Forwards LER 79-013/03L-0 | Forwards LER 79-013/03L-0 | | | 05000348/LER-1979-013-03, /03L-0 on 790227:B1F Sequencer Found in Test Mode, Rendering 1-2A Diesel Generator Inoperable.Caused by Faulty Switch Mechanism.Sequencer Repaired | /03L-0 on 790227:B1F Sequencer Found in Test Mode, Rendering 1-2A Diesel Generator Inoperable.Caused by Faulty Switch Mechanism.Sequencer Repaired | | | 05000348/LER-1979-015-01, /01T-0 on 790327:during Inservice Insp,Linear Svc Indications Found on ECCS Line to Loops 1 & 2 Cold Legs & Loop 3 Hot Leg.Caused During Handling.Two Corrective Actions Proposed:Cut Out & Replace or Grind Out | /01T-0 on 790327:during Inservice Insp,Linear Svc Indications Found on ECCS Line to Loops 1 & 2 Cold Legs & Loop 3 Hot Leg.Caused During Handling.Two Corrective Actions Proposed:Cut Out & Replace or Grind Out | | | 05000348/LER-1979-016-03, /03L-0 on 790325:loss of Sys Pressure B1F Sequencer Failed to Meet Time Requirements in Test.Agastat Timer Setpoint Drifted Below Setpoint Required for Test. Timer Adjusted;Test Redone | /03L-0 on 790325:loss of Sys Pressure B1F Sequencer Failed to Meet Time Requirements in Test.Agastat Timer Setpoint Drifted Below Setpoint Required for Test. Timer Adjusted;Test Redone | | | 05000348/LER-1979-017-01, /01T-2 on 790330:util Notified by Westinghouse of Single Dropped Rod W/Potential for Calculated DNB Ratios Lower than Reported to NRC for Floating Nuclear Plants. Caused by Incorrect Measurement During Rod Drop Events | /01T-2 on 790330:util Notified by Westinghouse of Single Dropped Rod W/Potential for Calculated DNB Ratios Lower than Reported to NRC for Floating Nuclear Plants. Caused by Incorrect Measurement During Rod Drop Events | | | 05000348/LER-1979-017, Forwards LER 79-017/01T-2 | Forwards LER 79-017/01T-2 | | | 05000348/LER-1979-019, Forwards LER 79-019/03L-1 | Forwards LER 79-019/03L-1 | | | 05000348/LER-1979-019-03, /03L-1 on 790420:fluoride & Chloride Concentrations in RCS in Violation of Tech Spec Limits.Cause Not Determined.Rcs Integrity Not Impaired & Acceptable for Continued Operation | /03L-1 on 790420:fluoride & Chloride Concentrations in RCS in Violation of Tech Spec Limits.Cause Not Determined.Rcs Integrity Not Impaired & Acceptable for Continued Operation | | | 05000348/LER-1979-021-01, /01T-3 on 790412:statistical Sampling of Seismic Category I Anchor Bolts Would Not Provide Probability Greater than 95% Reliability.Caused Under Investigation. Testing Extended to 100% Verification of Anchors on Pipe | /01T-3 on 790412:statistical Sampling of Seismic Category I Anchor Bolts Would Not Provide Probability Greater than 95% Reliability.Caused Under Investigation. Testing Extended to 100% Verification of Anchors on Pipe | | | 05000348/LER-1979-021, Forwards LER 79-021/01T-3 | Forwards LER 79-021/01T-3 | | | 05000348/LER-1979-022-03, /03L-0 on 790620:surveillance Test Procedure FNP-1-STP-29.2 Not Performed on 790620.Caused by Inadequate Surveillance Test Schedule Review by Shift Foreman on 790620.Importance of Accurate Daily Review Stressed | /03L-0 on 790620:surveillance Test Procedure FNP-1-STP-29.2 Not Performed on 790620.Caused by Inadequate Surveillance Test Schedule Review by Shift Foreman on 790620.Importance of Accurate Daily Review Stressed | | | 05000348/LER-1979-023-01, /01T-0 on 790622:notified by Westinghouse That High Energy Line Break Inside Containment Could Cause Heatup of Steam Generator Level Transmitter Ref Legs. LER Will Be Issued Upon Completion of Investigation | /01T-0 on 790622:notified by Westinghouse That High Energy Line Break Inside Containment Could Cause Heatup of Steam Generator Level Transmitter Ref Legs. LER Will Be Issued Upon Completion of Investigation | | | 05000348/LER-1979-023, Forwards LER 79-023/01T-0 | Forwards LER 79-023/01T-0 | | | 05000348/LER-1979-024-03, /03L-0 on 790622:during Review of Surveillance Tests FNP-1-STP-40.1 & 40.2,noted That Certain Components Were Not Included in Test Procedures.Caused by Procedural Deficiencies.Procedure Change Has Been Made | /03L-0 on 790622:during Review of Surveillance Tests FNP-1-STP-40.1 & 40.2,noted That Certain Components Were Not Included in Test Procedures.Caused by Procedural Deficiencies.Procedure Change Has Been Made | | | 05000348/LER-1979-025-03, /03L-0 on 790623:during Surveillance Test FNP-1-STP-256.11 Both Source Range Channels Inadvertently Were Deenergized. Caused by Procedure Deficiency. Power Restored & Procedure Changed | /03L-0 on 790623:during Surveillance Test FNP-1-STP-256.11 Both Source Range Channels Inadvertently Were Deenergized. Caused by Procedure Deficiency. Power Restored & Procedure Changed | | | 05000348/LER-1979-026-03, /03L-0 on 790716:total of 135 Hydraulic Snubbers Did Not Meet Surveillance Test Requirements.Caused by Loss of Oil Due to Seal Leakage & Failure to Meet Lockup & Bleed Acceptance Criteria.Snubbers Repaired & Tested | /03L-0 on 790716:total of 135 Hydraulic Snubbers Did Not Meet Surveillance Test Requirements.Caused by Loss of Oil Due to Seal Leakage & Failure to Meet Lockup & Bleed Acceptance Criteria.Snubbers Repaired & Tested | | | 05000348/LER-1979-027-03, /03L-0 on 790607:radiation Monitor Declared Inoperable.Caused by Pump Malfunction.Pump Repaired & Declared Operable 790615 | /03L-0 on 790607:radiation Monitor Declared Inoperable.Caused by Pump Malfunction.Pump Repaired & Declared Operable 790615 | | | 05000348/LER-1979-028-03, /03L-0 on 790627:radiation Monitor R-5 Declared Inoperable Due to Loss of Power.Feedbreaker Found Open. Cause Unknown.Breaker Closed & R-5 Declared Operable | /03L-0 on 790627:radiation Monitor R-5 Declared Inoperable Due to Loss of Power.Feedbreaker Found Open. Cause Unknown.Breaker Closed & R-5 Declared Operable | | | 05000348/LER-1979-029-03, /03L-0 on 790713:penetration Room Filtration Sys Trains a & B Inoperable.Caused by Train B Exhaust Fan Not Starting & Train a Suction Damper Not Opening.Overload Reset & Fuse Replaced | /03L-0 on 790713:penetration Room Filtration Sys Trains a & B Inoperable.Caused by Train B Exhaust Fan Not Starting & Train a Suction Damper Not Opening.Overload Reset & Fuse Replaced | | | 05000348/LER-1979-029, Forwards LER 79-029/03L-0 | Forwards LER 79-029/03L-0 | | | 05000348/LER-1979-030, Forwards LER 79-030/03L-0 | Forwards LER 79-030/03L-0 | | | 05000348/LER-1979-030-03, /03L-0 on 790717:during Surveillance test,600 Volt Ctr 1C Supply Breaker EE07 Failed to Load Shed.Caused by Open Links in Local Control Panel.Links Closed & Breaker Verified | /03L-0 on 790717:during Surveillance test,600 Volt Ctr 1C Supply Breaker EE07 Failed to Load Shed.Caused by Open Links in Local Control Panel.Links Closed & Breaker Verified | | | 05000348/LER-1979-031, Forwards LER 79-031/03L-0 | Forwards LER 79-031/03L-0 | | | 05000348/LER-1979-031-03, /03L-0 on 790717:two Control Power Fuses Blew in N31 Source Range Drawer & Were Causing Loss of Power in Both Source Range Channels.Caused by Personnel Error | /03L-0 on 790717:two Control Power Fuses Blew in N31 Source Range Drawer & Were Causing Loss of Power in Both Source Range Channels.Caused by Personnel Error | | | 05000348/LER-1979-032-03, /03L-0:on 790730,determined That Diesel Generators 1C & 2C Output Breakers Were Racked Out.Caused by Personnel Error.Breakers Racked in & Control Power Restored | /03L-0:on 790730,determined That Diesel Generators 1C & 2C Output Breakers Were Racked Out.Caused by Personnel Error.Breakers Racked in & Control Power Restored | | | 05000348/LER-1979-033-03, /03L-0:on 790803,radiation Monitor R25B Declared Inoperable.Caused by Drive Belt Failure.New Drive Belt Installed | /03L-0:on 790803,radiation Monitor R25B Declared Inoperable.Caused by Drive Belt Failure.New Drive Belt Installed | | | 05000348/LER-1979-034, Forwards LER 79-034/03L-0 | Forwards LER 79-034/03L-0 | | | 05000348/LER-1979-034-03, /03L-0:on 790824,determined That Functional Surveillance Test Had Not Been Performed on Certain Seismic Monitoring Instrumentation within Specified Time.Caused by Personnel Error.Proper Procedure re-emphasized | /03L-0:on 790824,determined That Functional Surveillance Test Had Not Been Performed on Certain Seismic Monitoring Instrumentation within Specified Time.Caused by Personnel Error.Proper Procedure re-emphasized | | | 05000348/LER-1979-035, Forwards LER 79-035/01T-0 | Forwards LER 79-035/01T-0 | | | 05000348/LER-1979-035-01, /01T-0:on 790824,Westinghouse Notified Util of Potential Heat Sink Shorting to 7300 Rack Card Guides within 7300 Process Instrumentation & Control Printed Card Circuits.Caused by Mfg Defect.Cards Replaced | /01T-0:on 790824,Westinghouse Notified Util of Potential Heat Sink Shorting to 7300 Rack Card Guides within 7300 Process Instrumentation & Control Printed Card Circuits.Caused by Mfg Defect.Cards Replaced | | | 05000348/LER-1979-036-03, /03L-0:on 790903,train B RHR Relief Isolation Valves Closed When Power Was Applied to Actuators to Enable Valve Position Indication.Caused by Pulled Fuses That Forced Output Circuit to Send Signal to Close Valves | /03L-0:on 790903,train B RHR Relief Isolation Valves Closed When Power Was Applied to Actuators to Enable Valve Position Indication.Caused by Pulled Fuses That Forced Output Circuit to Send Signal to Close Valves | | | 05000348/LER-1979-037-03, /03L-0:on 790906,auxiliary Bldg Battery Verification Was Two Days Late.Caused by Personnel Error. Performance of Surveillance Tests on Scheduled Dates Will Be Discussed W/Affected Personnel | /03L-0:on 790906,auxiliary Bldg Battery Verification Was Two Days Late.Caused by Personnel Error. Performance of Surveillance Tests on Scheduled Dates Will Be Discussed W/Affected Personnel | | | 05000348/LER-1979-038-03, /03L-0:on 790912,while Performing Surveillance Test FNP-1-STP-1.0,containment Gaseous Activity Purge & Exhaust Isolation Monitor Declared Inoperable.Caused by Monitor Bypass Valve Being in Open Position | /03L-0:on 790912,while Performing Surveillance Test FNP-1-STP-1.0,containment Gaseous Activity Purge & Exhaust Isolation Monitor Declared Inoperable.Caused by Monitor Bypass Valve Being in Open Position | | | 05000348/LER-1979-039-03, /03L-0:on 790924,fuel Storage Pool Area Radiation Monitor Declared Inoperable Due to Reading Discrepancy. Caused by Instrument Drift.Monitor Recalibr & Returned to Svc on 790930 | /03L-0:on 790924,fuel Storage Pool Area Radiation Monitor Declared Inoperable Due to Reading Discrepancy. Caused by Instrument Drift.Monitor Recalibr & Returned to Svc on 790930 | | | 05000348/LER-1979-040-01, /01T-0:on 791011,wrong Valves Installed in Piping Sys.Caused by Deficiency in Original Plant Design Equipment Specs.Valves Being Replaced | /01T-0:on 791011,wrong Valves Installed in Piping Sys.Caused by Deficiency in Original Plant Design Equipment Specs.Valves Being Replaced | |
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