05000302/LER-1979-026-03, /03L-0 on 790318:during Reactor Startup,Discovered Absolute Position Indication for Rod 8 Was Inoperable.Caused by Sticking Reed Switch.Variable Ac Frequency,Applied to Reed Switch Circuit,Eliminated Sticking

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/03L-0 on 790318:during Reactor Startup,Discovered Absolute Position Indication for Rod 8 Was Inoperable.Caused by Sticking Reed Switch.Variable Ac Frequency,Applied to Reed Switch Circuit,Eliminated Sticking
ML19274E685
Person / Time
Site: Crystal River 
Issue date: 04/05/1979
From: Cooper J
FLORIDA POWER CORP.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19274E683 List:
References
LER-79-026-03L, LER-79-26-3L, NUDOCS 7904170171
Download: ML19274E685 (2)


LER-1979-026, /03L-0 on 790318:during Reactor Startup,Discovered Absolute Position Indication for Rod 8 Was Inoperable.Caused by Sticking Reed Switch.Variable Ac Frequency,Applied to Reed Switch Circuit,Eliminated Sticking
Event date:
Report date:
3021979026R03 - NRC Website

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EVENT QESCRIPTLCN AND #RC9ASLE COreSECuENCES h oi: I At 1921, durine a reactor startun. It was discovered that the absolute o:2 t position indication for rnd 8 n rnim 6 u,n innnor,ble This crn,rna

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No effect upon public health and safety. Rod position was verified y

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,,. [ The cause of this event can be attributed to a sticking reed switch. The

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M(SEE ATTACHED SUFPLE.MENTARY INFORPEIGN 7 9 0417 o / ~7/

SUPPLEMENTARY INFORMATION Report No.:

50-302/79-026/03L-0 Facility:

Crystal River Unit #3 Report Date:

5 April 1979 Occurrence Date:

18 March 1979 Identification of Occurrence:

Absolute rod position indication inoperable contrary to Technical Specification 3.1.3.3.

Conditions Prior to Occurrence:

Mode 2 operation (reactor critical)

Description of Occurrence:

At 1921, during a reactor startup, following criticality, absolute rod position indication for rod 8, group 6, tas inoperable. Entered action statement "a".

Reactor maintained in a stable condition. Verified nuclear overpower trip set-point at 5%.

Verified rod 8, group 6 position through relative rod position indication.

Operability was restored at 2020 following maintenance.

Designation of Apparent Cause:

The cause of this event can be attributed to a stuck reed switch. Magnetization, eminating from spurious magnetic fields generated during control rod operation,causes the reed switch to stick.

Analysis of Occurrence:

There was no hazard to the plant or general public as rod position was verified through relative rod position indication.

Corrective Action

The application of a variable AC frequency to the reed switch circuit eliminates the magnetic field.

This maintenance action restored operability. No further corrective action required.

Failure Data:

This is the seventh occurrence reported. Reference LER's (77-71, 112, 125) and (78-49, 62, 68).

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