05000302/LER-1979-052-03, /03L-0 on 790516:in Mode 6,diesel Driver Fire Svc Pumps Discovered to Be Out of Svc.Caused by Diesel Manufacturer Representative Being Unfamiliar W/Approved Plant Procedures.Personnel Instructed

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/03L-0 on 790516:in Mode 6,diesel Driver Fire Svc Pumps Discovered to Be Out of Svc.Caused by Diesel Manufacturer Representative Being Unfamiliar W/Approved Plant Procedures.Personnel Instructed
ML19273B918
Person / Time
Site: Crystal River Duke Energy icon.png
Issue date: 06/07/1979
From: Cooper J
FLORIDA POWER CORP.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19273B917 List:
References
LER-79-052-03L, LER-79-52-3L, NUDOCS 7906180508
Download: ML19273B918 (2)


LER-1979-052, /03L-0 on 790516:in Mode 6,diesel Driver Fire Svc Pumps Discovered to Be Out of Svc.Caused by Diesel Manufacturer Representative Being Unfamiliar W/Approved Plant Procedures.Personnel Instructed
Event date:
Report date:
3021979052R03 - NRC Website

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(SEE AITAM SU?PLF' DENTARY INFORMATION SEZZT)

a SUPPLEMENTARY INFORMATION Report No.*

50-302/79-052/03L-0 Facility:

Crystal River Unit #3 Report Date:

7 June 1979 Occurrence Date:

16 May 1979 Identification of Occurrence:

The Fire Suppression System inoperable contrary to Technical Specification 3.7.ll.l.a.

Conditions Prior to Occurrence:

Mode 6 refueling.

Description of Occurrence:

At 1300, it was discovered tha both diesel driven fire service pumps, FSP-2A and 2B, were inoperable.

Investigation revealed that a clearance had been issued for the yearly inspection of Fire Service Pump FSP-2B.

However, the diesel manufacturer rep-resentative, in an effort to avoid delay, disconnected the starter on FSP-2A without meintenance personnel assistance and proceeded to perform SP-606. Maintenance personnel assigned to the job arrived at the jobsite and assisted the Technical Rep-resentative. During the performance of the SP-606 it was dis-covered that FSP-2A was not under clearance.

Supervisory personnel were notified and FSP-2B was returned to service at 1315.

Designation of Apparent Cause:

The cause of this event is attrib 2ted to the manufacturer's representative not having adequat.e training to follow the Clearance Procedure.

Analysis of Occurrence:

No effect upon public health and safety.

Fire Service Pump FSP-1 was available and operable.

Corrective Action

A Discrepancy Report #5873 was initiated as a result of this event.

Personnel involved were instructed on the importance of adhering to approved procedures and on proper maintenance practices. No further corrective action required.

2354 008 Failure Data:

This is the first occurrence of this type reported.

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