ML19261B622

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LER 79-017/03L-0 on 790201:boric Acid Makeup Tank Level Below Tech Spec Min.Caused by Equalization of Boric Acid in Both Tanks
ML19261B622
Person / Time
Site: Arkansas Nuclear Entergy icon.png
Issue date: 02/22/1979
From: Shively C
ARKANSAS POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19261B616 List:
References
LER-79-017-03L, LER-79-17-3L, NUDOCS 7902280294
Download: ML19261B622 (1)


Text

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EVENT DATE 74 75 sh>OH 1 0 A T F Bo EVENT DESCRIPTION AND PROSAOLE CONSEQUENCES O'o o 2 l Following the Power Escalation Remote Shutdown "'est, Mode 3 operation, ,

O 3 both Boric Acid Makeun Tank gravity feed valves were opened simultaneousl'(

o 4 L as required by procedure, allowing BAM Tank's levels to equalize. g n

3 lmc ,.nen1+na in levels in each below the limit recuired by T.S.3.1.2.8. l t o lc l I The total volume available in both BAMT's was almost double the minimum g o i [ required by T.S. Figure 3.1-1. No similar occurrences. Reportable per i

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43 44 4; C AUSE DESCR# TION AND CORREC flVE ACTIONS i O l Boric Acid was transferred from one tank to the other, and one tank l' ' I i n, n 1 v,m onablished Above the required minimum. This met the i i 2 requirement of Action Statement T.S.3.1.2.8a for one tank maintaining  ;

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