05000348/LER-1979-062-03, /03L-0:on 791204,during Turbine Load Reduction Due to Failed DEH Voltage/Frequency Converter,Indicated Axial Flux Difference Was Not Maintained within Tech Spec Band. Caused by Failed DEH Voltage to Frequency Converter

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/03L-0:on 791204,during Turbine Load Reduction Due to Failed DEH Voltage/Frequency Converter,Indicated Axial Flux Difference Was Not Maintained within Tech Spec Band. Caused by Failed DEH Voltage to Frequency Converter
ML19257A914
Person / Time
Site: Farley 
Issue date: 01/02/1980
From: Hairston W
ALABAMA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19257A906 List:
References
LER-79-062-03L, LER-79-62-3L, NUDOCS 8001090383
Download: ML19257A914 (1)


LER-1979-062, /03L-0:on 791204,during Turbine Load Reduction Due to Failed DEH Voltage/Frequency Converter,Indicated Axial Flux Difference Was Not Maintained within Tech Spec Band. Caused by Failed DEH Voltage to Frequency Converter
Event date:
Report date:
3481979062R03 - NRC Website

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Tech. Spec. 3.2.1.a.2 action statement requirements were met.

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