LER-1979-096, /01T-0:on 790780,vol of Sodium Hydroxide Tank Exceeded Tech Spec,But Not Reported.Caused by Inadequate Design.Daily Operating Surveillance Procedure SP-300 Revised to Include Operating Band Requirement |
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SUPPLEMENTARY INFORMATION Report No.:
50-302/79-096/0lT-0 Facility:
Crystal River Unit #3 Report Date:
26 October 1979 Identification of Occurrence:
Sodium hydroxide tank BST-2 inoperable contrary to Technical Specification 3.6.2.2 and reportable under Section 6.9.1.8.b.
Conditions Prior to Occurrence:
Mude 1 pcwer operation (100%)
Description of Occurrence:
It was determined at 1530 following a discussion with the onsite NRC inspector that a previous event, discovered on 8 July 1979 and evaluated not reportable, en-uld have been reported contrary to Techaical Specification 3.6.2.2 and reported under Section 6.9.1.8.b.
On 8 July 1979, in Mode 5, it was discovered that the level of the Na0H tank (BST-2) was being maintained at a volume greater than Technical Specification limit. Further investigation re-vealed that level transmitter BST-2-LT was calibrated with a zero reference point two (2) feet above the tank discharge. The usable volume provided by the additional two feet resulted in the level exceeding the limit. This event was not reported initially due to a misinterpretation of reporting requirements involving limiting conditions for operation and their applicable Mode requirements.
The event involving BST-2 was discovered and corrected before entering into the applicable Mode.
Designation of Apparent Cause:
The cause of this event is attributed to inadequate design. The existing design did not provide adequate indication of useable tank volume.
Analysis of Occurrence:
No effect upon the plant or general public. The level of BST-2 was brought to within specification limits prior to entering into Mode 4.
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Corrective Action
Daily operating Surveillance Procedure, SP-300, was revised to in-clude an operating band requirement that will maintain the NaOH tank volume within the Technical Specification limits.
In addition, re-sponsible personnel have been instructed in regard to the reporting requirements for events of this type. Future events will be evalu-ated in this regard and reported aoproprit.tely.
Supplementary Information 50-302/79-096/01T-0 Page 2 Failure Data:
This is the first occurrence of this type reported.
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| 05000302/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000302/LER-1979-001-03, /03L-0 on 790101:during Operating Daily Surveillance Log Survey (SP-300),noted That Pressure in B Core Flood Tank Was 630 Psi.Caused by Operator Error During Repressurization | /03L-0 on 790101:during Operating Daily Surveillance Log Survey (SP-300),noted That Pressure in B Core Flood Tank Was 630 Psi.Caused by Operator Error During Repressurization | | | 05000302/LER-1979-002-03, /03L-0 on 790102:33 Ft Wind Direction Monitor Was Inoperable.Caused by Wind Direction Sensor Bearing Being Contaminated W/Coal Dust.Sensor Renewed Thru Normal Maint | /03L-0 on 790102:33 Ft Wind Direction Monitor Was Inoperable.Caused by Wind Direction Sensor Bearing Being Contaminated W/Coal Dust.Sensor Renewed Thru Normal Maint | | | 05000302/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000302/LER-1979-003-03, /03L-0 on 790106:during Rx Runback Following Turbine Trip,Main Feedwater Block Valve FWV-30 Did Not Close.Caused by Valve Sticking on Its Back Seat.Corrective Action:Manual Cycling | /03L-0 on 790106:during Rx Runback Following Turbine Trip,Main Feedwater Block Valve FWV-30 Did Not Close.Caused by Valve Sticking on Its Back Seat.Corrective Action:Manual Cycling | | | 05000302/LER-1979-003, Forwards LER 79-003/03L-0 | Forwards LER 79-003/03L-0 | | | 05000302/LER-1979-004-03, /03L-0 on 790115:cable Tunnel Sump Pump Failed to Start During Operability Verification.Maint Restored Sump Pump Operability.Caused Attributed to Failure of Pump | /03L-0 on 790115:cable Tunnel Sump Pump Failed to Start During Operability Verification.Maint Restored Sump Pump Operability.Caused Attributed to Failure of Pump | | | 05000302/LER-1979-004, Forwards LER 79-004/03L-0 | Forwards LER 79-004/03L-0 | | | 05000302/LER-1979-005-01, Discusses Commitment Stated in LER 79-005-01T-1 Re MSIV Valves Not Closing within Design Time of Five Seconds During Double Ended Pipe Rupture.Util Has Determined That Upgrading Air Circuit to Seismic Class I Will Not Be Nec | Discusses Commitment Stated in LER 79-005-01T-1 Re MSIV Valves Not Closing within Design Time of Five Seconds During Double Ended Pipe Rupture.Util Has Determined That Upgrading Air Circuit to Seismic Class I Will Not Be Necessary | | | 05000302/LER-1979-006, Forwards LER 79-006/01T-0 | Forwards LER 79-006/01T-0 | | | 05000302/LER-1979-006-01, /01T-0 on 790201:figures for Transient Limits on Rapid Depressurizations & High Pressure Injection Tests in Disagreement W/Cycle 2 Reload Rept.Tech Specs Will Be Revised | /01T-0 on 790201:figures for Transient Limits on Rapid Depressurizations & High Pressure Injection Tests in Disagreement W/Cycle 2 Reload Rept.Tech Specs Will Be Revised | | | 05000302/LER-1979-007-03, /03L-0 on 790117:reactor Coolant Dose Equivalent I-131 Exceeded 1.0 Mci.Caused by Expected Transient Spikes Following Reactor Trip & Known Leaking Fuel Pins | /03L-0 on 790117:reactor Coolant Dose Equivalent I-131 Exceeded 1.0 Mci.Caused by Expected Transient Spikes Following Reactor Trip & Known Leaking Fuel Pins | | | 05000302/LER-1979-007, Forwards LER 79-007/03L-0 | Forwards LER 79-007/03L-0 | | | 05000302/LER-1979-008-03, /03L-0 on 790119:RC3-GP3-BL4 Light Did Not Extinguish When Test Switch Returned to Off Position.Caused by Dirty Contacts in Relay | /03L-0 on 790119:RC3-GP3-BL4 Light Did Not Extinguish When Test Switch Returned to Off Position.Caused by Dirty Contacts in Relay | | | 05000302/LER-1979-008, Forwards LER 79-008/03L-0 | Forwards LER 79-008/03L-0 | | | 05000302/LER-1979-009, Forwards LER 79-009/03L-0 | Forwards LER 79-009/03L-0 | | | 05000302/LER-1979-009-03, /03L-0 on 790124:while Performing Reactor Protection Sys Functional Testing,Rod Group 6 Dropped Into Core,Rod Group Overlap Was Exceeded.Caused by a AC Power Breaker Being Left Open | /03L-0 on 790124:while Performing Reactor Protection Sys Functional Testing,Rod Group 6 Dropped Into Core,Rod Group Overlap Was Exceeded.Caused by a AC Power Breaker Being Left Open | | | 05000302/LER-1979-010-03, /03L-0 on 790125:during Routine Operations,Air Handling Fan Failed to Start.Caused by Faulty Overcurrent Timing Relay | /03L-0 on 790125:during Routine Operations,Air Handling Fan Failed to Start.Caused by Faulty Overcurrent Timing Relay | | | 05000302/LER-1979-010, Forwards LER 79-010/03L-0 | Forwards LER 79-010/03L-0 | | | 05000302/LER-1979-011-03, /03L-0 on 790210:reactor Coolant Dose Equivalent I-131 Exceeded Tech Spec Limits.Caused by Expected Spike Following Reactor Trip & Known Leaking Fuel Pins.Reactor Coolant Sys Cleanup Returned to Acceptable Limits | /03L-0 on 790210:reactor Coolant Dose Equivalent I-131 Exceeded Tech Spec Limits.Caused by Expected Spike Following Reactor Trip & Known Leaking Fuel Pins.Reactor Coolant Sys Cleanup Returned to Acceptable Limits | | | 05000302/LER-1979-012, Forwards LER 79-012/03L-0 | Forwards LER 79-012/03L-0 | | | 05000302/LER-1979-012-03, /03L-0 on 790214:during Safeguards Test, RB-3GP-2 Light Did Not Illuminate.Caused by Burr on Relay Shaft.Relay Cleaned & Burr Removed | /03L-0 on 790214:during Safeguards Test, RB-3GP-2 Light Did Not Illuminate.Caused by Burr on Relay Shaft.Relay Cleaned & Burr Removed | | | 05000302/LER-1979-014, Forwards LER 79-014/03L-0 | Forwards LER 79-014/03L-0 | | | 05000302/LER-1979-014-03, /03L-0 on 790220:decay Heat Cooler 3A Outlet Remote Shutdown Temp Indicator Inaccurate & Rendered Inoperable.Caused by Failed Resistance Temp Detector (Rtd). RTD Replaced & Sys Recalibr | /03L-0 on 790220:decay Heat Cooler 3A Outlet Remote Shutdown Temp Indicator Inaccurate & Rendered Inoperable.Caused by Failed Resistance Temp Detector (Rtd). RTD Replaced & Sys Recalibr | | | 05000302/LER-1979-015-03, /03L-0 on 790221:fire Svc Tanks 1-B & 1-A Contained Less than Min Volume Required by Tech Specs. Caused by Improper Design.Engineering Evaluation Initiated | /03L-0 on 790221:fire Svc Tanks 1-B & 1-A Contained Less than Min Volume Required by Tech Specs. Caused by Improper Design.Engineering Evaluation Initiated | | | 05000302/LER-1979-015, Forwards LER 79-015/03L-0 | Forwards LER 79-015/03L-0 | | | 05000302/LER-1979-016, Forwards Supplementary Info Re LER 79-016/04X-0 | Forwards Supplementary Info Re LER 79-016/04X-0 | | | 05000302/LER-1979-017, Forwards LER 79-017/03L-0 | Forwards LER 79-017/03L-0 | | | 05000302/LER-1979-017-03, /03L-0 on 790223:heat Trace Recorder for Concentrated Boric Acid Flowpath Was Malfunctioning & Rendered Inoperable.Caused by Failed Recorder Drive Wheel. Drive Wheel Replaced & Heat Trace Recorder Returned to Svc | /03L-0 on 790223:heat Trace Recorder for Concentrated Boric Acid Flowpath Was Malfunctioning & Rendered Inoperable.Caused by Failed Recorder Drive Wheel. Drive Wheel Replaced & Heat Trace Recorder Returned to Svc | | | 05000302/LER-1979-018, Forwards LER 79-018/03L-0 | Forwards LER 79-018/03L-0 | | | 05000302/LER-1979-018-03, /03L-0 on 790301:inner Airlock Door Found Unlatched.Caused by Inadequate Latching Design.Corrective Action Will Be Determined Upon Results of Engineering Info Request | /03L-0 on 790301:inner Airlock Door Found Unlatched.Caused by Inadequate Latching Design.Corrective Action Will Be Determined Upon Results of Engineering Info Request | | | 05000302/LER-1979-019, Forwards LER 79-019/03L-0 | Forwards LER 79-019/03L-0 | | | 05000302/LER-1979-019-03, /03L-0 on 790223:motor Driven Emergency Feedwater Pump Discharge Pressure Gauge EF-2-PI Was Out of Calibr. Caused by Inoperable Dampening Snubber Located in Sensing Line.Snubber Was Replaced | /03L-0 on 790223:motor Driven Emergency Feedwater Pump Discharge Pressure Gauge EF-2-PI Was Out of Calibr. Caused by Inoperable Dampening Snubber Located in Sensing Line.Snubber Was Replaced | | | 05000302/LER-1979-020, Forwards LER 79-020/03L-0 | Forwards LER 79-020/03L-0 | | | 05000302/LER-1979-020-03, /03L-0 on 790228:following Reactor Trip,Chem/Rod Sampling Revealed Reactor Coolant Dose Equivalent I-131 Exceeded 1.0 Mci Per Gram,Contrary to Tech Specs.Caused by Spike Following Reactor Trip & Leaking Fuel Pins | /03L-0 on 790228:following Reactor Trip,Chem/Rod Sampling Revealed Reactor Coolant Dose Equivalent I-131 Exceeded 1.0 Mci Per Gram,Contrary to Tech Specs.Caused by Spike Following Reactor Trip & Leaking Fuel Pins | | | 05000302/LER-1979-021-04, /04L-0 During 1978:difference of More than Two Std Deviations Existed Between Preoperational Study & Operational Study in Metabolic Functions of Discharge Salt Marshes Adjacent to Facility.Cause Natural or Seasonal | /04L-0 During 1978:difference of More than Two Std Deviations Existed Between Preoperational Study & Operational Study in Metabolic Functions of Discharge Salt Marshes Adjacent to Facility.Cause Natural or Seasonal | | | 05000302/LER-1979-021, Forwards LER 79-021/04L-0 | Forwards LER 79-021/04L-0 | | | 05000302/LER-1979-023, Forwards LER 79-023/03L-0 | Forwards LER 79-023/03L-0 | | | 05000302/LER-1979-023-03, /03L-0 on 790308:discovered RCS C1 Concentration Was .17ppm,contrary to Tech Specs.Caused by Appearance of Suspended Solids During Cooldown When Boron Concentration Increased.Purification Sys Reduced Concentration | /03L-0 on 790308:discovered RCS C1 Concentration Was .17ppm,contrary to Tech Specs.Caused by Appearance of Suspended Solids During Cooldown When Boron Concentration Increased.Purification Sys Reduced Concentration | | | 05000302/LER-1979-024-03, /03L-0 on 790315:during Plant Heatup,Discovered That Temp Device at 175 Ft Elevation of Meteorological Monitoring Tower Was Inoperable.Cause Unknown.Temp Device Tested Satisfactorily & Returned to Svc | /03L-0 on 790315:during Plant Heatup,Discovered That Temp Device at 175 Ft Elevation of Meteorological Monitoring Tower Was Inoperable.Cause Unknown.Temp Device Tested Satisfactorily & Returned to Svc | | | 05000302/LER-1979-024, Forwards LER 79-024/03L-0 | Forwards LER 79-024/03L-0 | | | 05000302/LER-1979-026, Forwards LER 79-026/03L-0 | Forwards LER 79-026/03L-0 | | | 05000302/LER-1979-026-03, /03L-0 on 790318:during Reactor Startup,Discovered Absolute Position Indication for Rod 8 Was Inoperable.Caused by Sticking Reed Switch.Variable Ac Frequency,Applied to Reed Switch Circuit,Eliminated Sticking | /03L-0 on 790318:during Reactor Startup,Discovered Absolute Position Indication for Rod 8 Was Inoperable.Caused by Sticking Reed Switch.Variable Ac Frequency,Applied to Reed Switch Circuit,Eliminated Sticking | | | 05000302/LER-1979-027, Forwards Supplemental Info for LER 79-027/04X-0 | Forwards Supplemental Info for LER 79-027/04X-0 | | | 05000302/LER-1979-028, Forwards LER 79-028/03L-0 | Forwards LER 79-028/03L-0 | | | 05000302/LER-1979-028-03, /03L-0 on 790321:while Performing Emergency Feedwater Sys Demonstration,Discovered Pump Discharge Pressure Gauge EF-2-PI Inoperable.Caused by Failed Pressure Gauge.Gauge Replaced | /03L-0 on 790321:while Performing Emergency Feedwater Sys Demonstration,Discovered Pump Discharge Pressure Gauge EF-2-PI Inoperable.Caused by Failed Pressure Gauge.Gauge Replaced | | | 05000302/LER-1979-029, Forwards LER 79-029/03L-0 | Forwards LER 79-029/03L-0 | | | 05000302/LER-1979-029-03, /03L-0 on 790321:discovered Makeup Pump 3-C Discharge Stopcheck Valve MUV-2 Was Improperly Positioned. Cause unknown.MUV-2 Reset to Proper Throttle Setting & Returned to Svc | /03L-0 on 790321:discovered Makeup Pump 3-C Discharge Stopcheck Valve MUV-2 Was Improperly Positioned. Cause unknown.MUV-2 Reset to Proper Throttle Setting & Returned to Svc | | | 05000302/LER-1979-031-01, /01T-0 on 790412:during Routine Radwaste Release, Release Monitor Went Into High Alarm Because Radwaste Isolation Valves WDV-320 & 321 Failed to Close.Caused by Sticking Contacts in Monitor Bypass Switch | /01T-0 on 790412:during Routine Radwaste Release, Release Monitor Went Into High Alarm Because Radwaste Isolation Valves WDV-320 & 321 Failed to Close.Caused by Sticking Contacts in Monitor Bypass Switch | | | 05000302/LER-1979-031, Forwards LER 79-031/01T-0 | Forwards LER 79-031/01T-0 | |
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