ML19250A711

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IE Insp Repts 50-269/79-20,50-270/79-18 & 50-287/79-20 on 790806-10.Noncompliance Noted:Failure to Maintain Positive Control Over Individual Entries to High Radiation Areas
ML19250A711
Person / Time
Site: Oconee  Duke Energy icon.png
Issue date: 09/10/1979
From: Allen J, Gibson A, Hosey C
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML19250A702 List:
References
50-269-79-20, 50-270-79-18, 50-287-79-20, NUDOCS 7910240312
Download: ML19250A711 (7)


See also: IR 05000269/1979020

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UNITED STATES

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NUCLEAR REGULATORY COMMISSION

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REGION 11

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101 MARIETTA ST.. N.W.. SUITE 3100

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ATLANTA, GEORGIA 30303

Report Nos. 50-269/79-20, 50-270/79-18, and 50-237/79-20

Licensee: Duke Power Company

422 South Church Street

Charlotte, North Carolina 28242

Facility Name: Oconea

Docket Nos. 50-269, 50-270, and 50-287

License Nos.: DPR-38, DPR-47, and DPR-55

Inspection at Oconee si

, near Seneca, South Carolina

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Inspectors:

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C. M. Hose

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Date 'Sigded

Approved by:

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A. F. Gibson, Section Chief, FF&MS Branch

Date Signed

SUMMARY

Inspection on August 6-10, 1979

Areas Inspected

This routine, unannounced inspection involved 74 inspector-hours onsite in the

areas of radioactive waste management program, including radioactive effluent

release reports, procedures for controlling the release of effluents, effluent

control instrumentation, solid radioactive waste disposal; radiation protection

program, including licensee audits, posting, labeling and control of radiologi-

cally controlled areas and material and external radiation exposure control;

and followup on previously identified items.

Results

Of the eight areas inspected, no apparent items of noncompliance or deviations

were identified in seven areas; one apparent item of noncompliance was found in

one area (Infraction - Failure to Maintain Positive Control Over Individual

Entries to High Radiation Areas (269/287/79-20-01; 270/79-18-01) Paragraph 10).

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DETAILS

1.

Persons Contacted

Licensee Employees

  • J. E. Smith, Station Manager

R. M. Koehler, Superintendent of Technical Services

  • C. T. Yongue, Station Health Physicist

L. A. Blue, Health Physicist

S. R. Newcomb, Junior Health Physicist

J. Owens, Health Physics Supervisor

T. A'exander, Health Physics Supervisor

C. Harlin, Junior Health Physicist

D. Davidson, Health Physics Supervisor

D. Yoh, Shift Supervisor

  • R. T. Bond, Technical Services Supervisor.
  • D. Dalton, Quality Assurance Engineer

Other licensee employees contacted included five technicians, two operators,

two mechanics, and three office personnel.

  • Attended exit interview

2.

Exit Interview

The inspection scope and findings were summarized on August 10, 1979 with

those persons indicated in Paragraph I above. The Station Manager acknow-

ledged the item of noncompliance. With regard to the training of utility

operators, the Station Manager stated that presently employed operators

would complete the formal training program prior to December 31, 1980. He

further stated that in the future utility operators would only be assigned

to perform tasks for which they have been trained and qualified. The

inspector outlined the NRC's program for increased surveillance of activi-

ties related to the transportation of radioactive material. The following

areas were discussed: NRC inspection of shipments received at burial

sites, compliance with Department of Transportation regulations and burial

site licenses and adherance to requirements in certificates of compliance

for NRC approved containers.

3.

Licensee Action on Previous Inspection Findings

(Closed) Noncompliance (269/287/78-27-01; 270/78-26-01), Failure to Keep

Entrance to High Radiation Area Locked.

During tours of the plant, the

inspector observed that new hollow-metal doors with metal frames and

automatic closer had been installed.

The inspector had no further

questions.

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4.

Unresolved Items

Unresolved items were not identified during this inspection.

5.

Radioactive Effluent Release Report

Technical Specification 6.6.1.4 requires that a report on the radioactive

discharges released from the site be submitted to the NRC semiannually. An

inspector reviewed the plants Semi-annual Radioactive Effluent Release

Report for the period of July 1978 through December 1978 and discussed the

report with licensee representatives. The inspector had no further questions

concerning the report.

6.

Effluent Control Instrumentation

An inspector observed the alarm / trip setpoints for the low pressure service

water monitors (RIA-31 and RIA-35) and the liquid waste discharge line

monitors (RIA-33 and RIA 34) and verified that the setpoints for the monitor

were set as required by plant procedure PT/0/A/230/01, " Radiation Monitor

Check."

7.

Radioactive Effluent Release Monitoring and Records

Technical Specification 3.9.8 specifies the sampling and monitorin require-

ments for radioactive material in liquid waste effluents.

An inspector

observed.the collection and analysis of a liquid sample from the Units 1

and 2 laundry and hot shower tank (LHST) "B" and verified that the collection

and analysis was performed in accordance with plant procedure HP/0/B/1000/60C,

Procedure for Sampling and Release Requirements for CTT, CMT, and LHST, and

the technical specification. The ins;.r-tor observed the discharge of the

contents of the LHST "B" and verified that the release was made in accordance

with plant procedure OP/0/B/1104/34, Laundry and !..t Shower Waste System -

Operations Procedure.

The verification included a review of the valve lineup

used and the setpoints for liquid radwaste discharge monitors (RIA-33 and

RIA-34). The inspector reviewed the completed liquid waste release permit

for the discharge and verified that the release w4s witLin the limits

established in the technical specifications.

8.

Solid Radioactive Waste Disposal

By review of records, chservations and discussions with licensee representa-

tives, an inepector reviewed the plants solid radioactive waste processing

and disposal program. The inspector selectively reviewed shipping records

for radioactive material shipped out during 1978 and 1979.

The shipments

appear to have been made in accordance with 10 CFR 71 and Department'of

Transportation regulations. The inspector had no further questions.

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9.

Licensee Audits

An inspector discussed the audit program related to radiation protection

and radioactive waste management with a licensee representat.ive and reviewed

the following audit reports:

a.

QA Audit 0-79-5, dated June 21, 1979, Audit of Technical Service

Department (includes health physics and chemistry).

b.

Surveillance 0-579/5, February 14-26, 1979 (whole body count, ALARA

program, dosimetry, HP personnel training and qualifications, exposure

records, dose extensions).

The inspector evaluated the frequency,

scope and followup action of radiation protection related audits and

had no questions.

10.

i;ostlug and Control

The inspector revieved the licensees posting, and control of radiation

areas, high radiation areas, airborne radioactivity areas, contamination

areas, radioactive material areas, and the labeling of radioactive material

Juring tours of the auxiliary buildings and Unit 3 reactor building.

Luring a tour on August 6, 1979, a set of keys was found in the doot leading

to the waste gas decay tank room. Although the waste gas decay tank room

was posted as a radiation area at the titre the keys were found, the keys

could have been used to < pen the door leading to most high radiation areas

in the auxiliary building.

No one was in the room at the time the keys

were found. A licensee representative stated that a check of the key

check-out records indicated the keys had not been signed out.

The inspector

stated that failure to maintain positive control over each individual entry

into high radiation area by maintaining control over keys to such areas is

in noncompliance (269/287/79-20-01; 270/79-18-01) with 10 CFR 20.203(c).

11.

External Radiation Dose Control

During tours of the plant, the inspector observed workers wearing TLD

a.

badges and pocket dosimeters.

The inspectors discussed the radiation

dose monitoring program with workers and licensee representatives. An

inspector reviewed the daily exposure control report for August 9,

1979 and the computer printout of doses for the quarter ending March 31,

1979 An inspector verified that radiation exposure history records

(NRC Form 4) required by 10 CFR 20.101(b) were on file for each indi-

vidual who had exceeded 1250 mrem for the calendar quarter.

b.

An inspectc reviewed the radiation dose monitoring program for diving

operations in the spent fuel pools associated with installing new

storage racks. Multiple TLDs are being worn by the divers to monitor

exposure to the whole body (head and trunk) and extremities.

The TLDs

are being read onsite by plant personnel.

Plant procedure.HP/0/

B/1000/65, " Issue and Readout of CaSO : Dy Dosimeter for Spent Fuel

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Pool Diving Operations" stated that periodic checks of the instrument

calibration would be performed using TLDs exposed to known doses.

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However, the procedure did not specify what action should be taken if

the check indicated the calculated internal reference light value was

different from the value determined the last time the instrument was

calibrated. The inspector commented that the procedure should state

how much the reference light value calculated during these checks

would be allowed to differ from the value determinad at the last cali-

bration before the instrument would require recalibration. A licensee

representative stated that the procedure would be reviewed to provide

an acceptable range for the checks. The procedure also states that

the TLD laboratory supervisor would be notified if the peak preheat

temperatures differed by more than 5 C from the previous reading

listed on the performance log. A review of the perfcrmance log

entries for the period of June 1979 through August 1979 revealed that

on five occasions the temperature differed by more than 5 C.

However,

the records did not indicate what specific action was taken as a

result of the preheat temperature readings being out of specification.

The inspector commented that the out-of-specification temperature

cc uld have resulted in error in the dosage assigned to the divers.

The station manager stated that a review of the dosage assigned the

divers would be conducted and the corrections made if necessary.

He

further stated that this review would be completed by September 1, 1979.

The inspector stated this would remain an open item (269/287/79-20-02;

270/79-18-02) pending coupletion of the review.

12.

Other Areas Inspected

An inspector reviewed the plants procedure for releasing material and

a.

equipment from the radiation control areas. Plant Procedure HP/0/B/

1000/09, Procedure for Removal of Items from Radiation Control Zones

(RCZ) or from Radiation Control Areas , requires that a radiation and

smear survey be performed on items prior to their release.

The in-

spector reviewed the survey results of a Dillion Dynamometer (serial

No. 3338) that was released for unrestricted use on November 13, 1978.

The radiation levels and removable surface contamination levels were

below the release limits established for the plant. The inspector had

no further questions concerning the release of equipment from radia-

tion control areas or zones.

b.

An inspector reviewed the corrective action taken to prevenc a recur-

rence of an incident which occurred on December 5,1978.

A small

shielded cask used to transfer incore material fell from a truck as

the truck was being backed down the ramp providing access to the Unit

2 reactor building equipment hatch. The cask is used only for moving

material around the site and is not designed for off-site shipments.

An area of approximately 113 square feet was contaminated when approx-

imately one gallon of water spilled from the cask. The area was

promptly decontaminated. The inspector had no further questions.

Aninspectorreviewedtheradiologicalaspectsofspillso[ radio-

c.

active water from the Unit 3 Borated Water Storage Tank (BWST) on

May 16 and May 17, 1979. The Unit 3 fuel transfer canal was being

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pumped down to the Unit 3 BWST via the low pressure injection (LPI)

system. While the canal was being pumped down the BWST was being

recirculated using the BWST recirculation pump. Pressure buildup in

the BWST due to rapid filling from the LPI system caused the recirc :-

lation flow, which connect to the BWST tank overflow line, to go over

a 50 inch loop seal and into the liquid waste system. A valve in the

line leading to the radwaste system had been opened witheut a written

procedure. Upstream of where the four inch overflow line reduces to a

2 inch line, the west penetration room floor drain line ties in.

The

water backed up into the west penetration room, ran over a dam at the

door, down the steps and through a door to the outside.

It is esti-

mated that approximately 1000 gallons of water was released to the

west penetration room twice durirm the draining of the fuel transfer

canal on May 16 and 17, 1979, and approximately 100 and 200 gallons of

water respectively reached an area outside the Auxiliary Building

during each release. An area of approximately 100 square feet outside

the auxiliary building was contaminated. The area outside the auxil-

iary building and the nomally uncontaminated areas in the plant were

decontaminated and returned to uncontaminated status. Noncompliance

items concerning this incident were discussed in Region II inspection

report no. 269/270/79-14; 287/79-15 dated July 17, 1979.

d.

An inspector reviewed the radiological aspects of a release of radio-

active water to Lake Keowee on July 4, 1979 which resulted from a tube

leak in the low pressure injection (LPI) cooler A. At approximately

1:30 a.m.

on July 4, 1079, the radiation monitor in the low pressure

service water (RIA-35) reached the alarm setpoint. At the time M the

alarm, LPI cooler B was in use and cooler A was isolated.

The plant

isolated the B cooler and brought A cooler on line. Radioactive

concentration in the Low Pressure Service Water (LPSW) as measured by

RIA-35 increased significantly. At 6:30 p.m.

on July 4, 1979, it was

determined that a tube in the A cooler was leaking. The A cooler was

immediately isolated. The initial increase in activity in the LPSW

was caused by leakage passed an isolation valve. Analysis of samples

taken of LPSW indicated that apparently all activities were less than

the maximum permissible concentrations allowed by 10 CFR 20.

The LPSW

is a once through system and discharges to Lake Keowee after dilution

in the recirculating water system. Samples taken in the condenser

cooling water discharge indicated very low levels of radioactivity

present. The radioactivity levels returned to background levels on

July 11, 1979. The inspector had no further questions.

e.

On May 24, 1979, the laundry and hot shower tank (LHST) A was released

without prior sampling.

LHST B was sampled and was to be released.

However, the B pump was inoperative. A utility operator attempted to

line up the A pump to the B tank without benefit of a written proce-

dure. A misalignment was detected when a second operator was sent to

align the valves to flush the line. 2335 gallons were released to the

Keowee hydro tailrace. All activities in the unrestricted ,rea were

less than the maximum permissible concentrations allowed by 10 CFR 20.

The inspector reviewed the cortpctive action taken by the station in

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response to the incident. The inspector commented that the corrective

action did not address the training rnd qualification of the utility

operator who performed the initial valve line up.

The utility operator

is relatively new and during a review performed prior to signing the

operator qualification sheet, the utility operator could not demon-

strate that he had sufficient knowledge to line up the LHST for

sampling and analysis, yet he was given the task of performing the

valve line up to release the B tank. The inspector commented that

assigning an unqualified utility operator to perform the valve line up

contributed significantly to the incident.

The plant manager stated

that a formal qualification system has been developed and that all

currently qualified utility operators will complete the qualification

program prior to December 31, 1980. He further stated that only

qualified personnel would be assigned to perform task such as per-

forming valve line ups associated with the release of radioactive

liquid. The inspector stated that the qualification of utility

operators would be carried as an open item (269/287/79-20-03;

270/79-18-03) pending completion of the formal qualification program

for utility operators. Noncompliance items concerning this incident

were discussed in Region II Inspection Report 269/270/79-14;

287/79-15, dated July 17, 1979.

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