ML19248D005

From kanterella
Jump to navigation Jump to search
IE Insp Repts 50-329/79-09 & 50-330/79-09 on 790201-0329.No Noncompliance Noted.Major Areas Inspected:Site Conditions, Vendor Supplied Electrical Penetrations, Reactor Vessel Internal Storage & Mgt Meetings
ML19248D005
Person / Time
Site: Midland
Issue date: 05/07/1979
From: Cook R, Knop R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML19248D001 List:
References
50-329-79-09, 50-329-79-9, 50-330-79-09, 50-330-79-9, NUDOCS 7907300096
Download: ML19248D005 (6)


See also: IR 05000329/1979009

Text

.

4

.

U.S. NUCLEAR REGULATORY COMMISSION

OFFICE OF INSPECTION AND ENFORCEMENT

REGION III

Report No. 50-329/79-09; 50-330/79-09

Docket No. 50-329; 50-330

License No. CPPR-81; CPPR-82

Licensee:

Consumers Power Company

1945 West Parnall Road

Jackson, M1 49201

Facility Name:

Midland Nuclear Power Plant, Units 1 and 2

Inspection At:

Midland Site, Midland, Michigan

Inspection Conducted:

February 1 - !brch 29,1979

I' te { f o-

L

> / ' / ', c/

e

Inspector:

R. J. Cook

NN i be

'

/,{, f e ,/

l

,

s

Approved By:

R.C.

Knop, Chief

'/

Projects Section

Inspection Summary

Inspection on February 1

.'brch 29, 1979 (Report No. 50-329/79-09;

50-330/79-09)

Areas Inspected:

Examination of the site conditions, tensioning of

steam generator and reactor vessel hold down bolting, settlement of

diesel generator foundations and structures and associated settlement

monitoring program, inadequate crimping in vendor supplied electrical

penetrations, Unit 2 reactor vessel internals storage, adequacy of

decay heat removal pump technical maintenance information, fire in the

solid radwaste building, management meetings betweer. agional principa!

staf f members and licensee corporate personnel, welding of Unit 2 reactor

coolant system seismic supports / restraints, base line inservice inspection

preparations, safety practices of site radiographers, hydrostatic tesing

of Unit 2 incore instrument tank 2T-87, cable tray and wire installation

in the spreading rooms, and violations of QC Hold Tags.

This inspection

effort involved a total of 96 inspection hours by one NRC inspector.

Results:

No items of noncompliance or deviations were identified.

-

)

'

-

9

s

-

7907300096

.

.

.

DETAILS

Persons Contacted

  • D. Miller, Site Manager
  • J.

Corley, Quality Assurance Section Head IE and TV

  • B.

Peck, Construction Supervisor

  • P.

Kyner, Field Quality Assurance Engineer

D. Horn, Quality Assurance Engineer

  • L. Drei sbach, Bechtel Corporation Quality Assurance Engineer
  • E.

Smith, Bechtel Corporation Quality Assurance Engineer

  • D.

Hollar, Bechtel Corporation Quality Assurance Engineer

  • R.

Shope,

B6'..' Proj ec t Engineer

W.

Lee, B&W Construction Site Consultant

Numerous other principal staff and personnel were contacted during the

reporting period.

  • Denotes those present during at least one of the four exit interviews

conducted during the report period.

Licensee Action on Previous Inspection Findings

(Closed) Item of Noncompliance (329/78-13-02; 330/78-13-02):

B&W field

Procedure FCp No. 11 was developed to allow hydraulic tensioners to be

used for setting the steam generator and reactor holddown bolts at the

pretension level established by Drawing No. 376Q, Revision 8.

During

the reporting period, tensioning of Unit 2.

North Steam Generator

holddown bolts were v2*i.ossed.

The above referenced procedure was being

applied at this time.

Reportable Deficiencies - 50. 55 (e ) Items

Settlement of Diesel Generator Foundations and Structures

(open) Item of Noncompliance (329/78-13-03; 330/78-13-03):

During the

reporting period the licensee has informed the Resident Inspection of

additional soil borings and data which have been taken pertinent to

monitoring the settlement of the diesel generator building.

The prelim-

inary qualitative results of this data were subsequently relayed to

Regional Office Personnel. A Regional Based Inspector performed an

inspection onsite on March 28 and 29, 1979, to perform a quantitative

review of the settlement monitoring program (NRC Inspection Report No.

50-329/79-06; 50-330/79-06).

-

)

b

/

C, b '

J

-2-

.

.

Inadequate Crimpling '.n Vendor Supplied Electrical Penetrationg

During the reporting period, vendor representatives performed a visual

examination of six contamination electrical penetrations which had

exhibited discrepancies in the crimpling of terminations.

Their examin-

ation confirmed the results of previous inspections of the electrical

penetrations. Tae vendor has agreed to perform extended examinations of

all penetrations and to replace defective crimps.

The Resident

inspector was invited and attended a meeting between the licensee and

vendor to discuss the condition of the penetration.

Functional ar.d Program Areas Inspected

1.

Site Tours

At periodic intervals generalized site tours were conducted by the

Resident Inspector.

During the reporting period, these tours

particularly covered Units 1 and 2 containments, upper and lower

spreading rooms, safety related motor control centers, battery

rooms, penetration rooms, solid radwaste storage building, and

diesel generator building.

The se tours were intended to assess the

cleanliness of the site, storage condition of equipment and piping

being used in site construction; the potential f r fire or other

hazards which might have a dilatorious affect on pe sonnel and

equipment and to witness construction activities 1a progress.

2.

Unit 2 Reactor Vessel Internals Storage

The final storage condition of the partially assembled Unit 2

core barrel was examined.

The core barrel is positioned on the

st: age stand which is being supported by polyethylene covered

wood located on the floor of the fuel pool.

The core barrel is

drapped with polyethylene and has remained plum within the

required 0.010 inches per foot.

The licensee is constructing

temporary " clean room" with controlled access around the core

a

' arrel for continued assembly of the core barrel.

3.

Decay Heat Removal Pump Technical Literature

During a review of technical literature and drawings associated

with the assembly of impellers on the shaft of the decay heat

removal pumps, ambiquity was noted which relied heavily on the

experience of maintenance personnel to correctly assemble the

pumps.

T.ie licensee has agreed to insert clarifying information

and/or drawings to remove any uncertainties in future maintenance

work performed on these pumps.

W

J'

t

bJ

(j u \\

-3-

.

.

.

4.

Fire in the Solid Radwaste Building

At about 4:00 a.m., on February 4,

1979, the licensee experienced

a fire at the roof elevation (approximately 648 ft elevation) at

the south face of the westend of the solid radwaste building.

The

is attributed to a temporary gas operated unit heater being

cause

close to wood formers which ignited the formers and adjacent

scaffolding.

The Midland City Fire Department responded to the

fire alarm and brought assistance to fire fighters onsite.

Minimal

damage to the building and no serious personnel injuries were

sustained.

5.

Manaaement Meetincs

On February 7, 1979, principal NRC Region III staff met with

representatives of Consumer Power Company senior corporate staff

and senior Bechtel Corporation Midland Staff members at the

Midland Site.

The Resident Inspector attended these meetings.

Details pertinent to these meetings are discussed in NRC

Inspection Reports No 50-329/79-04; 50-330/79-04.

6.

Welding of Unit 2 Reactor Coolant System (RCS) Seismic Supports /

Restraints

During the installation of seismic support / restraints for the RCS

in Unit 2 containment, linear indications of cracking of inbeds has

been experienced.

This cracking has been taued in B&W Nonconform-

ance Report No. 459 and subsequent repairs of linear indications

are documented in the B&W Minor Repair Procedure file.

On

February 6-8, 1979, a Regional Based Inspector performed an

inspection and reviewed the licensee's activities pertinent to

repair of these linear indications.

7.

Base Line Inservice Inspection

During the reporting period the Resident Inspector was informed

that the licensee was developing scheduling plans and procedural

details for performance of the base line inservice inspection.

The licensee stated that actual NDE is scheduled to start in May,

1979.

8.

Site Radiographers

During the reporting period, radiographers from X-Ray Engineering,

Company were observed working on the night shift.

Radiation areas

were marked, personnel were in attendance, and survey meters

appeared to be in use.

1'

J

)"

,

- 4-

.

.

.

Du. ing the reporting period B&W has experienced some personnel

changes in the night shift radiography crews.

Some discrepancies

have been noted by the licensee pertinent to safe operation.

B&W

has attempted to rectify these discrepancies by procuring addi-

tional experienced radiographers.

The licensee was observed

performing an overview inspection of the B&W radiographers.

The

Resident Inspector was informed that minor discrepancies were noted

in posting of radiation areas.

9.

Hvdrostatic Test of Unit 2 Incore Instrument Tank 2T-87

The licensee performed a hydrostatic test of Unit 2 Incore

Instrument Tank 2T-87.

However, it appeared that portions of two

vertical welds which penetrate the floor area at about the 626 foot

elevation could not be physically examined to e ablish zero

leakage using the techniques employed.

This was subsequently

established to be a potential item of noncompliance during the next

reporting period.

10.

Cable Tray and Wire Installation

During the report period cable pan and wire installation in the

spreading rooms was inspected.

Sharp edges were noted at the

inside surface of cable pan IBFB01 into 1RJG01 located in the upper

spreading room.

These sharp edges were pointed out to the

licensee. At the time frame that these " sharp edges" were noted

the licensee had identified weakness in the program which allowed

personal judgement to determine if a need exists for placing edge

protectors on sharp edges based on how the sharp edge might tend to

affect a given cable pull.

The affects of sharp edges on indi-

vidual cables, once the cable pan was filled, was not necessarily

considered for the need and placement of edge protectors.

The

licensee has added additional edge protectors to those locations

addressed in the Nonconformance Reports; instructed Electrical QC

Engineers in cable installation with emphasis on the use of edge

protectors; and modified QC Instructions to include those locations

where a cable presses against a sharp edge.

11.

QC Hold Tac Violations

During the inspection of cable pan and wire installation in the

upper spreading room (referenced above), a QC Hold Tag No. NCR 1727

was noted on cable pans designated IBGB, IBFB, IBFA, and IBGA. The

hold tags were placed because of pan identification markings not

1,

1\\

-

J"

.

(

-5-

.

being in agreement with Drawing No. E-642(Q) SH.

1, Revision 6.

It

was noted that the hold tags were inconspicuous 1y placed at the

opposite end of the cable can from where cable was being installed

and cables were pulled into these pans without a conditional

release from the NCR placing the hold tags.

The licensee had previously identified that violations of hold tags

had occurred and was able to demonstrate this by letters which had

been exchanged among management personnel, NCR's written addressing

violations of Hold Tags, and the existance of a Hold Tag Violation

File.

The licensee has given additional instructions to QC

Engineers in the use of Hold Tags with emphasis on placing Hold

Tags in such a manner as to be recognized by construction per-

sonnel; issued a strong letter from the Bechtel Power Corporation

Project Superintendent ir.sisting that procedura! requirements

concerning hold tags are strictly adhered to; and demonstrated

strong management reaction to violations of QC Hold Tags.

Because the licensee has taken dramatic action to curb violations

of QC Hold Tags, and because this action appeared to be in progress

prior to the Resident Inspector noting a violation of Hold Tags and

these actions have emphatically continued, violations of QC Hold

Tags is considered an unresolved item.

This item shall remain

unresolved until such times that it has been demonstrated (or

cannot be demonstrated) that the licensee's actions have become

effective in curbing violations of QC Hold Tags and is able to

adequately adJress isolated intances should they occur with good

reason. Unresolved Item (329/79-09-01; 330/79-09-01).

Unresolved Matters

Unresolved items are matters about which more information is required in

order to ascertain whether they are acceptable items, items of noncom-

pliance or deviations.

One unresolved item disclosed during the

inspection is discussed in Paragraph 11.

Exit Interview

The Resident Inspector attended the Exit Interview conducted by 1. Yin,

P. Ba r re t t , and E. Gallagher, RIII Reactor Inspectors on February 8 and

9; and March 29, 1979, respectively.

The Resident Inspector met with licensee representatives (denoted under

Persons Contacted) on February 2, February 15, February 21, and March 20,

1979.

The inspector summarized the scope and findings of the inspection

effert to date.

The licensee acknowledged the findings reported herein.

m

/

J"

is

-6-

(