05000368/LER-1979-037-03, /03L-1 on 790514:supply Valves 2CV-1039-2 & CV-1076-2 to Steam Generator 2E24B Would Not Respond During Mode 3 Operation.Caused by Blown Fuse & Stuck Relay.Repairs Made & Valves Proven Operable

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/03L-1 on 790514:supply Valves 2CV-1039-2 & CV-1076-2 to Steam Generator 2E24B Would Not Respond During Mode 3 Operation.Caused by Blown Fuse & Stuck Relay.Repairs Made & Valves Proven Operable
ML19241B166
Person / Time
Site: Arkansas Nuclear Entergy icon.png
Issue date: 07/06/1979
From: Shively C
ARKANSAS POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19241B163 List:
References
LER-79-037-03L, LER-79-37-3L, NUDOCS 7907120660
Download: ML19241B166 (1)


LER-1979-037, /03L-1 on 790514:supply Valves 2CV-1039-2 & CV-1076-2 to Steam Generator 2E24B Would Not Respond During Mode 3 Operation.Caused by Blown Fuse & Stuck Relay.Repairs Made & Valves Proven Operable
Event date:
Report date:
3681979037R03 - NRC Website

text

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