05000368/LER-1979-042-03, /03L-0 on 790607:reheat Stop Valve 4 Would Not Open During Mode 1 Operation W/Main Turbine Latched. Caused by Mechanical Binding of Reheat Stop Valve to Seat. Valve Freed & Trip Tested

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/03L-0 on 790607:reheat Stop Valve 4 Would Not Open During Mode 1 Operation W/Main Turbine Latched. Caused by Mechanical Binding of Reheat Stop Valve to Seat. Valve Freed & Trip Tested
ML19241B165
Person / Time
Site: Arkansas Nuclear 
Issue date: 07/06/1979
From: Shively C
ARKANSAS POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19241B163 List:
References
LER-79-042-03L, LER-79-42-3L, NUDOCS 7907120654
Download: ML19241B165 (1)


LER-1979-042, /03L-0 on 790607:reheat Stop Valve 4 Would Not Open During Mode 1 Operation W/Main Turbine Latched. Caused by Mechanical Binding of Reheat Stop Valve to Seat. Valve Freed & Trip Tested
Event date:
Report date:
3681979042R03 - NRC Website

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[#4 Reheat Stop Valve would not open. At 1 cast one turbine i

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i__mt, t iL A'PTION l ' ! o l Llibt N A I !i1iiii!Iiri1 we cF PntPang, Chris N. Shively 503/968-2519 mo a p(7 t.U C 7 907120[$M