05000302/LER-1979-060-03, /03L-0 on 790613:containment Purge Isolation Valves Had Excessive Seat Leakage.Caused by Improper Seating of Valves.Adjustments Were Made

From kanterella
(Redirected from ML19225A180)
Jump to navigation Jump to search
/03L-0 on 790613:containment Purge Isolation Valves Had Excessive Seat Leakage.Caused by Improper Seating of Valves.Adjustments Were Made
ML19225A180
Person / Time
Site: Crystal River Duke Energy icon.png
Issue date: 07/06/1979
From: Cooper J
FLORIDA POWER CORP.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19225A175 List:
References
LER-79-060-03L, LER-79-60-3L, NUDOCS 7907180524
Download: ML19225A180 (2)


LER-1979-060, /03L-0 on 790613:containment Purge Isolation Valves Had Excessive Seat Leakage.Caused by Improper Seating of Valves.Adjustments Were Made
Event date:
Report date:
3021979060R03 - NRC Website

text

s N RC F Qf1M ::4

(*

U. S. NUCLC AA R E CULAf onY C:Mu s s.sicre (7 771 LICENSEE EVENT RE? ORT EXHIBIT A CONinct stoc<.1 I

f-t I

i l@

tetr Ast maer on tvee att aEcusaEs i sonMATICM 1 g -i _;g 0 0 j Oj 0 l

0 ; O g 4 ; l l;l 01 1

i i

r o li l F i Li CR(Pt3ig,0l0l-1

..e s m m i.

.m s,. s. -

coa. r ojij I t raj o r 510 i -!0 I 3t0 i 2 P: og si i i al vi o G[ ni,i n I a l - t,. i @

awa'

..v.$

at w r :4r e

.2 v.2 sav ct a

- v.i
o r s..,s u es=:a4:4 s

w EvtNT OEsCm* TION AND 8A0SaaLE CONsE0t,ENCEs h o 121 l It -aas discovered durine the'norfor anco of c u r o i l !,n -o nrocedure I

ai2 i i sp-170 t ',, t the

- ent,4n-one

,,,-,o

,2,1,reen

.,1.. n c T H'.' 1A& 1B had I

o 64 I excessive seat le davo.

It cas than d e t o r-i od on 10 Tun a. th at eSta

-,,*.>.1 3.,

an*

.,nn*-,.-

",-b.,4,4 1

C.,, - 4 c 4

,,*J--

1A 1

% & 3 O $. I' 2.

'N O l

  • )

l 4

o is f effect unen tho n17-t or conorql nublic 1 the n1 7,t 'n c in 7 sofo I

]

^#

tbia

  • '."o [0 t 7 I l shi: Pin %n c'ndition.

This la the #irst O c a ' "

  • o n_ n e
i.i renorted.

I

'O F

5 9 svsrsu

i;se
.si s.

c:ea sa ::::

.:st.: :::

sa :::1 3a :::a ci+1 isfcl@ QlG I B IS IV 1 A ! LI VI d X IG f BlQ l Dl 9 v

v v

- w
- v 7

8 9

'3 11 il i'

's

+r at.ss :q C':7.-4 8 (.:!

a g s t. e

  • s l e.'J i s
  • i a.

i se

=i =rsa c >:

@so*..!asisri.a ti at :" l7 I al

[-J

! n I c, t of 1t inI,i I i!

l-i i n!

sea L v u

.s u

s v (sss:-

3..

  • :r g.

e a -

,a!.1 s a a :.;

sa vg _ ue

...:., gy v acTi:s.

.e e, a !

.3.es'

+i*-::

C. a g I :.' t s y l.** ** !

  • 8:89 s.s

!.88 ta var. se:..ega rAAg-

' :s P

L.2. e@l.iOy

! 8_.

i Wu i nin in oi h!G i; G A :(D l pl 31 af M et

..-v

,, s.

~

s cA ss :E s =i a r: 0 a. A.: ::= = E:. is E ::- :'.s L :"

v ileil The cause of this event is attributed to imorocar seatin2 of f

it i

valves AHV 1A & R.

Adiustrents *;ero ade en AHV-1A & 19 and f

I the leaka'e rate 'ans reduced to eichin 11 ! n'aM li its 16 Tune 1070

,i; I I

I tii4, i 50 7

3, 4 : r...,

o er -:: :=

n e

sr.ra

,,:ns-

-s v2-.s b
s::. 4 = -
s :.i :n: -:. m tiit Ic,I S i af of c6f

':A I

I 3 GI Le n r,te test I

v

- s v

.2

.: rm r, o

u

.i 7

s ist q

. i,. c. s i : : n.im

... :..s r :. i, u v t c a :s : =1.12:a e

':A I

l s: -

I 1,1J@ 1!@l i I6 i

i,

.2

. s :s. a

< i.> 2s. u s

s s......:s @

s o....

ti7l 1 n I nI n@li @l I

': A y

a e ie t.'

so sta$:ssigis;,m t!

l' NLv?te

g3;eie' s G [I llid { q l nl I

'i t r

s.=

i r:

as c.s :s := : v a t : e e:..t e-O,'

.*~st

ss.co.:.

w 1.

r J

, 1o l

, i 4 'l

?s-

.a v --

.? e, g % Ot t;s ** :s s : e.; E e, t r

~. *.. ' ~

iii: i tiiii iil j_!ul W g!

n n

na i

s,

,2 w

s,..,,Q',Q h_aJ. Co op e r, J r.

(904j 705-6486 7 90718osM (S

7 3

- Xi T A C'c..r 'J S U.". 7.". _.'4m:<.v.
7..'.' ~c C ',..i.~i. C '.' S '.3.r r ~.' )

c.

m

,3 bhI L. i l-

SUPPLEMENTARY INFOR"ATION Report No.

5 0-302 / 7 9-060/13L-0 Facility:

Crystal River Unit 3 Report Date:

05 July 1979 Occurreice Date:

13 June 1979 Identif ation of Occurrence:

Combined containment leakage rate greater than the limits specified in Technical Specification

3. 6.1. 2. b., and, containment penetration inop-erable contrary to Technical Specification 3.9.4.C.2.

Conditions Prior to Occurrence:

Mode 5 cold shutdown.

Description of Occurrence:

It was discovered during the performance of the contain=rce leakage test types B & C SP-179, tha'. the containment purge isolation valves ARV-:A & 13 had excessive seat leakage.

It was later determined on 19 June through the discovery of a calculation error, that the leakage had exceeded the combined con-tainment leakage rate limit of.60La allowed by Technical Specifications.

Maintenance, performed upon initial discoverv of the leak-age reduced the ccmbined containment leakage rate to within allowed limits 16 June 1979.

Designation of Apparent Cause:

The cause of this event is attributed to im-proper seating of valves AHV-1A and AHV-13.

Analysis of Occurrence:

Core alterations were made prior to determi-nation that the combined containnent leakage rate was outside Technical Specification limi-tations.

No effect upon the plant or general public as the plant remained in a safe shut-down condition.

Corrective Action

A shim adjustment was made to the pivot point on AHV-1A.

Adjustments were made on the seat-ing edge and the torque arm of AHV-13.

The adjustments to both valves reduced the leakage rate to within allowed limits.

A procedure revision to SP-179 has also been implemented to clarify the calculations.

Failure Data:

This is the first occurrence of this type reported.

J 4 l7

^7f 7, ! -

LI s