05000348/LER-1978-043-03, /03L-0 on 780624:FNP-O-STP-12.0 Had Not Been Performed Between 780611-24.Caused by Incorrect Scheduling. Personnel Notified & Surveillance Schedule Reviewed

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/03L-0 on 780624:FNP-O-STP-12.0 Had Not Been Performed Between 780611-24.Caused by Incorrect Scheduling. Personnel Notified & Surveillance Schedule Reviewed
ML19224D343
Person / Time
Site: Farley Southern Nuclear icon.png
Issue date: 07/14/1978
From:
ALABAMA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19224D336 List:
References
LER-78-043-03L, LER-78-43-3L, NUDOCS 7907110415
Download: ML19224D343 (1)


LER-1978-043, /03L-0 on 780624:FNP-O-STP-12.0 Had Not Been Performed Between 780611-24.Caused by Incorrect Scheduling. Personnel Notified & Surveillance Schedule Reviewed
Event date:
Report date:
3481978043R03 - NRC Website

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8 60 64 OOCKET NUMSER 6d 63 EVENT DATE 74 75 REPORT DATE 40 EVENT DESCRIPTION AND PROSABL'l CONUQ';ENCES h 2 l At 0500 on 6/24/78 it was noted that FNP-0-STP-12.0 had not been nerformed between Q 16/11/78 an' '!24/78. This interval of 13 days is in excess of the 7 day t 25% interv7

'@ I specified in Technical Specification 4.5.4.1. FNP-0-STP-12.0 was perforned imediatel-O land the BIT was demonstrated operable as per Technical Specification 4.5.4.1.

The 9 lhealth and safety of r_ne eeneral oublic was not affected.

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[ l Schedule B for June, 1978 incorrectly scheduled FNP-0-STP-12.0 as a 31 day interval O linstead of the recuired 7 day interval. Personnel involved were notified and a revie g jof the Surveillance Schedule was performed.

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