ML19210D013

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LER 79-101/03L-0:on 791017,safety Rod 8 Absolute Position Indication Would Not Respond to Rod Movement During Rod Control Exercises.Cause Unknown.Further Investigation Scheduled
ML19210D013
Person / Time
Site: Crystal River Duke Energy icon.png
Issue date: 11/09/1979
From: Lancaster K
FLORIDA POWER CORP.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19210D007 List:
References
LER-79-101-03L, LER-79-101-3L, NUDOCS 7911200415
Download: ML19210D013 (2)


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s P SUPPLEMENTARY INFORMATION Report Number: 50-302/79-101/03L-0 Facility: Crystal River Unit #3 Report Date: 9 November 1979 Occurrence Date: 17 October 1979 Identification of Occurrence:

Inoperable absolute position indication for Rod 8 Group 1 contrary to Technical Specification 3.1.3.3.

Conditions Trior to Occurrence:

Mode.1 power operation (98%).

Description of Occurrence:

At 2300, in Mode 1, it was discovered that safety rod 1-8 absolute rod position indication would not respond to red movement during the. performance of SP-333, Control dod Exercises.

Rod 1-8 position was verified at 2340 at 100% withdrawn. Control rod position is'being verified at 100% withdrawn every eight (8) hours.

Designation of Apparent Cause:

The cause of this event is unknown.

Analysis of Occurrence:

No effect upon the plant or general public. Relative rod position indication for Rod 1-8 was operable.

Corrective Action:

Further investigation will be conducted during subsequent sur-veillance activities. Corrective action will be based upon the results of that investigation. P.I. tube will be replaced during next plant outage.

Failure Data:

This is the second occurrence of this type reported for Rod 1-8.

Reference LER 79-79.

/rc 1363 338