05000483/LER-2019-003, Reactor Trip Due to Source Range Hi-Flux

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Reactor Trip Due to Source Range Hi-Flux
ML19196A093
Person / Time
Site: Callaway 
Issue date: 07/15/2019
From: Bianco F
Ameren Missouri, Union Electric Co
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
ULNRC-06521 LER 2019-003-00
Download: ML19196A093 (7)


LER-2019-003, Reactor Trip Due to Source Range Hi-Flux
Event date:
Report date:
Reporting criterion: 10 CFR 50.73(a)(2)(iv)(A), System Actuation

10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded

10 CFR 50.73(a)(2)(viii)(A)

10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

10 CFR 50.73(a)(2)(viii)(B)

10 CFR 50.73(a)(2)(iii)

10 CFR 50.73(a)(2)(ix)(A)

10 CFR 50.73(a)(2)(x)

10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor

10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat

10 CFR 50.73(a)(2)(v), Loss of Safety Function

10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown

10 CFR 50.73(a)(2)(vii), Common Cause Inoperability

10 CFR 50.73(a)(2)(i)

10 CFR 50.73(a)(2)(iv)(A)(1)

10 CFR 50.73(a)(2)(iv)(A)(6)
4832019003R00 - NRC Website

text

Ameren MISSOURI July 15, 2019 Callaway Plant U.S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, DC 20555-000 1 Ladies and Gentlemen:

ULNRC-0652 1 10 CFR 50.73 DOCKET NUMBER 50-483 CALLAWAY PLANT UNIT 1 UNION ELECTRIC COMPANY RENEWED FACILITY OPERATING LICENSE NPF-30 LICENSEE EVENT REPORT 2019-003-00 REACTOR TRIP DUE TO SOURCE RANGE HI-FLUX The enclosed license event report is submitted in accordance with 10 CFR 50.73(a)(2)(iv)(A) to report a reactor protection system actuation during startup and an auxiliary feedwater system actuation due to a plant trip caused by Source Range Hi-Flux.

This letter does not contain any new commitments Executed on:

I )ic)19 Enclosure LER 20 19-003-00 Sincerely, Senior Director, Nuclear Operations

$3 15 County Road 459 Steedman, MO 65077 AmerenMissouri.com

ULNRC-0652 1 July 15, 2019 Page 2 of 3 cc:

Mr. Scott A. Morris Regional Administrator U. S. Nuclear Regulatory Commission Region IV 1 600 East Lamar Boulevard Arlington, TX 76011-4511 Senior Resident Inspector Callaway Resident Office U. S. Nuclear Regulatory Commission 8201 NRC Road Steedman, MO 65077 Mr. L. John Klos Project Manager, Callaway Plant Office ofNuclear Reactor Regulation U. S. Nuclear Regulatory Commission Mail Stop 09E3 Washington, DC 20555-0001

ULNRC-0652 1 July 15, 2019 Page 3 of 3 Index and send hardcopy to QA File A160.0761 Hardcopy:

Certrec Corporation 6100 Western Place, Suite 1050 Fort Worth, TX 76107 (Certrec receives ALL attachments as long as they are non-safeguards and may be publicly disclosed.)

Electronic distribution for the following can be made via LER ULNRC Distribution:

F. M. Diya T. E. Herrmann B. L. Cox F. J. Bianco S. P. Banker L. H. Kanuckel R. C. Wink T. B. Elwood Corporate Oversight NSRB Secretary Performance Improvement Coordinator Resident Inspectors (NRC)

STARS Regulatory Affairs Mr. Jay Silberg (Pillsbury Winthrop Shaw Piftman LLP)

Missouri Public Service Commission

NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY 0MB: NO. 3150-0104 EXPIRES: 0313112020 (04-2018)

, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.

3. Page Callaway Plant Unit I 05000-483 i of 4
4. Title Reactor ThD duto Source Ranae Hi-Flux
5. Event Date
6. LER Number
7. Report Date
8. Other Facilities Involved
zti Day L

Year YEAR Seuenbaj Monthay Year Facility Name Docket Number 05 16 2019 2019 003 00 07 15 2019 FacilityName Number

9. Operating Mode
11. This Reportis Submitted Pursuanttothe Requirements offO CFR: (Check all that apply) i: 20.2201 (b)

D 20.2203(a)(3)(i)

Q 50.73(a)(2)(ii)(A)

Q 50.73(a)(2)(viii)(A) 2 20.2201 (d)

D 2O.2203(a)(3)()

0 50.73(a)(2)(i)(B) l 50.73(a)(2)(viii)(B) 0 20.2203(a)(1) l 20.2203(a)(4) fl 50.73(a)(2)(iii)

Q 50.73(a)(2)(ix)(A) i: 202203(a)(2)(i)

D 50.36(c)(1)(i)(A) 5073(a)(2)(iv)(A)

Q 50.73(a)(2)(x)

10. Power Level Q 20.2203(a)(2)(ii)

Q 50.36(c)(1)(ii)(A) 11 50.73(a)(2)(v)(A)

Q 73.71 (a)(4)

D 20.2203(a)(2)(iii) fl 50.36(c)(2) 50.73(a)(2)(v)(B)

Q 73.71 (a)(5) i: 20.2203(a)(2)(iv)

Q 50.46(a)(3)(ii)

Q 50.73(a)(2)(v)(C)

Q 73.77(a)(J) 000 D 20.2203(a)(2)(v)

Q 50.73(a)(2)(i)(A)

Q 50.73(a)(2)(v)(D)

Q 73.77(a)(2)(i) i: 20.2203(a)(2)(vi)

Q 50.73(a)(2)(i)(B) 50.73(a)(2)(vii) 73.ZZ(a)(2)(ii) 0 50.73(a)(2)(i)(C)

J OTHER Specify in Abstract below or in NRC Form 366A

12. Licensee Contact for this LER icenaee Contact elephone Number (Include Area Code)

Supervising Engineer,Reulatory Affairs and Licensing 314-225-1905

13. COMPLETE ONE UNE FOR EACH COMPONENT FAILURE DESCRIBED IN ThIS REPORT TManufficturefabIos
14. Supplemental Report Expected Month I oJ Year Yes(ffiyes,cometeJ5EXPECTEDSUBFvNSSION DATE)No J50 BSTRACT (Limitto 1400 spaces, i.e., approximately 14 single-spaced typewritten lines) t 2303 on May 16, 2019, Callaway planttripped during reactor startup due to a Source Range (SR) Hi-Flux trip signal, vhich resulted in reactor protection system and auxiliary feedwater system actuations. The control room operators failed to block the SR Hi-Flux trip prior to reaching the setpoint of 10E5 counts per second. All plant systems responded as expected.

nalysis identified the following causes and contributing causes:

I The Reactor Operators did not have an appropriate strategy for monitoring SR detector count rate relative to other critical parameters that were being monitored.

2.

The Control Room Supervisor was also fulfilling the role of Reactivity Management Senior Reactor Operator but became distracted from this primary function. The reactor startup procedure required going to several attachments and performing lower priority steps prior to blocking the SR Hi-Flux trip, thus delaying performance of this action.

3.

The reactor startup procedure did not support expeditious action to block the SR Hi-Flux trip.

4.

Operators were not aware of the time constraints when blocking the SR Hi-Flux trip.

Corrective actions include revising the reactor startup procedure to ensure the correct monitoring behaviors and revising he standard to require an additional Senior Reactor Operator who can focus solely on reactivity control.

NRC FORM 366 (04-2018)U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY 0MB: NO. 3150-0104 EXPIRES: 313112020 (04-2018)

, the NRC may not conduct or http://www.nrcqov/readinq-rm/doc/colledions/nuregs/staff/srl 0221r31) sponsor, and a person is not required to respond to, the information collection.

1. FACILITY NAME
2. DOCKETNUMBER
3. LERNUMBER YEAR SEQUENTIAL REV Callaway Plant Unit I 05000-483 NUMBER NO.

2019

- 003 00
1. DESCRIPTION OF STRUCTURE(S), SYSTEM(S),AND COMPONENT(S):

The reactor trip system at Callaway Plant includes a Source Range (SR) Hi-Flux reactor trip [EIIS System: ABJ, Component: Xl] function with a setpoint of 10E5 counts per second. The P-6 bistable [ENS System: AB] is an interlock that ensures the intermediate range instrumentation is properly monitoring reactor power, prior to blocking the SR trip setpoints and relying on the intermediate range instrumentation during reactor startup (approach to critical). When one channel of the intermediate range instrumentation picks up (at approximately I OE-1 0 amperes), the P-6 bistable activates, allowing the SR Hi-Flux reactor trip to be blocked.

2.

INITIAL PLANT CONDITIONS

Callaway was at 0% Power/Mode 2 at the discovery time of this event.

3.

EVENT DESCRIPTION

Control room operators failed to block the SR Hi-Flux reactor trip in time after the P-6 bistable interlock was reached, resulting in an automatic reactor trip. The following describes the sequence of events leading up to this event, the causes and contributing causes of the event, and corrective actions taken to prevent recurrence of such an event.

On May 16, 2019 at 1900, control room operators began to perform a reactor startup to conclude refuel 23 and resume plant operations. At approximately 2000, a dilution was performed to get reactor coolant system (RCS) [EIIS System:

ABJ boron concentration within 10 parts per million ofthe estimated critical position boron requirement. While the control room operators waited for proper RCS boron mixing, a review of the reactor startup procedure was performed.

At 2100, a status brief was held to discuss an overview of reactor startup performance, continuous actions, individual roles, and actions to address blocking the SR Hi-Flux trip.

At 2224, the plant procedurally entered Mode 2 with SR instruments N31 and N32 indicating 220 counts per second and 340 counts per second, respectively. At 2226, reactor startup was commenced by withdrawing A Control Bank in 50 step increments. At 2248, D Control Bank withdrawal to 5 steps was complete. When the SR count rate was stable, the Inverse Count Rate Ratio (ICRR) measurement was performed. An alternate ICRR was performed using the plant computer which permits using the plot to ensure data points were taken at stable conditions. The ICRR using the alternate method predicted criticality for both source range instruments channels with the D Control Bank at 60 steps.

At approximately 2300, the D Control Bank was withdrawn and reached a transient startup rate (SUR) of 0.5 decades per minute (dpm), at which time it was stopped at 45 steps. After observing lowering of the SUR, it was determined that criticality had not been achieved. At approximately 2301, the rods were withdrawn to 55 steps for the D Control Bank.

When the control room operators began to withdraw rods again, the SUR was approximately 0.2 dpm and lowering.

The N31 and N32 SR instruments indicated approximately 4500 counts per second and approximately 9100 counts per second, respectively.

At 23:01 :43, the rods in D Control Bank at were stopped at 55 steps. The SUR was 0.7 dpm, which immediately dropped to 0.4 dpm and lowering. SR instruments N31 and N32 indicated approximately 6000 counts per second and approximately 13000 counts per second, respectively. Simultaneously, the P-6 bistable light lit. An informal announcement was made that P-6 was lit, which was heard by several control room operators. The SR count value was not observed after completing the rod withdrawal, and the control room operators were unaware they were approaching the SR Hi-Flux trip setpoint of 10E5 counts per second.Page 2 of 4U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY 0MB: NO. 3150-0104 EXPIRES: 313112020 (04-2018)

, the NRC may not conduct or hftp://www.nrc.gov/readinq-rm/doc/collections/nureqs/staff/srl 0221r31) sponsor, and a person is not required to respond to, the information collection.

1. FACILITY NAME
2. DOCKETNUMBER
3. LERNUMBER YEAR SEQUENTIAL REV Callaway Plant Unit I 05000-483 NUMBER NO.

2019

- 003 00 At approximately 23:02:40, the control room operators began to perform the steps in the procedure to block the SR Hi-Flux trip. At 2303, the SR Hi-Flux reactor trip annunciator was received and the reactor tripped. The control room operators performed the required immediate actions and stabilized the unit in Mode 3.

Since feedwater was isolated in response to the reactor trip, concurrent with low RCS average temperature at 564F, the Balance-of-Plant Operator manually started both auxiliary feedwater pumps and established flow to all four steam generators due to lowering steam generator water levels. The control room operators then transitioned to Normal Unit Recovery Guideline Following Reactor Trip.

At the time of the trip, the reactor had not yet been declared critical. All systems responded as expected.

4. ASSESSMENT OF SAFETY CONSEQUENCES

There were no actual nuclear, radiological, or personnel safety impacts associated with this event. The potential impact was on nuclear safety, with respect to challenging a reactor trip setpoint. All equipment functioned as designed, and the reactor automatically tripped (i.e., shutdown) per design when the SR Hi-Flux setpoint was reached.

5. REPORTING REQUIREMENTS

This LER is submitted pursuant to 50.73(a)(2)(iv)(A) to report a reactor protection system actuation during startup and an auxiliary feedwater actuation.

Specifically, 10 CFR 50.73(a)(2)(iv)(A) states in part, The licensee shall report:

(A) Any event or condition that resulted in manual or automatic actuation of any of the systems listed in paragraph (a)(2)(iv)(B) of this section...

(B) The systems to which the requirements of paragraph (a)(2)(iv)(A) of this section are:

(1) Reactor protection system (RPS) including: reactor scram or reactor trip....

(6)

PWR auxiliary or emergency feedwater system The RPS was actuated on May 16, 2019, at 2303, during startup. This fulfills the reporting requirement of 10 CFR 50.73(a)(2)(iv)(A) by actuation ofthe system specified in 10 CFR 50.73(a)(2)(iv)(A)(1).

A valid auxiliary feedwater system actuation was manually initiated as a direct consequence of the lowering of the steam generator water levels (due to the main feedwater isolation that occurred in response to the reactor trip). This fulfills the reporting requirement of 10 CFR 50.73(a)(2)(iv)(A) by actuation ofthe system specified in 10 CFR 50.73(a)(2)(iv)(A)(6).

6. CAUSE OF THE EVENT

The following causes or contributing causes were identified that lead to this reactor trip:

I The reactor operators did not have an appropriate strategy for monitoring SR detector count rate relative to other critical parameters that were being monitored.

2.

The Control Room Supervisor was also fulfilling the role of Reactivity Management Senior Reactor Operator but became distracted from this primary function. The reactor startup procedure required going to severalPage 3 of 4U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY 0MB: NO. 3150-0104 EXPIRES: 313112020 (04-2018)

, the NRC may not conduct or httpi/www.nrc.qov/readinq-rm/doc/collections/nuregs/staff/srl 0221r31) sponsor, and a person is not required to respond to, the information collection.

I. FACILITY NAME

2. DOCKET NUMBER
3. LER NUMBER

YEAR SEQUENTIAL REV Callaway Plant Unit I 05000-483 NUMBER NO.

2019

- 003 00 attachments and performing lower priority steps prior to actually blocking the SR Hi-Flux trip, thus delaying the performance of this action.

3.

The reactor startup procedure did not support expeditious action to block the SR Hi-Flux trip.

4.

Operators were not aware of the time constraints when blocking the SR Hi-Flux trip.

7. CORRECTIVE ACTIONS

Corrective actions to prevent recurrence are as follows:

I Revise the reactor startup procedure to ensure the correct monitoring behaviors and to support expeditious actions for blocking the Hi-Flux trip by establishing a continuous action step for monitoring SR counts I blocking the SR Hi-Flux trip, 2.

Revise the standard for the Reactivity Management Senior Reactor Operator to always require an additional Senior Reactor Operator who can focus solely on reactivity control.

8. PREVIOUS SIMILAR EVENTS

A review of similar events over the past 3 years indicated that no previous plant trips have occurred at Callaway due to automatic actuation of a reactor trip system function.Page 4 of 4