| | | Reporting criterion |
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| 05000483/LER-1986-001, :on 860119,at 100% Power,Esf Actuation Occurred.Caused by Restoration of Power to Containment Purge Radiation Monitor Due to Failure to Place Monitor in Bypass.Technicians Counseled |
- on 860119,at 100% Power,Esf Actuation Occurred.Caused by Restoration of Power to Containment Purge Radiation Monitor Due to Failure to Place Monitor in Bypass.Technicians Counseled
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000483/LER-1986-003, :an 860224,firewatch Requirements Not Met When Grinding Caused Smoke & Dust to Set Off Alarm.Caused by Need to Obtain Keys from Key Room & Slow Response Time.Keys Now Provided on Firewatch Key Rings |
- an 860224,firewatch Requirements Not Met When Grinding Caused Smoke & Dust to Set Off Alarm.Caused by Need to Obtain Keys from Key Room & Slow Response Time.Keys Now Provided on Firewatch Key Rings
| 10 CFR 50.73(a)(2)(1) |
| 05000483/LER-1986-004, :on 860307,reactor Protection Sys Logic Actuation Occurred.Caused by Spurious Electrical Noise in Source Range Cables.Personnel Directed to Use Local Grounds for Welding Activities |
- on 860307,reactor Protection Sys Logic Actuation Occurred.Caused by Spurious Electrical Noise in Source Range Cables.Personnel Directed to Use Local Grounds for Welding Activities
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000483/LER-1986-005, :on 860316,during Reenergization of Startup Transformer Inadvertent Isolations Occurred.Caused by Procedural Deficiency Resulting in Loss of Power to Radiation Monitors.Procedure Revised |
- on 860316,during Reenergization of Startup Transformer Inadvertent Isolations Occurred.Caused by Procedural Deficiency Resulting in Loss of Power to Radiation Monitors.Procedure Revised
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000000/LER-1986-005-03, Informs of Planned Site Visit to Obtain Info Supporting Implementation of Emergency Response Data Sys,Including Availability of PWR or BWR Parameters in Digital Form & Characterization of Available Data Feed Points | Informs of Planned Site Visit to Obtain Info Supporting Implementation of Emergency Response Data Sys,Including Availability of PWR or BWR Parameters in Digital Form & Characterization of Available Data Feed Points | |
| 05000483/LER-1986-006, :on 860318 & 0406 Four ESF Actuations Occurred. One Actuation Caused by Loosened Connector.Three Actuations Caused by Spurious Signals During Gas Sampling Evaluations Due to Vacuum Sensing Circuitry Fault |
- on 860318 & 0406 Four ESF Actuations Occurred. One Actuation Caused by Loosened Connector.Three Actuations Caused by Spurious Signals During Gas Sampling Evaluations Due to Vacuum Sensing Circuitry Fault
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000483/LER-1986-008, :on 860403,control Room Emergency Ventilation Sys Train a Discovered Inoperable Since 860318.Caused by Procedural Deficiencies & Personnel Error.Procedures Revised & Personnel Reminded of Tech Spec Requirements |
- on 860403,control Room Emergency Ventilation Sys Train a Discovered Inoperable Since 860318.Caused by Procedural Deficiencies & Personnel Error.Procedures Revised & Personnel Reminded of Tech Spec Requirements
| 10 CFR 50.73(a)(2)(1) |
| 05000483/LER-1986-009, :on 860412,intermediate Head Safety Injection Trains Discovered Inoperable & Plant Entered Tech Spec 3.0.3.Caused by Personnel Error During Performance of Surveillance Procedure OSP-EP-V0003 |
- on 860412,intermediate Head Safety Injection Trains Discovered Inoperable & Plant Entered Tech Spec 3.0.3.Caused by Personnel Error During Performance of Surveillance Procedure OSP-EP-V0003
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i) |
| 05000483/LER-1986-009-01, :on 860412,discovered That Both Intermediate Head Safety Injection Trains Inoperable.Caused by Util Personnel Error.Test Scheduled in Mode 4.Programmatic Controls Reemphasized |
- on 860412,discovered That Both Intermediate Head Safety Injection Trains Inoperable.Caused by Util Personnel Error.Test Scheduled in Mode 4.Programmatic Controls Reemphasized
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(1) |
| 05000483/LER-1986-011, :on 860416 & 17,continuous Sampling of Effluent Releases from Radwaste Bldg Vent Sys Not Performed.Caused by Isolation & Nonstarting of Radiation Sampler & Miscommunication.Procedures Revised |
- on 860416 & 17,continuous Sampling of Effluent Releases from Radwaste Bldg Vent Sys Not Performed.Caused by Isolation & Nonstarting of Radiation Sampler & Miscommunication.Procedures Revised
| 10 CFR 50.73(a)(2)(1) |
| 05000483/LER-1986-012, :on 860416,during Startup,Containment Atmosphere Radiation Monitors Inoperable During Containment Purge,Violating Tech Specs.Cause Not Stated.Personnel Counseled Re Necessity of Tech Spec Compliance |
- on 860416,during Startup,Containment Atmosphere Radiation Monitors Inoperable During Containment Purge,Violating Tech Specs.Cause Not Stated.Personnel Counseled Re Necessity of Tech Spec Compliance
| 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(1) |
| 05000483/LER-1986-013, :on 860419,reactor Trip,Feedwater Isolation, Auxiliary Feedwater Actuation & Steam Generator Blowdown Isolation Occurred.Caused by Low Level in Steam Generator. Level Control Emphasized in Training |
- on 860419,reactor Trip,Feedwater Isolation, Auxiliary Feedwater Actuation & Steam Generator Blowdown Isolation Occurred.Caused by Low Level in Steam Generator. Level Control Emphasized in Training
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000483/LER-1986-014, :on 860419 & 22,while in Mode 1,containment Purge & Control Room Ventilation Isolations Occurred.Caused by Spikes Received on Containment Purge Sys Noble Gas Activity Monitors |
- on 860419 & 22,while in Mode 1,containment Purge & Control Room Ventilation Isolations Occurred.Caused by Spikes Received on Containment Purge Sys Noble Gas Activity Monitors
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000483/LER-1986-015, :on 860423,auxiliary Feedwater Actuation Sys & Steam Generator Blowdown Isolation Occurred.Caused by Radwaste Technician Unintentionally Opening Dc Fused Disconnect Switch.Incident Reviewed W/Staff |
- on 860423,auxiliary Feedwater Actuation Sys & Steam Generator Blowdown Isolation Occurred.Caused by Radwaste Technician Unintentionally Opening Dc Fused Disconnect Switch.Incident Reviewed W/Staff
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000483/LER-1986-017, :on 860521,inadvertent Reactor Protection Sys Logic Actuation Occurred as Result of source-range Hi Flux Reactor Trip Signal on Channel SE-NI-31 Due to Personnel Errors.Personnel Disciplined |
- on 860521,inadvertent Reactor Protection Sys Logic Actuation Occurred as Result of source-range Hi Flux Reactor Trip Signal on Channel SE-NI-31 Due to Personnel Errors.Personnel Disciplined
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000483/LER-1986-018, :on 860530,auxiliary Feedwater Actuation Occurred as Result of Main Feedwater Pump Trip Due to Initiation of Condenser Steam Sparging.Caused by Inadequate Procedural Controls & Tech Spec Violation |
- on 860530,auxiliary Feedwater Actuation Occurred as Result of Main Feedwater Pump Trip Due to Initiation of Condenser Steam Sparging.Caused by Inadequate Procedural Controls & Tech Spec Violation
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(1) |
| 05000483/LER-1986-019, :on 860606,during Mode 1,reactor Trip Occurred on Low Pressurizer Pressure.Caused by Technician Deviation from Calibr Procedure.Progressive Discipline Administered. Guidelines Given to Technicians |
- on 860606,during Mode 1,reactor Trip Occurred on Low Pressurizer Pressure.Caused by Technician Deviation from Calibr Procedure.Progressive Discipline Administered. Guidelines Given to Technicians
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000483/LER-1986-020, :on 860614,containment Purge Isolations & Control Room Ventilation Isolations Occurred.Caused by Noble Gas Activity in Containment Due to Leakage from Pressurizer Level Transmitter Root Valve |
- on 860614,containment Purge Isolations & Control Room Ventilation Isolations Occurred.Caused by Noble Gas Activity in Containment Due to Leakage from Pressurizer Level Transmitter Root Valve
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000483/LER-1986-021, :on 860617,operations Personnel Failed to Restore Operability of Control Room HVAC Radiation Monitor within 1 H of Loss of Flow,Per Tech Spec 3.3.3.1.Monitor Filters Replaced & Personnel Counseled |
- on 860617,operations Personnel Failed to Restore Operability of Control Room HVAC Radiation Monitor within 1 H of Loss of Flow,Per Tech Spec 3.3.3.1.Monitor Filters Replaced & Personnel Counseled
| 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(1) |
| 05000483/LER-1986-022, :on 860621,reactor Trip Occurred as Result of Water Level in Steam Generator D Reaching lo-lo Level Trip Setpoint.Caused by Spurious slow-close Signal Generated by Valve Control Module.Faulty Module Replaced |
- on 860621,reactor Trip Occurred as Result of Water Level in Steam Generator D Reaching lo-lo Level Trip Setpoint.Caused by Spurious slow-close Signal Generated by Valve Control Module.Faulty Module Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000483/LER-1986-023, :on 860624,operations Discovered Containment Isolation Valves for Penetration 78 Opened on 860519 W/O Meeting Tech Spec Action Statement.Caused by Mgt Oversight. Draining Procedure Revised |
- on 860624,operations Discovered Containment Isolation Valves for Penetration 78 Opened on 860519 W/O Meeting Tech Spec Action Statement.Caused by Mgt Oversight. Draining Procedure Revised
| 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(1) |
| 05000483/LER-1986-025, :on 841203,851102 & 1203,plant Operated Above 100% Power Level.Caused by Incorrect Calorimetric & Feedwater Flow Instrument Drift.Power Maintained at Required Level & Design Change Evaluated |
- on 841203,851102 & 1203,plant Operated Above 100% Power Level.Caused by Incorrect Calorimetric & Feedwater Flow Instrument Drift.Power Maintained at Required Level & Design Change Evaluated
| |
| 05000483/LER-1986-026, :on 860707,Tech Spec Surveillance of Large Stationary 125-volt Batteries Not Performed.Caused by Personnel Error.Personnel Reminded of Weekly Surveillance Responsibilities |
- on 860707,Tech Spec Surveillance of Large Stationary 125-volt Batteries Not Performed.Caused by Personnel Error.Personnel Reminded of Weekly Surveillance Responsibilities
| 10 CFR 50.73(a)(2)(1) |
| 05000483/LER-1986-027, :on 860726,reactor Trip,Feedwater Isolation & Auxiliary Feedwater Actuation Occurred,Resulting from Turbine Trip.Caused by Actuating Mechanism Settings.Jumper Switch to Lockout Solenoid Valve Added |
- on 860726,reactor Trip,Feedwater Isolation & Auxiliary Feedwater Actuation Occurred,Resulting from Turbine Trip.Caused by Actuating Mechanism Settings.Jumper Switch to Lockout Solenoid Valve Added
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000483/LER-1986-028, :on 860818,high Radiation Area Door Not Locked Per Tech Spec 6.12.2.Caused by Damaged Lock Mechanism.Latch Replaced,Other Locked Entrances Inspected & Plant Personnel Instructed in Operation of Locks |
- on 860818,high Radiation Area Door Not Locked Per Tech Spec 6.12.2.Caused by Damaged Lock Mechanism.Latch Replaced,Other Locked Entrances Inspected & Plant Personnel Instructed in Operation of Locks
| 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(1) |
| 05000483/LER-1986-029, :on 860825,reactor Manually Tripped Due to Rod Control Sys Failure Following Turbine Runback.Caused by Slave Cycler Control Card Failure.Card Replaced & Cooling to Rod Control Cabinets Increased |
- on 860825,reactor Manually Tripped Due to Rod Control Sys Failure Following Turbine Runback.Caused by Slave Cycler Control Card Failure.Card Replaced & Cooling to Rod Control Cabinets Increased
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000483/LER-1986-030, :on 860909,reactor Trip on Loop Low Flow Signal Occurred.Caused by Failure of Equalization Valve to Close During Restoration of Flow Transmitter to Svc.Work Request Written to Replace Manifold Valve |
- on 860909,reactor Trip on Loop Low Flow Signal Occurred.Caused by Failure of Equalization Valve to Close During Restoration of Flow Transmitter to Svc.Work Request Written to Replace Manifold Valve
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000483/LER-1986-032, :on 860918,power-range Low Setpoint Not Verified Per Surveillance Requirements.Caused by Deficiencies in Surveillance Procedures.Mode Change Ltr Specifying Procedures Modified |
- on 860918,power-range Low Setpoint Not Verified Per Surveillance Requirements.Caused by Deficiencies in Surveillance Procedures.Mode Change Ltr Specifying Procedures Modified
| 10 CFR 50.73(a)(2)(1) |
| 05000483/LER-1986-033, :on 860920,control Room Ventilation Isolation Occurred.Caused by Blown Fuse on Control Room Radiation Monitor.Fuse Replaced.Monitor Restored.Downscale ESF Actuation Feature to Be Removed from Monitors |
- on 860920,control Room Ventilation Isolation Occurred.Caused by Blown Fuse on Control Room Radiation Monitor.Fuse Replaced.Monitor Restored.Downscale ESF Actuation Feature to Be Removed from Monitors
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000483/LER-1986-034, :on 860908,pre-action Sprinkler Sys Protecting Cable Trays of Auxiliary Bldg Inoperable W/O Continuous Fire Watch.Caused by Personnel Error.Design & Annunciator Response Procedure Evaluated |
- on 860908,pre-action Sprinkler Sys Protecting Cable Trays of Auxiliary Bldg Inoperable W/O Continuous Fire Watch.Caused by Personnel Error.Design & Annunciator Response Procedure Evaluated
| 10 CFR 50.73(a)(2)(1) |
| 05000483/LER-1986-035, :on 860928,containment Purge & Control Room Ventilation Isolation Occurred After Monitor GT-RE-32 Taken Out of Bypass.Caused by Random Fluctuations of Radioactivity Level.Plant Procedures Revised |
- on 860928,containment Purge & Control Room Ventilation Isolation Occurred After Monitor GT-RE-32 Taken Out of Bypass.Caused by Random Fluctuations of Radioactivity Level.Plant Procedures Revised
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000483/LER-1986-036, :on 860321,two Sealed Sources Discovered Placed Into Use W/O Performing Leak Testing.Caused by Cognitive Personnel Error.Sealed Sources Leak Tested by Vendor Prior to Shipment |
- on 860321,two Sealed Sources Discovered Placed Into Use W/O Performing Leak Testing.Caused by Cognitive Personnel Error.Sealed Sources Leak Tested by Vendor Prior to Shipment
| 10 CFR 50.73(a)(2)(1) |
| 05000483/LER-1986-037, :on 861105,spurious Turbine Driven Auxiliary Feedwater Actuation Occurred.Possibly Caused by Failure of Input Buffer Card.Card Replaced & Sent to Vendor for Evaluation |
- on 861105,spurious Turbine Driven Auxiliary Feedwater Actuation Occurred.Possibly Caused by Failure of Input Buffer Card.Card Replaced & Sent to Vendor for Evaluation
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000483/LER-1986-038, :on 861107,containment Purge Isolation Signal & Control Room Ventilation Isolation Occurred Due to Increased Gaseous Radioactivity Levels in Containment.Caused by Unanticipated Leakage from Pressurizer PORV Block Valve |
- on 861107,containment Purge Isolation Signal & Control Room Ventilation Isolation Occurred Due to Increased Gaseous Radioactivity Levels in Containment.Caused by Unanticipated Leakage from Pressurizer PORV Block Valve
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000483/LER-1986-039, :on 861019 & 20,liquid Radioactive Release from Discharge Monitor Tank Performed W/Liquid Radwaste Discharge Monitor at Trip Setpoint Less Conservative than Tech Specs. Caused by Software Error.Part 21 Related |
- on 861019 & 20,liquid Radioactive Release from Discharge Monitor Tank Performed W/Liquid Radwaste Discharge Monitor at Trip Setpoint Less Conservative than Tech Specs. Caused by Software Error.Part 21 Related
| 10 CFR 50.73(a)(2)(1) |
| 05000483/LER-1986-040, :on 861223,auxiliary Feedwater Actuation of motor-driven Auxiliary Feedwater Pump B Occurred.Caused by Inappropriate Human Performance.Event Discussed W/Operations Personnel |
- on 861223,auxiliary Feedwater Actuation of motor-driven Auxiliary Feedwater Pump B Occurred.Caused by Inappropriate Human Performance.Event Discussed W/Operations Personnel
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000483/LER-1986-041, :on 861231,containment Purge Isolation & Control Room Ventilation Isolation Occurred.Caused by Failure of Replaced Circuit Board.Replacement Circuit Board Removed & Original Circuit Board Reinstalled |
- on 861231,containment Purge Isolation & Control Room Ventilation Isolation Occurred.Caused by Failure of Replaced Circuit Board.Replacement Circuit Board Removed & Original Circuit Board Reinstalled
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000483/LER-1986-042, :on 861222,Tech Spec Surveillance on Valve AL-HV-0034 Not Performed within Specified Time Interval. Caused by Personnel Error & Procedural Inadequacy. Surveillance Test Request Form Will Be Revised |
- on 861222,Tech Spec Surveillance on Valve AL-HV-0034 Not Performed within Specified Time Interval. Caused by Personnel Error & Procedural Inadequacy. Surveillance Test Request Form Will Be Revised
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