ML18153C326

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Insp Repts 50-280/90-21 & 50-281/90-21 on 900603-30. Violations Noted.Major Areas Inspected:Plant Operations,Ler Reviews,Plant Maint,Action on Previous Insp Findings,Plant Surveillance & 10CFR21 Closeout
ML18153C326
Person / Time
Site: Surry  
Issue date: 07/20/1990
From: Fredrickson P, Holland W, Tingen S, York J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18153C324 List:
References
50-280-90-21, 50-281-90-21, NUDOCS 9008080251
Download: ML18153C326 (14)


See also: IR 05000280/1990021

Text

L

Report Nos. :

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W.

ATLANTA, GEORGIA 30323

50-280/90-21 and 50-281/90-21

Licensee:

Virginia Electric and Power Company.

5000 Dominion Boulevard

Glen Allen, VA

23060

Docket Nos.:

50-280 and 50-281

License Nos.:

DPR-32 and DPR-37

Facility Name:

Surry 1 and 2

Inspection Conducted:

June 3 through June 30, 1990

Inspectors:

7 ~

-JJ.

w.*E. Ho~d, Senior Resident Inspector

y~ :/'/ ~,;'

J. W. Yo~jfgTuent i'Ws~;~tor

S. G.fo~sidentlnspector

Accompanying Inspector:

A. Ruff

Approved by*~ /;.,,,,,12A

/i1<-.

-~~on, Section Chief

Division of Reactor Projects

SUMMARY

Scope:

o£t1f~d

&Av

Da'te Signed

~r:/£c

O,.ate sf gned

Date Signed

1This routine resident inspection was conducted on site in the areas of plant

operations, plant maintenance, plant surveillance, licensee event report

reviews, action on previous inspection findings, and 10 CFR Part 21 closeout.

Backshift or weekend tours were conducted on June 9, 10, 16, 17, 26, 27, and

29.

Results:

During this inspection period, a violation was identified for failure to follow

procedure while testing the Unit 1 turbine driven auxiliary feedwater pump

(paragraph 5.b).

This violation was similar to violation 280/89-24-01

discussed in NRC Inspection Report, dated September 28, 1989.

Also a non-cited

violation was identified for failure to accomplish a periodic test (PT-24.38)

within the Technical Specification frequency requirements (paragraph 5.e).

An unresolved item was identified involving the re~iew of proper classification

of safety related parts (paragraph 4.b).

9008080251 900723

PDR

ADOCK 05000280

Q

PDC

9oo'3'o~~sl

2

I~ the area of engineering/technical support, strengths were noted involving

system engineer knowledge of their systems and review of completed periodic

test procedures (paragraphs 3.d and 5.b).

In the area of safety assessment/quality verification, a strength was noted in

the licensee's evaluation of the Unit 1 low pressure heater drain system pipe

leak due to excessive pipe wall thinning (paragraph 6).

The licensee's task

team report was very comprehensive in scope and made recorrunendati ons which

would minimize recurrence of the event .

1.

Persons Contacted

Licensee Employees

REPORT DETAILS

  • W. Benthall, Supervisor, Licensing

R. Bilyeu, Licensing Engineer

D. Christian, Assistant Station Manager

  • H. Collar, Supervisor, Quality Assurance

J, Downs, Superintendent of Outage and Planning

D. Erickson, Superintendent of Health Physics

W. Gross, Supervisor, Shift Operations

  • R. Gwaltney, Superintendent of Maintenance
  • J. Hartka, Staff Engineer, Licensing *
  • M. Kansler, Station Manager

T. Kendzia, Supervisor, Safety Engineering

J, McCarthy, Superintendent of Operations

  • A. Meekins, Supervisor, Administrative Services

A. Price, Assistant Station Manager

  • K. Sloane, Supervisor, Operations Support

E. Smith, Site Quality Assurance Manager

  • T. Sowers, Superintendent of Engineering
  • R. Thornsberry, Supervisor, Scheduling
  • L. White, Senior Fire Protection Specialist
  • Attended exit interview.

Other licensee employees contacted included control room operators, shift

technical advisors, shift supervisors and other plant personnel.

Acronyms and initialisms used throughout this report are listed in the

last paragraph.

2.

Plant Status

Unit 1 and Unit 2 began the reporting period at power.

Both units

operated at power for the duration of the inspection period.

l..

3.

Operational Safety Verification (71707 & 42700)

a.

Daily Inspections

The inspectors conducted daily inspections in the following areas:

control room staffing, access, and operator behavior; operator

adherence to approved procedures, TS, and LCOs; examination of panels

containing instrumentation and other reactor protection system

elements to determine that required channels are operable; and review

of control room operator logs, operatfog orders, plant deviation

reports, tagout logs, temporary modification logs, and tags on

2

components . to verify compliance with approved procedures.

The

inspectors also routinely accompanied station management on plant

tours and observed the effectiveness of their influence on activities

being performed by plant personnel.

b.

Weekly Inspecti9ns

The inspectors conducted weekly inspections in the following areas:

operability verification of selected ESF systems by valve alignment;

breaker positions, ccindition of equipment or component, and

operability of instrumentation and support items essentfal to system

actuation or performance.

Plant tours were conducted which included

observation of general plant/equipment conditions, fire protection

and preventative measures, control of activities in progress,

  • radiation protection controls, physical security controls, plant

housekeeping conditions/cleanliness, and missile hazards.

The*

inspectors routinely noted the temperature of the AFW pump discharge

piping to ensure increases in temperature were being properly

monitored and evaluated by the licensee.

c.

Biweekly Inspections

.

.

.

The inspectors conducted biweekly inspections in the following areas:

verification review and walkdown of safety-related tagouts in effect;

review of sampling program (e.g., primary and secondary coolant

samples, boric acid tank samples, plant liquid ~nd gaseous samples);

observation of control room shift turnover; review of implementation

of the plant problem identi'fication system*; verification of selected

portions of containment isolation lineups; and verification that

notices to workers are posted as required by.10 CFR 19.

d.

Other Inspection Activities

Inspections included areas in the Units 1 and 2 cable vaults, vital

battery rooms, steam safeguards areas, emergency switchgear rooms,

diesel generator rooms, control room, auxi.liary building, cable

penetration areas, independent spent fuel storage facility, low level

intake structure, and the safeguards valve pit and pump pit areas.

RCS leak rates were reviewed to ensure that detected or suspected

leakage from the system was recorded, investigated, and evaluated;

and that appropriate actions were taken, if required~

The inspectors

routinely independently calculated RCS leak rates using the NRC

Independent Measurements Leak Rate Program (RCSLK9).

On a regular

basis, RWPs were reviewed, and specific work activities were

monitored to assure they were being conducted per the RWPs.

Selected

radiation protection instruments were periodically checked, * and

equipment operability and calibration frequency we.re verified .

During this inspection period, the inspectors walked down the SW,

CCW, FW, CH, CS, SI, EDG, MS, ventilation, UPS, radiation monitoring,

reactor protection, and electrical systems with the respective system

3

engin~ers.

The inspectors noted that the system engineers*

experience. levels varied~ but overall they appeared to be

knowledgeable on their systems which was identified as a strength.

e.

Physical Security Program Inspections

In the course of monthly activities, the inspectors included a review

of the licensee

I s physical security program.

The performance of

various shifts *of the security force was observed in the conduct of

daily activities to include: protected and vital areas access

controls; searching of personnel, packages and vehicles; badge

issuance and retrieval; escorting of visitors; and patrols and

compensatory posts.

No discrepancies were noted.

f.

licensee 10 CFR so.12* Re~orts

On June 7, 1990, the licensee made a report to the NRC withdrawing a

10 CFR 50.72 report that was made on May 13, 1990.

That report

addressed a condition concerning IRPI.

The withdrawal was based on

additional licensee reviews which concluded that the condition was

~ot unanalyzed due to their conclusion that rods remained operable

throughout th.e event and that TS 3.12.E.3 was applicable to this

condition.

Within the areas inspected; no violations were identified.

4.

Maintenance Inspections (62703 & 42700)

During the reporting period, the inspectors re~iewed maintenance

activities to assure compliance with the appropriate procedures.

  • Inspection areas included the following:

a.

Repair of ESW Pump lA Fuel Oil Line

On June 12 the licensee atte~pted to adjust the governor of ESW pump

lA in order to correct a lower than normal speed which had been

identified during past periodic testing.

This attempt by* a vendor

representative was unsuccessful, and it was concluded that a

distorted fuel line may have*been limiting fuel oil flow to the

diesel engine.

The license~ then processed a work request to replace

the distorted fuel line and completed the maintenance activity on

June 15.

After completion of work, ESW pump lA was satisfactorily

tested and returned to an operational status.

The testing was

reviewed by the inspector and is discussed in paragraph 5.a.

The inspector monitored licensee's activities associated with the ESW

pump lA repairs, including a review of initial conditions and

prerequisites to accomplish the work, material and testing

requirements, discussions with the system engineer, and periodic

trips to the low level intake structure to evaluate corrective

actions and monitor maintenance activities.

A review was also made

4

of the completed work order and associated documentation for the

maintenance activity.

No discrepancies were identified.

b.

Replacement of Unit 2 SI Test Switch

On June 26 the licensee replaced the Unit 2 Train A, Channel III,

high steam flow SI test switch.

This work was accomplished on work

order 3800092251 and was witnessed by the inspectors from the Unit 2

switchgear room.

Temporary jumpers were required to be installed for

this maintenance.

The inspectors reviewed the work order, the

temporary modification log, and the electrical schematics.

Since

the work order indicated the switch to be a non-safety related

component, the inspectors questioned the system engineer as to this

classi-fication. The system engineer did not have an immediate answer,

but did initiate action to verify the switch's classification. After

the switch was i nsta 11 ed, it was determined that the component

classification on the work order was in error.

The switch was

satisfactorily tested but it remained in an inoperable status pending

the necessary work* to upgrade it to a safety related component.

The licensee is continuing the investigation of this discrepancy.

Since this was identified late in. the inspection period and an

investigation is still in .. ,process, this item is identified as URI

280,281/90-21-03, Review "'of Classification of Safety Related

Components.

Two additional problems were identified by the licensee during the

replacement of the switch.

The first was that the initial switch used

for rep 1 a cement was discovered to be defective after it was

installed.

This precipitated the installation of a second switch.

Based on this problem, the licensee

wa~ evaluating if a 10 CFR 50

Part 21 Notice is required: The second problem was that the control

room Q-list was was found to be outdated. The licensee initiated a

deviation report in response to the outdated control room Q-list.

Within the areas inspected, no violations were identified.

5.

Surveillance Inspections (61726 & 42700)

During the reporting period, the inspectors reviewed various surveillance

activities to assure compliance with the appropriate procedures as

follows:

Test prerequisites were met.

Tests were performed in accordance with approved procedures.

Test procedures appeared to perform their intended function.

Adequate coordination existed among personnel involved in the test.

Test data was properly collected and recorded.

5

Inspection areas included the following:

a.

Testing of ESW Pump lA

On June 15, 1990, ESW Pump lA was tested in accordance with PT 25.3A,

Emergency Service Water Pump (1-SW-P-lA) dated October 10, 1989.

The

test was performed to verify pump operability after completion of

corrective maintenance on the pump diesel fuel oil line.

This

maintenance activity was discussed in paragraph 4.a.

The inspector

reviewed the completed periodic te~t with the system engineer.

No

discrepancies w~r.e nqt~d.

b.

Testing of Turbine Driven AFW Pump 1-FW-P-2

On June 2 Unit 1 turbine driven auxiliary feedwater pump was tested

in accordance with 1-PT-15.lC, T.urbine Driven Auxiliary Feedwater

Pump {l-FW-P-2), dated May 10, 1990. This pump was tested after unit

restart as required by TS .. The pump was then declared operable and

unit startup continued.

On June 12, during a review of the completed

PT by the system engineer, it was discovered that the procedure had

been perfonned incorrectly and deviation report Sl-90-815 was issued.

On June 17, after management became aware of the DR, the problem -of

imp~oper testing was discussed with the residents.

The DR addressed the fact* that procedural steps were performed which

-_ were not required.

Step 5.29 of periodic test 1-PT-15. lC states in

part,

11 If the shaft speed does not exceed 4250 RPM, N/A all steps

below and proceed to step 5.30.

11

During performance of step 5.28,

the operator recorded shaft speed as 4145 RPM.

If procedure had been

followed, the operator would not have made adjustments to shaft speed

and would have proceeded to step 5.30.

However, the operator

adjusted the pump shaft speed upward to 4200 RPM at the direction of

the SRO in charge of the test in accordance with Step 5.29.

This

adjustment was not in accordance with procedural requirements.

It

was also noted that this readjustment was a recurrence of a past

similar problem.

TS 6.4 requires, in part, that procedures for the testing of

components and systems involving nuclear safety of the station

shall be followed.

Failure to follow the procedural requirements of

1-PT-15.lC on June 2 is identified as a violation of TS 6.4

(280/90-21-01).

This is a repeat of a similar violation that

occurred when this pump was tested using the same PT on August 1,

1989.

The violation for this occurrence is discussed in NRC

Inspection Report 280,281/89-24, dated September 28, 1989.

The inspectors discussed the DR with the system engineer and were

informed that an analysis was conducted which concluded that the pump

operability was not affected by the governor adjustment.

The system

engineer explained that previous test results show that when the pump

c.

d.

6

is operated at 4200 RPM*, the pump head fa 11 s within the acceptable

range and that the pu~p will not trip from overspeed when started.

On June 20 the inspectors witnessed the test on the same pump using

the same PT.

The valve alignment, pump start, and the taking of the

data was observed by the inspectors.

The reading recorded for step

5.28 was 4196 RPM and no adjustments were made.

The test was

performed satisfactorily with no-discrepancies.

The inspectors noted that the .problem with the* auxiliary feedwater

pump periodic test was identified during the system engineer's revie~

of the completed test procedure and was documented on a DR.

Additional reviews of DRs by the inspectors noted where heat trace

circuits were left outside their setpoint tolerances during periodic

testing. This problem was also identified and documented by a system

engineer as the result of his review of the completed test procedure.

These examples of problem identification by

systems engineers are

.constdered a strength with regards to engineering/technical support

at the station.

Verification of Position and Stroke Testing on Valve TV-DG-208A

Trip valve No. TV-DG:..208A had indicated an intermediate position on

the control room board i.e. both the closed and open light positions

were illuminated.

This required the licensee to make a containment

entry in order to repair this valve.

On Jurie 7 the inspectors

witnessed verification of valve position using periodic test

2-PT-18.lOA, Verification of Local and Remote Valve Position

Indications of Containment Trip Valves Inside Containment, dated

October 27, 1989.

The inspectors observed the coordination between

the control room operators and the maintenance personnel in adjusting

the valve position and the position indicator. After completion of

the adjustment, the stroke testing of the valve was performed in

accordance with 2-PT-18.6B, Quarterly Testing of Miscellaneous

Containment Trip Valves, dated December 12, 1989.

2-PT-18.lOA was

subsequently completed to return the valve to service.

The*

inspectors observed the manipulation of the valve by the control room

operators, the illumination of the appropriate valve position

indication light, and the timing of .the stroking of the valve.

No

discrepancies were noted.

Control Rod Assembly Testing

On May 21 the inspectors witnessed the performance .of periodic test

1-PT-6.0, Control Rod Assembly Partial Movement, dated February 15,

1990, from the control room.

The purpose of this test was to verify

movement of the control rod assemblies as required by'TS 4.1.

During

the test, the inspectors noted that control bank D was not tested .

Operations explained that control bank D was routinely moved to

control reactor temperature and flux distribution which satisfied the

TS requirement to verify contra l rod system operability every two

7

weeks.

Al so during the test, a *icomputer printout rod control

system" alann occurred and would not clear.

The operator .annotated

the procedure critique sheet of this condition.

After the test was

satisfactorily completed, it was reviewed by the inspectors. A work

request, No. 689961, was also issued to clear the alarm.

With the

approved work request, an I&C technician then cleared the alarm by

resetting the P250 computer.

The operator annotated on the procedure

critique sheet that this condition had occurred.

The inspectors.have

noted similar occurrences in the past where annunci_ators would not

automatically. clear when their alarm condition cleared.

The

inspectors will continue to monitor this _condition during routine

tours to evaluate the effect of similar occurrences on operator

performance.

No discrepancies were noted.

e.

Failure to Conduct Periodic Testing of Fire Dampers

On June 28, the licensee discovered that periodic test PT-24.38, HVAC

Fire Damper Operability, had not been perfonned within the allowable

TS frequency requirements.

TS 4.18.G.l.a requires that PT-24.38 be

perfonned every 18 months.

It was last performed on May 26, 1988.

Therefore, .after addition of a 25% grace period, the periodic test

was required to be performed by March 1990. Failing to accomplish

this testing resulted in the fire dampers associated with the control

room, emergency swithgear rooms, and battery rooms being classified

as inoperable.

Upon discovery that *the periodic test had not been

perfonned, the licensee established fire watches in the affected

areas within one *hour in accordance with TS 3.21.B.7.

PT-24.38

was then satisfactorily accomplished and the fire watches secured.

At the end of the inspection period, the licensee was still

investigating why the test was not accomplished within the allow-

able TS frequency requirements.

Failure to accomplish PT-24.38

within TS frequency requirements was identified as a violation (NCV

280,281/90-21-02).

This licensee identified violation is not being

cited because criteria specified Section V.G.l.of the NRC Enforcement*

Policy were satisfied.

Within the areas inspected, one violation and one NCV were identified.

6.

Licensee Event Report review

(92700)

The inspector reviewed the LER's listed below to ascertain whether NRC

reporting requirements were being met and to evaluate initial adequacy of

the corrective actions.

The inspector's review also included followup on

implementation of corrective action and review of licensee documentation

that all required corrective actions were complete.

(Closed) LER 280/89-35, Unplanned ESF Actuation, Automatic Start of an

Auxiliary Ventilation System Fan Due to an Incorrectly Landed Lead.

The

issue involved improper landing of a previo.usly lifted lead on a pressure

switch due to personnel error. The incorrectly landed lead resulted in an

auto-start of the subject fan when the fan control. switch was returned to

8

the auto position. Immediate corrective action included properly relanding

the lead and verifying correct fan operation. A root cause investigation

of the event was conducted.

That evaluation identified the root cause to

be poor self checking techniques by the craft.

In addition, the licensee

determined that additional engineering guidance for this type of work

would be provided.

The inspector reviewed the root cause evaluation and

agreed with the licensee's conclusions. This LER is closed.

(Closed) LER 280/90-03, Unit 1 LP Heater Drain System Pipe Leak Due to

Excessive Pipe Wall Thinning.

The issue involved a failure of piping

do~nstream of one of the _Unit 1 low pressure heater drain pumps due to

excessive pipe wall thinning,

Immediate corrective action included

  • isolation of the leak area by stopping the pump and shutting the required

valves.

Some spurious actuations of fire protection equipment occurred

due to the heat and moisture cause by the br.eak. Moisture affected

electrical circuits to alarm and heat caused some sprinklers to activate.

The failure was attributed to single phase flow erosion/corrosion caused

by the higher localized flow in the line inrnediately downstream of a flow

control valve.

Corrective action included replacement of the failed pipe

and additional inspections of similar configurations for thinning.

Based

on these inspections, the piping in the same locatioh for the other pump

was replaced. A licensee task team was formed and investigated the event.

They concluded in a report dated June 20, 1990, that several additional

corrective actions were warranted to prevent recurrence of the event tnd

identified these actions as concerns.

The licens~e added these concerns

to their COOIJlitnient tracking program for proper disposition.

The

inspectors monitored licensee corrective actions and reviewed the task

team report.

The inspectors noted that the task team* report was very

comprehensive in scope and is considered as a strength in the lic~nsee's

self assessment capability. This LER is closed.

(Closed) LER 280/90-04, Unit 1 Reactor Trip/Turbine Trip Due to Deluge

Actuation on the

11A

11 Main Transformer and Unit 2 Manual Reactor Trip Due

to Erratic IRPI Indications. * The details of this LER along with the

corrective actions required to subsequently restart Units l and 2 were

discussed in NRC Inspection Report 280,281/90-20.

In order to preclude

similar occurrences, the licensee will evaluate enhancements to the IRPI

system and its power supply and also evaluate the separation between the A

Main Transformer and the A Reserve Station Service bus .bars. In the.

interim, the.licensee has isolated the deluge system from the A Main

Transformer.

The inspectors consider the licensee's corrective actions to

be adequate.

(Closed) LER 281/90-01, TAVE Protection Channel I ~eclared Inoperable* Due

to a Faulty Summator. This issue involves installation of a faulty

summator in one of the three average temperature channel inputs to the

reactor protection system.

The original summator was replaced with a

rebuilt su1T111ator that provided more noise filtration in the circuit to

minimize spurious alarms.

The replacement summator was satisfactorily

bench tested before installation.

However, after installation the

temperature of the summator increased due to the_ambient temperature of

9

the cabinet.

The licensee considers that the surnmator failure which

occurred after installation was caused by an increase in .ambient

temperature.

This failure mechanism was not able to be duplicated_during

the bench test. In order to simulate the increased temperature on electri-

cal components when bench testing, the licensee has obtained an oven to

heatup electrical components prior to performance of a bench test. This

type of testing should detect failure of electrical components such as the

faulty summator prior to installation.

The inspectors consider the

licensee actions adequate.

(Closed) LER 281/90-02, Inoperable Individual Rod Position Indicators Due

to Instrument Drift.

At 77% during a rampdown from 100% power, IRPI fo~

two control rods of control bank D differed from the rod group demand

counter by greater that 12 steps which exceeded the TS limit. Corrective

action involved changing abnormal procedure O-AP-1.02., Individual Rod

Position Indication, dated May 19, 1990 to require operators to stop the

ramp if !RPI and rod group demand counter differ by more than 10 steps.*

The inspectors.reviewed O-AP-1.02 and consider the licensee actions

adequate.

7.

Action on Previous Inspection findings

(92701, 92702)

a~

(C"!osed) VIO 280/89-24-01, Failure to Comply With TS 3.0.1. This

issue involved the licensee's incorrect use of a JCO to exit TS 3.0.1

action statement which resulted in a failure to follow the TS's

action statement requirements.

The licensee responded to this

violation in a letter dated October 27, 1989.

In that letter, the

licensee stated that administrative procedure SUADM-LR-12, Safety

Analysis/10 CFR 50.59/72.48 Safety Evaluations And Justifications For

Continued Operation, was revised to clarify that JCOs alone may not

be used to exit a TS action statement. The inspectors reviewed

SUADM-LR-12 and consider that the licensee's corrective action was

adequate.

b..

(Closed) VIO 280, 281/89-24-03, Failure to Comply With the Allowable

TS Intervals For Station Battery Testing.

This issue involved

battery surveillances not being performed in accordance within TS

frequency requirements.

The licensee responded to this violation in

a letter dated October 27, 1989.

In that letter, the licensee stated

that corrective action involved daily listing of outstanding.

electrical surveillances, designating an electrical shop fo~eman to

be responsible for the completion of electrical surveillances, and

placing an increased emphasis on scheduling electrical surveillances

on the plan of the day.

The inspectors discussed this issue with the

station battery system engineer who is responsible for reviewing and

trending battery surveillance results.

With the implementation of

the above corrective action, the system engineer stated that

surveillances have been performed in accordan_ce with the TS frequency

requirements.

The inspectors consider that the licensee's corrective

actions were adequate.

I

10

8.

10 CFR Part 21 Closeout

(92700)

(Closed) 280,281/P2190-04, Notification by Rosemount, Inc. of Potential

Failure for Models 1153 and 1154 Transmitters.-

On December 12, 1988 and

February 7, 1989, Rosemount notified the industry of a potential failure

mode for their 1153 and 1154 transmitters.

As a result of identification

of this _problem, the NRC issued. Information Notice 89-42, Failure of

Rosemount Model 1153 and 1154 Transmitters on April 21, 1989; and more

tecently, on March 9, 1990, the NRC issued NRC Bulletin 90-01, Loss of

Fi 11-0il in Transmitters Manufactured by Rosemount.

The Part 21 nottfication indicated that the_ internal loss of fill-oil can

cause the transmitters to exhibit reduced performance prior to a

detectable failure.

The reduced performance is considered most noticeable

by a drift in the zero setpoint, by a drift in span setting, or as a slow

response time to changes in pressure input.

The notice also indicated

that all reported failµres occurred during the first 3o*months of service

and that all were preceded by the detectable degraded conditions discussed

above.

The inspector discussed this issue with the licensee and was provided the

_ following information:

Most of the subject transmitters have been in service at Surry longer

than the 30 months called out in the Part 21 notice.

An engineering/evaluation for Rosemount transmitters has been

established.

Operations and l&C personnel have been briefed on the potential

internal fill-oiJ loss failure mechanism and associated symptoms.

Procedure IMP-C-MI-50, Transmitter Pre-installation, Testing and

Replacement, had been revised to notify engineering and the NPRDS

coordinator when replacing a transmitter that required changeout due

to a failure.

Surry has had transmitters fail in the past that exhibited_

characteristics similar to those discussed in the NRC Information

Notice.

In those cases, the transmitters were replaced in accordance

with approved maintenance practices.

The inspector noted that NRC Bulletin 90-01 requested licensee's to

provide NRC with information/data on Rosemount transmitters and to take

specific corrective actions to minimize undetected failures of the subject

transmitters.

Based on the licensee's actions to date and the requested

actions of NRC Bulletin 90-01, this item is closed.

11

9,

Exit Interview

The inspection scope and results were sulTITiarized on July 3, 1990 with

those individuals identified by an asterisk in paragraph 1. The follow.ing

summary of inspection activity was discussed by the inspectors during *this

exit.

A violation (280/90-21-01) was identified for failure to follow

procedure while testing the Unit 1 turbine driven auxiliary feed

  • water pump which was similar to a previously issued violation
  • (paragraph 5.b).

A non-cited violation (280, 281/9b-21-02) was identified for failure

to accomplish PT-24.38 within the Technical Specification frequency

requirements (paragraph 5.e).

An unresolved item (280, 281/90-21-03) was identified involving

NRC review of the licensee's evaluation of proper classification of

safety related parts (paragraph 4.b).

In the area of engineering/technical support, strengths involving

system engineer knowledge of their system and system engineer review

of completed periodic test procedures were noted (paragraphs 3.d and

5.b).

In the area of safety assessment/quality verification, a strength was

identified with regards to the licensee's evaluation of the Unit 1

low pressure heater drain system pipe leak due to excessive pipe wall

thinning.

The inspectors noted that the task team report was very

comprehensive in s'cope .and made recorrmendations which should minimize

recurrence of the event.

This report was considered to be an

excellent example of the licensee's self assessment capability

(paragraph 6),

Licensee management was informed of the items closed in paragraphs 6

and 7.

The licensee acknowledged the inspection conclusions with no dissenting

corrrnents.

The licensee did not identify as proprietary any of the

materials provided to or reviewed by the inspectors during this

inspection.

10.

Index of Acronyms and Initialisms

AFW

CFR

CCW

CH

cs

DR

EDG

ESW

AUXILIARY FEEDWATER

CODE OF FEDERAL REGULATIONS

COMPONENT COOLING WATER

CHARGING

CONTAINMENT SPRAY

DEVIATION REPORT

EMERGENCY DIESEL GENERATOR

EMERGENCY SERVICE WATER

I '

t *

FW

HVAC

I&C -

!RPI

JCO

LCO

LER

N/A

MS

NCV

NPRDS

NRC

PT

RCS

RPM

RWP

SI

SRO

SW

TS

UPS

12

FEEDWATER

HEATING 'VENTILATION AND AIR CONDITIONING

INSTRUMENTATION AND CONTROL

INDIVIDUAL ROD POSITION INDICATION

JUSTIFICATION FOR CONTINUED OPERATION

LIMITING CONDITION FOR OPERATION

LICENSEE EVENT REPORT

NOT APPLICABLE

NON-CITED VIOLATION

NUCLEAR PLANT RELIABILITY DATA SYSTEM

NUCLEAR REGULATORY COMMISSION

PERIODIC TEST

REACTOR COOLANT SYSTEM

REVOLUTIONS PER MINUTE

RADIATION WORK PERMIT

SAFETY I.NJECTION

SENIOR REACTOR OPERATOR

SERVICE WATER

TECHNICAL SPECIFICATIONS*

UNINTERRUPTIBLE POWER SUPPLY