ML18152A444

From kanterella
Jump to navigation Jump to search
Insp Repts 50-280/92-25 & 50-281/92-25 on 921129-930102.No Violations Noted.Major Areas Inspected:Operations,Maint, Safety Assessment & Quality Verification
ML18152A444
Person / Time
Site: Surry  Dominion icon.png
Issue date: 01/27/1993
From: Belisle G, Tingen S, York J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18152A445 List:
References
50-280-92-25, 50-281-92-25, NUDOCS 9302020028
Download: ML18152A444 (12)


See also: IR 05000280/1992025

Text

Report Nos.:

UNITED STATES

NUCL~AR REGULATOFJY COMMiSSION

. REGION II

101 MARIETTA STREET,N.W.

ATLANT~. GEORGIA 30323

50-280/92-25.and 50-281/92-25

licensee:_ Virginia Electdc and Power Compan_y

5000 Dominion Boulevard *

~ljn All~n, VA

23060

Docket Nos.:

50-280 and 50-281

License Nos.: *DPR-32 and DPR-37

Facility-Name:* Surry-I and 2

,

Inspection Conducted:

November 2_9, 1992-January 2, 1993 .

Inspectors:

Approved by:

Scope:

G. A. Belisle,S'Chief

Division of Reactor Projects

SUMMARY

/- 27- 7" 3

Date Signed

/ - ). 7-t1)

Date Signed

/-J]-fs

. Date Sign~d

This routine resident inspection was conducted on site in the area of

operations, maintenance, internal plant evaluation corr~c~ive action, safety

assessment and quality verification, and licensee event review.

During the

performance of this i n.spect ion,. the resident inspectors condu.cted review of

the licensee's backsh i fts, holiday *or weekend operat i ans on. November 29,

December 6, 11, 12, 13,. 16, and 24.

.

Results: *

In the operations ar~a, the follriwing ite~ was noted:

Operatot~ responded properly to a leak in the letdown system and their

prompt action minimized the loss of reactor coolant (paragraph 3.b) .

9302020028 930127

PDR

ADOCK 05000280

G

PDR

2

-

In the maintenance/surveillance functional area, the following items were

noted:

The cause determihation evaluation backlog has been reduced but still

remains high.

Additional act~ons ~ere being imple~ented to further

reduce the backlog (p~ragraph 4.a).

The intermediate seal cooler was replaced, tested, and returned. to

service within the Technical Specification allotted time period,

however, a temporary*repair performed during a previous cooler

rep 1 acement was* not documented.

This d*e 1 ayed the coo 1 er rep 1 acement and

its ret~rn to service (paragraph 4.b).

The m~(:hanical maintenance outage group has taken a proa_ctive role in

scheduling maintenance* items for the upcoming refueling outage

(paragraph 4.c).

Performance of periodic maintenance associated with replacement of

backflow preventers was delayed because an upgraded procedure did not

  • contain leak rate acceptance criteria (paragraph 5.a).

In the safety assessment/quality verification area, the fril1owing items were

noted:

-

,,

The inspectors concluded that the root cause evaluation associate*d with

the failure of the Unit 2 turbine building service water joint in July

1992 was thorough and the root ciuses of the event were identifi~d

(paragraph 5. a).*.

Throughout 1992, problems a*ssociated with Kaman radiation-monitor

spiking have occurred.

The cause determinati6n ev,luation performed as

corrective action in response to this problem was unabl_e to identify the

root cause of the problem.

Although the 1 i censee was unable to identify

the root ca~se, th~ problem-was aggressively pursued (paragraph 6.b). *

Recurring problems were identified in the areas of intermediate seal

cooler tube leakage, ground water intrusion, and roof leakage.

(paragraphs 3.c and 4.b).

-

REPORT DETAILS

1.

Persons Contacted

licensee Employees

R. Allen, Supervisor, Operations

  • W. Benthall, Supervisor, Licensing
  • R. Bilyeu, Licensing Engineer *
  • H. Blake, Superintendent of Site Services -

M. Bowling, Manager, Corporate Nu~l~ar Licensing.

  • R. Blourit, superintendent of Engineering
  • D. Christian, Assistant Station Manager

J. Downs, Superintend~nt of Outage arid Planning

D. Ericksoni Superintendent of Radiation Protection

  • R. Gwaltney, S~perintendent of Maintenance
  • M. Kansler, Statiop Manager

. .

.

  • A. Meekins; Supervisor, Administrative Service~
  • J. McCarthy, Superintendent of Operations

J. O'Hanlon, Vice President, Nuclear Operations

A. Price; Assistant Station Manager *

.

  • * _ R. Saunders, Assistant Vice Presiderit, Nuclear Operations
  • E. Smith, Site Quality Assurance Manager

B. Stanley, Supervisor, Station Procedures

-NRC Personnel *

  • S. Tingen~ Resident Insp~ctor
  • J. York, Acting Senior Resident Inspector.

Accompanying NRC Inspector

A. Ruff

  • Attended Exit Interview

Othe.r licenseeemployees contacted included control room operators,*

.

shift technical advisors, shift supervisors and other plant personnel.

On December *a, the Region II Regional Administrator,*s.* Ebheter; visited

the Surry Power Station for a familiarjzation tour.

He also met with

licensee management and *staff and reviewed the current status of the

station.

The Regional Administratof was accompanied by M. Sinkule,

Brarich Chief, Region II. Later in the day,- the Regional Administrator

held a press conference in Richmond, Virginia.

Acronyms and initialisms used throughout this report are listed ~n the

last paragrap_h ..

2

2.

Plant Status

Unit 1 began the reporting period in power operation and was at power -at

the end of the -inspection period, day 118 of co_ntinuous op_eration.

Unit- 2 began the reporting period in power operation and was at power at

the end of the inspecti~n period, day 168 of_continuous operation.

3:

Operational Safety Verifitation (71701, 42700)

The *inspectors conducted _frequent tours of the control room to verify

-proper staffing, operator attentiveriess and adherence to approved

ptocedures .. The inspettors attended plant status meetings and reviewed

operator logs on a daily basis to veri,fy operations safety and

compliarice with TSs and to maintain awareness ~f the overall ~peration

of the facility.

Instrumentation and ECCS lineups* were periodically

reviewed from control room indication to assess operability.

Frequent

p1~h~ tours were conducted to bbserve equipment status; fire protection

programs, radiological ~ork practit~s, plant security programs and

housekeeping.

Deviation reports were reviewed tci assure that .potential

safety concerns were pfoperly addressed and reported.

a.

b.

Cold Weather Protectio~ Preparations (71714)

During this fnspection period, the*.inspectors reviewed the

licensee's program for-implementation of protective measures for

cold weather.

This program is implemented by monthly performance

(October through March) of STP-52, Cold Weather Protec_tion, dated

April 3~ 1992.

This proced~re contains a_detailed checklist of

areas and components that need to be routinely inspected to ensure

that there is adequate protection to preve~t freeiing;

STP-52 is

performed by both operations and maintenance personnel ..

Defici~ncies that are noted durihg the performance of STP-52 are

documented and discrepancy reports/work requests are written to

ichedule cortective action. A designated individual from the

operations department i-s assigned the- re_spons i bi l i ty for

_

prioritizing these w_ork requests for _action.

The inspectors

discussed the performance of STP-52 with this individual and

operations management, and no concerns were identified.

The

inspectors toured severa1 areas listed in.STP-52 and no

discrepancies were identified.

The inspectors reviewed the results of a QA assessment that was

perfojmed during the per~od October 12-15, 1992.

This assessment

evaluated the performance of STP-52 and concltided that the methods

used to protect station equipment from cold weather were adequate.

RCS Leak on Unit 2 Letd6wn System Flow Trans~itter

On December 12, a swag el ok/tubi_ng connection failed and

approximately twenty-to thirty gallons of reactoi coolant spilled.

  • -**

3,

_,

into the lower level <_>f the auxiliary building.

Two lfcensee-

wotkers in the ar~a were contaminated.

The*swagelok connectioh

that failed_ .was on the high pressure side drain va*lve for letdown

flow transmitter.2-CH-FT-2150. -When the conne~tion failed,

-control room letdown flow indication decreased to_ zero and VCT and

pressurizer lev~ls itarted to decreas~.

The ~rintrol room.

operators immediately isolated letdown and charging**flow, and

stabilized VCT and pressurizer levels.

TS 3.1.C.5 was -entered

because the RCS leakrate had exceeded 10 GPM. _ The failed

connection was repaired and letdown-flow was reestablish~d later*

in the shift. The inspectors concluded that the operators * _

_

r~sponded*proper1y to*the event and their prompt action minimized

  • *

At the end of the inspection period, the licensee was performing

an RCE to determine the cause~for the failure of the connection.

c~.

Roof Leaks and Ground Water Intruiion

_ On December 12, the inspectors toured the_ itation and identified

the fo 11 owing locations and components that were wetted from

ground water intrusion and roof leakage:

In the auxiliary building, the Uriit 2 MSTV SOVs and Test Box_

and an emergency lighting panel _near the Unit 1 MSTV SOVs

were wet from ground water intr~sion.

In the Unit 2 safeguards building~ the A and B outside

recirculation spray pumps were wet. _ No electrical

components on these pumps were wet; however; the fasteners

on the base of the B pump were corroded indicating that this

problem has existed for some time ..

  • In the Unit 2 safeguards buflding Valv~ pit, sections df the

Unit 2 LHSI and outside recirculation spray pumps piping

were wet and corroded.

Also, several cable triy~ in the

area were wet.

The fuel bu il d_i ng roof* was leaking, but rain water was not

observed to be ~ripping into the fuel ~ool.

The Unit 2 safeguards roof was leaking onto the floor behind

the containment spray pumps.

There was approximately one inch of water on the floor of -

the boron recovery room whith appeared to be caused from

  • .*ground water intrusion.
  • -

Roof leakage and grourid water intrusion were idintified as~ problem

  • duting the previous SALP assessment period, and the licensee has

- implement~d the following cbrrective actions: repair roofs, improve

grading around the buildings in-order to direct water away

4

from the building, and improve the performance of sump pumps.

These

corrective actions -are still ongoing.

The majority of the components

  • identified during this inspection were wetted by gro~nd water intrusion.

No roof leaks were fdenti.fied in the auxiliary building which recently

had a new roof installed .

. Within the areas inspected; no virilations were identified.

'

'

4.

Maintenance Inspectio~s (62703) (42700)

~

.

.

.

During the ~eporting period; the inspectors re~iewed the following

maintenance activities to assure compliance w.ith the appropriate

procedures.

a:

- Maintenance Engineering CDE Backlog

During the previous SALP assessment periods, the backlog of CDEs

increased.

The CDE backlog has been reduced but still remains

high.

The previous backlog. of approximately 400 CDEs has been

reduced to lesi that 200 CDEs.

In order to further re~uce the CDE

backlog, two engineers were assigned to-the maintenance

engineerihg department at the end bf the ihspection period to aid

in the performance of CDEs, -and the maintenance engineering

department has established a goal to complete CDEs within 45 days

of WO closure.

b.

Unit 1 Jntermediate_ Seal Coolef Replatement

The inspectors witnessed the repl~cement of the Unit 1 charging

- pump intermediate seal cooler 1-SW-~-lA.

The intermediate seal

cooler was replaced due to tube leakage. This maintenance was

accomplished in accordance with WO 3800135897, and procedures

O-MCM-1004-01, Flange Gasket Replacement, dated June 14, 1991, and

O-MCM'-1801-01, Piping/Components Repair/Replacement, dated

February 27,1992.

The inspectors observed ~ortions of the m~intenance, and* reviewed

the work package, post maintenahce test requirements, and work

histories for the Unit 1 and 2 intermediate seal coolers.

During

  • the maintenance, a scratch on one cooler union connection's mating

surfaces was identified. ~he licensee repair~d the defect by seal

. welding the union.-

The resolution for the defect delayed

completi~n of.the seal ~ooler replacement.

This defect was a pre-

existing condition that had been temporarily repaired in September

1992.

Proper documentation ~of the temporary *repair would have -

resulte_d in maintenance planning for the permanent seal weld

repair thereby reducing the equipment out of service time.

The*

~ooler was replaced, tested,* and placed back into service within

  • rs time constraints.

The post maintenance test requirements were

considered correct.

-

  • -

5

Review of the maintenance histories for thefour intermediate seal

coolers -indicated that the c.oolers in both Units had to be

_

fr~quently replaced due to tube leikage. * Since 1986, intermediate

. seal coole~, 1-SW-E-lA, has been replaced seven times, 1-SW-E-lB

has been replaced six times, 2-SW-E-lA has been _replaced four

times, and 2~SW-E-la has been replaced three times.

The licensee

replaced the coolers due to excessive tube leakage, but has not

implemented corrective actions to prevent the problem from

recurring.

c.

_ Mechanical Maintenance .outage Planning

The mechanical mainte~ance de~art~~ht formed a special group to

~lan f6r the upcoming Untt 2 RFO.

The goals of this group ar~ to.

  • min1mi~e the radiation dose and ma~imize the cost effectivehess

for mechanical maintenance j9bs scheduled,for,the upcoming RFO.

Some'of the functions of the group are to maximize pre-outage

work, and if the work is required to be done during the outage,

determine the best opportunities (windows} for *performance.

They

are also providing priorities for performance of these items,

doing walk downs on components* arid work items, and developing

pre-job briefings.

The inspectors met with this group and it appeared .that the.

group's activities should have a positive impact on the upcoming

.RFO.

For example, the original Unit 2 1993 outage schedule

required that 5 of he 15 MS safety valves be remov~d, overhauled

and tested with the remaining MS saf_ety valves tested in place.

However, the outage group review~d the 1994 RFO schedule and noted

- that all MS safety va]ves were to be removed and the MS lines

blanked to support a ten-year ISi hydrostatic test of the system.

The group concluded that it would be more cost effective to remove

and ov~rhaul all the valve~ during the 1994 RFO.

Additionally,*

one of the lessons learned _from the previous RFO was_that shift

turnovers were ~ot always adequate.

The group revised foreman

shift schedules for the upcoming RFO to enhance shift turnovers.

The inspectors concluded that the mechanical maintenante group was

taking.a proactivi role in scheduling for the upcoming RFO.

Within the ,reas jnspected, no Violations were identified.

5.

Review of IPE Flooding Corrective Actions *(71~00)

a.

Floor Drain Stop Valve Replacement

One of th~ protective measures implemented to mitigate the

consequences of turbine. building flooding was to enhance the

performance of.specific floor-drain backflow preventers by

implementing a periodic maintenance progr~m.

The inspectors

witnessed the testing and replacemen~ of the flopr drain backflow

preventers in MER 3, the Unit 1 and 2 cable vaults, MER 4, and the

Unit 1 and 2 ESGRs.

This quarterly PM wa~ accomplished per WO

6

. .

.

.

3800135842 and upgraded procedure O-MPM~1900-02, Quarterly Flood

Ptotection Floor Drain s,ck Water Stop Valve Replacement, dat~d

February 13, 1992.

-Each backf\\ow preventer was seat leak tested fn a test rig and

then installed in the ~lant.

One of the backflow preventers

leaked e~cessively and th~ seating surfaces had to be lapped in

order-for .it to pass the leakage testa Procedure O-MPM-1900-02

did not ~ontain a quantitative seat le~kage speci.fication which

delayed the PM completion.-

The mechanics consulted with _system

engineering to obtain a satisfactory acceptance crited a for

-leakage.

The licensee planned to revise the procedure to include_

the appropriate acceptance criteria.

No other discrepancies ~ere

identified..

-

Within the areas inspected, no violations were identified.

6.

Safety Assessment and Quality Verification {40500)

a.

Review of Root Cause Evaluation

Ad~inistrati~e *Procedure*VPAP-1601, Correcifve Action, Revfsion 1,

requires that RCEs be performed for events that are *safety

significant. The purpo~es of the RCE are to: 1) provid~ a method

for i dent i fyi ng root causes of human, equipment, and programmatic -

performance probl~ms; 2) identify adverse trends; and 3) identify.

corrective action.

  • *

The inspector_s reviewed RCE Report 92-006, dated October 14, 1992.

This report addressed the event _associated \\'{ith the Unit 2 *turbine

building chiller SW line joint failure of July 13; 1992, which was

discussed i~ NRC Inspection -Report Nos. S0-2Bo; 281/92-17.

This

event-was caused by the failure of a chiller supply breaker to

open when the chiller was removed from service.

As .a result, the

chiller continued to operate with SW flow secured: This resulted

tn overheating of the SW in the system, overpressurizati_on of the*

SW supply to the chiller-and the subsequent failure- of a SW pi~ing

joint_.

The inspectors concluded that RCE 92-06 was thrirough in

identifying the root causes of the event.

Hunian performance

problem were identified in the areas of operator-performance and*

procedural adequacy.

Equipment performance prob 1 ems were *

identified in the areas of chiller configuration and SW-piping

epoxy joints. The inspectors also concluded that the* RCE's

proposed corrective actions were adequate~

Many of the proposed

corrective actions required review and evaluation of procedures or

operating practices for necessary revisions. Since these reviews

have not been completed, .the adequacy of the corrective actions

could not be evaluated.

7

b~ * -

Review of ~orrective Action for Repeated Kaman Spikes

Ka~an radiation monitor, RI-VG-131-1, operated er~atically at the

end o~the assessment period in that it repeat~dly spiked into the

alarfu range.

Approximately 39 station devi~tions hav~ been

written in 1992 documenting spikes or erratic operation of the

Kaman monitor.

The Kaman radiation monitor is required by TSs to

be operational and ITJOnitors par~iculate* activity in the

  • ventilation system vent stack.

Each time.a spike occurred the.*

ventilation system was sampled .. The sample results indicated that.

a radiation release did not occur.

On *numerous b~casions the

Kamari was decl~red inoperable and the appropriate TS LCO entered._

An engineering stlid_y and a CDE were performed to identify the

cause of the Kaman radiation monitor spiking. These reports.

concluded that the exact cause of the spikes.could not be

determined;. NUmerou~ corrective actions such as disassembling and

troubleshooting the components in the system, resoldering wires,

replacing*compone*nts, and the installing insulati_on on wiring were

  • performed.

From the second ha 1 f of_ October_ through the first ha 1 f

of December, ilo spikes occurred and the 1 i censee. speculated that

the problem might have been corrected.

At the end of December,

lhe .Kam~n monitor spikin[ began to r~cur. A comparator board was

replaced and a flow switch was adjusted.

The Kaman monitor was*

- tested and. return~d to service. The Kaman has not spiked since

being return~d to service. *

The inspectors concluded that the licensee has aggressively

pursued corrective action for thi's problem; however, the: _inability

_ to i den ti fy the root ca*use of the spi ~es has resulted in recurring

of *the. problems over the past year.

c.

_Monthly QA Meetin~

The inspectors continued to meet with QA personnel *on a monthly.*

basis to discuss recent QA assessments and audits. The following

items were discuss~d: QA monitoring of the independent

verification process, Triennial and Annual_ Fire Protection Audit,

Inservice Inspection Audit, and the QMT Assessment.

The

inspectors concluded that QA oversight of station acti_vities

remains active.

Within the areas inspected, no violations were identified.

7. *

Lice~~ee Event Review (92700)

The inspectriri reviewed the LERs lfsted helow and evaluat~d the adequacy

of corrective action.

The inspector's review also included followup of

I.

the license*e's .corrective acti_on- implementation.

.8

a.

(Closed) LER 281/91-003, Pressurize'r Safety *Valve Setpoints *

Outside of Technical Specification Allowable Limits.

On April 24,

1991, with Unit 1 at pow~r and Unit 2 shutdown for refueling, two

Unit 2 pressurizer safety valve lift ~et points were found to have

c:lrifted lower than the min_imum allowed by TSs.

Actuation at these

. lower pressures could have an adverse affect on the DNBR. *An

evaluation by the licensee demonstrated that the.setpoinfs assumed

  • by the DNBR analysis were less than .the actual set~oints 6f the

~two relief valves and that the safety valves _were capable.of

performing their overpressure mftigatibn function.

There were no

actual o_r potential consequences to the public health_and safety.

The i~tpoint drift of the~e type safety valves has been a ~eneric

issu~ and resulti from a number of causes, such as, loop seal

pufge ti~e, and the fluid medium (steam or water) used to test the

valve.

As a consequence, Westinghouse and the WOG have held*

meetings to expedite a satisfactory.resolution o.f this issue.

  • sased on these. meeting and studies, Westihgho4se submitted a

position papei (WCAP 12910, Pfessurizer Saf~ty Valve Set Pressure

Shift) to the NRC for a safety evaluation. Surry has issued new

or revised procedures (l/2-MPT-0424-01, 02~ and 03) to test and

set the pressurizer safety valves in a manner that is supported by

Westingh~use and the WOG position (WCAP 12910).

These protedures

have been approved by the station SNSOC.

T~sting is performed

with steam~

Settings are adjusted to a+/- 1 percent tolerance.

Since th~ loop se~l purge times affected the maximum RCS pressure

during transients and is the major contributor to the apparent

_ pressure shift, plant modifications have been formulated to

provide additional operating.margin for these valves:. The loop

seal purge time will be eliminated by installing loop seal drain

lines.

Plant ~odifications in this area (i.e., steam trim package

  • for the valves, loop seal drain lines, and the appropriate piping

supports) are scheduled for the Unit 1 RFO in the spring of .1994

and the Unit 2 RFO in the fall of 1994.

b.

(Closed) LER 281/91-004, Inadvertent Overfilling of Refueling

. Water Storage Tank.

This issue involved the results of a

techt:iical review that was performed for an evaluation of an.

inadvertent overfilling of the Unit 2 RWST.

This reevaluation of

the as-built configuration of the location of the Unit 2 overflow

line showed that the tank could be filled-to a volume of

approximately 399,000 gallons prior to a tank overflow.

Th~ TSs *

allowed 398,000 gallons (TS 3.4.A.3).

The Unit l_RWST's maX"imum

capacity calculated by the position of the overflow piping was

found to be within the TS limits.

The licensee cons6lted with the

Architect/Engineer and discoverea that an analysis had-been made*

during a previous evaluati.o~ for increasing the volume in the RWST

to their current levels. Using this analysis, it was concluded

that the tank design was adequate.

Since no structural concerns

eiisted, a TS change request was .submitted to delete the reference

to maximum capacity for RWSTs.

9

t.

(Closed) LER 281/91-009, *Failure t6 Full Flow Jest 2~RH-47 Due to

Procedure Deficiency. This issue* involved full flow te~ting of

check valve 2-RH-47 during the Unit 2 outage.

The station' ISL *

group's ind~pendent review of the ASME Section Xl program*

,

implementation identified the failure to accomplish full flow

testing of 2-RH~47.

The test procedure co~tained an improp~r

valve lineup.

The RHR sysfem has*a common discharge header which

sp_lits into separate discharge headers. The flow in one loop

passes .through_ a loop_ discharge check valve*, 2-RH-47, before _

discharging into the B reactor coolant loop;

The other loop

discharges directly into the C loop with no check.valve but the

loop does have an isolation valve. *To get full .flow through check

valve, 2-RH-47, the isolatfon ~alve to the C loop would have to be

closed.

The affected procedure was ~hanged and full flo~ testi~g

was performed duririg ~ forced outage.

The RHR syst~m had been

verified capable of delivering design basi~ flow during _the

previous Unit 2 normal outage and the subsequent testing of the

valve d~termined that it was operable. Therefore, no safety

implications were posed during the event.

Within the areas inspected, no viol~tions were identified.*

8.

Exit Interview

.The results were summarized on January 5, 1993, with those individuals

i dent_i fi ed by an asterisk in Paragraph 1.

The following summary of

inspection activity was discussed by the inspectors during this exit:

. * Item Number

Status

. LER .281(91-003

Closed

LER 281/91-004

Closed

LER 281/91-009

Cl os.ed

Description

Pressurizer Safety Valve

Setpoints Outside of Technical

Specification Allowable Limits

(paragraph 7.a).

Inadvertent Overfilling of

Refueling Water Storage Tank

(paragraph 7.b).

Failure t6 Full Flow Test

2-RH-47 Due to Procedure

  • Deficiency (paragraph 7 .c).

Proprietary information is not contained in this report. -Dissenting

comments were not received from the licensee.

9.

Index of Acronyms and Initialisms

ASME

CDE

DNBR

ECCS

AMERICAN SOCIETY OF MECHANICAL ENGINEERS

CAUSE DETERMINATION EVALUATION

DEPARTURE FROM NUCLEATE BOILING RATIO

EMERGENCY CORE COOLING SYSTEM

-~

I

I.

ESGR -

GPM

. I&C

  • IPE

IR

ISI

LCO

LER

LHSI

-

MER

..,

MS

MSTV

NRC

PM

QA

QMT

RCE

RCS

RFO

-RHR

RWST

SALP

SNSOC -

sov

SW , . -

  • TS .

VCT

VPAP

WO . --

WOG

. 10

EMtRGENCY SWITCHGEAR ROOM

GALLON_S P'ER MINUTE *

INSTRUMENTATION AND CONTROL_

INDIVIDUAL PLANT EVALUATION

INSPECTION REPORT

INSERVICE INSPECTIOij

LIMITED CONDITION-OF OPERATION

LICENSEE EVENT REPORT.

LOW HEAD SAFETY INJECTION

MECHANICAL EQUIPMENT ROOM

MAIN STEAM

MAIN STEAM TRIP VALVE

N.UCLEAR REGULATORY COMMISSION

PERIODIC MAINTENANCE

QUALITY ASSURANCE

QUALITY MAINTENANCE TEAM

ROOT CAUSE EVALUATION

REACTOR COOLANT SYSTEM.

REFUELING OUTAGE

RESIDUAL HEAT-REMOVAL

_

REFUELING WATER STORAGE TANK

SYSTEMATIC ASSfSSMENT OF LICENSEE PERFORMANCE

STATION NUCLEAR SAFETY AND OPERATING COMMITTEE ..

. SOLENOID OPERATED VALVE

SERVICE WATER

TECHNICAL.SPECIFICATION

VOLUME CONTROL TANK*

VIRGINIA POWER ADMINISTRATIVE PROCEDURE.

WORK ORDER .

WESTINGHOUSE OWNERS GROUP