ML18152A376

From kanterella
Jump to navigation Jump to search
Insp Repts 50-280/88-26 & 50-281/88-26 on 880605-0702.One Violation Noted.Major Areas Inspected:Licensee Action on Previous Enforcement Matters,Plant Operations,Plant Maint & Surveillance & LER Closeout
ML18152A376
Person / Time
Site: Surry  Dominion icon.png
Issue date: 08/11/1988
From: Cantrell F, Holland W, Larry Nicholson
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18152A377 List:
References
50-280-88-26, 50-281-88-26, NUDOCS 8808290073
Download: ML18152A376 (13)


See also: IR 05000280/1988026

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W.

ATLANTA, GEORGIA 30323

Report Nos.:

50-280/88-26 and 50-281/88-26

Licensee:

Virginia Electric and Power Company

Richmond, Virginia 23261

Docket Nos.:

50-280 and 50~281

Facility Name:

Surry 1 and 2

License Nos.:

DPR-32 and DPR-37

Approved by~* E. ~ctor

F. s.~ASectoef

Division of Reactor Proj ts

Date Signed

8'/1; /g:FJ

tfate Signed

Scope:

SUMMARY

This routine resident inspection was conducted on site in the areas

of licensee action on previous enforcement matters, plant operations,

plant maintenance, plant surveillance, and licensee event report

closeout.

Results:

One violation was identified in this inspection report.

The

following new items were identified in this inspection-report.

One violation (paragraph 6) was identified for failure to provide an

adequate procedure for installation of non-reversible flow orifices

( 280; 281/88-26-01).

-

.. __ .. - ..... .

One unresolved item (paragraph 6) was identified with regards to

cleanliness

controls

and

foreign

material

exclusion

(280;

281/88-26-02).

One licensee identified violation (paragraph 8) was identified with

regards to failure to maintain proper configuration control of a

containment isolation valve as required by Technical Specification

(280/88-26-03).

8808290073 ggggA~BO

PDR

ADOCK

PNU

Q

" *

1.

Persons Contacted

Licensee Employees

REPORT DETAILS

J. Bailey, Superintendent of Operations

  • D. Benson, Station Manager
  • H. Blake, Superintendent of Site Services

R. Blount, Super~ntendent of Technical Services

  • E. Grecheck, Assistant Station Manager

R. Johnson, Operations Supervisor

G. Miller, Licensing Coordinator, Surry

  • H. Miller, Assistant Station Manager
  • F. Mone, Supervisor, Quality, Quality Assurance
  • J. Ogren, Superintendent of Maintenance

J. Price, Site Quality Assurance Manager

S. Sarver, Superintendent of Health Physics

  • Attended exit meeting.

Other licensee employees contacted included control room operators, shift

technical advisors, shift supervisors and other plant personnel.

2.

Plant Status

Unit 1

Unit 1 began the reporting period in day 59 of a maintenance/refueling

outage.

During this period, all reactor coolant pump work was completed,

the reactor cool ant system was fi 11 ed and vented, and the containment

integrated leak rate test was completed.

The unit ended the inspection

period in cold shutdown making preparations to complete required testing

on safety-related pumps.

Unit 2

Unit 2 began the reportins period in cold shutdown with repairs being made

to the 11A11 reactor coo 1 ant pump.

Repairs were completed to the pump on

June 12; however, the discovery of foreign material in the containment

sump, and cleaning delayed leaving cold shutdown until June 18.

The unit

was critical on June 19, and resumed power operations late the same day.

The unit operated at power for the remainder of the inspection period .

2

3.

Licensee Action on Previous*Enforcement Matters

(92702)

(Closed) Unresolved Item 280; 281/88-18-02, Review the controls and

procedure regarding installation of flow orifices.

This item was the

subject of a specific maintenance inspection discussed in paragraph 6

and is being identified as a violation for failure to have adequate

maintenance procedures.

This unresolved item is therefore closed.

(Closed)

Violation 280; 281/ 87-21-B (02), Failure to adequately perform

safety injection undervoltage functional tests.

The inspector reviewed

the licensee response to this violation dated January 28, 1988,

and

verified compliance with that response during the Unit 1 refueling outage

testing which occurred during this period.

Testing to demonstrate that

the loss of voltage protection is defeated and subsequently reinstated

whenever the emergency diesel generator is the sole source of power to the

emergency bus was included, and was performed as part of the refueling

test program.

The inspector witnessed testing and documentation of test

discrepancies during this outage (see paragraph 7) and considers the

licensee corrective actions to be adequate.

This violation is closed.

4.

Unresolved Items

Unresolved items are matters about which more information is required to

determine whether they are acceptable or may involve violations or

deviations.

One new unresolved item (paragraph 6) was identified for

review of the licensee 1 s program for control of cleanliness and foreign

material exclusion in safety-related systems or components.

5.

Plant Operations

Operational Safety Verification (71707)

The inspectors conducted daily inspections in the following areas:

control room staffing, access, and operator behavior; operator adherence

to approved procedures, technical specifications, and limiting conditions

for operations; examination of panels containing instrumentation and other

reactor protection system elements to determine that required channels are

operable; and review of control room operator logs, operating orders,

plant deviation reports, tagout logs, jumper logs, and tags on components.

to verify compliance with approved procedures.

-.. ..

The inspectors conducted weekly inspections in the following areas:

verification of operability of selected emergency safety features systems

by

valve alignment,

breaker positions, condition of equipment or

component(s),

and operability of instrumentation and support items

essential to system actuation or performance.

Plant tours which included observation of general

plant/equipment

conditions, fire protection and preventative measures,

control

of

activities in progress, radiation protection controls, physical security

controls, plant housekeeping conditions/cleanliness, and missile hazards.

'* **~

3

The

inspectors routinely monitor the temperature of the auxiliary

feedwater pump discharge piping to ensure steam binding is prevented,

The inspectors conducted biweekly inspections in the following areas:

verification review and walkdown of safety-related tagout(s) in effect;

review of sampling program (e.g., primary and secondary coolant samples,

boric acid tank samples, plant liquid and gaseous samples); observation of

control room shift turnover; review of implementation of the plant problem

identification system; verification of selected portions of containment

isolation lineup(s); and verification that notices to workers are posted

as required by 10 CFR 19.

Certain tours were conducted on backshi fts or weekends.

Backshi ft or

weekend tours were conducted on June 7, 10, 12, 13, 14, 19, 26, 27, 30,

and July 2.

Inspections included areas in the Units 1 and 2 cable vaults,

Units 1 and 2 containments, vital battery rooms, steam safeguards areas,

emergency

switchgear

rooms,

diesel generator rooms,

control

room,

auxiliary building, cable penetration areas, independent spent fuel

storage facility, low level intake structure, and the safeguards valve pit

and pump pit areas. Reactor coolant system leak rates were reviewed to

ensure that detected or suspected leakage from the system was recorded,

investigated, and evaluated; and that appropriate actions were taken, if

re qui red.

The inspectors routinely independently ca 1 cul ated RCS 1 eak

rates using the NRC Independent Measurements Leak Rate Program (RCSLK9).

On a regular basis, radiation work permits (RWPs) were reviewed and

specific work activities were monitored to assure they were

being

conducted per the RWPs.

Selected radiation protection instruments were

periodically checked, and equipment operability and calibration frequency

were verified.

In the course of monthly activities, the inspectors included a review of

the licensee's physical security program.

The performance of various

shifts of the security force was observed in the conduct of daily

activities to include: protected and vital areas access controls;

searching of personnel,

packages and vehicles; badge issuance and

retrieval; escorting of visitors; and patrols and compensatory posts.

On June 19, the inspector observed *the restart of Unit 2 after completion

of a forced outage that lasted over 30 days.

The inspector reviewed the

appropriate procedures and watched selected startup activities including

taking the reactor critical.

No discrepancies were noted.

Engineered Safety Feature System Walkdown

(71710)

The inspector performed a walkdown of the vital and emergency electrical

distribution system.

This verification also included the following:

confirmation that the licensee's system lineup procedure matches plant

drawings and actual plant configuration;

hangers and

supports are

operable; housekeeping is adequate; valves and/or breakers in the system

are installed correctly and appear to be operable; fire protection/

prevention is adequate; major system components are properly labeled and

6.

4

appear to be operable; instrumentation is properly installed, calibrated,

and functioning; and valves and/or breakers are in correct position as

required by plant procedure and unit status.

Within the areas inspected, no violations or deviations were identified.

Maintenance Inspections (62703)

During

the

reporting

period,

the

inspectors

reviewed

activities to

assure

compliance

with

the appropriate

Inspection areas included the following:

ASSEMBLY OF FLANGED JOINTS

maintenance

procedures.

The inspector reviewed the licensee program for reassembly of flanged

joints.

This inspection was initiated in part due to the discovery of

flow orifices in the auxiliary feedwater (AFW)

system being found

backward as discussed in Inspection Report 280;281/88-18.

The scope of

this inspection included the following procedures:

MMP-C-G-201

dated 2/3/86, Corrective Maintenance Procedure For

Flanged Joints In General.

MMP-C-G-201 dated 5/5/88, Corrective Maintenance Procedure Flanged

Joints In General.

MMP-C-G-201.1 dated 6/10/88,

Corrective Maintenance Procedure For

Blank Flanges, Spectacle Flanges And Orifice Plate Flanges.

The inspector submitted the following comment applicable to all the above

procedures:

A step in the front of the procedures requires the verification that

all bolt or studs have at least one and one-half threads above the

top of the nut prior to disassembly of the flange, yet no step

verifies the as-left thread standout meets any criteria.

Prior to

beginning bf the outage, the inspector discussed this item with the

licensee and identified several fasteners on the Unit 1 service -water

flanges to the reci rcul at ion spray heat exchangers that were much

less than flush with the top of the nut.

These flanges with

insufficient bolt thread standout/engageme~t--were- removed

and

repaired during the current refueling outage.

The licensee agreed

with the inspection findings, and stated that all craft personnel had

been reinstructed on proper thread standout. The licensee considers

that thread standout falls within

11 skill of the craft

11 requirements.

The inspectors also researched the problem of installing flow orifices

backward as identified in unresolved item 280;281/88-18-02.

Prior to

June 10, 1988, orifice flanges were reassembled in accordance with the

genera 1 flange procedure MMP-C-G-201.

This procedure made no reference

or provisions for special cases such as orifice installation or blank and

spectacle flange installation.

As a result, on March 31, 1988, station

5

deviation S2-88-161 identified that AFW flow orifice 2-FW-FE-200A was

installed backward.

The corrective action documented on the deviation

was to reverse the orifice.

Subsequent blockage of the AFW system

required further work on this system; and on June 7, 1988, it was

discovered that the same flow orifice was again installed backward.

The licensee performed an extensive field walkdown and identified the

following six flow orifices that were installed backward:

2-CH-FE-2127

l-CC-FE-1308

l-SW-FE-120A

l-SW-FE-1208

2-RS-R0-210A

2-RS-R0-2108

11 8

11 RCP Seal Injection

l-CC-P-2A Discharge to HHS! Pump Seal Cooler

1-SW-P-lOA Flow to Intermediate Seal Cooler

l-SW-P-108 Flow to Intermediate Seal Cooler

Outside RS Pump Restricting Orifice

Outside RS Pump Restricting Orifice

Engineering Work Request (EWR)88-252 documented the field inspection

findings, and concluded that the incorrect orientation of the above

orifices did not constitute an operational concern.

The EWR states that

reversing the orifice, resulting in the beveled edge oriented upstream,

moves the vena contracta in relation to the downstream pressure tap and

causes an approximately 5 percent lower than actual indicated flow.

The inspectors reviewed the findings and the corrective actions performed

to date and consider them acceptable.

The licensee has performed

extensive work to recover from the lack of adequate controls, including

issuing maintenance procedure MMP-C-G-201.1 dated June 10, 1988, to

specifically address the installation of flow orifices, and prevent this

problem from recurring.

The failure to have an adequate maintenance

procedure that included instructions and verification that flow orifices

were

installed

correctly

constitutes

a

violation

of

Technical

Specification 6.4.A.7. (280; 281/88-26-01).

Based on the NRC's review of

this violation and review of the corrective action, this violation is

closed.

UNIT 1 AND 2 CONTAINMENT SUMP INSPECTIONS AND CORRECTIVE ACTIONS

The screen assembly that surrounds the containment sump is designed to

exclude debris large enough to cause clogged spray nozzles or to affect

the operability of the systems.

The first stage of the screen assembly

consists of inclined bars, which act as trash scre~ns to prevent large

pieces of debris from reaching the sump.

Inside the bars, there are two

layers of screening, the first consists of a roughing mesh, and the

second of a final mesh with an opening approximately the size of the

smallest nozzle orifice in the recirculation spray header. The second

stage of screens consists of cylindrical screens of fine mesh over each

pump suction point. This sump arrangement provides suction for the inside

and outside recirculation spray pumps as well as the low head safety

injection pumps.

6

After discovery of foreign material in the Unit 1 inside recirculation

spray pump lA test strainer, (see paragraph 7), the licensee decided to

inspect the Unit 2 containment sump for similar problems.

The unit was in

cold shutdown while repairs were being accomp 1 i shed on the

11A

11 reactor

coolant pump motor.

On June 9, the licensee commenced the inspections of

the Unit 2 containment sump and gained ful 1 access to the six suet ion

areas on June 11.

Damage and/or imp-roper configuration of screening was

observed during removal of the screen sections.

The licensee contracted

for Westinghouse personnel to conduct visual inspections using fiber optic

equipment in order to survey the six sump areas, and determine if foreign

material was located in these areas.

The inspection scope included the

two

inside recirculation spray pump containers,

the

two

outside

recirculation spray pump suction lines from the sump to the pump suction

isolation valves, and the two low head safety injection pump suction lines

from the sump to the pump suction isolation valves.

The inspection

revealed that foreign objects were present in the two inside recirculation

spray pump containers, and the two low head safety injection pump suction

lines.

No foreign objects were found in the outside recirculation spray

pump suction lines during the initial inspection; however, one foreign

object was found during the final closeout inspection.

Licensee actions to correct these deficiencies included removal of all

foreign objects that were found in the pump containers or suction lines.

Additional actions included repairing of the sump screens, (both circular

and roughing), and maintaining foreign material exclusion during the

reassembly process.

The inspectors monitored licensee actions and also

monitored the repair work in the Unit 2 containment sump area.

Also, the licensee performed an engineering evaluation of all materials

and conditions found, and concluded that the operability of the sump

screens, recirculation spray, and safety injection systems were not

seriously impacted by the discrepancies found.

The licensee provided

copies of the report to NRC Region II and Headquarters staffs.

The

resident inspector reviewed the report and all corrective actions

accomplished by the licensee, and considers that the foreign material issue

in the containment sump for Unit 2 has been resolved.

However, the inspectors conducted a review of the station programs which

allowed this condition to occur. That review concentrated on appropriate

procedures or controls which should have insured exclusion of foreign

materi a 1 , and re qui red that cleanliness was ma i nta iried.

During this

inspection period, the inspectors reviewed the following procedures:

Engineering and Construction Work Procedure WP-G08 dated 3-31-88,

Confinded Entry and Tool Control.

Engineering and Construction Work Procedure WP-MOl dated 11-20-87,

Shop Fabrication and Installation of Piping Systems.

7

Surry

Power Station Administrative Procedure SUADM-M-03 dated

April 28, 1988, Cleanliness Control of Plant Systems and Components.

During the review of the procedures, the inspectors noted that cleanliness

and

accountability

controls

had

been

addressed.

SUADM-M-03

requires controls for primary systems, steam generators, and feedwater

piping from feedwater regulating valves to the steam generators.

However,

the procedure did not specifically address any other systems or areas

other than those deemed by station management as requiring cleanliness or

access control.

WP-G08 also requires controls for basically the same

systems listed above.

However, this procedure also does not specifically

address any other systems or areas other than those deemed by engineering

and construction as requiring cleanliness or access control.

WP-MOl

requires that open ends of pipe, pipe-fittings, valves, and connections

be temporarily capped to maintain proper cleanliness until ready for

fitup; however, no reference is made to identify proper cleanliness

requirements.

The inspector then reviewed the following work orders which were performed

in the past two years to determine if appropriate controls were in place

with regards to cleanliness and/or accountability.

Work Order Job Number (WOJN) 3800040809, Rem./Inst. RS Sump Grating

dated 10/10/86.

WOJN 3800040816, Inst/Remv 12

11 Suet Fng Pen 68 dated 10/10/86.

WOJN 3800040817, Inst/Remv Suet Fng Pen 69 dated 10/10/86.

WOJN 3800046068, Inst. RS Sump Grating dated 11/24/86.

The inspector noted that all of the above work orders were classified as

being safety related; however, all of the work was done without a. formal

procedure.

The inspector did note that each work order cover sheet

identified the work as minor maintenance which he concluded was the

licensee's reasoning for not using procedure to perform the work.

The

inspector concluded that the above work involved some form of entry into*

the containment sump for Unit 2 during the refueling outage in the fall of

1986.

From review of the available information, the inspector also

independently concluded that no controls were placed on these maintenance

activities with regard to cleanliness in the sump(s) nor was tool/

material accountability control documented during these evolutions.

The inspector also reviewed the following design change packages which

were recently accomplished during the Unit 1 refueling/maintenance outage

in the Spring of 1988.

Design Change (DC) -86-13-1 which was approved by the station safety

committee

on

3-24-87, R.G.

1.97 -

CONTAINMENT

SPRAY

FLOW

AND

PRESSURIZER HEATER STATUS/SURRY/1.

8

DC-87-22-01 which was approved by the station safety committee on

3-29-88,

REPLACEMENT

OF CONTAINMENT

RECIRCULATION SPRAY COOLERS/

SURRY /1.

The inspector noted in DC-86-13-1 that a precaution step was included in

the procedure which required system cleanliness to be maintained during

installation.

However,

no

steps in the procedure documented any

conditions fer maintenance of system cleanliness or accountability. This

area was discussed with engineering personnel, and the reply was that craft

and quality control personnel

are trained to maintain appropriate

cleanliness during evolutions in which systems are open for repair.

Discussions with quality control supervision indicated that while quality

control personnel w*ill do inspections for foreign materials during fitup

and

welding

evolutions

requiring

quality

control

verifications,

inspections

are

not

normally

made

for cleanliness or material

accountability during the entire time that systems are open for

maintenance unless specifically required by procedure.

The inspector noted in DC-87-22-1 that no mention of cleanliness or

accountability requirements was made in the precautions or body of the

procedures.

This condition was also discussed with engineering and the

reply was that cleanliness was controlled by WP-MOl, which requires open

ends of pipe, pipe-fittings, valves, and connections be temporarily

capped to maintain proper cleanliness until fit-up.

The

inspector

concluded that although administrative procedure does require temporary

capping, the cleanliness or foreign material exclusion consideration was

not adequately addressed to ensure foreign material exclusion was being

maintained.

At the end of the inspection period, the inspector discussed his concerns

with station management and requested any additional information which

would provide assurances that appropriate cleanliness or foreign material

exclusion was

being maintained during maintenance on safety-related

systems or components.

This i tern is i dent i fi ed as unreso 1 ved ( 280;

281/88-26-02) pending the inspector

1 s review of additional information

concerning the issue.

HEAT TRANSFER CAPABILITY OF UNIT 2 RECIRCULATION SPRAY HEAT EXCHANGERS

During this inspection period, a concern was identified regarding

operability of the Unit 2 recirculation spray heat exchangers due to

fouling of the heat exchanger tubes thereby reducing the heat transfer

capability.

The fouling was due to service water leakage into the heat

exchangers when the design considerations assumed that the heat exchangers

would be maintained dry.

Unit 1 was not immediately affected by the

concern due to the fact that it was in the middle of a refueling outage in

which new recirculation spray heat exchangers were being installed.

At

the time the concern was identified, Unit 2 was in cold shutdown while

repairs were being accomp 1 i shed to a reactor coo 1 ant pump motor.

The

licensee had conducted an engineering evaluation of this condition in 1984.

That evaluation concluded that sufficient design margin existed with

7.

I

9

regard to fouling factor to conclude that the heat exchangers could perform

their safety function with higher values than was originally considered

during design.

These values were larger than 0.001, but less than 0.0015.

The licensee, because of the concern, decided to open and inspect the

service water side of the four recirculation spray heat exchangers prior

to Unit 2 restart.

The licensee also contracted a heat exchanger

specialist for these in~pections.

Although initial inspections concluded

that the fouling factor was approximately 0.001, the licensee decided to

clean the tubes of the four heat exchangers in order to further reduce the

fouling.

Cleaning was accomplished, and the final inspections estimated

that the fouling factor was 1 ess than O. 001.

The 1 i censee issued a

report,

(TECHNICAL

REPORT

NO.

ME-0166)

dated

June

10,

1988,

which concluded that the Unit 2 recirculation spray heat exchangers, after

cleaning, are capable of performing their design function as stated in the

Final Safety Analysis Report.

In addition, the licensee instituted new operational actions which monitor

for leakage past the service water supply valves, and thereby allow for

determination as to whether the heat exchangers are being maintained in

dry layup.

The inspectors monitored the licensee actions, reviewed the

engineering report, and verified that procedures were in place to monitor

for service water leakage prior to Unit 2 restart.

Also, the NRC

Region II and Headquarters offices were

kept apprised of licensee

actions, and were provided a copy of the licensee

1 s technical report prior

to Unit 2 restart.

Additional reviews in this area are discussed in

Inspection Report 280,281/88-27.

OVERHAUL OF AUXILIARY FEEDWATER PUMP

The

inspector witnessed portions of the overhaul

and preventive

maintenance on motor-driven AF'vJ pump 1-FW-P-38.

This work was performed

under work order #3800067955 in accordance with procedure MMP-C-FW-092,

Dissasembly, Inspect and Repair of Auxiliary Feedwater Pump 1-FW-P-2 &

2-F\\v-P-2.

This procedure was written for the turbine-driven pump, and

required deviating for work on the motor-driven pump.

The inspector

reviewed documentation for the parts that were replaced, and verified all

measurements were within the acce.ptab 1 e range.

The work package was

complete and maintained up to date.

No discrepancies were noted.

Within-the areas inspected, one violation was identified.

Surveillance Inspections

(61726)

During the reporting period, the inspectors reviewed various surveillance

activities to assure compliance with the appropriate procedures as

fo 11 ows:

Test prerequisites were met

Tests were performed in accordance with approved procedures

10

Test procedures appeared to perform their intended function

Adequate coordination existed among personnel involved in the test

Test data was properly collected and recorded

Inspection areas included the following:

Testing of the Unit 1 Inside Recirculation Spray Pumps (1-RS-P-lA and B)

During this inspection period, the inspectors witnessed testing of

1-RS-P-lA in accordance with special test l-ST-214, Operability of IRS

Pumps.

The stated purpose of this test was to prove operability of the

inside recirculation spray pumps, and to establish reference values for

inside recirculation spray pump testing in accordance with ASME Section

XI, Subsection IWP.

The inspectors reviewed the test procedure prior to

test performance, attended the shift briefing prior to test performance,

and observed the initial testing of 1-RS-P-lA from the control room, and

from inside containment.

The first series of test runs on the

11A

11 pump occurred on June 7, 1988.

During the first run, the pump was secured after approximately a three

minute run due to the discharge strainer in the test 1 i ne becoming

partially clogged with debris from the sump.

The sicond pump start was

secured from the control room after the pump ran for approximately two

minutes due to no flow indication output from the flow instrument.

There

had been actual flow, but due to communication problems, this was not

understood in the control room.

The third pump run lasted approximately

24 minutes, and the pump was secured after the discharge strainer again

indicated partial blockage.

The inspector noted that flow indication as

specified in the test was not available during any of the runs. Also, the

causes for the partial blockage of the strainers was debris including

paint chips, nuts, bolts, washers, welding rods, and other material .. The

licensee conducted an inspection of the second stage sump screen, and

found evidence of degradation that would allow passage of material as

found in the strainer. Additional corrective actions for the condition of

the sump cleanliness and screen repair are addressed in paragraph 6.

On June 16, 1988, the licensee tested the inside recirculation spray pump

(2-RS-P-lA) in accordance with Unit 2 periodic test 2-PT-17.2, Containment

Inside- Recirculation Spray Pump.

During that run, the pump was.-stopped

after approximately 10 seconds due to high current readings.

The sump well in which the

11 1N' pump is located and, therefore, the pump

itself, had been drained of water during inspection of the sump area (see

paragraph 6).

The well was not refilled with water prior to this short

"bump" test ( nor was it required by procedure).

It was theorized that

without the water acting as a lubricant, the motor drew much higher

current.

An engineering evaluation was written at this point and the sump

well was refilled with water.

On June 17, 1988, the inspector witnessed

the retesting of the

11 1A

11

pump.

Prior to the test, the inspector

8.

11

independently verified that the pump would turn freely by hand, before and

after the test.

Also, the inspector reviewed the engineering evaluation

of the

11 lA

11 pump due to an unsuccessful pump run on the

11 lA

11 pump the day

before.

The engineering evaluation was documented in Engineering Work

Request (EWR)88-256 dated June- 17, 1988.

The EWR was approved by the

station safety committee on the same day.

The

EWR cone l uded that

2-RS-P-lA was operable based on the successful performance of the pump

periodic test, and the statement by the pump representative that water in

the pump can result in satisfactory pump operation.

No discrepancies were

noted.

On Jur,e 27, 1988, the inspector witnessed part of testing of the safety

injection system in accordance with 1-PT-18.1, High Steam Flow Test of

Steam Line Trip and RWST Crossconnect Valves.

This test simulates a high

steam flow in conjunction with low Tave, verifies the main steam trip

val~es close, and the RWST crossconnect valves realign to the opposite

unit.

The inspector noted that the operators performing this test were

knowledgeable, and communicated well with the control room.

All equipment

appeared to perform as required.

No discrepancies were noted.

On June 29 & 30, 1988, the inspectors witnessed portions of the Unit 1

periodic test 1-PT-18.2A & B, Safety Injection Train A - H Bus Under-

voltage Functional Test and Safety Injection Train B - J Bus Undervoltage

Functional Test. This test verifies proper alignment and operation of the

safety injection system, when initiated in conjunction with an undervol-

tage condition on the emergency bus.

The inspector witnessed pre-job

planning and noted that communications and assignments were adequate.

Testing was well coordinated by two Senior Reactor Operators.

The inspec-

tor reviewed the test results and documentation of discrepancies and found

this area to be improved from previous tests of this nature.

No discrepan-

cies were noted.

On June 30, 1988, the inspector witnessed testing of the safety injection

check valves per periodic test 1-PT-18.3A, Refueling Testing of High Head

Safety Injection Check Valves to the Cold Legs.

This test verifies flow

from the refueling water storage tank to the cold leg.

The inspector

verified that testing was performed in accordance with the procedure, and

that equipment performed as required.

No discrepancies _were noted.

Within the areas inspected, no violations or deviations were identified.

Licensee Event Report (LER) Review

(92700)

The inspector reviewed the LERs listed be 1 ow to ascertain whether NRC

reporting requirements were being met, and to determine appropriateness of

the corrective action(s).

The inspector's review also included followup

on implementation of corrective actions, and review of licensee documenta-

tion that all required corrective action(s) were complete.

LERs that identify violation(s) of regulation(s) and that meet the

criteria of 10 CFR, Part 2, Appendix C,Section V are identified as

Licensee Identified Violations (LIV) in the following closeout paragraphs.

12

LIVs are considered first-time occurrence violations which meet the NRC

Enforcement Policy criteria for exemption from issuance of a Notice of

Violation.

These items are identified to allow for proper evaluation of

corrective actions in the event that similar events occur in the future.

(Closed) LER 280/88-01,

Containment Isolation Valve Not Properly Locked

Under Administrative Control Due To Human Error.

This report involved a

non-automatic containment isolation valve (1-SI-150) that was not properly

locked under administrative control, although the valve was found in the

required closed position.

The inspector verified that the valve is

currently locked, and reviewed the licensee enhancements regarding control

of keys.

Technical SpGcification 1.0.H.1 requires that all non-automatic

containment isolation valves be locked closed and under administrative

control.

Technical Specification Table 3.8-1 further identifies valve

1-SI-150 as a manual containment isolation valve.

The failure to maintain

this valve locked is a violation of technical specifications and is

identified as a LIV (280/88-26-03).

This item is closed.

9.

Exit Interview

The inspection scope and findings were summarized on July 5, 1988, with

those individuals identified by an asterisk in paragraph 1.

The following

new items were identified by the inspectors during this exit.

One violation (paragraph 6) was identified for failure to provide an

adequate procedure for installation of non-reversible flow orifices (280;

281/88-26-01).

One unresolved item (paragraph 6) was identified with regard to cleanli-

ness controls and foreign material exclusion (280; 281/88-26~02).

One

licensee-identified violation (paragraph 8) was identified with

regard to failure to maintain proper* configuration control of a

containment isolation valve as required by Technical

Specification

(280/88-26-03).

The licensee acknowledged the inspection findings with no dissenting

comments.

The licensee did not identify as proprietary any of the

materials provided to or reviewed by the inspectors during this

inspection.

. .. **-...::-****--* .

,...,_ .._ __