ML18152A341

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Insp Repts 50-280/94-17 & 50-281/94-17 on 940605-0702. Violations Noted.Major Areas Inspected:Plant Status, Operational Safety Verification,Maint & Surveillance Insps & Action on Previous Insp Items
ML18152A341
Person / Time
Site: Surry  Dominion icon.png
Issue date: 07/21/1994
From: Branch M, Tingen S
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18152A342 List:
References
50-280-94-17, 50-281-94-17, NUDOCS 9408090310
Download: ML18152A341 (17)


See also: IR 05000280/1994017

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W., SUITE 2900

ATLANTA, GEORGIA 30323-0199

Report Nos.: 50-280/94-17 and 50-281/94-17

Licensee: Virginia Electric and Power Company

Innsbrook Technical Center

5000 Dominion Boulevard

Glen Allen, VA

23060

Docket Nos.:

50-280 and 50-281

License Nos.:

DPR-32 and DPR-37

Facility Name:

Surry 1 and 2

Inspection Conducted: June 5 through July 2, 1994

Inspectors:

L.c.J ~

~

S. G. Tingen, ~Inspector

Accompanying Personnel:

D. M. Tamai

Approved by:

f )( k- ~

G. A. B~lisle, ~

Reactor Projects Section 2A

Division of Reactor Projects

SUMMARY

Scope:

?.-:J-1- Cf 'f

Date Signed

?- )-/-9r

Date Signed

This routine resident inspection was conducted on site in the areas of plant

status, operational safety verification, maintenance and surveillance

inspections, and action on previous inspection items.

Inspections of

backshift, holiday, and weekend activities were conducted on June 6, 16, 24,

and 25 and July I.

Results:

Operations functional area

Command and control, use of procedures, and the quality of startup procedures

utilized during the Unit 2 startup were good {paragraph 3.4).

9408090310 940721

PDR .ADOCK 05000280

G

PDR

2

The failure to secure closed a Unit 2 makeup water isolation valve within 15

minutes after makeup as required by technical specification 3.2.F was

identified as a violation (paragraph 3.5).

Maintenance functional area

The Unit 2 steam generator chemical cleaning was well managed and the

contractor oversight provided by the licensee during this evolution-was

excellent (paragraph 3.3).

In the last 18 months, the Unit 1 and 2 turbine driven auxiliary feedwater

pumps have tripped on overspeed on 5 different occasions.

The corrective

actions for each of the overspeed trip events were considered reasonable.

Root Cause Evaluation 93-25 was being re-opened to further evaluate governor

valve binding (paragraph 4.1).

Actions previously implemented to correct deficiencies associated with foreign

material exclusion (FME) control did not preclude repetition. Three examples

where personnel did not maintain FME controls in accordance with the station

FME program were identified as a violation (paragraph 4.2).

Engineering functional area

Two accident analyses reviewed in conjunction with the Design Basis Document

for the Auxiliary Feedwater and Safety Injection Systems contained assumptions

that were not bound by operational practices.

An Inspection Followup Item was

identified to track resolution (Paragraph 5.2).

. *.*

~ ..

REPORT DETAILS

1.

Persons Contacted

I.I Licensee Employees

  • R. Bartnikowski, Supervisor, Mechanical Maintenance
  • W. Benthall, Supervisor, Licensing
  • H. Blake, Jr., Superintendent of Nuclear Site Services
  • R. Blount, Superintendent of Maintenance
  • D. Christian, Assistant Station Manager
  • R. Cross, Coordinator, Nuclear Procedures
  • J. Downs, Superintendent of Outage and Planning
  • D. Erickson, Superintendent of Radiation Protection

A. Friedman, Superintendent of Nuclear Training

  • S. Hall, Mechanical Maintenance
  • W. Harrell, Vice President, Nuclear Engineering

B. Hayes, Supervisor, Quality Assurance

  • D. Hayes, Superintendent of Administrative Services
  • M. Kansler, Station Manager

C. Luffman, Superintendent, Security

J. McCarthy, Superintendent of Operations

  • J. McGinnis, Station Nuclear Safety

A. Price, Assistant Station Manager

  • R. Saunders, Vice President, Nuclear Operations
  • K. Sloan, Supervisor, Operations Support
  • E. Smith, Site Quality Assurance Manager
  • T. Sowers, Superintendent of Engineering
  • J. Swientoniewski, Supervisor, Station Nuclear Safety
  • G. Thompson, Supervisor, Maintenance Engineering

G. Woodzell, Nuclear Training

Other licensee employees contacted included plant managers and

supervisors, operators, engineers, technicians, mechanics,

security force members, and office personnel.

1.2

NRC Personnel

  • M. Branch, Senior Resident Inspector
  • S. Tingenj Resident Inspector
  • D. Tamai, Intern
  • Attended Exit Interview

Acronyms and initialisms used throughout this report are listed in the

last paragraph .

2

2.

Plant Status

3.

Unit 1 operated at power for the entire inspection period.

Unit 2 was in cold shutdown at the beginning of the inspection period to

perform SG chemical cleaning. This chemical cleaning was necessary to

remove corrosion deposits/flow blockage from the SG tube support plate

area that was causing level oscillation problems in the C SG.

After the

chemical cleaning, the unit returned to power operations on June 25 and

operated at 100% power throughout the remainder of the period without

experiencing SG level oscillations.

Operational Safety Verification (71707, 37551)

The inspectors conducted frequent tours of the control room to verify

proper staffing, operator attentiveness and adherence to approved

procedures.

The inspectors attended plant status meetings and reviewed

operator logs on a daily basis to verify operational safety and

compliance with TSs and to maintain overall facility operational

awareness.

Instrumentation and ECCS lineups were periodically reviewed

from control room indications to assess operability. Frequent plant

tours were conducted to observe equipment status, fire protection

programs, radiological work practices, plant security programs and

housekeeping.

Deviation reports were reviewed to assure that potential

safety concerns were properly addressed and reported.

3.1

Biweekly ESF Inspections

3.1.1 Unit 1 AFW System

The inspectors walked down the Unit 1 AFW piping located in

the safeguards building following maintenance performed on

the turbine driven AFW pump on June 15 and 16.

Valve

positions, piping temperatures, snubber oil levels and

general component conditions were inspected.

The inspectors

concluded that the system was operable and in good material

condition.

3.1.2 Unit 2 AFW System

An inspection of the AFW system was conducted.

The

inspectors walked down piping in containment and pumps and

piping in the safeguards building. Valve position, snubber

condition, and material condition of the equipment were

inspected. The inspectors concluded that the system was

operable and in good material condition .

3

3.2

Unit 2 RCS Draindown to 18.3 Feet

On June 6, the inspectors witnessed draining the Unit 2 RCS from a

level of 5% in the pressurizer (approximately 29.0 feet) to a

level of 18.3 feet in the reactor vessel. Draining the RCS system

to this level was required to support installing pressurizer

safety valve loop seal drain lines. This evolution was

accomplished in accordance with section 5.7 of 2-0P-RC-004,

Draining the RCS to Reactor Flange Level, revision 2.

During the

initial drain down phase, pressurizer level was monitored.

During

the draindown from 0% level in the pressurizer (approximately 27.5

feet) to the 24 foot level on the reactor vessel standpipe,

indication was not on scale and an inventory balance was utilized

to determine the amount drained from*the RCS.

Upon reaching the

24 foot level, the reactor vessel standpipe was utilized to

monitor RCS level. The inspectors monitored the rate of

increasing level in the boron recovery tank, seal injection flow

rate and letdown flow rate during the evolution where inventory

balancing was required.

The inspectors also verified that once

RCS level was in the range of the reactor vessel standpipe, main

control board indication of RCS level agreed with the local

standpipe indication.

No discrepancies were noted.

Prior to placing the reactor vessel standpipe in service, the

inspectors accompanied the system engineer and operations engineer

on a walkdown of the portion of the standpipe assembly that vents

the reactor head to the top of the pressurizer. The purpose of

this walkdown was to identify conditions that could create false

reactor vessel indication on the standpipe.

In a letter to the

NRC dated April 8, 1994, the licensee committed to review the

Unit 2 reactor vessel standpipe installation prior to placing it

into service. This commitment was generated due to perturbations

in Unit 1 reactor vessel standpipe level indication which were

discussed in NRC Inspection Reports Nos. 50-280, 281/94-02.

No

problems were identified during the walkdown and no perturbations

in the Unit 2 reactor vessel standpipe level indication occurred

while the system was inservice during the draindown evolution.

3.3

Unit 2 SG Cleaning Activities

The inspectors monitored activities associated with chemically

cleaning the secondary sides of the Unit 2 SGs.

SG cleaning

activities were accomplished by contractors. Chemical cleaning

involved a 3-step stage/process. Step 1 included injecting and

recirculating a copper solvent solution at 95 degree F followed by

a SG rinse. Step 2 included injecting and recirculating an iron

solvent solution at 195 degrees F followed by a SG rinse. Step 3

repeated the step 1 copper solvent process.

Following this

process, each SG was drained and refilled with water several times

to ensure that all chemicals were removed.

Throughout the

cleaning process, high pressure nitrogen was injected into the SG

to increase turbulence. After completing chemical cleaning, each

3.4

4

SG was drained and sludge lancing was performed.

The final

estimates, in pounds, of removed materials were:

Copper

Iron

Sludge

SG A

350

2600

1258

SG B

470

3050

984

SG C

500

3900

610

Once the actual cause of level oscillation in the C SG was known,

the licensee rapidly assembled a dedicated team of both plant and

contractor personnel for the project. This team completed the

project ahead of schedule and without impacting other scheduled

activities. Extensive briefings were held and video records were

assembled to share information gained with others in the industry.

The inspectors concluded that evolutions associated with the

Unit 2 SG chemical cleaning were well managed, and that the

contractor oversight provided by the licensee during this

evolution was excellent.

The inspectors also reviewed SE 94-115, Unit 2 Steam Generator

Chemical Cleaning.

The SE required that each reactor coolant loop

be drained and isolated during the chemical cleaning process.

This was primarily because a SG temperature of 195 degrees F was

required to perform the iron removal phase and that TSs required

containment integrity to be established when RCS temperature

exceeded 200 degrees F.

With the loop drained, RCS temperature

could be maintained well below 200 degrees F and the SG could be

heated up to the desired temperature without the need to establish

containment integrity.

No discrepancies were noted with the SE.

Unit 2 Startup

On June 24 and 25, the inspectors witnessed the Unit 2 startup.

Evolutions monitored were taking the unit critical, opening the

MSTVs, turbine driven AFW pump testing, placing the turbine in

service and transferring control of FW regulating valves from

manual to automatic control. The only significant equipment

problem that occurred during the startup was that the A loop delta

T indication corresponded to 10% power when the reactor was at 2%

power.

The channel was declared inoperable and placed in trip as

required by TSs.

The startup was delayed while technicians

attempted to repair the channel. Technicians were unable to

repair the channel and the startup was resumed with the A loop

delta Tin trip.

An RTD lead imbalance was later identified as

.

the cause of the channel not indicating properly and was repaired

after the unit was placed on line. The inspectors concluded that

command and control, use of procedures, and quality of startup

procedure were good .

5

3.5

Isolating Makeup Water to the RCS During Cold Shutdown

On June 17, 1994, following a makeup evolution to the RCS, the

primary water isolation valve was not secured closed.

TS 3.2.F

requires during cold shutdown and refueling conditions that valve

2-CH-223 or valves 2-CH-212, 215, and 218 be locked, sealed or

otherwise secured closed except during planned boron dilution or

makeup activities. Following a planned dilution or makeup

activities, the valve{s} must be secured closed within 15 minutes.

The licensee was operating with 2-CH-223 open and 2-CH-212, 215,

and 218 secured closed. At 12:11 p.m., makeup activities were

initiated. The control room operator notified the auxiliary

building operator to open 2-CH-212.

After terminating makeup

activities at 12:14 p.m., the valve was not closed. The incorrect

valve position was not discovered until 4:22 p.m. when the next

shift requested the valve to be opened for makeup activities.

Operations identified that a violation of TS 3.2.F had occurred.

They initiated a DR, and requested chemistry to measure the RCS

boron concentration to ensure that a dilution had not occurred.

The inspectors reviewed the event and concluded that the following

factors contributed to exceeding the 15 minute TS limit:

Two control room operators were overseeing a trainee

performing the makeup.

The control room operators failed to

control the trainee's actions and the makeup evolution.

A procedure did not exist for makeup activities during cold

shutdown conditions. This was considered a skill of the

craft evolution.

The purpose of the TS is to prevent an inadvertent boron dilution

of the RCS during cold shutdown or refueling conditions.

As immediate corrective actions, trainee manipulations of control

board switches were suspended, and the trainees were prohibited

from communicating instructions to the field operators. The

corporate fuels division performed an analysis to demonstrate that

an alarm would actuate early in the dilution allowing control room

operators adequate time to prevent a criticality. The inspectors

reviewed the analysis and concluded the results were satisfactory.

The licensee indicated that a procedure was being written for

makeup activities during cold shutdown and refueling conditions.

The licensee currently intends for the procedure to include a

pre-evolution briefing and logging of critical steps including

compliance with the 15 minute TS requirement.

On June 17, 1994, valve 2-CH-212 was open for a period of 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />

and 8 minutes following makeup activities. This exceeded the 15

minute TS limit by 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> and 53 minutes.

The failure to close

and secure 2-CH-212 within 15 minutes following a makeup activity

while in a cold shutdown condition in accordance with TS 3.2.F was

6

identified as VIO 50~281/94-17-01, Failure to Close Unit 2 Makeup

Water Isolation Valve*Within 15 Minutes After Makeup.

Within the areas inspected, one violation was identified.

4.

Maintenance And Surveillance Inspections (62703, 61726)

During the reporting period, the inspectors reviewed the following

maintenance/surveillance activities to assure compliance with the

appropriate procedures.

4.1

Unit 1 Turbine Driven AFW Pump Maintenance/Testing

On June 15, the Unit 1 turbine driven AFW pump, l-FW-P-2, tripped

on overspeed while performing monthly test, l-OPT-FW-003, Turbine

Driven AFW Pump l-FW-P-2, revision 3.

The pump was declared

inoperable and a 72-hour LCO was entered in accordance with TS 3.6.F. Later that same day, the pump was restarted to investigate

the cause of the overspeed trip. The inspectors witnessed the

second start of the pump and noted.that the pump started and

operated satisfactorily.

WO 291712-01 was initiated to investigate/repair the turbine

governor valve.

The inspectors witnessed this maintenance which

was accomplished in accordance with procedure O-MCM-0401-01,

Valves & Traps in General, revision 2.

The governor linkage was

disconnected from the governor valve and mechanics manually

exercised the governor valve stem.

The stem was identified as

sticking/binding when manually exercised. The governor valve

bonnet was then disassembled and the bonnet components were

inspected.

The stem was slightly bent and approximately 80% of

the carbon packing bushings were broken into two or more pieces.

A hard deposit buildup was also identified *on the stem at the

pa~king area. A new bonnet, stem, and packing bushings were

installed.

Following the new bonnet, stem and packing bushing installation,

the inspectors under the supervision of the licensee manually

exercised the stem and noted that the stem moved freely with no

binding or sticking. The stem was then connected to the turbine

governor linkage and the turbine driven AFW pump was tested in

accordance with l-OPT-FW~003.

The inspectors witnessed this

testing and the pump operated satisfactorily. After completing

the test, the pump was declared operable and the TS 3.6.f 72-hour

LCO was exited.

Unit 2 was in CSD when the turbine driven AFW pump failure

occurred on Unit l; therefore, the Unit 2 turbine driven AFW pump

could not be started to verify operability. However, the Unit 2

turbine governor linkage was disconnected from the governor valve

and mechani~s manually exercised the governor valve stem.

The

-

7

stem was identified as stuck and could not be manually exercised.

The governor valve bonnet was then disassembled and the bonnet

components were inspected. A hard deposit buildup was also

identified on the stem at the packing area. A new stem and

packing bushings were installed. After the unit was restarted,

the inspectors witnessed the Unit 2 turbine driven AFW pump

testing in accordance with 2-0PT-FW-003.

The pump started and

operated satisfactorily during testing.

The inspectors reviewed the operational history for Unit 1 and 2

turbine driven AFW pumps and noted that since January 1993, these

pumps have oversped five times during surveillance testing.

On

January 15, 1993, the Unit 2 turbine driven AFW pump tripped on

overspeed after being started for a monthly surveillance test.

On

March 26, 1993 the Unit 1 turbine driven AFW pump tripped on

overspeed after being started for a monthly surveillance test.

The cause of these failures was attributed to failure of the steam

trap located in the turbine steam supply piping to each individual

turbine. These events and corrective actions were discussed in

NRC Inspection Report Nos. 50-280, 281/93-07.

On December 2, 1993, the Unit 1 turbine driven AFW pump tripped on

overspeed after being started for a monthly surveillance test.

The governor valve linkage was disconnected and the stem was

checked for freedom of movement.

The valve stem was found to be

stuck in the open position. The governor valve bonnet, stem and

packing were replaced. This event was discussed in NRC Inspection

Report Nos. 50-280, 281/93-26.

RCE 93-25 was performed in order

to determine the cause of the failure.

RCE 93-25 concluded that pitting corrosion and mineral deposits on

the valve stem caused the valve stem to bind with the packing

materials in the bonnet.

The RCE also concluded that the mineral

deposits were possibly the accumulation of mineral residue from

moisture carryover over a long period of time (five to six years).

The RCE referenced a report by the governor valve manufactures,

Dresser Industries, dated March 24, 1993, that stated that there

had been a few nuclear plants exhibiting corrosion related valve

stem binding. The report stated that the environment of the

governor valve was critical and that a dry environment for stem

and packing assembly was desired when the equipment was not

operating.

RCE 93-25 implemented modifications to enhance draining moisture

from the governor valve packing area and a PM item to periodically

inspect governor valves stems in each unit every refueling outage.

The RCE also implemented a program to monitor and trend governor .

valve position and turbine speed ramp rate on a quarterly basis.

The RCE recommended that the turbine driven AFW pumps in both

units continue to be tested monthly because stroking the governor

valve might assist in reducing or controlling the mineral deposit

buildup on the stem.

8

The inspectors reviewed the surveillance tests completed after

December 2, 1993, on the Unit 1 turbine driven AFW pump.

On

December 3 and 29, 1993, the pump was satisfactorily tested.

On

January 22, 1994, Unit 1 was shutdown for a RFO and restarted on

March 24, 1994.

On March 25, 1994, the Unit 1 turbine driven AFW

pump tripped on overspeed after being started for the first time

since December 29, 1993.

The Unit 1 turbine driven AFW pump

operated satisfactorily on the second and third starts.

No

additional corrective action was performed and the pump was

determined to be operable. The failure was attributed to air

introduction into the governor during periodic maintenance

performed during the outage.

On April 21, and May 14 and 18,

1994, the Unit 1 turbine driven surveillance tests were

satisfactorily performed.

On May 11, the Unit 1 turbine driven

AFW pump automatically started and operated as designed after the

reactor was manually tripped. However, on June 15, the Unit 1

turbine driven AFW tripped on overspeed while performing the

monthly surveillance test.

The inspectors also reviewed the surveillance test performed on

the Unit 2 turbine driven AFW pump completed since January 12,

1994.

On January 12, February 9, March 10, April 6 and May 4, the

Unit 2 turbine driven AFW pump surveillance tests were

satisfactorily performed. There were no indication of the

governor valve binding subsequently discovered in June 1994.

At the end of the inspection period the licensee was in the

process of re-opening RCE 93-25 in order to reevaluate the root

cause of governor valve binding.

To ensure that the turbine

driven AFW pumps remain operable while correctives actions are

developed and implemented, the licensee was inspecting the

governor valve stems in both units weekly for a hard deposit

buildup and were continuing to perform surveillance testing at a

monthly frequency.

The inspectors concluded that the corrective

actions for each of the five Unit 1 and 2 turbine driven AFW pump

failures were reasonable.

The inspectors will continue to monitor

the licensee's actions in this area.

4.2

FME Control Deficiencies

VPAP-1302, Foreign Material Exclusion Program, rev1s1on 5,

specifies requirements to prevent foreign material, such as

maintenance residue, dirt, debris, and tools from entering open

systems or components.

During the inspection period, the

following examples were identified where VPAP-1302 requirements

were not adhered to during maintenance performance.

On June 10 the inspectors toured the Unit 2 containment.

When walking down the design change to install drain lines

on the pressurizer safety valve loop seals, the inspectors

noted that openings in the piping on the bottom of the A and

C pressurizer safety valve loop seal drain line penetrations

=..:=-..::=..:===-:==--=-=--=-=-=--=-=--=--==-=-=== ~-- - ----

9

did not have FME covers installed. Maintenance in the area

was not in progress when this condition was identified. It

appeared that at one time the openings had been taped over,

but the tape was not attached to the piping when the

inspectors walked down the area. The inspectors notified

the licensee of this condition and FME covers were

installed.

DR S-94-1232 was issued documenting that the FME

control boundary was violated.

During the Unit 2 outage, the A pressurizer safety valve was

removed and a wire mesh screen installed over the opening.

This configuration provided a vent path for the reactor

coolant system in accordance with TS 3.1.G.l.b.(5).

On

June 17 an operator noted that the FME cover installed over

the A pressurizer safety valve flange was not adequately

attached. Personnel had breached the cover to install a

purge hose for welding the loop seal drain line modification

and did not properly secure the cover following purge hose

installation. After this condition was identified the FME

cover was properly attached and DR S-94-1280 issued.

On June 21, the component cooling heat exchanger 1-CC-E-lA

was determined to be inoperable while performing

surveillance l-OSP-SW-002, Measurement of Macrofouling

Blockage of Component Cooling Heat Exchanger 1-CC-E-lA,

revision 4.

The procedure's SW flow rate acceptance

criterion would not be met.

On June 22 the SW side of the

heat exchanger was opened for inspection and a 14-inch by

64-inch piece of plywood, tape, and wire mesh used for

scaffolding were found in the tube sheet area. It was

concluded that the scaffolding material was left in the heat

exchanger after it was cleaned on June 16.

DR S-94-1323 was

issued documenting that materials were found in the heat

exchanger.

The materials were removed and the heat

exchanger was satisfactorily tested in accordance with

l-OSP-SW-002.

The first two examples involving improper FME controls involved a

design change performed in accordance with DCP 92-044, Pressurizer

Safety Valve And Loop Seal Modification - Surry Unit 2, dated

May 3, 1994.

DCP 92-044 invoked GMP-M-152, Fabrication and

Installation of Piping, revision 2. Step 6.1.4 of GMP-M-152

required that FME be established in accordance with VPAP-1302.

Paragraph 6.3 of VPAP-1302 requires that system openings be

covered with temporary covers when leaving the work area

unattended to prevent intrusion of foreign material.

Heat exchanger 1-CC-E-lA had been cleaned in accordance with

procedure MMP-C-HX-277, Tube Sheet and Channel Cleaning For

Bearing and Component Cooling Heat Exchangers, revision 1. Step

4.1 of MMP-C-HX-277 required that system cleanliness be maintained

and QC closeouts be performed prior to closing the system.

10

VPAP-1302 was invoked to maintain cleanliness and perform the QC

closeout. Step 6 of VPAP-1302 required that a FME control log be

maintained and that this log be reviewed prior to closing a system

to ensure that all articles introduced to the system during the

maintenance were removed and accounted for. Step 6.4 required

that the system be inspected for debris and tools prior to closing

the system.

The inspectors reviewed the completed copy of

MMP-C-HX-277 and noted that the FME Control Log was annotated that

all the material was removed from the heat exchanger prior to the

final closeout. After further investigation it was concluded that

the scaffolding material had not been removed.

On April 29, 1992, Violation 50-280/92-07-93 was issued for

failure to prevent foreign material from entering the SW system

during maintenance.

The corrective action for this violation

focused on issuing VPAP-1302 which established station-wide FME

controls applicable to implementing design change packages, as

well as, performing maintenance activities. The inspectors

previously reviewed VPAP-1302 and considered that it provided

adequate instructions but FME deficiencies have continued to

occur.

The inspectors reviewed DRs dating from December 1992 to

June 1994 and noted seven examples in addition to the ones

previously discussed where personnel did not follow station

procedures for maintaining FME control.

In addition, NRC

Inspection Report Nos. 50-280, 281/94-08 identified a weakness in

the area of FME control.

The inspectors concluded that the actions previously implemented

to correct deficiencies associated with FME controls did not

preclude repetition. 10 CFR 50, Appendix B, Criterion XVI,

Corrective Action, requires that when a significant condition

adverse to quality is identified, the cause of the condition is to

be determined and corrective action taken to preclude repetition.

The failure to implement corrective actions to preclude FME

deficiency repetitions was identified as VIO 50-280, 281/94-17-02,

Failure to Implement Corrective Actions to Preclude Repetition of

FME Deficiencies.

Within the areas inspected, one violation was identified.

5.

Action on Previous Inspection Items (92701, 92702)

5.1

(Closed) URI 50-280/94-02-03, Evaluation of Pressurizer Hydrogen

Burn. This issue involved corrective actions taken to prevent the

hydrogen burn from recurring.

In a letter dated April 8, 1994 the

licensee responded to the URI and outlined corrective actions to

prevent recurrence. The inspectors verified that necessary

actions were taken during the Unit 2 outage to prevent hydrogen

burn during shutdown operations and pressurizer modifications.

The licensee procured new explosive meters to sample for explosive

gasses in an oxygen poor atmosphere. Training briefs for the new *

meters were given to the contractors performing the pressurizer

11

modification work. Training on using the new meters was

incorporated into the welder's craft training and is planned to be

included in the confined space entry training as well. Procedures

were updated for shutdown, pre-job briefs, PRT operations,

removing pressurizer safety valves, and welding and cutting

procedures for piping and instrumentation systems. Special work

instructions were written to address pressurizer modification

welding and cutting during the outage. The licensee continues to

evaluate the need for further enhancements on shutdown and

degasification procedures.

The inspectors reviewed the licensee's

committed corrective actions and consider this URI closed.

5.2

(Closed) URI 50-280, 281/93-07-01, Evaluation of DBD Program.

This issue involved a NRC concern that system DBDs at both Surry

and North Anna contained large numbers of open punchlist items

that may involve safety issues that should be promptly reviewed

and resolved.

On an average, 180 open punchlist items were

identified for each of the nine system DBDs developed as part of

the group 1 effort.

Meetings were held with the licensee to discuss the NRC concern

expressed above.

The licensee reviewed the specific issues

addressed in North Anna NRC Inspection Report Nos.

50-338, 339/92-32 associated with the RSS and determined that the

open items had been screened for safety significance in accordance

with the DBD program.

However, the licensee did realize from this

second review that documentation of their screening and decision

process could be improved. This realization prompted the licensee

to perform a more formal re-review of all open punchlist items.

The inspectors reviewed both the licensee's screening criteria for

open punchlist items and their re-review of all open punchlist

items for two of the nine Group 1 systems, which had completed

DBDs.

The systems selected by the inspectors for review were the

AFW and SI systems.

The licensee's screening criteria placed open items into 1 of 3

categories. The Immediate Category included both operability or

safety concerns which required prompt resolution as well as

missing critical calculations which required reconstitution within

30 days.

The Intermediate Term Category was defined as not an

immediate concern, but should be resolved in the interest of

having a quality body of design information.

The last category,

the Resolve If Needed Category included items that would be

resolved only if necessary to support future design or for

operational support. If properly applied and documented, the

criteria appeared to the inspectors to be appropriate. However,

it should be recognized that those items in the Resolve If Needed

Category may never be closed since they represent a low priority

for the licensee's DBD group.

The licensee is evaluating how the

DBD project can be closed with the low priority open items

remaining open.

12

The inspectors determined, based on a sampling of resolved and

remaining open items, that the licensee's re-review of the initial

open items from the Group 1 revision O DBDs was effective. This

additional effort resulted in both reducing the number of open

items, as well as, providing documented evidence that no safety

issues remain open fqr an extended period of time.

Based on

statistics provided by the licensee, approximately 33% of the 1670

initial open items were resolved leaving approximately 1092 still

open. Approximately 50% of the remaining open items are in the

Resolve If Needed Category.

The inspectors' review of the two DBDs above did however identify

two accident analyses that contained assumptions that were not

_bounded by operational practices. The item identified while

reviewing the SI system involved standard operating practices that

allowed the RWST temperature to go below the 40 degrees F value

assumed in the steam break analysis (Calculation SM-191, Main

Steamline Break Response Assuming No Boron in the Boron Injection

Tank for Surry Power Station with Offsite Power Available, Using

the RETRNPOl Code, dated July 1983}.

Based upon another issue,

the licensee had issued a standing order to operations to maintain

the RWST temperature above the 40 degree minimum temperature.

Based on the inspectors' concerns, the licensee issued a DR which

prompted performing a sensitivity study as to the impact of colder

RWST water on the steam break accident analysis. The result of

calculation SM-0942, Evaluate the Impact of Reducing the RWST

Minimum Temperature from 40 degrees F to 38 degrees Fon the MSLB

and LOCA Analyses for Surry Power Station, dated July 1994 were

summarized in a July 6, 1994, memo from K.L. Basehore (NAF} to

W.R. Benthall (Surry Licensing).

The July 6, 1994 memo indicated

that the MSLB calculation of record (SM-191) contained several

conservative assumptions.

The calculation assumed that a BIT full

of non-borated water was injected into the core. This is

impossible since the BIT no longer exists. The memo indicated

that conservatism in the calculation more than offset the minimal

effect of reduced RWST water temperature on core activity. The

inspectors will review calculation SM-0942 when available.

The item identified while reviewing the AFW system involved the

ability of one AFW pump's flow (350 GPM) to remove sufficient heat

with the RCPs operating. Safety analysis (NFE Technical Report

No. 204, Surry Loss of Normal Feedwater Analysis Using RETRANO 1,

dated July 1981) assumes that the RCPs are tripped.

However, EPs

1,2-E-O, Reactor Trip or Safety Injection, revision 14 and ES-0.1,

Reactor Trip Response, revision 12 do not instruct the operator to

trip the RCPs to preclude a loss of heat sink.

Upon loss of the

heat sink, the EPs do provide steps to shutdown the RCPs.

At the time of the analysis the action statements of the Surry TS

allowed unit operations with only I operable AFW pump.

A TS

.

amendment was requested to no longer allow unit operations with I

AFW pump operable.

The amendment was approved by NRC letter dated

.

.*

~-------

-~ -__ .,,:,. -------~~

13

April 27, 1982.

The inspectors reviewed the data provide by the

licensee and found it acceptable.

However, the safety analysis of

record did not reflect the licensee's efforts since the safety

analysis was performed and the DBD also did not provide a complete

record of issue resolution. The licensee is reviewing the basis

for the values and the information contained in the EPs to

determine if earlier RCP tripping with only one AFW pump operating

would be prudent. The inspectors will continue to follow this

item.

Resolution of these two specific items, as well as, reviewing

other analyses for unverified assumptions was identified as

IFI 50-280, 281/94-17-03, Followup on Unverified Assumptions in

Accident Analyses.

5.3

(Closed) IFI 50-280/94-12-0l, Interpretation of TS 3.6.D. This

issue involved TS requirements for CST MCR level indication.

The

NRC staff review of TSs 3.6.D and 3.6.B.2 concluded that CST level

indication was not required by TSs.

TSs only require MCR

indication for AFW system valve alignment for feedwater flow to

the SGs.

Within the areas inspected, no violations or deviations were identified.

6.

Exit Interview

The inspection scope and findings were summarized on July 6, with those

persons indicated in paragraph 1.

The inspectors described the areas

inspected and discussed in detail the inspection results addressed in

the Summary section and those listed below.

Item Number

VIO 50-281/94-17-01

VIO 50-280, 281/94-17-02

URI 50-280, 281/93-07-01

URI 50-280/94-02-03

IFI 50-280/94-12-01

Status

Open

Open

Closed

Closed

Closed

Description/(Paragraph No.}

Failure to Close Unit 2 Makeup

Water Isolation Valve Within

15 Minutes After Makeup

(paragraph 3.5).

Failure to Implement

Corrective Actions to Preclude

Repetition of FME Deficiencies

(paragraph 4.2).

Evaluation of DBD Program

(Paragraph 5.2).

Evaluation of Pressurizer

Hydrogen Burn (paragraph 5.1).

Interpretation of TS 3.6.D

(paragraph 5.3).

_cc_--..c-"-- --

Item Number

IFI 50-280, 281/94-17-03

14

Status

Open

Description/(Paraqraph No.}

Followup on Unverified

Assumptions in Accident

Analyses {paragraph 5.2).

Proprietary information is not contained in this report. Dissenting

comments were not received from the licensee.

7.

Index of Acronyms and Initialisms

AFW

BIT

CFR

CSD

CST

DBD

DCP

DR

ECCS

EP

ESF

F

FME

FW

GPM

IFI

LCO

LOCA

MCR

MOV

MSLB

MSTV

NAF

NRC

PM

PRT

PT

QC

RCE

RCS

RCP

RFO

RPS

RSS

RTD

RWST

SALP

SE

SG

SI

SW

AUXILIARY FEEDWATER

BORON INJECTION TANK

CODE OF FEDERAL REGULATIONS

COLD SHUTDOWN

CONDENSATE STORAGE TANK

DESIGN BASIS DOCUMENT

DESIGN CHANGE PACKAGE

DEVIATION REPORT

EMERGENCY CORE COOLING SYSTEM

EMERGENCY PROCEDURES

ENGINEERED SAFETY FEATURE

FAHRENHEIT

FOREIGN MATERIAL EXCLUSION

FEEDWATER

GALLONS PER MINUTE

INSPECTION FOLLOWUP ITEM

LIMITING CONDITIONS OF OPERATION

LOSS OF COOLANT ACCIDENT

MAIN CONTROL ROOM

MOTOR OPERATED VALVE

MAIN STEAM LINE BREAK

MAIN STEAM TRIP VALVE

NUCLEAR ANALYSIS & FUELS

NUCLEAR REGULATORY COMMISSION

PREVENTIVE MAINTENANCE

PRESSURIZER RELIEF TANK

PERIODIC TEST

QUALITY CONTROL

ROOT CAUSE EVALUATION

REACTOR COOLANT SYSTEM

REACTOR COOLANT PUMP

REFUELING OUTAGE

REACTOR PROTECTION SYSTEM

RECIRCULATION SPRAY SYSTEM

RESISTANCE TEMPERATURE DETECTOR

REFUELING WATER STORAGE TANK

SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE

SAFETY EVALUATION

STEAM GENERATOR

SAFETY INJECTION

SERVICE WATER

15

T

TEMPERATURE

TS

TECHNICAL SPECIFICATION

UFSAR

UPDATED FINAL SAFETY ANALYSIS REPORT

URI

UNRESOLVED ITEM

VIO

VIOLATION

VPAP

VIRGINIA POWER ADMINISTRATIVE PROCEDURE

WO

WORK ORDER