ML18152A313

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Insp Repts 50-280/90-28 & 50-281/90-28 on 900902-29.Noncited Violations Noted.Major Areas Inspected:Plant Operations, Plant Maint,Plant Surveillance,Ler Closeout & Action on Previous Insp Findings
ML18152A313
Person / Time
Site: Surry  Dominion icon.png
Issue date: 10/26/1990
From: Fredrickson P, Holland W, Tingen S, York J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18152A314 List:
References
50-280-90-28, 50-281-90-28, NUDOCS 9011090307
Download: ML18152A313 (16)


See also: IR 05000280/1990028

Text

R~port Nos.:

50-280/90-28 and 50-281/90-28

Licensee:

Virginia Electric and Power Company

5000 Domi_nion Boulevard

Glen Allen, VA

23060

Docket Nos.:

50-280 a~d 50-281

License Nos.:

DPR-32 and DPR-37

Facility Name:

Surry 1 and 2

Inspection Conducted:

September 2 through 29, 1990

Inspectors: d ~

~

w.E.ocf~sident Inspector

J.~~ctor

S. G. ~i

1

,JWJ,

.e ,~de~tg_ ~

Approved by:

( /

- -~

Scope:

P. E: Fredrickson, Section Chief

Division of Reactor Projects

SUMMARY

This routine resident inspection was conducted on site in the areas of plant

operations, plant maintenance, plant surveillance,* licensee event report

closeout, and action on previous inspection findings:

During the performance

of this inspection, the resident inspectors conducted review of the licensee 1 s

backshift or weekend operations on September 3, 6, 7, 8, 9, 11, 24, 25, 26,

and 28.

Results:

In the area of maintenance both a weakness and a strength were identified. The

weakness involved incorrect understanding of the internal configuration of a

valve

positioner

by

I&C

during

initial

troubleshooting

activities.

(paragraph 4.a). The strength involved the repair of emergency service water

pump 1-SW-P-lC (paragraph 4.b.).

Two noncited violations were identified.

One was for failure to follow the

requirements of a radiat1on work permit (paragraph 3.d).

The second noncited

violation was for failure to provide an adequate procedure for troubleshooting

a Unit 1 containment system pressure instrument (paragraph 6) .

,:,ci *t 1. c,*:,;,o:~:q.7_

F' f.1 \\;;:

(-1 Du i_. \\-: ..

I)

1.

Persons Contacted

Lice~see Empl6yees_ *

REPORT DETAILS

    • W. B~nthall, Supe~visor, Licensing

~R. Bilyeu, Licensing Engineer

    • 0. Christian*, Assistant Station* Manager
  • J. Downs, Superintendent of Outage and Planning

D. Erickson, Superintendent of Health Physics

W. Gross, S1Jpervisor, Shift Operations

"'*R .. Gwaltney, Superintendent of Maintenance

    • M. Kansler, Station Manage~

l. Kendzia, £upervisor, Safety Engineering

  • J. McCarthy, Superinte~dent of Operations
  • L. Morris, Superintendent of-Radiation Waste
    • A. Price, Assistant Station Manager
    • E. Smith; Site Quality Assurance Man~ge~
  • T. Sowers, Superintendent of Engineering
    • Attended.exit inte~view on October 3, 1990.
    • Attended exit interview on October Bi 1990.

Other licensee employees contacted included c6ntrol room operators, shift

technical advisors, shift supervisors and other plant personnel.*

Acronyms and iniiialisms used through~ut this report are listed in the

last paragraph.

2.

Plant Status

Unft 1 *began. the reporting period at approximately 78%. power.

On

Se~tember 19i the unit experienced unexpected load swings due to erratic

  • operation of the EHC system.

This event is. further discussed in*

paragraph 3.d. * The Llnit continued to operate in a coa~tdown m6de at power

during the period and was operating at approximately 57% power when the

inspection period ended.

-

Unit .2 began the reporting period at _power.

The unit operated at power

for the duration of the inspection period.

3.

Operational Safety Verification

(71707 & 42700)

a.

Daily Inspections

The inspectors conducted daily inspections in the following areas:

control

room staffing, - access,. and operator behavior; operator

adherence to approved procedures, TS, and LCOs; examination of panels

2

containing instrumentation and other reactor protection syst~m

elements to determine that required channels ~re operabl~; and review

of control room operator logs, operating orders, plant deviation

reports, tagout logs, temporary modification logs, and tags on *

componen~s to verify compliance with approved procedures.* The

inspectors also routinely accompanied station management on plant

tours and observed the effectiveness of their influence on a*ctivities

being performed by pl ant personnel. *

b.

Weekly Inspections

The inspectors conducted weekly inspectioris in the following areas:*

operability verification of selected ESF systems by valve alignment,

breaker ,positions,

condition of equipment

or component,

and

. operability of instrumentation and support items essential to system

actuation or perfo~mance.

Plant tours were conducted which included

observation of general plant/equipment conditions, fire protection

and preventative measures,

control of. activities in progress,

radiation protection controls, physical _security controls, plant

housek~eping

conditions/cleanliness,

and

missile hazards.

The

inspectors routinely noted th~ temperature of the AFW pump discharge

piping to ensure increases in temperature were being properly

monitored and evaluated by the licensee.

c.

Biweekly Inspections

The inspectors conducted biweekly inspections in the following areas:

verification review and walkdown of safety-related tagouts in effect;

review of sampling program (e.g., primary and secondary coolant

samples, boric acid tank samples, plant liquid and gaseous samples);

observation of control room ~hift turnover; review of implementation

of the plant problem identification system; .verification of selected

portions of containment isolation lineups; and verification that

notices to workers are posted as required by 10 CFR 19.

d.

Other Inspection Activities

Inspections included areas in the Units 1 and 2 cable vaults, vital

battery rooms, steam safeguards areas, emergency switchgear rooms,

diesel generator rooms, control room,

auxiliary building, cable

penetration areas, independent spent fuel storage facility, low level

intake structure, and the safeguards valve pit and pump pit areas.

RCS leak rates were reviewed to ensure that detected or suspected

leakage from the system was recorded, investigated, and evaluated;

and that appropriate actions were taken, if required. The inspectors

routinely independently calculated RCS leak rates using the NRC

Independent Measurements Leak Rate Program (RCSLK9).

On a regular

basis,

RWPs were reviewed,

and specific work activities were

monitored to assure they were being conducted per the RWPs.

Selected

radiation protection instruments were peri odi ca lly checked, and

equipment operability and calibration frequency were verified.

3

During

this

inspection

period, "licensee

radiation* protection

personne 1 i dent i fi ed a condition where. an operator had entered a

locked high radiation area on two different occasions without a

survey instrument.

The applicable RWP required a survey instrument

for entry into a locked high radiation area.

The inspectors reviewed these events with the HP Superintendent and

operations supervision.

The licensee stated that the operator in*

question was confused as to the requirements for entry into the

locked high* radiation *area due to the posting of the area at that

time.

The posting of the radiation area indicated that a DAD, survey

instrument, or HP coverage was required for entry.

However, the RWP

in use for entry into a locked high radiation area required a survey

instrument.

Station supervision informed the inspectors that they

considered the event was

an isolated occurrence; however, they

implemented corrective actions that were directed at all operations

personnel.

These corrective actions included supervisory discussions

with shift crews on the requirements of following the applicable

RWPs.

In addition, an entry was made in the operations shift orders

log reviewing the event and addressing RWP requirements.

Also, the

HP department reviewed postings to radiation areas and clarified any

signs which might have been misleading.

The in specters were provided with a copy of the deviation report

which identified the violation of RWP requirements and a copy of the

radiological deficiency report.

They reviewed these reports and the

licensee's corrective actions and consider that the problem was

appropriately addressed.

This item is identified as an NCV (280,

281/90-28.-01) for fa-i lure to fo 11 ow the requirements of the RWP for

en-try in.~_6-a Jocked high radiation area.

This licensee identified

violati6n fs .-not being cited because criteria specified in Section

V.G.l of the NRC Enforcement Policy were satisfi~d.

On

September 19, Unit l

experienced problems with the turbine

generator governor valve EHC system resulting in a sudden increase of

turbine generator output from 550 to 590 Mwe, fo 11 owed by a sudden

decrease of turbine generator output from 550 to 250 Mwe, and a

subsequent sudden increase of turbine generator output from 250 to

380 Mwe.

These swings in turbine generator output occurred over a 22

minute period and while the swings were occurring, operators

attempted to regain control by changing the modes of turbine

generator control and increasing or decreasing the output as

necessary.

Turbine generator output was decreased to 240 Mwe and

remained stable.

Inspection of the No. 3 governor valve revealed

that the nut securing the EHC LVDT feedback arm in the valve's EHC

linkage vibrated loose causing the arm to become disenga~ed from the

LVDT resulting in a loss of turbine generator control.

EHC fluid to

the No. 3 governor valve was isolated and turbine generator control

was restored.

4

The turbine* generator load swings created transients that caused

several steam leaks. in the A main steam dump header.

Packing blew

out of main ste~m_du~p valv~ TCV-MS-105A.

T~ stop the steam leak, -a

leak sealing material(furmanite) was injected in the packing area. A

sec~nd steam leak occurred whe~ a pressure gage isolation valve blew

off. A damage control plug was tempo~arily installed in the opening

to stop the steam 1 eak. * During this event !RPI for rod 1(-6 drifted

to 14 steps abo~e the _demand counter exceeding the TS limit. of 12

steps .. The applicable TS action statement was entered and adjust-

ments were made to correct the indication discrepancy ... Following

this event, the licensee reinstalled the No. 3 governor valve LVDT

feedback arm.

The licensee _inspected the remaining Units 1 and 2

  • governor valves I

EHC

LVDT feedback arms and verified that the_

. fasteners ~ere secure.

The inspe~tors monitored this event from the

control. room and turbine *building.

e.

Physical Security Program Inspections

In the course of monthly activities, the inspecto*rs included a review*

of the licen-see 1 s physical *security program.

The performance of

various shifts of the security force was observed in the conduct of

daily activities to include: protected and vital areas access

controls;

searching of personnel, packages and vehicles; badge

issu*ance and retrieval; escorting of v.isitors; *. and patrols. and

tompen~at~ry posts~

No discrepancies w~re noted.

  • f.

Licensee 10 CFR 50_.72 Reports

On September 2, the licehse~ mide a rep~rt*in accordanc~ with 10 CFR

,.50.72 concerning an event involving the inadvertent closure of two of

the four Unit l circulating water inlet valves. This condition is

_considered outside the design basis of the plant.

op*erators noticed

the valves clos,ing * and took manual control in order to ma_intain

condenier vacuum and prevent a uhit trip. They deenergized*the power

supplies for the :motor operated va_lves in question and placed these

power suppli~s under administrative control. The valves are designed

to close on_ an ESF s1gnal associated with a loss of off site power in

coincidence with a Hi-Hi CLS condition. The problem was diagnosed to

be defective circuitry which caused a makeup of the logic of the

turbine building flood protection syst~m.

After corrective actions

were accomplished to the turbine building flood protection circuitry,

(within 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />), normal powe~ was restored to. the two circulating

water MOVs.

During the time that the valves were without power, all

plant conditions were normal.

On September 26; the licensee made a call to the NRC retracting the

10 CFR 50.72 report that was made on Septembe~ 2.

The retraction

stated that further analysis of the. plant conditions at the time of

this event led to the conclusion that reacto~ operators had ade9uate

5

time to identify and execute cl6sure of the two circulating water

valves.

Administrative.controls were initiated tb ensure that plant

conditions .did not* exceed any de~ign bas-is.* The inspectors re-wiewed

th~ initial call and actions taken by the operators and consider that

adequate control of the valves in question were maintained throughout

the event.

g.

Extension of Testing Requirements

On September 14, 1990 the licensee requested a one-time exemption

from type C testing requirements as specified in 10 CFR 50,

Appendix J,Section III.D.3 until June 30, 1991 for Surry, Unit 2.

A

temporary waiver was granted from the requirement by the NRC on

September 18, 1990; and a one-time exemption of the requirements was

granted- by the NRC on September 26, 1990.

Within the areas inspected, one NCV was identified.

4.

Maintenance Inspections (62703 & 427CJ)

Ouri~g

the

reporting

period,

the

inspectors

reviewed

activities to assure compliance with

the

appropriate

In~pection areas included the following:

maintenance

procedures.

a.

Repair of Unit 2 Pressurizer Spray Valve (2~RC-PCV-2455A) Positioner

During the latter part of the last inspection period, the licensee

identjfied a problem with the subject valve in that when the valve

received a full-close demand signal, it remained partially open.

Work order 3800099504 was issued on August 24, 1990 to troubleshoot

the valve controller and adjust the demand signal as necessary. This

work required

containment entries at power be made in order to

accomplish troubleshooting/repair activities.

Between August 24 and September 13, the licensee made a total of 10

containment entriei to troubleshoot/repair 2-RC-PCV-2455A positioner.

Difficulities with respect to inadequate vendor manuals and incorrect

use of repair parts contributed to repeated unsuccessful attempts to

fix the problem.

On August 24, the first containment entry was made by I&C personnel

to check out the controller.

During that entry, the technicians

determined that with less that a 3 psi E/P signal the valve dome was

receiving approximately a 9 psi signal.

For any E/P signal equal to

or less than 3 psi the dome signal should have been approximately 0

psi and the valve should remain shut. After making minor adjustments

and concluding that the valve was closed, the technicians left

containment.

Later that evening, operations reported back to I&C

that the valve was still not going fully shut.

A containment entry

6

was made that night by I&C personnel who determined that the

same

problem existed.

During this entry, instrument air was isolated to

the valve and the valve was observed to go fully shut.

On August 25, a containment entry was made by I&C technicians to

check the valve air fittings for leaks and check. tightness of

screws.

No air l eak.s were found.. Pictures were taken of the

valve controller configuration prior to le~~ing containment.

On August 28, a containment entry was made to change out valve

internals associated with

mounting the pilot valve to the

positioner.

The troubleshooting instructions required the

removal of three 0-rings and installation of new O-rings. After

completion of the work, the valve controller problem was still

evident.

Following this attempt to correct the problem, I&C

requested *maintenance engineering support and contacted the

valve positioner vendor for additional help.

On August 30, a containment entry was made to remove the bottom

0-ring installed during the August 28 entry and to replace this

0-ring with a foam plug.

This work did not correct the valve

controller problem.

On August 31, a containment entry was made to remove the valve

positioner from the valve and to bring the compo_nent out of

containment for further troubleshooting and corrective action.

The positioner was taken to the station hot shop for additional

work.

On September 1, the licensee reinstalled the foam plug in the

pilot valve and conducted additional check.outs and setup in

accordance with maintenance engineering instructions. All work,

which was accomplished in the hot shop, indicated that the

positioner was working properly.

On September 4, the 1 i censee made a containment entry to

reinstall the valve positioner. However, after reinstallation,

the positioner exhibited the same original problem.

Instrument

air was i so 1 a ted to the valve and I&C personnel left contain-

ment.

On September 6, a containment entry was made to troubleshoot the

positioner again and replace selected components.

I&C was

unable to correct the positioner problem and left containment.

On September 7, a containment entry was again made to remove the

valve po~itioner from the valve and bring the component out of

containment for further troubleshooting and corrective action.

The positioner was taken to the stati~n hot shop for additional

work.

7

On

September 8,

during positioner disassembly,

the

I&C

technicians, working with maintenance engineering, observed that

the foam plug was incorrectly positioned sideways and that a

piece of a hard rubber material was lodged under the pilot valve

port containing the foam plug.

From these observations and

additional testing, it was

concluded that the valve was

ma l fun ct i oni ng because the pilot va 1 ve port was not properly

sealed with a hard rubber plug.

Additionally, it was concluded

that the cause of the original valve problem was air leakage

past the failed pilot valve port hard rubber plug.

On September 12, I&C refurbished the positioner in the hot shop

using new parts which incfoded a new hard rubber plug.

After

refurbish~ent, the positioner was tested using a special

procedure prepared by maintenance engineering.

Test results

were satisfactory.

On September 13, a containment entry was made to reinstall the

refurbished positioner. After completion of the reinstallation

and checkout of the operation of the valve, 2-RC-PCV-2455A was

declared operable and returned to normal service.

The* inspectors began to follow the maintenance/troubleshooting

activities associated with this valve early in this inspection

period.

The inspectors reviewed all documentation associated with

this job and concluded that the final troubleshooting by I&C and

maintenance engineering that was accomplished on September 8 properly

determined the cause of the problem and a 11 owed for adequate *

corrective action.

The inspectors also noted the following observa-

tions:

After maintenance engineering became involved in the process,

the identification of the problem was better documented and

corrective action for the problem, including adequate retest

prior to final reinstallation, was accomplished.

I&C did not have a detailed vendor manual which could have

allowed for better understanding of the problem.

The inspectors

were provided a copy of Bailey Product Instructions, Section

P92-9 for positioner PT.

No .. 5311450.

The inspectors were

informed that this manual was a generic manual for use in

understanding. this type of valve; however, no specific valve

manual was available.

The inspectors also noted that positioner

supplemental drawing No.

Ll32155, Revision 3, was used in

conjunction with the manual to troubleshoot the valve positioner

condition. The inspectors consider that more detailed technical

instructions are warranted when vendor manuals do not provide

required information to accomplish troubleshooting of problems .

8

The inspectors noted that on August 28, the craft install~d an

o~ring in a valve port which required the installation of a

plug.

They also noted that a foaM plug was installed in place

of the 0-ring on August 30.

On September 12, a hard rubber plug

was installed in place of the foam plug.

The licensee wrote

deviation report S2-90-492 on

September 12

identifying a

condition where the vendor supplied the incorrect plug for the

valve positioner application.

This incorrect plug was used on

August 30, 1990.

The inspectors consider that the licensee

action* for identification of the incorrect part into their

corrective action program wi 11 a 11 ow for. adequate review and

resolution as to why the vendor supplied the incorrect part.

However, the incorrect use of a part on August 28 identified an

I&C weakness with regards to their understanding of the internal

configuration

of

the

subject

positioner

early

in

the

troubleshooting process.

The inspectors discussed the sequence of events with both I&C

supervision and station management and were informed that the

maintenance activity would be reviewed by" I&C to determine if any

lessons-learned from this job could be used to improve other

troubleshooting work.

The inspectors attended the meeting in which

the maintenance activity was reviewed and listened to general

discussion in *the* area of how the job was accomplished.

I&C.

supervision discussed lessons-learned from* the problems associated

with this job.

The inspectors a 1 so reviewed their findings with management and

concluded that continuing management attention is necessary in order

to effectively convey expectations to I&C with regards to correct

understanding of component configurations during troubleshooting

activities. Maintenance and station management stated that they had

recognized that the station had a problem with regards to insuring

that ade~uate vendor/technical instructions were available in ordef

for the craft to perform proper maintenance activities.

They also

stated that the ongoing configuration management

program was

addressing this concern.

b.

Maintenance on Emergency Service Water Pump 1-SW-P-lC

During a routine inservice test of pump 1-SW-P-lC, the pump's flow

rate was below the test procedure's minimum acceptable limits.

Testing of the pump is further discussed in paragraph 5.a.

The

inspectors monitored the licensee's maihtenance activities to restore

the pump I s fl ow rate.

Maintenance on pump 1-SW-P-l C started on

September 10 and was

completed on

September 13.

Work order 38000101101 and procedure MMP-C-SW-093, Overhaul of Emergency Service

Water Pumps, dated October 25, 1989, were utilized to accomplish this

maintenance .

C.

9

The pump

1 s components that are below the water line wer~ removed and

inspected.

The in~pection revealed that the pump exterior. casing and

endbell were heavily covered with barnacles and hydroids.

Hydroids

which are a biological growt~ that ~ccurs in the James River are only

present in a flowing water environment and are not present in

stagnant water conditions. The lower side of the pump 1 s impeller was

heavily covered with barnacles. The internal components of the pump

were lightly covered with barnacles. The lower end of the pump was

disassembled, cleaned, reassembled, and the pump was reinstalled and

tested.

The pump

1 s flowrate was significantly higher than the

previous test and was within acceptable limits.

The licensee concl~ded that the six to twelve inch long hydroids

present in the suction area of the pump were folding over into the

pu'mp suction path during pump operation and impeding the pump 1s

suction. The barnacles on the impeller also disrupted the pump 1 s flow

characteristics. Because the internal components of the

pump

contained stagnant water the marine growth was minimal. Corrective

actions to prevent reoccurrence are discussed in paragraph 5.a.

The

inspectors reviewed the work package associated with the

maintenance of pump 1-SW-P-lC, frequently visited the job sight to

observe work in progress, held discussions with the maintenance

engineer, system engineer, and craft supervisors, and certified

compliance with TSs and station adminstrative procedures.

The

inspectors consider that this maintenance was completed in an

efficient manner, and there appeared to be good cooperation between

system engineering, maintenance engineering, operations, and craft

personnel. This evolution was identified as a strength in the area

of maintenance.

Repair of Intake Canal Level Indicator

The in specters observed the rep 1 acement * of can a 1 1 eve 1 probe No.

2-CW-LS-202 on September 17.

There are four of these canal level

indicators, two on each unit.

Each *of the level indicators is

connected to an intake canal level high-low level alarm which

annunciates in the main control room.

If three out of four of the

annunciators are energized, then both units would receive an

automatic reactor trip signal.

The annunciator from level probe

No. 2-CW-LS-202 was energized and the channel was placed in trip.

The level probe was four.d to be defective and was replaced.

The work

was

performed on work order No.

380009~986

using

procedure

2-PT-2.21A,

Function Test of Low

Level Canal Circuity, dated

February 27, 1990.

In addition to reviewing the procedure and observing part of the

probe rep 1 acement effort, the inspectors reviewed the component

failure evaluation results. This report stated that the probe failed

10

due to water intrusion that resulted in a false o~tput voltage. The

report recommended that additional actions be taken to extend probe

life.

One recommendation resulted in the request for an

EWR to

explore the possibility of another method for sealing the probe. The

CFE al so stated that the amount of mar*ine. growth found at the probe

could affect the response time, and recommended that the marine

growth on these probes be removed at regular intervals.

The in specters consider the CFE and re 1 a-ted recommendations to be

adequate, and no discrepancies were noted in the maintenance on the

probe.

The inspectors noted that on September 17, periodic tests

were performed satisfactorily on all four of the canal level probes

indicating no apparent inleakage bf ~oisture.

Within the areas inspected, nn violations were identified.

5.

Surveillance Inspections

(61726 & 42700)

During the reporting period, the inspectors reviewed various surveillance

activities to assure compliance with the appropriate procedures as

follows:

Test prerequ~sites were met .

Tests were performed in accordance with approved procedures.

Test procedures appeared to perform their intended function.

Adequate coordination existed among personnel involved in the test.

Test data was prop~rly collected and recorded.

Inspection areas included the following:

a.

ESW Pump Testing

On September 6, the licensee tested ESW pump 1-SW-P-lA in accordance

with procedure l-PT-25. 3A, Emergency Service Water Pump (1-SW-P-lA),

dated October 10, 1989.

The purpose of this test is to verify pump

operability in accordance with the requirements of ASME Boiler and

Pressure Vessel Code,Section XI. The pump 1 s flow rate was 12,500 GPM

which was less than the test procedure

1s minimum acceptable flowrate

limit.

As a result, the pump was declared inoperable. TS 3.14.B

action statement was entered allowing continued unit operation with

one of the three ESW pumps being i noperab 1 e for a period not to

exceed seven days.

To restore the pump 1 s flow rate, a diver cleaned

the external surfaces of the pump 1 s suction area and the pump was

operated for several hours to remove any obstructions in the pump or

pump discharge piping.

On September 7, pump 1-SW-P-lA was retested

    • -

11

in accordance with procedure 1-PT-25.3A.

This testing was witnessed

by* the inspectors. The flow rate obtained during this testing was

16,832 GPM which was within the test procedures acceptable flow rate

limits.

The licensee considered that the pump was operable and

exited the TS 3.14.B action statement.

Because pump 1-SW:-P-lA

degradation had occurred, th~ licensee e*xpedited testing of the

remaini~g two ESW pumps, 1-SW-P-18 and 1-SW-P-lC.

On

September 8, pump 1-SW-P-lB was tested in accordance with

procedure 1-PT-25.38, and the inspecto~s witnessed this testing. The

pump's flow rate obtained during this testing wis 16,024 GPM which

exceeded the test procedures minimum acceptable flow rate limits but

wa~ lower than the flow rates previously obtained for the same pump.

The licensee considered that the pump was operable but had degraded.

On September 19, a diver cleaned the exterior surfaces of pump's

1-SW-P-18 suction area and the p~mp was retested in accordance with

procedure l-PT-25.38.

The pump's flow rate obtained during this

testing was 16,733 GPM which was an improvement from the previous

test results.

At this flow rate, the pump was no longer considered

to be in a degrad~d condition.

On

September 9,

pump 1-SW-P-lC was tested in accordance with

procedure 1-PT-25.3C.

The inspectors witnessed this testing.

The

flow rate obtained during this testing was 14,961 GPM which was less

than the test procedure's minimum acceptable flow rate limits,

therefore, the pump was declared inoperable and TS 3.14.B action

statement was entered. Actions to restore the pump's flow rate were

previously discussed in paragraph 4_.b.

On September 13, pump

1-SW-P-lC was test~d following repairs in accordance with procedure

1-PT:...25.3, and the* inspectors witnessed this testing.* The pump's

flow rate obtained during this testing was

17,619 GPM which

significantly exceeded the test procedure's minimum acceptable flow

rate limits. At this flow rate, the pump was no longer considered to

be in on inoperable condition and the TS action statement was exited.

The licensee has increased the surveillarice test interval for

the ESW pumps from quarterly to monthly until a permanent solution

for the marine growth pump degradation can

be resolved.

The

inspectors did not identify any discrepancies during review of the

test procedures or when witnessing pump testing.

b.

Flux Mapping of Unit 2 Core.

On September 26, 1990, the inspectors witnessed part of the flux

mapping for the Unit 2 core using periodic test 2-PT-28.2, Reactor

Core Flux Maps, dated February 1, 1990.

The purpose of this test is

to monitor the core neutron flux gradients to ensure TS compliance.

The inspectors observed the reactor engineer recording data from the

delta flux meters, and the upper and lower nuclear instrumentation

.meters.

In addition, the inspectors reviewed the signed-off steps of

the procedure.

No discrepancies were identified.

12

Within the areas inspected, np viblations were identified.

6 .. Licensee Event Report Review

(92700)"

The inspector reviewed the_ LER 1s listed below to ascertain whether NRC

reporting requirem~nts were being met and to evaluate initfal adequacy of

the* cotrective actions. The inspector's revie~ also included followup on

implementation of c6rrective action and review of licensee documentation

that all required corrective actions were complete.

.

.

'

.

.

.

(Closed) LER 280/90-05, Containment Pressure Channel. Rendered Inoperable

a~d Not Placed in Trip Conditiori Due to ~rocedure !nadequacy.

The issue

involved a failure to maintain the minimum degree of redundancy for*

containment pressure monitoring instrumentation required by TS due- to

inadequate procedures.

The problem occurred during craft troubleshooting

of a* co~tainm~nt vacuum system pressure instrument and was specifically

caused by an

i_mproper venting evolution being attempted using an*

inadequately revised. procedure.

After discovery of the problem by the

operators, the proper TS LCO was entered and the instrument was returned

to an operable status. An additional action. included reinstruction of*

procedure writers and reviewers to thoroughly review 'procedure revisions

and changes for impact on interacting systems.*. In a_ddition, .the specific

procedures for v~nting containment leakage monitoring lines were ch~nged

to include requirements for placing the affected channel in the tripped

condition.

The inspector verified .that the licensee 1 s corrective action

was imp.lemented.

This item is identified as an NCV (280/90-28-02) for

fa~lure to provide adequate procedure for evolutions affecting required

  • minimum degree of redundancy as required by TS.

This licensee identified

  • violation fs not being cited because criteria specified in Section V.G.l

of the. NRC Enforcement Policy were satisfied.

(Closed) LER 280/90-0~, Inoperable.Contain~ent Vacuum Pump Flow Paths Due*

to Failures of Process Vent Normal Range Radiation Monitor; During both

times that this event occurred (once on August 10 and again .on August 29,

1990) containment vacuum system flow paths for both units beca.me

inoperable when containment vacuum pump discharge va_lves automatically

closed as a result of the failure and ~ubsequent lockout of the.process

vent normal range radiation monitor, RM-GW-130-1.

The licensee determined

that the August 10 event was caused by a* defective flow switch and* the

August 29 event _was caused by a failed CPU card.

These events were*

considered to be isolated occurrences.

The inspectors consider the

licensee's corrective.actions to be adequate.

Within the areas inspected, one NCV was identified.

7.

Aciion on Previous Inspection Findings (92701, 92702)

a.

(Closed) Violation 280,281/89-24-05, Failure to Take Appropriate

Corrective Action for Past Problems Identified During Performance of

Maintenance Activities.* The issue involved examples where corrective

13

action for past problems associated with foreign material exclusion,

torquing of fasteners, and orientation of flow orifices had been

ineffective.

The licensee, in their response to the violation dated

December 21, 1989, stated that a lack of appropriate management

controls with regards to a station administrative procedure governing

the use of standing orders existed.

Corrective action included an

administrative procedure revision to address requirements, a meeting

with maintenance persohnel emphasizing the importance of adhering to

requirements, and implementation of inclusion of foreign material

requirements in upgraded maintenance procedures.

The inspectors

verified that licensee corrective actions were implemented.

b.

(Closed)

Inspector Followup

Item 280,281/89-24-08,

Followup on

Licensee Review of.Inteinal Station Communications Issue.

The is~ue

involved the licensee 1s review of internal station communication

issues in the area of the Gai-tronics system, i.e. improvement of the

system and decrease in the number of open work orders.* Gai-tronics

is a five channel public address and intercom system.

The licensee

had a vendor representative on site from March 22 to April 13, 1990,

to adjust and balance this communications system.

The inspectors

believe that this effoft improved the sound quality.

In 2ddition,

the inspectors noted that the number of outstanding work orders had

decreased. ftom 30 to 13 over the past two months .

C.

(Closed) Violation 281/89-31-01, Failure of Operations .Personnel to

Follow Procedure.

The issue involved two instances where ~perators

failed to follow procedures.

The first instance resulted in

incorrect system alignment during testing of an auxiliary feedwater

pump and the second instance resulted in an unplanned dilution of the

Unit 2 reactor coolant system without proper establishment of

containment integrity.

The licensee, in their response to the

violation dated December 28, 1989, stated that both events were due

to a failure of operators to operate equipment in accordance with

approved procedures.

Management took the necessary actions to'

emphasize that procedural adherence and attention to detail were

expected from all personnel.

The inspectors have continued to

monitor operator performance and consider that strict procedural

adherence has been properly conveyed to all operations personnel.

d.

(Closed) Violation 280,281/89-34-03, Failure to Sample the Service

Water Effluent of the CCW Heat Exchangers as Required by Technical

Specifications.

The issue involved a repeat failure to sample

service water effluent from the CCW heat exchanger as required by TS.

The licensee

1 s response to the violation dated February 6, 1990,

stated that one of the corrective actions was to change the liquid

waste control room operator's log to include a section which

sp'ecifical ly identifies the time and date the heat exchangers were

last sampled and the time by which the next sample must be taken.

)

8.

14

The inspectors reviewed the section in the log and verified that the

sampling is being properly performed.

Additional corrective steps

invplv~d the replacement of the temaining three CCW heat exthangers.

The new design for these heat ex-changers includes a radiation monitor

that is mounted in a dry well. With the new radiation monitors;* it

will not be necessary to take the twice~daily grab samples currintly

required.

Two of the heat exchangers are scheduled to be replaced

during the Unit 1 outage starting in October, 1990, and the final

heat exchanger is scheduled to be replaced during the Unit 2 outage

. starting in April, 1991.

The inspectors considered that adequate

corrective actions have either been implemented or are scheduled.

Exit Interview

The inspection scope and results were summarized on October 3 and 8, 1990

with those individuals identified in paragraph 1.

The following summary

of inspection activity was discussed by the inspectors d~ring this exit.

In the ~rea of maintenance both a weakness a~d a strength were identified.

The weakness involved I&C not correctly understanding the internal

configuration of a valve

positioner during early troubleihooting

activities. The strength involved the repair of emergency service water

.pump 1-SW-P-lC .

Two noncited violations were identified.

One was for failure to follow

the requirements of a radiation work permit and the second was for failure

to provide an adequate procedure

to troubleshoot a U~it 1 containment

system pressure instrument.

The licensee acknowledged the inspection conclusions wi_th no dissenting

comments.

The

1 icensee did not identify as proprietary any of the

materials provided to or reviewed by the inspectors during this

inspection.

Licensee management was informed of the items closed in paragraphs 6

and 7.

9.

Index of Acronyms amd Initialisms

AFW

-

ASME -

ccw

cw

CFE

CFR

CLS

CPU

DAD

AUXILIARY FEEDWATER

AMERICAN SOCIETY OF MECHANICAL ENGINEERS

COMPONENT COOLING WATER

CIRCULATING WATER

COMPONENT FAILURE EVALUATION

CODE OF FEDERAL REGULATIONS

CONSEQUENCE LIMITING SAFEGUARD

CENTRAL PROCESSING UNIT

DIGITAL ALARMING DOSIMETRY

EHC

-

E/P

-

ESF' -

ESW

-

EWR

-

GPM

-

GW

LER

-

HP

I&C

-

!RPI -

LCO. -

LVDT -

MMP

-

MOV

-

Mwe

-

NCV

-

NRC

-

PCV

-

PM

PT

PSI

-

RCS

-

RWP

-

SW

TCV -

TS

15

ELECTRO-HYDRAULIC CONTROL

ELECTRICAL TO PNEUMATIC

ENGINEERED SAF~TY FEATURE

EMERGENCY SERVICE-WATER

ENGINEERING WORK REQUEST

GALLONS PER MINUTE.

GASEOUS WASTE

LICENSEE EVENT REPORT

HEALTH PHYSICS

INSTRUMENTATION AND CONTROL

INDIVtDUAL ROD POSITION INDICATION

LIMITING CONDITIONS OF OPERATION

LINEAR VARIABLE DISPLACED TRANSDUCER

MECHANICAL MAINTENANCE PROCEDURE

MOTOR OPERATED VALVE

MEGAWATTS- ELECTRICAL

NON-CITED VIOLATION

NUCLEAR REGULATORY COMMISSION

PRESSURE CONTROL VALVE

PREVENTIVE MAINTENANCE

PERIODIC TEST

POUNDS PER SQUARE INCH

REACTOR COOLANT SYSTEM

RADIATION WORK PERMIT

SERVICE WATER

TEMPERATURE CONTROL VALVE

TECHNICAL SPECIFICATIONS