ML18152A309

From kanterella
Jump to navigation Jump to search
Insp Repts 50-280/90-14 & 50-281/90-14 on 900304-31. Violation Noted.Major Areas Inspected:Plant Operations, Maint,Surveillance,Ler Review,Action on Previous Findings, Evaluation of Assessment Capability & QA
ML18152A309
Person / Time
Site: Surry  
Issue date: 04/26/1990
From: Fredrickson P, Holland W, York J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18152A310 List:
References
50-280-90-14, 50-281-90-14, NUDOCS 9005080044
Download: ML18152A309 (17)


See also: IR 05000280/1990014

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

\\

REGION II

101 MARIETTA STREET, N.W .

ATLANTA, GEORGIA 30323

Report Nos.:. 50-280/90-14 and 50-281/90-14

Licensee:

Virginia Electric and Power Company

5000 Dominion Boulevard

Glen Allen, VA

23060

Docket ~os.: 50-280 and 50-281

License Nos.:

DPR-32 and DPR-37

Facility Name:

Surry 1 and 2

Inspection Conducted:

March 4 through March 31, 1990

Inspectors: ~~~

/C'-c;r;...

W. LHoi lari;SeniorRes i dent Inspector

J. w~--: ~;;,;tor&P::~

Accompanying Inspectors: K.

Approved

Scope:

Reactor Inspector, RII

tor Inspector, RII

SUMMARY

4' -:lt*-to

Date Signed

1-f - .J.t -fo

Date Signed

t/- zr;. - -~

Date Signe?r

This routine resident inspection was conducted on site in the areas of plant

operations, plant maintenance, plant surveillance, licensee event report

review, action on previous inspection findings, evaluation of licensee self

assessment capability,1and licensee quality assurance program implementation.

Certain tours were conducted on backshifts or weekends.

Backshift or weekend

tours were conducted on March 4, 5, 7, 11, 24, 25, and 27.

Results:

During this inspection period, one violation with two example was identified

(paragraph 6) for failure to follow procedure during testing of components, and

systems as required by TS 6.4.D.

The inspectors consider that the two examples

of failure* to follow procedure by craft personnel are not related to a

progranmatic problem in the surveillance area.

However, they raised concerns

about the level of reviews that are conducted by cognizant supervision who

9005080044 900427

PDR

ADOCK 05000280

G!

.

PDC

2

approve the periodic test results on the critique page of the completed

survei 11 ances.

The inspectors contend that these reviews should identify

problems similar to the ones cited in the violation and consider that

additional management attention is necessary in this area.

In addition, an

unresolved item was identified (paragraph 6) in the same inspection area with

regards to required surveillance testing frequency.

An inspector followup item (Paragraph 3.d) was identified on licensee's leak

reduction program which is required by TS 6.4.K.1.

During a review of operator performance in the control room, it was noted that

the operations staff that performs control room duties were performing these

functions in a satisfactory manner.

Cooperation between shifts was noted as a

strong area.

However, some minor problems regarding strict adherence to

requirements and attention to detail were also noted as needing additional

attention.

An inspector followup item (paragraph 4) was identified on licensee action for

replacement of type BFD 'relays.

REPORT DETAILS

1.

Persons Contacted

Licensee Employees

2.

  • W. Benthall, Supervisor, Licensing
  • R. Bilyeu, Licensing Engineer

D. Christian, Assistant Station Manager

D. Erickson, Superintendent of Health Physics

  • G. Grecheck, Assistant Station Manager

D. Hart, Supervisor, Quality, QA Department

  • E. Harrell, Vice President, Nuclear Operations
  • M. Kansler, Station Manager

T. Kendzia, Supervisor, Safety Engineering

J. McCarthy, Superintendent of Operations

  • R. Gwaltney, Superintendent of Maintenance

J. Downs, Superintendent of Outage and Planning

  • T. Sowers, Superintendent of Engineering
  • E. Smith, Site Quality Assurance Manager

NRC Personnel

  • K. Poertner, Reactor Inspector, Region II
  • Attended exit interview.

On March 27, 1990, a management meeting was held at

Station in order for the licensee to provide an update

headquarters personnel on issues of mutual interest.

attendance at the meeting were:

S. Ebneter, Regional Administrator, RII

the Surry Power

to NRC regional and

NRC management in

G. Lainas, Associate Director for Region II Reactors, NRR

H. Berkow, Director, Project Directorate II-2, NRR

P. Fredrickson, Section Chief, DRP, RII

B. Buckley, Project Manager, NRR

The me~ting focused on plant status and improvement updates from middle

managers 2in the areas of operations, maintenance, engineering, procedures

upgrade, assessments, quality assurance, and outage planning.

After the

meeting; t:he Station Manager conducted a plant tour for the participants.

Acronyms and initialisms used throughout this report are listed in the

last paragraph.

Plant Status

Unit 1 and Unit 2 began the reporting period at power.

Both units

operated at power for the duration of the inspection period *

2

3.

Operational Safety Verification

(71707 & 42700)

a.

Daily Inspections

b.

c.

The inspectors conducted daily inspections in the following areas:

control room staffing, access, and operator behavior; operator

adherence to approved procedures, TS, and LCOs; examination of panels

containing instrumentation and other reactor protection system

elements to determine that required channels are operable; and review

of control room operator logs, operating orders, plant deviation

reports, tagout logs, jumper logs, and tags on components to verify

compliance with approved procedures.

The inspectors also routinely

accompanied station management on plant tours and observed the

effectiveness of their influence on activities being performed by

plant personnel.

Weekly Inspeftions

The inspectors conducted weekly inspections in the following areas:

verification of operability of selected ESF systems by valve

alignment, breaker positions, condition of equipment or component,

and operability of instrumentation and support items -essential to

system actuation or performance.

Plant tours were

conducted which

included observation of general plant/equipment conditions, fire

protection and preventative measures, control of activities in

progress, radiation protection controls, physical security controls,

plant housekeeping conditions/cleanliness, and missile hazards.

The

inspectors routinely noted the temperature of the AFW pump discharge

piping to ensure increases in temperature were being properly

monitored and evaluated by the licensee.

Biweekly Inspections

The inspectors conducted biweekly inspections in the following areas:

verification review and walkdown of safety-related tagouts in effect;

review of sampling program (e.g., primary and secondary coolant

samples, boric acid tank samples, plant liquid and gaseous samples);

observation of control room shift turnover; review of implementation

of the plant problem identification system; verification of selected

p.9r~tons of containment isolation lineups; and verification that

notites to workers are posted as required by 10 CFR 19.

d.

Other: Inspection Activities

Inspections included areas in the Units 1 and 2 cable vaults, vital

battery rooms, steam safeguards areas, emergency switchgear rooms,

diesel generator rooms, control room, auxiliary building, cable

penetration areas, independent spent fuel storage facility, low level

intake structure, and the safeguards valve pit and pump pit areas.

RCS leak rates were reviewed to ensure that detected or suspected

leakage from the system was recorded, investigated, and evaluated;

3

anq that appropriate actions were taken, if required.

The inspectors

routinely independently calculated RCS leak rates using the NRC

Independent Measurements Leak Rate Program ( RCSLK9).

On a regular

basis RWPs were reviewed, and specific work activities were monitored

to assure they were being conducted per the RWPs.

Selected radiation

protection instruments were periodically checked, and equipment

operability and calibration frequency were verified.

Based on inspections at North Anna, the inspectors examined the

licensee's program for compliance with TS 6.4.K.1. This TS requires

establishment of PM and inspection requirements as part of a leak

reduction program for systems outside containment that would or could

contain highly radioactive fluids during a serious accident or

transient.

Licensee personnel indicated that they consider the

Recirculation Spray, Low Head Safety Injection, and High Head Safety

Injection Systems to fall under this requirement.

The 1 icensee

further stated that the following procedures provide a program to

meet the requirements:

SUADM-M-43

ENG-40

PT-16

PT-17.3

PT-18.1

PT-18.7

Material Condition and Housekeeping Inspections

Quantification of External System Leakage

Series Leak Tests Surveillance Procedures~ After

Each Outage

Periodic Test Surveillances for the Systems

Periodic Test for Low Head SI Pumps

Periodic Test for High Head SI Pumps

ASME Pressure Tests and Type A&C Leakage Tests

Although the above documents may cover the required elements of the

program, there is no cohesive program document detailing the required

PMs and visual inspection requirements to meet this TS requirement.

Without a cohesive program document, it is not clear that all systems

needing to be covered by the program are being included.

This matter

wjll be inspected further in future inspections and is identified as

an Inspector Followup Item on licensee's leak reduction program which

is _r~~uired by TS 6.4.K.1 (280,281/90-14-01).

e.

Sustained Control Room and Plant Observations (71715)

On February 14, 1990, the inspectors conducted a 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> monitoring

watch of the operations department staff in the performance of their

duties.

The inspection specifically focused on the performance of

control room operators in the following areas:

Operator attentiveness and response to plant parameters.

-

4

)

Planning and control of plant evolutions and testing.

Adherence to procedures.

Communication and documentation of equipment status changes to

other appropriate personnel.

Effective monitoring of operating conditions and initiation of

corrective actions when required.

Effective usage of backup instrumentation and other information

when normal instrumentation is found to be defective or out of

tolerance.

Timely and accurate log keeping which adequately reflects plant

activities and status.

Operator adherence to good operating practices when conducting

plant operations.

During this inspection, the following observations were noted with

regards to operating shift performance:

The inspectors noted that the operations crews were generally

responsive to each annunciated condition and performed the

required responses.

However, some hesitation was noted with

regards to some annunciated conditions which were repetitive and

related to a known problem. Examples of these were the eves HEAT

TRACE TROUBLE and the FIRE DETECTED annunciators. These specific

annunciators were received several times during this inspection

and did not receive the attention that was'afforded others.

A review of selected portions of the plant status log for Unit 1

indicated that some confusion may still exist with regards to

requirements.

The inspectors consider that, although the

operators were knowledgeable on system configuration status,

they did not always follow through with assuring that the

temporary status indication was updated as required.

The inspectors observed the resolution of a problem that

    • occurred during the performance of a periodic test on one of the

emergency service water pumps.

This problem resulted in a 50.72

call to the NRC.

The operational personnel involved during the

  • day shift extended their hours to help the on-coming shift

resolve this problem.

The cooperation exhibited by these two

shifts is viewed as a strength.

In summary, the inspectors consider that the operations staff that

performs control room duties are performing these functions in a,

satisfactory manner. Cooperation between shifts was noted as a strong

area.

However, some minor problems regarding strict adherence to

5

requirements and attention to detail were also noted as needing

additional attention.

f.

Physical Security Program Inspections

g.

h.

In the course of monthly activities, the inspectors included a review

of the 1 i censee

I s phys i ca 1 security program.

The performance of

various shifts of the security force was observed in the conduct of

daily activities to include: protected and vital areas access

,controls; searching of personnel, packages and vehicles; badge

issuance and retrieval; escorting of visitors; and patrols and

compensatory posts.

Licensee 10 CFR 50.72 Reports

On March 14, 1990, the licensee made a report in accordance with

10 CFR 50.72 concerning the operability of the emergency service

water pumps.

The B emergency service water pump diesel failed to

start during the running of a periodic test because an air box damper

was determined to be closed.

The closed dampers prevented the supply

of air necessary to run this diesel engine.

A check of the A and C

diesels revealed these same dampers were closed thus rendering the

engines i noperab 1 e.

The air dampers were opened and a 11 three

diesels were tested successfully.

The licensee has appointed a

committee to perform an indepth root cause analysis as to why the

dampers were closed when they should have been open. The licensee has

modified the operating procedure to look for this condition prior to

starting the diesel.

Also currently, the operations personnel who

perform a walkdown of this area once a shift have been instructed to.

assure that these dampers are in the correct position.

Followup on Events

On March 23, 1990, at approximately 2305 hours0.0267 days <br />0.64 hours <br />0.00381 weeks <br />8.770525e-4 months <br />, a* secondary leak on

the discharge piping of Unit 1 low pressure heater drain pump 28

occurred.

The unit was operating at approximately 87% power at the

time due to ongoing correction of problems associated with maintain-

ing required level conditions in the condensate and feedwater system

heaters. Operators took immediate action to secure the affected pump

and isolate the discharge flow path.

However, the water that escaped

from-the break resulted in local wetting of some control components

near the break location in the Unit 1 turbine building.

Unit 1

continued to operate at power during the event.

One of the emergency

ventilation supply fans for the Unit 1 emergency switchgear room was

rendered inoperable by wetting of electrical circuitry.

This fan

problem did not require entry into any TS LCO due to other equipment

being operable.

No other safety-related equipment was affected.

Other wetted electrical components caused a spurious discharge of the

emergency switchgear room fire protection system (Halon) into the

rooms. Two sprinklers in the turbine building also actuated.

Also

affected were security system automatic access control components

6

and/or alarms and the radiation monitor for the service water

discharge from the D component cooling water heat exchanger

(RM-1070).

In addition, personnel who were performing periodic

testing on Unit 2 and a TS required fire watch had to leave the

emergency switchgear room because of the Halon discharge.

The line

involved in the event was a 4-inch, schedule 40, carbon steel pipe.

The size of the piping failure appeared to be approximately 3 inches

long in a fishmouth configuration~

The licensee formed a task team

to review the event.

Initial recommendations of the team included

inspection of the other Unit 1 low pressure heater drain train piping

at the same location and inspection of both Unit 2 trains in the same

locations.

The inspectors monitored the licensee actions through the weekend and

a maintenance team which arrived onsite the following Monday reviewed

the licensee

1s corrective actions associated with piping repair and

their erosion/corrosion monitoring program.

The inspectors concluded

that licensee actions with regards to event response and pipe

evaluations were adequate.

Additional information is available in

NRC Inspection Report 280,281/90-07.

i.

Temporary Waiver of Compliance - Unit 1

On March 15, 1990, at 2008 hours0.0232 days <br />0.558 hours <br />0.00332 weeks <br />7.64044e-4 months <br /> both of the Unit 1 containment

vacuum pumps were determined to be inoperable by the operators.

One

pump is required to be operable by TS 3.15.B when the unit is above

350 degrees or 450 psi g.

The 1 i censee requested a waiver of

compliance of this requirement for 72* hours to affect repairs and

provided justification for this request.

The waiver of compliance ,

was granted by the NRC and was docketed to the licensee by letter

dated March 19, 1990.

The licensee completed repairs to one of the

vacuum pumps and returned the system to service on March 16, 1990 at

1225 hours0.0142 days <br />0.34 hours <br />0.00203 weeks <br />4.661125e-4 months <br />.

Within the areas inspected, no violations was identified.

4.

Maintenance Inspections (62703 & 42700)

During the reporting period, the inspectors reviewed maintenance

activities to assure compliance with the appropriate procedures.

Inspec'tion areas included the following:

Replacement of*a BFD Type Relay

During the performance of periodic test, PT-8.1, relay PRB-XB failed.

The

inspectors review of EWR No.88-385, Installation of Westinghouse Type

NBFD65NR Relays As Replacements for BFD Relays, noted that the BFD relay

failures occur mainly due to heat generated by each continuously energized

relay coil and poor heat dissipation caused by close spacing of the

relays.

These relays are 125 volt de used mainly in the reactor protec-

tion and safeguard circuits.

On March 13, 1990, the inspectors observed

7

the process for replacing one of these relays with the newer two coil

relay.

Initially the station safety committee (SNSOC) review of the

drawings and amended procedure was observed.

The actions of the systems

engineer, QC inspector, and the electricians performing the work were

noted.

The procedure used for replacing the relay was ECM-1801-1,

Westinghouse Type BFD Relay Replacement, dated November 18, 1989. Work

Order No. 38000093038 was used to perform the work.

No discrepancies were

noted.

However, after this relay was replaced, two other relays of this type were

found to have failed.

The inspectors were informed by the licensee that

they were considering replacement of the subject relays during the next

outage.

The inspectors will review ongoing licensee action for these

relays and will open an inspector followup item, on licensee action for

replacement of type BFD relays (280,281/90-14-02).

Within the areas inspected, no violations were identified.

5.

Surveillance Inspections (61726 & 42700)

During the reporting period, the inspectors reviewed various surveillance

activities to assure compliance with the appropriate procedures as

follows:

Test prerequisites were met.

Tests were performed in accordance with approved procedures.

Test procedures appeared to perform their intended function.

Adequate coordination existed among personnel involved in the test.

Test data was properly collected and recorded.

Inspection areas included the following:

a.

Turbine Inlet Valves Unit 1

On March 8, 1990, the inspectors witnessed the performance of

perio9ic test 1-PT-29.1, Turbine Inlet Valve Stroke and Oil Pump

Autostart Tests, dated January 16, 1990.

This test is performed to

ensure proper operation of the turbine stop valves, governor valves,

retiea:t valves, and the interceptor va 1 ves.

The inspectors observed

parts of the test being performed

from the control room.

No

discrepancies were identified.

b.

Heat Tracing For the Hydrogen Analyzer

On. March 9, 1990, the inspectors witnessed the performance of

periodic test 1-PT-27F, Heat Tracing (H2A-GW-104) dated October 16,

1989.

This test is performed to ensure that the heat trace circuits

8

for two independent containment hydrogen analyzers are operable.

The

inspectors observed the energizing of several channels in cabinet No.

HTP-6 and the observation of the time required to reach a specified

minimum temperature.

One channel had a deviation for a light

indication and this was noted on the test results.

No discrepancies

were identified.

Within the areas inspected, no violations were identified.

6.

Surveillance Procedures and Records (61700)

During this inspection period, the inspectors reviewed the licensee's

program for implementation and scheduling of the surveillance requirements

required by the TS.

The licensee's program

consists of a computerized

system to schedule routine surveillance requirements and procedur.al

controls to schedule non-routine surveillance requirements.

Surveillance

requirements to be performed during refueling outages are scheduled in

accordance with procedure ENG-39.3, Refueling Outage Periodic Test

Scheduling. Surveillance requirements

r.equired to be performed during

maintenance outages are scheduled in accordance with procedure ENG-39.2,

Maintenance Outage Periodic Test Scheduling.

The inspector reviewed

ENG-39.3 and 39.2 against the TS requirements and did not identify any

surveillance requirements that were not addressed .

The inspector reviewed SUADM-LR-05, Attachment 1, Summary of Surveillance

Requirements and Test Procedures, against the TS surveillance require-

ments.

The inspectors verified that the surveillance requirements were

identified in the SUADM and that the specified frequency for performance

corresponded to the TS required frequency.

The inspector reviewed PT-17.4

which implements the requirements of TS 4.5C and is required to be

performed every 18 months during shutdown.

This review identified that

the frequency of every refueling outage, specified for PT-17.4, did not

meet the 18-month frequency specified in the TS.

The inspector discussed

this item with the licensee and determined that the licensee was aware

that PT 17.4 was required to be performed every 18 months during shutdown.

The licensee presently has a submittal to the NRC requesting that PT-17.4

be deferred to the next scheduled refueling outage.

The licensee al so

plans to initiate a TS change to modify the required frequency from 18

months during shutdown to refueling.

Based on these discuss ions the

l i cens.ee changed the PT scheduled frequency from refueling to 18 months

until the TS change is received to ensure that the TS requirement as

presently_ state_d is not exceeded.

The inspector verified that this PT

frequency 1naccuracy had not resulted in any TS violations.

The licensee's method for scheduling PTs consists of scheduling the PTs

~aving a constant routine frequency for all departments except Operations.

The Operations Department schedules routine PTs to be performed on the

same day of the month as the previous PT was performed.

The licensee .

schedules PTs on a specified date and identifies an early completion date

and a late completion date.

If the PT is performed between the early and

late date, the surveillance is considered to have been completed within

9

the TS required frequency.

The early date ,is established by subtracting

25 percent of the specified frequency from the scheduled date and the late

date is established by adding 25 percent of the specified frequency to the

scheduled date.

TS 4.0.2 states that surveillance requirements specified

time intervals may be adjusted plus or minus 25 percent to accommodate

normal test schedules.

During review of the licensee's program for

scheduling PTs, the inspector identified that if a PT was performed on the

early date during one scheduled performance and then performed on the late

date during the next scheduled performance, the time interval between

performance would exceed the specified surveillance frequency plus 25

percent (i.e., performing a 31 day surveillance seven days early during

one scheduled performance and then performing the next scheduled

performance seven days late would results in a time interval between

surveillances of 45 days.

The inspector identified the following instances where the surveillance

interval between PTs exceeded the specified frequency:

Periodic Test 1-PT-2.26 was performed on 5/10/89 and again on

6/19/89.

The interval between surveillances was 40 days.

The PT was

performed on 10/12/89 and again on 11/21/89.

The interval between

surveillances was 42 days.

1-PT-2.26 is a monthly test, with monthly

being defined in station administrative procedures as 31 +/- 7 days.

The performance of the PT exceeded the 38 day maximum allowable by

two days and four days, respectively.

Periodic Test 1-PT-18.9* was performed

on 1/17/88 and again on

5/10/88.

The interval between survei 11 ances was 124 days.

The PT

was also performed on 9/30/88 and again on 1/26/89.

The interval

between surveillances was 118 days.

1-PT-18.9 is a quarterly test

with quarterly being defined in station administrative procedures as

92 +/- 23 days.

The performance of the PT exceeded the 115 day maximum

allowable by nine days and three days, respectively.

The inspector questioned the licensee as to whether the present method of

scheduling PTs meets the requirements of TS 4.0.2 in that the surveillance

interval could exceed 1.25 times the specified' frequency.

The licensee's

position is that the scheduling of PT's as presently implemented is

acceptable and meets the requirements of the TS. The licensee stated that

the progrijm for scheduling PTs has been the same since the units were

licensed~~and that this issue had been discussed and reviewed by the NRC in

the past and found acceptable.

However, the licensee was unable to

_ _I;roduce * a*ny documentation to support the statement that the NRC had

approved the present method of scheduling PTs.

Based on*the licensee's

-position that their program meets the requirements of the TS for test

frequency, this issue is identified as an unresolved item (280,

281/90-14-02) pending further NRC review and resolution.

The inspector also reviewed several PTs for conduct and performance.

The

inspector reviewed 2-PT-23.88, Main Station Battery 28 Cell Voltage Check,

that was performed on December 29, 1989.

The inspector determined that

10

the acceptance criteria for Battery Cell 51 had not been satisfied. The

PT requires the voltage of each battery cell to be more than 2.13 volts

for the battery to be considered fully operable. If cell voltage is less

than 2.13 volts but greater than 2.07 volts, the battery is still consid-

ered operable, however, the battery is required to be placed on an

equalizing charge for 135 hours0.00156 days <br />0.0375 hours <br />2.232143e-4 weeks <br />5.13675e-5 months <br /> and noted on the PT Critique Sheet.

The

cell voltage for Cell 51 was recorded as 2.12 volts. The battery was not

placed on an equaliting charge as required nor was the condition noted on

the

PT Criti ql:le Sheet.

The inspector discussed this item with the

Battery System Engineer.

The system engineer had identified the discre-

pancy and evaluated the operability of the battery based on subsequent

performances of 2-PT-23.8B.

The system engineer also stated that Battery

Cell 51 was scheduled to be replaced during the next refueling outage.

After this discussion, a plant deficiency report was initiated to document

that the requirements of 2-PT-23.8B had not been satisfied on 12/29/89

when it was performed.

TS 6.4.D requires that detailed written procedures with appropriate

check-off lists involving the testing of instruments, components, and

systems with regard to the ,nuclear safety of the station shall be

followed.

The fail_ure to adequately implement the requirements of

2-PT-23.8B conducted 12/29/89 is identified as a violation of TS 6.4.D,

(280,281/90-14-03).

On March 20, 1990, the inspectors observed the licensee performing PT

25.3C, Emergency Service Water Pump (1-SW-P-lC) dated October 10, 1989.

The inspectors observed the running of the diesel pump and noted some of

the parameters being recorded i.e., temperature, pressure, amperage, etc.

The inspectors noted one of the craftsmen taking an electrical reading .

with a digital ammeter and observed that the readings were fluctuating

between 0.2 amperes and 1.4 amperes.

These readings were being taken to

satisfy step 5.10 of the procedure which required the use of an ammeter on

the positive lead of the alternator circuit*to measure the current.

A

value of 0.5 amps plus or minus (no value recorded) was recorded on the

procedure and the* test was accepted as satisfactory.

When the test was

questioned by the inspectors, the licensee voided it and reran the test

the next day with the system engineer present.

The system engineer

observed that the electrician was taking the readings on small cables to

the battery charger.

These cable currents should have essentially been

zero.

This was the wrong location specified for taking. the readings in

step 5.10 of the procedure.

The fluctuating current readings observed

during the first test by the inspectors was due to the changing distance

(causing -*a:. charige in the interference) between adjacent battery cables.

The failure of the electrician to follow the procedure for taking the

readings is a second example of violation 280,281/90-14-03.

The inspectors consider that the two examples of failure to follow

procedure by craft personnel are not related to a programmatic problem in

the surveillance area.

However, they raise concerns about the level of

reviews that are conducted by cognizant supervision who approve the

periodic test results on the critique page of the completed surveillances .

11

The inspectors reviewed the following periodic tests to verify that the

Technical Specification surveillance requirements were specified in the

procedures.

PT-24.SA, Reactor Coolant Pump Heat Detectors

PT-24.SC, Smoke and Thermal Detectors - Robertshaw System

PT-24.33, Fire Protection - Valve Position Surveillance

PT-17.3, Containment Outside Recirculation Spray Pumps

PT-18.7, Charging Pump Operability and Performance Test

PT-23.7A, Batteries Weekly Pilot Cell Check (2A, 28, EDG2, Black

Battery)

PT-2.26, Reactor Coolant System Pressure (P-1-458)

PT-2.26, Reactor Coolant System Pressure (P-1-403)

PT-38.41,,Main Steam System

PT-38.1, Primary Coolant Chemistry

PT-2.6, Steam Line Pressure (P-2-475)

PT-36, Instrument Surveillance

PT-24.12, Fire Pump Flow Rate Test

PT-24.1, Fire Protection Water Pump

During review of PT-2.26, the inspector questioned the adequacy of the

periodic test.

TS 4.1.B.1.a requires that each PORV be demonstrated

operable at least once per 31 days by performance of a channel functional

test, excluding valve operation. TS table 4.1.2A requires that the Reactor

Vessel Overpressure Mitigating System be functionally and setpoint tested

prior to decreasing RCS temperature below_350 degrees F and monthly while

the RCS is less than 350 degrees F and the reactor vessel head is bolted.

PT 2.26 performs a functional test of the Reactor Coolant Narrow Range

Overpressure Mitigating System and a quarterly stroke time test of the ,

PORV block valves.

The PT did not perform a functional test of the PORV

circuits for normal operating pressure conditions.

Based on the

inspectors review of TS 4.1.B.1.a and TS table 4.1-2A the inspector

questioned the licensee on March 9, 1990, as to whether the requirements

of TS 4.1.B.1.a was being adequately implemented.

The licensee reviewed

the concern and concluded that the TS survei 11 ance was not being

adequately implemented.

The licensee entered the applicable action -

statement for inoperable PORVs and discussions were held between the

licensee,- Region II, and NRR.

Based on the fact that this issue is

currently under NRR review for another licensee, a decision was made not

to tak.e ~PY enforcement action at this present time.

The licensee agreed

to test '{fiis function of the PORV circuitry based on the Emergency

TechnicaJ_ Speci_fication change for pressurizer safety valves, issued on

November 16, 1989.

This TS required at least one PORV be operable. The

licensee completed

testing of the PORV high setpoint on both units prior

to midnight on March 9, 1990.

The licensee plans to continue testing of

the PORV high setpoint monthly as long as PORV operability is necessary to

support the pressurizer safety valve interim TS.

Within the areas inspected, one violation was identified.

12

7.

Action on Previous Inspection Findings (92701, 92702)

Summary of Closeout Actions for Enforcement Letter Issued on May 18, 1989.

The following is a listing of all violations that were identified in the

subject enforcement 1 etter a 1 ong with identification of inspection

activity that closed out the licensee's corrective action for each item:

VIOLATION# AND DESCRIPTION

I.A.1 - Inadequate safety evaluation for

cavity seal design modification resulting

in violation of 10 CFR 50.59.

I.A.2 - Inadequate evaluation of true

nature of the cavity seal failure

resulting in violation of 10 CFR 50, Appendix B, Criterion XVI.

I.B.1 - Inadequate procedures for the

operation of air and backup nitrogen systems

to the cavity seal inflatable portion.

I.B.2 - Inadequate abnormal operating procedure

for a rapid loss of cavity seal level and

failure to assure actions developed in

response IE Bulletin 84-03 were maintained.

I.B.3 - Inadequate procedures for

recovery of reactor cavity level

after cavity seal event.

II.A - Failure to identify a significant

condition adverse to quality in a timely

manner with regards to potential gas

binding of high head SI pumps.

II.B - Failure to conduct a safety

evaluatiort of a reduction in control

room clifl'"fer which was identified by

a devia~i~n rep~rt in 1987

II.C -* Failure to identify a significant

condition adverse to quality in a timely

manner with regards to operability of the

control room and emergency switchgear

room ventilation system *

REPORT CLOSEOUT#

280,281/88-34

280,281/88-41

280,281/88-45

280,281/88-47

Item closeout is

discussed at the end

of this listing

280,281/88-38

280,281/88-38

280,281/88-38

280,281/89-20

280,281/89-28

280,281/90-05

280,281/90-05

280 ,281/89-17

?80,281/90-05

13

II.D - Failure to identify a significant

condition adverse to quality in a timely

manner with regards to the use of nonqualified

parts in a safety-related applications.

II.E - Failure to identify a significant

condition adverse to quality in a timely

manner with regards to wetting of safety-

related components for long periods of time.

II.F - Failure to document corrective

actions for QC inspection identified

deficiencies.

II.G - Failure to take adequate

corrective actions for repeat QA

audit findings.

III.A - Failure to translate the

design basis into specifications,

drawings, and/or procedures for the

RSHXs with regards to intake canal level.

III.B - Failure to translate the

design basis into specifications,

drawings, and/or procedures with regards

to effects of temperature ranges on

emergency pump house equipment.

III.C - Failure to translate the design

basis into specifications, drawings and/or

procedures with regards to the effects of

added loads on the 125 VDC Vital Bus

battery sizing.

III.D - Failure to translate the

design basis into specifications,

drawings, and/or procedures with regards

to the effects of minimum wall thickness

on CCWHX l~CC-E-1B.

IV - Violation of TS 3.14.A.4 with

regards *to~haviTig at least two ESW pumps

operable prior to taking the reactor(s)

critical.

V.A - Failure to test RS system

service water valves as required by

the ASME code.

280,281/90-05

280,281/90-05

280,281/89-36

280,281/89-36

280,281/89-36

280,281/89-36

280,281/89-36

280,281/89-36

280,281/89-36

280,281/89-36

V.B - Failure to provide adequate

procedures for ESW pump battery

14

testing and for checking of disc to

seal clearances on SW check valves.

V.C - Failure to provide adequate

procedure for proper torquing of safety-

related system closure fasteners.

V.D. - Failure to establish measures for

identification and control of materials

with regards to material control tags

being missing from work order packages.

V. E - Failure to properly test a safety-

related pressure control valve after

conducting maintenance on the valve.

280,281/89-36

280,281/89-36

This issue was

addressed in report

280, 281/89-36. The

issue remains open

pending resolution

of items identified

in that report.

280,281/89-36

-

-

--

~~~~

(Closed) Item I.A.2 - Inadequate evaluation of true nature of the cavity

seal failure resulting in violation of 10 CFR 50, Appendix B,

Criterion XVI.

The licensee actions with regards to this issue included

revision of the administrative procedure associated with identification

and review of conditions adverse to quality (Station Deviation Reports).

The inspectors have reviewed *the licensee's latest revision to administra-

tive procedure

SUADM-LR-13,

11Station Deviation Reports

11

,

dated

December 29, 1989.

This procedure establishes a deviation report review*

process including classification, multidiscipline review, cause determina-

tion evaluation, and root cause evaluation process. This process has been

reviewed by several different NRC inspectors and is considered adequate.

This item is closed.

8.

Exit Interview

The inspection scope and results were summarized on April 4, 1990, with

those individuals identified by an asterisk in paragraph 1.

The following

summary of inspection activity was discussed by the inspectors during this

exit._

An inspec.:tor fqllowup item (Paragraph 3.d) was identified on licensee's

leak reduction program which is required by TS 6.4.K.1 (280,281/90-14-0l).

During a review of operator performance in the control room, it was noted

that the operations staff that performs control room duties are performing

these functions in a satisfactory manner.

Cooperation between shifts was

noted as a strong area.

However, some minor problems regarding strict

adherence to requirements and attention to detail (paragraph 3.e) were

also noted as needing additional attention.

15

An inspector followup item (paragraph 4) was identified for followup on

licensee action for replacement of type BFD relays (280,281/90-14-02).

During this inspection period, one violation with two examples was

identified (paragraph 6) for failure to follow procedure during testing of

components, and systems as required by TS 6.4.D (280,281/90-14-04).

The

inspectors consider that the two examples of failure to follow procedure

by craft personnel are not related to a programmatic problem in the

surveillance area.

However they raise concerns about the level of reviews

that are conducted by cognizant supervision who approve the periodic test

results on the critique page of the completed surveillances.

The

inspectors consider that these reviews should identify problems similar to

the ones cited in the violation and consider that additional management

attention is necessary in this area.

In addition, an unresolved item was

identified in the same inspection area with regards to required surveil-

lance testing frequency (280, 281/90-14-03) .

. 9.

Index Of Acroynms And Initial isms

AFW

CCWHX

CFR

eves

DR

ESF

EWR

EOP

FSAR

HX

LER

LCO

NRC

OP

PM

PORV

PSIG

PT

QA

QC

RCS

RG

RO

RSHX

RWP

SNSOC

SRO

SW

TS

TSC

UFSAR

URI*

Auxiliary Feedwater

Component Cooling Water Heat Exchanger

Code Of Federal Regulations

Chemical And Volume Control System

Deviation Report

Engineered Safety Feature

Engineering Work Request

Emergency Operating Procedures

Final Safety Analysis Report

Heat Exchanger

Licensee Event Report

Limiting Conditions Of Operation

Nuclear Regulatory Commission

Operating Procedure

Preventative Maintenance

Pressure Operator Relief Valve

Pounds Per Square Inch Gauge

Periodic Test

Quality Assurance

Quality Control

Reactor Coolant System

Regulatory Guides

.Reactor Operator

Recirculation Spray Heat Exchanger

Radiation Work Permit

Station Nuclear Safety and Operating Committee

Senior Reactor Operator

Service Water

Technical Specifications

Technical Suppory Center

Updated Final Safety Analysis Report

Unresolved Item