ML18152A297

From kanterella
Jump to navigation Jump to search
Insp Repts 50-280/89-06 & 50-281/89-06 on 890129-0304. Violations Noted.Major Areas Inspected:Plant Operations, Maint & Surveillance,Ler Review,Installation & Testing of Mods & Licensee Action on Previous Insp Findings
ML18152A297
Person / Time
Site: Surry  Dominion icon.png
Issue date: 03/31/1989
From: Fredrickson P, Holland W, Larry Nicholson, York J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18152A298 List:
References
50-280-89-06, 50-280-89-6, 50-281-89-06, 50-281-89-6, NUDOCS 8904180340
Download: ML18152A297 (16)


See also: IR 05000280/1989006

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W._

ATLANTA, GEORGIA 30323

Report Nos.:

50-280/89-06 and 50-281/89-06

Licensee:

Virginia Electric and Power Company

Glen Alleri~ VA

23060

Dock.et Nos.:

50-280 and 50-281

License Nos.: DPR-32 and DPR-37

Facility Name:

Surry 1 and 2

Inspection Conducted:

January 29 - March 4, 1989

r* h

. _,,,,. ,t7 /ff/'. , _- .

Inspectors: ~/

./'/' V--c:~L---*- /J'* Cl/~

Scope:

Results:

W. E. Holland', S~enior.Resident Inspector

<;?~ ~<;;t:-

-c_ -

,Cb,('

Date S1gned

y] ~?*?C

--~ /

0 7*

Date

i gned

. *?,/Jif;S7

Date igned

. '

SUMMARY

This routine resident inspection was conducted on site in the areas

of plant operations, plant maintenance, plant surveillance, licensee

event report review, installation and testing of modifications, and

licensee action

on

previous

inspection findings.

A special

evaluation of the licensee 1 s program used to walk. down selected

systems prior to unit(s) restart was documented in last month 1 s

report, and this ~nspection effort continues as documented in this

inspection report.

Certain tours were conducted on back.shifts or week.ends.

Back.shift or

week.end tours were conducted on January 29, 30, 31, February 5, 8, 9,

16, 18, 20; 26, and March 2.

During this inspection period, three violations, one

item*, and t~o inspector followup items were identified.

are listed below.

unresolved

These items

One violation was identified (paragraph 3.f(3)) for fallure to

provide adequate procedure for testing of systems involving nuclear

safety of the station (280/89-06-01).

This violation meets the

8904180340 890403

PDR

ADOCK 05000280

G

PNU

2

criteria s~ecified in Section V of the NRC Enforcement Policy for not

issuing a Notice of Violation.

The *second violation was identified

(paragraph

9.a) for failure to take prompt corrective action on

potential wetting of safety-re*lated components (280,28l/89-06-02).

The third violation was identified (paragraph 9.b) for failure to

take adequate corrective action on purging potential unqualified

parts from the site supply system (280,281/89-06-03).

This violation

closes Inspector Follow-up Item 280,281/88-51-04.

One inspector followup item was identified (paragraph 4.a) for review

of audits and weaknesses concerning drawings and design change

control (280, 281/89-06-04).

A second inspector followup item was*

identified (paragraph 5.b) for followup on the licensee commftment to

refurbish all safety-related 4160 volt breakers prior to respective

unit restart (280, 281/89-06-05).

One unresolved item was identified (paragraph 5.c) for additional

inspector review bf licensee requirements for returning to service,

after maintenance or modification, systems involving nuclear safety

of the station (280/89-06-06).

  • Unresolved items are matters about which more information is required to

determine whether they are acceptable or may involve violations or deviations .

REPORT DETAILS

1..

Persons Contacted

Licensee Employees

R. Bilyeu, Licensing Engineer

  • R. Blount, Superintendent of Technical Services
  • D. Christian, Assistant Station Ma~ager

D. Erickson, Superintendent of Health Physics

  • E. Grecheck, Assistant Station Manager
  • M. Kansler, Station Manager
  • J. McCarthy, Superintendent of Operations
  • G. Miller, Licensing Coordinator, Surry
  • J. Ogren, Superintendent of Maintenance
  • T. *sowers, Superintendent of Engineering
  • J. Price, Site Quality Assurance Manager

Other licensee employees contacted included control room operators, shift *

technical advisors, shift supervisors and other plant personnel.

  • Attended exit meeting.

The newly assigned NRC Region II Projects Division Section Chief, visited

the Surry Power Station on February 23, 1989.

The Section Chief was taken

on a tour of the plant, including the low level intake structure, by the

resident inspectors.

He also met with licensee management.to discuss

the current status of issues and other matters of mutual interest .

. On February 28, 1989, NRC senior management personnel from headquarters

and the Region II offices visited the Surry Power Station.

The senior

managers were given a tour of the station by the resident inspectors.

After the touri NRC senior management met with licensee management.

The

licensee also provided a presentation on the current issues and their

status.

Acronyms and initialisms used throughout this report are listed in the

last paragraph.

2.

Plant Status

Units 1 and 2 began the reporting period in cold shutdown.

The units

remained in cold shutdown.for the duration of the inspection period while

substantial operational reviews and maintenance activities were being

conducted .

3.

2

Operational Safety Verification

(71707)

a.

Daily Inspections .

b.

C.

The inspectors conducted daily inspections in the follow*ing areas:

Control

room staffing, access, and operator behavior; operator

adherence to approved procedures, technical specifications, and

limiting conditions fo~ operations; examination of panels containing

instrumentation and other reactor protection system elements to

determine that required channels are operable; review of control room

operator logs, operating. orders, plant deviati_on reports, tagout

logs, jumper logs, and tags on components to verify compliance with

approved procedures.

Weekly Inspections

The inspectors conducted weekly inspections in the following area~:

verification of operability of selected ESF systems by valve

alignment, breaker positions, condition of equipment or component(s),

and operabi 1 i ty of instrumentation and support i terns es sent i a 1 to

system actuation or performance. Pl ant tours were conducted which

included observation of general plant/equipment conditions, fire

protection and preventative measures, control of activities * in

progress, radiation protection controls, physical security controls,

plant housekeeping conditions/cleanliness, and missile hazards.

The

inspectors routinely monitor the temperature

Qf

the auxiliary

feedwater pump*discharge piping to ensure steam binding is prevented.

Biweekly Inspections

The inspectors conducted biweekly inspections in the following areas:

verification review and walkdown of safety-related tagout(s) in

effect; review of sampling program (e.g., primary and .secondary

coolant samples, boric acid tank samples, plant liquid and gaseous

samples); observation of control room shift turnover; review of

implementation

of

the

plant

problem

identification

system;

verificati-0n of selected portions of containment isolation lineup(s);

and verification that notices to workers are posted as required by

10 CFR 19.

d.

Plant Tours

Inspections fncluded areas in the Units 1 and 2 cable vaults, vital

battery rooms, steam safeguards areas, emergency switchgear rooms,

diesel generator rooms; control room, auxiliary building, Units 1 and

2 containments, cable penetration areas, independent spent fuel

storage facility, low level intake structure, and the safeguards

valve pit and pump pit areas. Reactor coolant system leak rates were

reviewed to ensure that detected or suspected leakage from the system

e.

3

was

recorded,*. investigated, and evaluated; and that appropriate

actions were

taken,

if required.

The

inspectors

routinely

independently calculated RCS leak. rates using the NRC Independent

Measurements Leak Rate Program ( RCSLK9).

_On a regular basis, RWPs

were reviewed and specific work activities were monitored to assure

they were being conducted per the

RWPs.

Selected radiation

protection instruments were periodically checked, and equipment

operability and calibration frequency were verified.

Monthly Inspections

In the course of monthly activities, the inspectors included a review

of * the licensee I s physical security program.

The performance * of

various shifts of the security force was observed in the conduct of

daily activities to include: protected and vital areas access

controls; searching of personnel, packages and vehicles;

badge

issuance and retrieval;*escorting of visitors; and patrols and

compensatory posts.

f.

Licensee 10 CFR 50.72 Reports

(1)

On January 29, 1989, the *licensee made a report to the NRC in

accordance with 10 CFR 50.72 with regards to degradation to the

insulation of the Unit 1 and Unit 2 inside recirculation spray

pump motor leads.

The degraded conditions were id~ntified as

extending into the motor sealing material making the motor seal

suspect.

In addition, it _was found that the motor lead lugs may

have been improperly crimped.

The licensee has shipped all four

pump motors to the pump vendor (General Electric) facility for

evaluation of the condition and repair as nec*essary.

Evaluation

of pump condition * and repair effort was ongoing when the

inspection period ended.

(2)

On February 5, 1989, the licensee made a report to the NRC in

accordance with 10 CFR 50.72 with regards to loss of normal

power to the*

11 F

11 bus.

This bus was supplying normal power to

the Unit 1

11 H

11 bus and the Unit 2

11J

11 bus. Loss of power to the

Unit 1

11 H

11 bus resulted in an automatic start of the Unit 1

generator.

Loss of power to the Unit 2

11J

11 bus resulted in an

automatic start of the No. 3 emergency diesel -generator and

loading of the "J". bus onto the generator.

All safety systems

performed as designed.

The cause of the loss of power to the

11 F11 bus was traced to improper closure of the tie breaker (25C2)

for backfeed of the bus from the Unit 2 unit. service

transformers.

The 1 icensee inspected and cleaned the suspect

breaker

and

then

tested

the

breaker

several

times

satisfactorily. The breaker was then placed back into service

and performed satisfactorily during power realignment to -the 11 F

11

bus.

Maintenance activities associated with this breaker are

discussed in paragrap~ 5 .

4

(3)

On February 8, 1989, the licensee made a report to the NRC in

accordance with 10 CFR 50.72 with regards to a spurious safety

injection on Unit 1.

The safety injection occurred during

special testing on Unit 1 i'n accordance with ST-241.. "Unit 1.A

Train Bus Deactivation Test

11 *

The actuation occurred when

circuit No. 29 on vi ta l bus 3A was deenergi zed in accordance

with procedure.

The SI resulted due to removal of the

11block

11

condition on-the low pressure SI bistables. All safe~y-related

components that were available performed as designed.

Initial

evaluation of the event concluded that.the test procedure was

inadequate in that it did not provide for special controls to

prevent the SI during deenergization of protection channel

  • cjrcuits.

The licensee revised the proceduie to prevent

recurrence.

The inspector reviewed the above event and considers that it is

a violation of Technical Specification 6.4, Failure to provide

adequate procedure for testing of systems involving nuclear

safety of the station (280/89-06-01).

However, this violation

meets the criteria specified in Section V of the NRC Enforcement

Policy for not issuing a Notice of Violation and is not cited.

Within the areas inspected, one violation was identified.

4.

Operational Readiness Program Review

(71710)

a.

Drawing System Verification ( RAI 88-01)

An audit was made of the control room and TSC drawings.

The drawings

available to the operators in the control room consist of half-size

mylars of the flow diagrams and electrical schematics.

Common

systems that apply to both units are included in the Unit 1 set and

have been transposed to a n~w CAD format to aid in legibility. The

basic difference in the new drawings for Unit 1 and the old-style

st i 11 used for Unit 2 is- that each page has been expanded to several

pages to reduce the amount of information per page. Although the new

drawings are easier to read, the operators *are familiar with the

old-style drawings and generally do not consider them a -problem.

A

program to convert the Unit 2 drawings is ongoing.

A full set of

station aperature cards is maintained by the operations department in

, the adjacent control room annex and the TSC:

The inspectors selected the following drawings to ascertain that

current drawings and related information are comparable in both the

control room and the TSC:

Unit 1

Drawing No.

11448-FM-072A

11448-FM-072D

1

11448-FM-073A

11448-FM-086A

11448-FM-089A

11448-FM-064A

11448-FM-0688

11448-FB-041A

11448-FE-lAA

11448-FE-010

Unit 2

Drawing No.

11548-FM-064A

11548-FM-068A

11548-FM-071A

11548-FM-072A

11548-FM~07 SJ

11548-FM-084A

11548-FM-0848

11548-FM-086A

11548-FM-0868

11548-FM-088A

11548-FM-0888

11548-FM-088C

11548--FM-089A

11548-FM-0898

11548-FM-1058

5

Design

Sheet No.

Rev. No.

Change

2

2

1

1

3

4

1

2

1

3

12

19

21

17

30

29

17

13

3

13

87~29

86-03

86-15

85-31

88-33-3

Design

Sheet No.

Rev. No.

Change

1

1

1

1

l

1

1

1

2

1

2

3

1

2

l

29

26

24

13

13

24

4

15

17

9

21

18

27

19

24

84-60

88-07

86-11

88-02

85-31 80-98A

System

Component Cooling

Component Cooling

Bearing Cooling

Reactor Cooling

Safety Injection

Main Steam

Auxiliary Feedwater

Chilled Water

App. R-Electrical

4160 Voltage Diagram

System

Main Steam

Feedwater

Circulating Service

Water

Component Coolfng

Instrument Air

Containment Spray

Recirculation Spray

Reactor Cooling

Reactor Cooling

Chem.& Vol. Control

Chem.& Vol. Control

Chem.& Vol. Control

Safety Injection

Safety Injection

Chem.& Vol. Control

No discrepancies were found with the Unit 1 drawings.

On Unit 2,

drawing number 11548-FM-1058 had the wrong revision in the control

room, i.e., Revision 24 in the control room, and Revision 25 on the

aperature card in the technical support center. In addition, drawing

numbers 11548-FM-064A and -0848 had the design change number noted on

the aperature card but not on the drawing in the control room.

The

ommi*ssion of the design change number on the control room drawing

does not affect operability as discussed later in this paragraph.

The incofrect revision is a problem and will be addressed in the

followup inspection for the !FI listed below .

6

The inspectors reviewed all or portions of the following station

administrative procedures which affect the drawing system:

SUADM-ENG-03

SUADM-ENG-01

SUADM-ADM-11

SUADM-LR-01

SUADM-0-11

Design Changes, dated 7-14-88

Engineering Work Request, dated 11~03-87

Station Drawing Revision and Distribution, dated

4-11-88

Station Nuclear Safety and Operating Comm., dated

10-14-87

Temporary Modifications, dated 11-22-88

A review of these procedures revealed that the licensee doej not

use advance change notices or marked up ( red-1 i ned) copies to flag

the operators of a system change.

Instead, a revision to the drawing

is issued and hand carried to the control room in parallel with the

technical review of the ~odification and the return of the system to

service, Controlled station drawings are, however, annotated with a

stamp to reflect when a design change has been issued for that

system. This stamp pro vi des no information to the contro 1 room

operator since they use the tagout and work order system to control

the system operabi 1 i ty status.

A system is not to be returned to

service following a full or partial modification until the required

drawings are revised and a technical review of the* modification* is

approved by SNSOC.

The annotation of the design change on the

drawing should not affect operability of the system because of these

controls.

The inspectors identified in paragraph 5.c an example

where a system was returned to service without the proper drawing

revision and technical review.

The inspectors reviewed design change packages 86-15 ( Unit 1) and

86-16 (Unit 2). These packages covered modifications to the reactor

coolant system level instrumentation to prevent loss of shutdown

cooling during midnozzle operadon.

On Unit 1, the inspectors

reviewed two design change technical reviews, one for mechanical and

one for electrical.

The request for drawing changes related to the

.design changes was reviewed.

Drawings and date of revisions on the

appropriate drawings .in the control room were noted.

The inspectors

concluded that the proper procedura 1 steps were taken before the

modification (install~tion of a standpipe and instrumentation) was

used during the Unit 1 refueling operation.

Station admi ni strati ve procedure SUADM-ADM-11 states that any person

~ay request that a change be made to a-controlled station drawing.

This drawing change request is reviewed by the cognizant supervisor

possessing expertiie in the particular area.

The request is

forwarded to the Station Supervisor for Plant Engineering for

concurrence and then forwarded to the drawing update group.

The

inspectors reviewed the method for identifying and correcting station

drawing discrepancies and expressed concern that the program does not

7

mandate a timeframe for correcting known drawing problems that. are

identified .outside the desig*n change and EWR process~

In addition;

the station drawing ch_ange requests are not assigned a*unique number*

and/or entered into a formal system for tracking and auditing.

Discussions with the licensee personnel responsib_le for making the.

drawing revisions revealed that the requests are entered into an

informal computer program (i.e. not covered by a procedure) upon

receipt into the drawing update group.

A review of the previous

drawing change requests that had been submitted to this drafting

group and entered into * their tracking system indicated that

approximately 80 percent of the 600 requests were corrected within 90

days., The above concern was identifi~d as a programmatic weakness

and will_be included in the IFI listed below (280, 281/89-06-02).

The inspectors re~iewed QA auditi in the area of dr~wing control.

Preliminary indications from an unfinished QA audit *(Audit No.

S89-16) indicated that the auditor found three (3) out of the

approximately 246 total drawings in the control rooms which were not

the latest revised dra~ing.

Several other potential que~tions were

raised such as receipt of controlled drawings and the list used for

selecting control room drawings.

The findings from this ongoing

audit and the review of additional audits previously performed in

this area will be followed by the inspectors.

This item and the

previously discussed items will* be identified as an Inspector

Followup Item, Review of audits and .weaknesses concerning drawings

and design change control (280, 281/89-06-04).

b.

Plant Configuration Confirmation (RAI 88-01)

Jhe inspectors reviewed the approximately 260 drawing discrepancies

identified to date by the system engineers during their Unit 1

walk.downs.

The *resident inspectors had evaluated part of this

ongoing effo.rt during the previous inspection period (ref. NRC-

Inspection Report 280, 281/88-51).

THe intent of these walkdowns are

stated as follows:

--

In sure that components a re physically 1 ocated in the system as

per the station drawings .

. Insure

that

proper identification is provided

for

the

components.

Insure that components are in proper orientation (e.g., check

valves in proper direction).

Insure that discrepancies are identified and addressed.

A majority of the items identified involved either an inaccurate

location of vent and drain valves or a failure to reflec~ the pipe

caps installed* downstream of the valves.

The licensee has st.:eit~d

that the system walkdowns have not identified*~ny ~iscrepanties that

would affect operability of a system or train. The inspector review

of the findings to date supports this conclusion.

  • In addition to the system walkdowns by cognizant system engineers,

the assessment of outstanding issues for each system includes a

review of outstanding temporary modifications and/or jumpers, station

deviations,

commmitment

items,

outstanding safety-related work

orders, outstanding EWRs and open Type I engineering evaluations.

The system engineers have been tasked with reviewing the above items

pertaining to their particular system and evaluating if closure of

the item is possible prior t~ unit startup.

For those items that

will not be closed prior to startup, a justification for not

completing the

i tern

must

be completed and approved by the

Superintendent of Technical Services.

The overa 11 status of the engineering work as of February 28, 1989,

for Unit 1 was as follows:

Restart

No. Identified

No. Reviewed

Resolutions

Walkdown Deviations

3181

1543

60

Commitments

727

277

54

Engr. Work Requests

598

0

0

Engr. Evaluations

.312

213

69

Temp. Modifications

16

16

5

The appropriate system engineers were just starting their document

review when the inspectio.n period ended.

The inspectors will

continue these inspection efforts by following a representative

sample of each of the above subjects thr9ugh the system engineers and

on to final disposition.

In. addition, the inspectors will continue

to perform some additional wa l kdowns of systems as we 11 as observe

selected deficiencies that have been identified.

Within the areas inspected, no violations ~r deviatioris were identified.

5.

Maintenance Inspections. (62703)

During

the

reporting period,

the inspectors *reviewed maintenance

activities to assure compliance with.the appropriate procedures.

a.

Maintenance of Emergency Service Water Pump

On February 1, 1989, the inspectors witnessed maintenance on the

diesel driver for the emergency service water pump 1-SW-P-18. This

work was authorized by work order 635872 and performed in accordance

with maintenance procedure TMMP-C-SW-293,

11 Emergency :service Water

b.

C.


-

9

Pump Diesel Engine Exhaust Manifolds/Overspeed Govenor Trip Mechanism

Gasket Replacement".

The inspectors reviewed-the job site paperwork

and *discussed- the work with the mechanics.

In addition, the

inspectors observed maintenarice engineers at the job site to evaluate

a broken stud in the diesel exhaust manifold.

No discrepancies were

noted.

Maintenance on 4160 Volt Breaker 25C2 (Isolation Breaker for Bus 2C

and Unit 2 Station Ser~ice Transformer)

On February 4, 1989, the subject breaker failed to close during

electrical realignments to support special testing.

Failure of the

breaker to close resulted in loss of offsite power to tie bus F and

a 1 so resulted in a loss of power to two vi ta 1 * busses (iH and 2J).

The licensee inspected the suspect breaker and determined that the

mechanical

linkage for the- breaker was dirty and not working

properly~

The licensee cleaned the mechanical portion of the breaker

mechanism, _tested the breaker satisfa*ctorily, and returned the

breaker to service.

However, further licensee evaluation of the

problem concluded that additional inspection of other breakers was

warranted. The licensee is currently in the process of shipping all

safety-related breakers. to a local

refurbishment facility for

inspection and overhaul.

Information received on the first three

breakers (!TE-BBC TYPE HK) indicates that the closing mechanisms were

dirty and needed cleaning and relubrication.

The inspectors closely monitored the licensee actions to date. They

have reviewed the licensee's procedures for breaker maintenance,

inspected a breaker to understand the problems encountered, and

reviewed the refurbishment facility reports on the first three

breakers.

The inspectors consider that refurbishment of all 4160

volt safety-related breakers is warranted based on these reports and

the licensee has committed to refurbish all. safety-related breakers

prior to restart of the respective unit as part of the Confirmation

of Action Letter dated March 9, 1989.

Followup on the licensee

commitment to refurbish all safety-related 4160 volt breakers prior

to respective unit restart is identified as an Inspector Followup

Item (280, 281/89-06-05).

Gas Binding of HPSI Pumps/Surry/Units 1 and 2

In August 1988,

the licensee identified

a potential

problem

associated with gas voids located in high point piping for safety

injection flowpaths to the suction of the HPSI pumps.

Licensee

corrective action for these problems' included the installation of

high point vents in these lines to allow for proper fill and vent of

this* system.

The installation of the high point vents was

accomplished in accordance with EWR 88-440.

The EWR was accomplished

for Unit 2 as required by work order 3800074880. . The inspector

10

reviewed the completed EWR and also verifjed the installation of the

new vents fbr both Units 1 and 2.

The inspector also reviewed the

control room drawings for Unit 2 and verified that they were updated

as required.

However, during review of the. drawings for Unit l on

February 2*2, 1989, the inspector noted that the applicable*control

room drawings had not been updated to agree with actua 1 pl ant

configuration.

Furthermore, the inspector noted that the portion of

the system in which the high point vents had been installed was in

service providing a suction flowpath to an operating charging pump.

Additional licensee review in this area concluded that the techri~cal

review for Unit 1 had not been completed prior to. returning the

system to an operable status. The licensee completed the appropriate

technical review for Unit 1 o*n- February 28, 1989.

The inspector

reviewed the final technical* review for Unit 1 and confirmed that all

requirements had been completed.

The licensee also concluded during review of *this* issue that the*

administrative procedure die not provide adequate guidance to assure

that systems were not returned to service prior to completion of

  • required reviews.

The licensee has instituted corrective actions on

February 28, 1989, to insure that the administrative procedure

provides for adequite guidance for completion of technic~l reviews

prior to returning systems to operation. The inspector verified that

appropriate action was initiated in the above case; however, the

inspectors were in the process of reviewing additional EWRs for

similar problems when the inspection period ended.

This issue is

therefore identified as an Unresolved Item (280/89-06-06), pending

additional inspector review of licensee requirements for r~turning to

service, after maintenance or modification, systems involving nuclear

safety of the station.

d.

Overhaul of HPSI Pumps

The inspectors reviewed work to overhaul and repair the damage that

occurred when the HPSI

pump 1-CH-P-lC was operated dry* for

approximately two minutes .. The inboard **pt.imp seal and bearing

displayed extensive damage and the pump casing was deter-mined to be

.warped.

This work was authorized by work order #76962 and invoked

maintenance procedure MMP-C-CH-089,

11Chargi ng Pump/High Head Safety

Injection Pump 11 , dated 12-14-87.

This inspection also included.the

applicable RWP (#1474) and station tag.gi"ng record (TIO #045293).

No

discrepancies ~ere noted.

Within the areas inspected,. no violations or deviations were

identified .

6.

11

Su~veillanci Inspettions (61726)

During the reporting period, the inspectors reviewed various surveillance

activities to assure compliance with the appropriate procedures as

follows:

Test prerequisites were met.

Tests were performed in accordance with appro~ed procedures.

Test procedures appeared to perform their intended function.

Adequate coordination existed among personnel involved in the test.

Test data was properly coilected and recorded.

Inspection areas included the following:

a.

Low Head Safety Injection Pump

b.

On February 14, the ,nspectors reviewed the completed results of

periodic test 1-PT-18.1, "Low Head SI Component Test and Flushing of

Sensitized Stainless Steel Piping", performed on pump 1-SI-P-lA. The

test results were adequately documented and appeared to meet the

acceptance criteria.

No discrepancies were noted .

Motor Operated Valves

On February 20, the inspectors witnessed testing of various Unit 1

motor operated valves in accordance with the following test

procedures:

l-PT-18.lOJ, dated 8/2?/87, "Verification of Local & Remote

Valve

Position

Indications of Safety Related Valves

in

Safeguards Valve Pit Area".

l-PT-18.lOH, dated 9/29/88, "Verification of Local & Remote

Valve Position Indications of Service Water Valves in Safeguards

Area and Turbine Building".

l-PT-18.lOM, dated 11/20/87, "Verification of Local & Remote

Valve Position* Indication of RWST Chemical Addition Tank and

Containment Systems in Safeguards Area".

The above testing stroked the valves from the main control room and

verified the corrett local and control

room valve position

indication, as well as the valve position indicated on the emergency

response facility computer. In addition, an operator was stationed at

the 480 volt switchgear as an operational check of the breakers. The

' -

12

inspectors o_bS-Brved testing ih progress and discussed the test

results . with the SRO conducting the test_.

No discrepancies were

noted.

Within the areas inspected, no violations or deviations were identified:

. 7.

Installation and Testing of Modifications (37828)

The inspectors reviewed Design Change 88-36-3, "Control Room Envelope HVAC

Interim Modification 11 , to verify that modification activities are in

conformance with the requirements of the Technical Specifications, 10 CFR

50.59, and 10 CFR Part 50, Appendix B, Criterion III.* This design change*

  • upgrades the ventilation system that provides cool air to the emergency

switchgear and control rooms during normal and post-acciderit co~dititins.

The inspection effort included a review of the approved work package

safety analysis,

10

CFR

50.59 analysis,

and

various additional

calculations pertaining to Appendix R and seismic requirements.

In

addition,

the

inspector

reviewed

the

post

modification

testing

requirements and walked down p6rtions of the modifications in the field

with craft personnel

to verify compliance with the appropriate

instruction~.

No discrepancies were noted.*

8.

Licensee Event Report (LER) Review

(92700)

The inspectors reviewed the LER's listed below to ascertain whether NRC

reporting requirements were being met and to determine appropriateness of

the corrective action(s). The .inspector's review also included followup on

implementation of corrective action and review of licensee documentation

that all required corrective actions were complete.

LERs that identify violations of regulations and that meet the criteria of

10 CFR, Part 2, Appendix C,Section V shall be identified a.s Licensee

Identified Violations (LIV) in the following closeout paragraphs.

LIVs

are considered first-time occurrence* violations which meet the .NRC

Eriforcement Policy for exemption from i*ssuance of a Notice o~Violation.

These items are identified to allow for proper evaluation~ of corrective

actions in the event that similar events occur .in the future.

(Closed) LERS 280/88-02, 06, 10, 24, and 26; 281/88-03, 07, 12, 16, and

20, Inoperable Individual Rod Position Indicators Due to Instrument Drift.

The* issue involved drift of more than one !RPI, which is contrary to

Technical Specification 3.12.E .. Immediate correcti~~ action in eac~ case

was to adjust the affected IRPis to read within the required technical

specification tolerence. Additional corrective action was to submit .a

technical specification change request to provide relief from this known

generic condition. The *inspector verified that the licensee complied with

technical specification requirements in each case, verified that the

licensee had submitted a technical specification change request, and

reviewed the change request.

These LERs are closed.

. 9.

13

Licensee Action on Previous Inspection Findings (92701) *

a.

(Open) IFI 280,*281/88-45-02, Weaknesses identified in the licensee's

program to identify and correct conditions adverse to quality.

The

issues* involved repeated.wetting of auxiliary feedwater pump motors_

during periods of heavy rainfall over an extended period of time, and

inadequate evaluation of the failure mechanism of a containment

isolatfon valve during repair.

After further review by the NRC

staff, the AFW wetting issue has been classified as a violation for

failure to take prompt corrective action *to preclude wetting of

safety-related ~omponents (280,281/89-06-02).

The issue associated

w1th inadequate failure mechanism evaluation will be reviewed along

with the licensee's root cause program; therefore, this IF! remains

open.

b.

(Closed) 280,281/88-51-04, Followup on Ucensee eval.uation of r,eplica

parts issue.

This issue involved inadequate licensee. action to

remove unacceptable safety-related parts from warehouse inventory in

1983. After further review by the NRC staff, the* replica" parts issue

has been_ classified as a violation for failure to take prompt

corrective action to* ensure that safety-related components are

repaired using only qualified replacement parts (280,281/89-06-03).

-This !FI is closed.

. Within the areas *inspected, two violations were identified.

10.

Exit Interview

The ~nspection scbpe and findings were summarized on March 6, 1989, with

those individuals identified by an asterisk in paragraph 1.

The following

new items were identified by the inspectors during this exit:

One violation was identified (paragra.ph 3.f(3)) for failure to provide

adequate procedure for testing of systems involving nuclear safety of the

station (280/89-06~01).

This violation meets the criteria specified in

Section V of the NRC Enforcement Policy for not issuing a Notice of

Violation.

One inspector followup item was identified (paragraph 4.a) for review of

audits and weaknesses concerning drawings a~d design change control (280,

281/89-06-04).

One inspector followup item was identified (paragraph 5.b) for followup on

the li_censee commitment to refurbish all safety-related 4160 volt breakers

prior td respective unit restart (280, 281/89-06-05).

One unresovled item was identified (paragraph 5.c) for additional

inspector review of licensee requirements for returning to service, after

maintenance or modification, systems involving nuclear safety of the

station (280/89-06-06).

14

On March 28, 1989, the following two additional items were identified to

the Station Manager:

One violation w~s identified (paragraph 9.a) for failtjre to tak~ prompt.

  • corrective action on potential wetting of _safety-related components

(280,281/89-06-02).

One violation was identified (paragraph 9.b) f~r fail~re to take adequate

corrective action on purging potential unqualified parts from the site

supply system (280,281/89-06-03).

This violation closes Inspector

Followup Item 280,281/88-51-04).

The licensee. acknowledged the inspection findings. with no dissenting

comments.

The licensee did not identify as proprietary any of the

materials provided to or reviewed by the inspectors during this

inspection.

11.

Index of Acronyms and Initialisms

AFW

ANSI

AP

CAD

cc

ccw

CFR

cw

DP!

DR

EMP

RCS

RHR

RA!

RG

RO

RPS

RSS

RWP

RWST

SI

SNSOC

SRO .

TS

TSC

UFSAR

URI

vs

TSC

.,.

-

Auxil_iary Feedwater

AMERICAN NATIONAL STANDARDS INSTITUTE

ABNORMAL OPERATING PROCEDURE

COMPUTER AIDED DESIGN

COMPONENT COOLING

.

COMPONENT COOLING WATER

CODE OF FEDERAL REGULATIONS

CIRCULATING WATER

DELTA PRESSURE INDICATORS

DEVIATION REPORT

ELECTRICAL MAINTENANCE PROCEDURE

REACTOR COOLANT SYSTEM

RESIDUAL HEAT REMOVAL

RESIDENT ACTION ITEM

REGULATORY GUIDES

REACTOR OPERATOR

REACTOR.PROTECTION SYSTEM

RECIRCULATION SPRAY SYSTEM

RADIATION WORK PERMIT-

REFUELING WATER STORAGE TANK -

SAFETY EVALUATION REPORT

SAFETY INJECTION

STATION NUCLEAR-SAFETY AND OPERATING COMMITTEE

SENIOR REACTOR OPERATOR

SERVICE WATER

-

TECHNICAL SPECIFICATIONS

TECHNICAL SUPPORT CENTER

UPDATED FINAL SAFETY ANALYSIS REPORT

UNRESOLVED ITEM -

VENTILATION SYSTEM

TECHNICAL SUPPORT CENTER