ML18152A277

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Insp Repts 50-280/98-04 & 50-281/98-04 on 980322-0502. Violations Noted.Major Areas Inspected:Operations, Engineering,Maintenance & Plant Support
ML18152A277
Person / Time
Site: Surry  Dominion icon.png
Issue date: 06/01/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18152A278 List:
References
50-280-98-04, 50-280-98-4, 50-281-98-04, 50-281-98-4, NUDOCS 9806160226
Download: ML18152A277 (19)


See also: IR 05000280/1998004

Text

Docket Nos.:

License Nos. :

Report Nos. :

Licensee:

Facility:

Location:

Dates:

Inspectors:

Approved by:

.9806160226 980601

PDR

ADOCK 05000280

G

PDR

U.S. NUCLEAR REGULATORY COMMISSION

REGION II

50-280, 50-281

DPR-32. DPR-37

50-280/98-04. 50-281/98-04

Virginia Electric and Power Company CVEPCO)

Surry Power Station, Units 1 & 2

5850 Hog Island Road

Surry, VA

23883

March 22 - May 2. 1998

R. Musser, Senior Resident Inspector

K. Poertner, Resident Inspector

R. Haag, Chief. Reactor Projects Branch 5

Division of Reactor Projects

Enclosure 2

EXECUTIVE SUMMARY

Surry Power Station. Units 1 & 2

NRC Inspection Report Nos. 50-280/98-04. 50-281/98-04

This integrated inspection included aspects of licensee operations. engineer-

ing, maintenance. and plant support.

The report covers a six-week period of

resident inspection.

Operations

Licensee actions with respect to a residual heat removal system through-

wall flaw demonstrated a good safety perspective and conservative

decision making.

Technical Specification requirements concerning decay

heat removal loops were met.

The decision to remove the flaw intact to

try to determine the root cause was appropriate (Section 01.2).

A violation was identified concerning an inadequate operating procedure

revision which fafled to properly adjust the steam generator power

operated relief valve setpoints. The failure to identify the procedure

inadequacy prior to and while performing the procedure demonstrated a

lack of attention to detail oh the part of the operator. other members

of the operating crew involved with the setpoint change, and the

procedure writers (Section 01.3).

Unit 1 startup activities were accomplished in accordance with approved

procedures in a thorough and controlled manner.

The operating crew

exhibited good communications during the startup activities and

distractions in the control room were minimized (Section 01.4).

The licensee's actions related to spent fuel storage pool issues were in

accordance with commitments made to the NRC.

The inspectors verified

that a change to the pool high temperature alarm and operational

procedural enhancements have been made.

The one remaining commitment.*

providing emergency power to the spent fuel pool cooling pumps. was

scheduled for completion by the end of February 1999 (Section 01.5).

The licensee performed an inadequate tagout on the bearing cooling water

system which demonstrated a lack of sensitivity to the tagout process.

Based on this event and previous problems the inspectors are concerned

with the declining performance by some operations department personnel

in regards to the tagout process and configuration control (Section

01.6).

The Unit 1 manual Auxiliary Feedwater System isolation valves inside

containment were properly aligned for normal operation and were properly

identified (Section 02.1).

Maintenance

A non-cited violation was identified concerning maintenance personnel

failing to verify that they were working on the proper component before

starting preventive maintenance activities.

As a result. work to be

performed on the B charging pump normal suction valve was performed on

2

the pump's normal discharge valve.

Identification and corrective

actions for this matter were prompt and thorough (Section Ml.1).

The inspectors reviewed the licensee's plans for the replacement of the

Unit 1 pressurizer manway access cover and found them to be adequate.

Although a steam leak had been present, the inspectors verified that the

pressurizer clad manway seating surface was fully intact (Section Ml.2).

Emergency Diesel Generator Number 3 alarm relay replacement activities

were accomplished in accordance with the work package. i nstructi ans.

The

electricians performing the work were knowledgeable of how to perform

the activities. The tagout for the work was acceptable (Section Ml.3).

Surveillance activities for a containment radiation monitor were

performed in accordance with procedure requirements and the

instrumentation and control technicians performing the procedure were

knowledgeable of the procedure requirements (Section Ml.4).

A non-cited violation was identified for application of a higher than

specified torque for the body to bonnet fasteners on two safety

injection check valves.

An incorrect pressure/torque conversion chart

for the torquing device was used to apply an approximate torque valve of

4500 foot-pounds in lieu of the specified 2600 foot-pounds of torque

(Section Ml. 5).

Engineering

Safety Evaluation 98-0040 and Engineering Transmittal 98-0058 adequately

justified a temporary modification to plug a leaking reactor coolant

pump thermowell (Section El.l).

Plant Support

Health physics practices were observed to be proper (Section Rl).

Security and material condition of the protected area perimeter barrier

were acceptable (Section Sl) .

Report Details

Summary of Plant Status

Unit 1 commenced the reporting period in a shutdown condition for a

maintenance outage.

The unit was returned to service on March 31. 1998. and

operated at power for the remainder of the reporting period.

Unit 2 operated at power the entire reporting period.

I. Operations

01

Conduct of Operations

01.1 General Comments (71707. 40500)

The inspectors conducted frequent control room tours to verify proper

staffing, operator attentiveness. and adherence to approved procedures.

The inspectors attended daily plant status meetings to maintain

awareness of overall facility operations and reviewed operator logs to

verify operational safety and compliance with Technical Specifications

CTSs).

Instrumentation and safety system lineups .were periodically

reviewed from control room indications to assess operability. Frequent

plant tours were conducted to observe equipment status and housekeeping .

Deviation Reports (DRs) were reviewed to assure that potential safety *

concerns were properly reported and resolved.

The inspectors found that

daily operations were generally conducted in accordance with regulatory

requirements and plant procedures.

01.2 Residual Heat Removal (RHR) System Leakage

a.

Inspection Scope (71707)

The inspectors reviewed l{censee actions associated with a through-wall

leak in the Unit 1 RHR system discharge piping.

b.

Observations and Findings

On March 22. 1998. with Unit 1 in intermediate shutdown and with the RHR

system in service, the licensee identified a through-wall leak in the

common RHR discharge piping upstream of RHR flow element 1-RH-FE-1605.

The leak was identified due to boron buildup on the piping.

When the

boron was removed to inspect the piping, slight weepage was identified

from a small 1/32 inch pit in the pipe surface.

The licensee declared

the RHR system inoperable based on the through-wall leakage.

TS 3.1

requires that a minimum of two non-isolated loops consisting of any

combination of reactor coolant loops or RHR loops be operable with

Reactor Coolant System (RCS) temperature less than 350°F.

At the time

of discovery, the RCS loops were operable.

With the RHR system

inoperable. the licensee was unable to continue with the plant cooldown

and depressurization for the scheduled maintenance outage.

2

The inspectors observed the RHR system leakage.

The leakage was

characterized by a slight localized buildup of moisture on the piping

surface following cleaning of the pipe surface.

The licensee performed

ultrasonic testing on the piping adjacent to the through-wall leak and

did not identify any wall thinning or flaw.

Based on the Non-

Destructive Examination (NOE) performed. the licensee requested a one-

time schedule relief from the American Society of Mechanical Engineers

(ASME) code for Section XI pressure boundary leakage corrective action

and flaw evaluation requirements.

The relief would allow the RHR system

to be considered operable with the defect in the discharge piping and

the plant could continue with the shutdown to cold shutdown conditions.

In the relief request the licensee agreed to repair the piping prior to

returning Unit 1 to service. The NRC approved the relief request and

the RHR system was declared operable at 5:00 p.m .. on March 23. 1998.

The RCS was depressurized and pressurizer level was maintained at

approximately 22 percent to support the outage activities. Following

depressurization of the RCS. the RHR system weepage stopped.

Following completion of the Unit 1 outage activities. the licensee

removed the RHR system from service to repair the RHR piping.

The

licensee removed the flawed area using a two-inch hole saw and installed

a socolet and plug.

The licensee also inspected the inside of the RHR

piping by removing an adjacent RHR system flow element.

No

discrepancies were noted during the inspections.

The inspectors

monitored repair activities and discussed NOE requirements with

cognizant licensee personnel.

The inspectors determined that the NOE

performed met ASME Code requirements.

RHR system repairs were completed

on March 29. 1998.

The flaw was removed intact from the RHR piping.

The licensee performed a preliminary visual evaluation of the flaw and

determined that a detailed metallurgical analysis was required to

determine the failure mechanism.

The licensee had not completed the

evaluation as of the end of the inspection period.

Review of the

licensee's failure analysis is identified as Inspection Followup Item

50-280/98004-01.

c.

Conclusions

Licensee actions with respect to a RHR system through-wall flaw

demonstrated a good safety perspective and conservative decision making.

TS requirements concerning decay heat removal loops were met.

The

decision to remove the flaw intact to try to determine the root cause

was appropriate.

01.3 Steam Gerierator (SG) Power Operated Relief Valve (PORV) Setpoint

Discrepancy

a.

Inspection Scope (71707)

The inspectors reviewed SG PORV setpoint requirements prior to RHR

system maintenance activities .

3

b.

Observations and Findings

C.

On March 28. 1998, the inspectors observed control room activities

during the initial mode change above 200°F to commence repair of a

pinhole leak in the Unit 1 RHR system.

During review of controlling

procedure 1-GOP-1.2. "Unit Startup, RCS Heatup from 195 to 345." the

inspectors observed a discrepancy between Step 5.3.3 and an implementing

substep 5.3.3.c. Step 5.3.3 required that the SG PORV controllers be

verified or adjusted to 50 psig prior to exceeding 212°F in accordance

with substeps a through g.

However. substep 5.3.3.c specified a

setpoint of 1035 psig.

The licensee was notified of the discrepancy and

the SG PORV setpoint controllers were subsequently adjusted from 1035

psig to 50 psig prior to exceeding 212°F.

The PORV setpoint was reduced

to decrease the required SG steam pressure that would be needed to

support RCS decay heat removal.

With a setpoint of 50 psig, the RCS

heatup would be much less than required for a SG PORV setpoint of 1035

psig.

The SG PORVs were intended as a backup to the condenser dump

valves for SG steam removal.

The inspectors discussed the problem with cognizant personnel.

Licensee

management had determined that additional controls (reduction of SG PORV

setpoint to 50 psig) would be prudent while the unit was in an unusual

configuration for an extended period during the RHR work.

On March 26.

  • a One-Time-Only (OTO) Procedure Action Request (PAR) to 1-GOP-1.2 was

issued to set the SG PORV controllers at 50 psig. Although Step 5.3.3

was revised, the procedure writer and reviewers failed to identify that

substep 5.3.3.c also needed revision.

During the pre-job brief the

change to the SG PORV setpoint controllers was not discussed.

The

operator performing Step 5.3.3 and substep 5.3.3.c failed to detect the

discrepancy and signed Step 5.3.3 as being complete after having

verified that the SG PORV controllers were set at 1035.

The inspectors

were concerned that several members of the plant staff demonstrated a

lack of attention to detail which resulted in controls identified for a

special evolution involving an unusual plant configuration not being

adequately implemented into procedures.

In addition. the operator

performing the step had an opportunity to identify the discrepancy

between step 5.3.3 and substep 5.3.3.c but failed to recognize this

error.

TS 6.4.A.1 requires that detailed written procedures and appropriate

instructions be provided for normal startup. operation. and shutdown of

a unit and all systems and components involving nuclear safety of the

station. The failure to revise substep 5.3.3.c of procedure 1-GOP-1.2

during implementation of a OTO PAR to change the SG PORV setpoint to 50

psig is identified as Violation 50-280/98004-02

Conclusions

A violation was identified concerning an inadequate operating procedure

revision which failed to properly adjust the steam generator power

operated relief valve setpoints. The failure to identify the procedure

inadequacy prior to and while performing the procedure demonstrated a

4

lack of attention to detail on the part of the operator. other members

of the operating crew involved with the setpoint change, and the

procedure writers.

01.4 Unit 1 Restart Activities

a.

Inspection Scope (71707)

The inspectors observed portions of the Unit 1 restart from a

maintenance outage.

b.

Observations and Findings

C.

The inspectors observed rod withdrawal to criticality and portions of

the initial power increase to place the turbine generator on line.

Control room activities were conducted in a thorough and controlled

manner.

Procedures were in use and followed during startup activities.

The operating crew exhibited good communications during the startup and

distractions in the control room area were minimized.

The unit was

returned to service on March 31, 1998.

Conclusions

Unit 1 startup activities were accomplished in accordance with approved

procedures in a thorough and controlled manner.

The operating crew

exhibited good communications during the startup activities and

distractions in the control room were minimized.

01.5 Review of Spent Fuel Storage Pool Issues

a.

Inspection Scope (71707)

b.

The inspectors performed a review of the status of the licensee's

actions related to spent fuel storage pool issues.

Observations and Findings*

In 1996. the NRC identified a number of issues related to the

reliability of spent fuel pool decay heat removal system and the

maintenance of an adequate spent fuel coolant inventory in the spent

fuel pool. A review was conducted to identify plant-specific and

generic areas for regulatory analyses.

One issue was identified at

Surry related to the absence of an on-site power supply for systems,

capable of spent *fuel pool cooling. This matter was brought to the

attention of the licensee in a letter from the NRC dated September 19.

1996. Subsequent responses from the licensee. dated November 21. 1996.

November 27. 1996, and March 28. 1997. discussed the intended actions

the licensee planned to perform to resolve this matter. These actions

included lowering the spent fuel pool high temperature alarm from 140°F

to ll5°F, implementing additional procedural controls that provide

further actions to be taken to restore cooling to the spent fuel pool in

5

the event of a loss of offsite power. and to provide emergency power

feeds to the spent fuel pool cooling pumps by the end of 1999.

The inspectors reviewed these actions.

The licensee lowered the spent

fuel pool high temperature alarm from 140°F to ll5°F. This was

reflected in the annunciator response procedure, O-VSP-A4. "Spent Fuel

Pit Hi Temp." Revision 2.

However. drawing 11448-ESK-14A6. sheet 13 had

not been updated to reflect this change and still reflected the old

setpoint of 140°F. This matter was discussed with the licensee who

submitted a deviation report to document and track the matter to

resolution (DR S-98-1159).

In addition, the inspector reviewed

procedures (1-AP:10.07. "Loss of Unit 1 Power." and O-AP-22.02. "Loss of

Spent Fuel Pit Level") and determined that adequate procedural guidance

was in place to provide further actions to operators to restore cooling

to the spent fuel pool in the event of a loss of offsite power.

This

included guidance to perform a feed and bleed operation of the pool and

instructions on evaluating alternate power sources to the spent fuel

pool cooling pumps.

Specific procedures do not exist on providing

alternate power sources to the spent fuel pool cooling pumps.

Each

individual scenario would have to be evaluated and a temporary power

routing would have to be performed based on the availability of power.

The inspectors reviewed the licensee's schedule to implement the

modification to provide emergency power feeds to the spent fuel pool

cooling pumps.

Currently, Design Change 97-004. is scheduled for

completion by the end of February 1999. This will provide the committed

emergency power feed to the spent fuel pool cooling pumps prior to the

end of 1999.

c.

Cone l usi ans

The licensee's actions related to spent fuel storage pool issues were in

accordance with commitments made to the NRC.

The inspectors verified

that a change to the pool high temperature alarm and operational

procedural enhancements have been made.

The one remaining commitment.

providing emergency power to the spent fuel pool cooling pumps. was

scheduled for completion by the end of February 1999.

01.6 Inadequate Tagout of the Unit 2 C Bearing Cooling Heat Exchanger

a.

Inspection Scope (71707)

b.

The inspectors reviewed the circumstances surrounding the tagout of the

Unit 2 C bearing cooling heat exchanger.

Observations and Findings

On April 22. 1998. plant operations tagged out the Unit 2 C bearing

cooling heat exchanger to support preplanned corrective maintenance.

This work involved the replacement of two heat exchanger tubes and

sacrificial anode plugs.

The bearing cooling water system is a non-

safety related closed loop cooling water system located in the turbine

6

building used to cool secondary plant loads.

When maintenance personnel

initiated the removal of the first tube. water began streaming from the

tube sheet into the service water plenum of the heat exchanger and onto

the turbine building floor. Maintenance personnel initiated the

securing of the heat exchanger by closing the heat exchanger exterior

access cover doors and informed the control room of the situation.

Operators were dispatched to assist maintenance personnel.

Approximately three minutes after being informed of the leak. operations

received an alarm indicating that the bearing cooling head tank had a

low level condition.

Initial measures to restore bearing cooling water

level in the head tank were unsuccessful. and fire water had to be

valved in to return water level to its normal operating band.

Unit

operation was unaffected by this transient on the bearing cooling water

system.

Following restoration of the bearing cooling system to a normal status.

it became apparent that the tagout for the intended maintenance work had

been inadequate. Specifically, the bearing cooling water side of the

heat exchanger had not been isolated. and when the mechanic removed the

heat exchanger tube, a direct leakage path existed through the tube

sheet.

The maintenance request for a tagout clearly stated that heat

exchanger tubes would be replaced as part of the intended maintenance.

The operators preparing and reviewing the tagout did not identify that

the bearing cooling side of the heat exchanger required isolation and

approved and placed the tagout without proper isolation. Because this

event occurred on a non-safety related secondary system, this matter

does not constitute a violation of NRC requirements.

However, the same

process is used when tagging safety related equipment. Since this event

occurred on a relatively low pressure and temperature system, neither

personnel nor equipment sustained any damage.

This event demonstrates a

clear lack of sensitivity to the tagout process and a continued problem

with configuration control as noted in NRC Inspection Report Nos. 50-

280, 281/98099.

Based on this event and previous problems the*

inspectors are concerned with the declining performance by some

operations department personnel in regards to the tagout process and

configuration control.

Further followup related to this issue revealed that the cross-tie

valve, which is used to provide make up to the bearing cooling head tank

from the opposite unit. was in a throttled position in lieu of being

fully open.

Because of this condition, it was necessary for operations

to utilize the fire water system to restore water level to the bearing

cooling head tank.

No reason has been determined for the valve being in

the throttled position.

c.

Conclusions

The licensee performed an inadequate tagout on the bearing cooling water

system which demonstrated a lack of sensitivity to the tagout process.

Based on this event and previous problems the inspectors are concerned

with the declining performance by some operations department personnel

in regards to the tagout process and configuration control.

7

02

Operational Status of Facilities and Equipment

02.1 Auxiliary Feedwater (AFW)

a.

Inspection Scope (71707)

The inspectors walked down portions of the Unit 1 AFW system inside

containment.

b.

Observations and Findings

The inspectors verified that the Unit 1 manual AFW isolation valves

inside containment were properly aligned.

The valves were locked open

as required by the system alignment procedure and properly identified.

No discrepancies were identified.

c . Cone 1 us i ons

The Unit 1 manual Auxiliary Feedwater System isolation valves inside

cont a i n*ment were proper 1 y aligned for normal operation and were properly

identified.

08

Miscellaneous Operations Issues (92901)

08.1

(Closed) VIO 50-280. 281/96011-01: Spent fuel pit cooling valve out of

position. This violation involved the failure to reposition a valve in

the spent fuel pool cooling system following a revision to the valve

alignment procedure. Corrective actions included review of other valve

alignment procedure changes to ensure proper alignment of systems and

implementation of a revision to procedure VPAP 0502, "Procedure Process

Control," to require that the Supervisor-Shift Operations be notified of

any valve lineup changes.

The inspectors reviewed the corrective

actions and verified that VPAP 0502 had been revised to require

notification of operations.

08.2 (Closed) VIO 50-280. 281/96012-01: Inadequate Alternate Alternating

Current (AAC) diesel generator return to service procedure.

This

violation involved the failure to return the AAC diesel generator output

breaker control switch to the auto position following maintenance

activities due to a deficient procedure.

Corrective actions included

revising procedure O-MOP-AAC-002. "Return to Service of the AAC Diesel

Generator.* to require that the control switch be returned to the auto

after trip position and revising operator logs to verify switch

positions on a daily basis. The inspectors verified that the above

corrective actions had been implemented .

8

II. Maintenance

Ml

Conduct of Maintenance

Ml.1 Maintenance Activity Performed on Incorrect Component

a.

Inspection Scope (62707)

The inspectors reviewed an error made by the maintenance department

during the performance of a preventive maintenance activity.

b.

Observations and Findings

On April 28, the Unit 1 B charging pump was removed from service to

perform pre-planned maintenance activities.

One of the scheduled tasks

was the performance of Preventive Maintenance (PM) activities on the

motor operator for the pump's normal suction valve, 1-CH-MOV-1269A.

This work was to be done in accordance with procedure O-MPM-0300-01,

"Limitorque Operator Type SB, SBD, SMB, and HBC Lubrication and

Inspection," Revision 4-P2, and with work order 00385581-01.

The actual

work to be performed included the 18 month lubrication and inspection of

the operator.

During this activity, the valve was to be manually

cycled.

Valve 1-CH-MOV-1269A was tagged out of service, and work order 00385581-01 was released by operations to the maintenance department for

work to commence.

At approximately 9:45 a.m., control room operators

noted that the control room indication for valve 1-CH-MOV-1286B (the

normal discharge valve for the B charging pump) indicated an

intermediate position. After holding discussions with maintenance

personnel and investigating the matter at the B charging pump cubicle,

the licensee determined that the PM activity intended to be performed on

valve 1-CH-MOV-1269A had in fact been performed on 1-CH-MOV-1286B.

No

maintenance activities were planned on valve 1-CH-MOV-1286B nor was it

tagged out.

No personnel or equipment sustained any injury or damage.

Since the B charging pump had been removed from service for maintenance

activities, the error in working on the discharge valve in lieu of the

suction valve did not affect the operability status of the B charging

pump.

Followup of the activity by the licensee indicated that the mechanic

assigned to perform the PM activity had been adequately briefed prior to

beginning the task.

The mechanic, however, did not adequately perform

the pre-maintenance verification to ensure the correct component was

identified prior to the commencement of work as required by procedure

O-MPM-0300-01.

This failure to follow procedure resulted in the

performance of the PM activity on the wrong component.

The inspectors reviewed the circumstances involving the identification

and corrective actions associated with this matter.

The issue was

promptly identified by an operator performing a walkdown of the control

panel.

Following identification, operations and maintenance quickly

interfaced to determine the cause of the intermediate indication on

valve 1-CH-MOV-1286B.

This identification demonstrated good attention

9

to detail on the part of operations associated with this maintenance

activity. The inspectors determined that the corrective actions for

this matter were prompt and comprehensive.

These corrective actions

included:

1) Initiating a deviation report to document and track the

issue, 2) Promptly identifying the cause of the issue as failure to

self-check and issuing the appropriate personnel action to ensure

managements expectations are understood, 3) A plan was developed to

stress managements expectations to the maintenance department with

regards to self-checking and verbatim compliance, and 4) A plan was

initiated to have all mechanical maintenance department personnel

utilize the licensee's self-checking simulator to reinforce self-

checking techniques.

The failure to follow procedure O-MPM-0300-01 and work order 00385581-01

while performing preventive maintenance on valve 1-CH-MOV-1269A is a

violation of technical specification 6.4.A.7 and 6.4.D. This non-

repetitive. licensee identified and corrected violation is being treated

as a Non-cited Violation (NCV) consistent with Section VII.B.1 of the

NRC Enforcement Policy. This matter is identified as NCV 280/98004-03.

c.

Conclusions

A non-cited violation was identified concerning maintenance personnel

failing to verify that they were working on the proper component before

starting preventive maintenance activities.

As a result, work to be

performed on the B charging pump normal suction valve was performed on

the pump's normal discharge valve.

Identification and corrective

actions for this matter were prompt and thorough.

Ml.2 Unit 1 Pressurizer Manway Inspection

.a.

Inspection Scope (62707)

The inspectors examined the Unit 1 upper pressurizer manway opening and

the licensee's effort to repair a previously identified leak in this

opening.

b.

Observations and Findings

Following the restart of Unit 1 from the spring 1997 refueling outage,

the licensee identified that the upper pressurizer manway was leaking.

As a part of the spring 1998 Unit 1 maintenance outage, the licensee

intended to replace the manway access cover and its associated gasket in

order to stop the pressurizer leak.

The inspectors reviewed the

licensee's plans to replace the installed manway cover with a primary

manway access cover removed from a previously installed steam generator.

These steam generators are stored on site in a specially constructed

mausoleum.

The inspectors reviewed Westinghouse technical manual 38-

W893-00033, which stated that the pressurizer access cover is identical

to and interchangeable with the steam generator primary manway access

cover.

The inspectors also verified, by visually inspecting and

10

comparing the parts to a technical manual drawing, that the gasket and

spacer being installed with the replacement manway access cover were the

appropriate parts.

The inspectors also visually inspected the pressurizer manway opening to

ensure its condition was adequate to support continued operation.

The

clad seating surfaces of the manway opening were fully intact. Some

minor cutting of the non-clad surfaces was seen. but because of the

location of the flaws. the sealing and seating of the manway would be

unaffected. After the unit was returned to normal operating pressure,

the licensee determined that the leak had been corrected~

c.

Conclusions

The inspectors reviewed the licensee's plans for the replacement of the

Unit 1 pressurizer manway access cover and found them to be adequate.

Although a steam leak had been present. the inspectors verified that the

pressurizer clad manway seating surface was fully intact.

Ml.3 Emergency Diesel Generator (EOG) Maintenance

a.

Inspection Scope (62707)

The inspectors observed portions of the work activities associated with

replacement of an EOG alarm relay.

b.

Observations and Findings

On April 24. 1998, the inspectors observed portions of the work

activities associated with Work Order (WO) 00388023. "Repair/Replace NVR

Relay." The work order was initiated to replace a failed relay in the

number 3 EOG remote alarm panel.

The relay failure resulted in a

continuous alarm condition in the control room and required increased

operator tours of the number 3 EOG room.

The work activity was

accomplished using procedure O-ECM-1806-01, "Protective Relay and

Associated Control Circuit Replacement.* Revision 5. and Engineering

Transmittal S98-074. "Mounting Details for NVR Relay in EOG Remote Alarm

Panel Surry Power Station Units 1 and 2." The work activities observed

were accomplished in accordance with the work package instructions and

the electricians performing the work activity were knowledgeable of the

how to perform the activities. The inspectors also reviewed the

associated tagging record and found it adequate.

c.

Conclusions

EOG number 3 alarm relay replacement activities were accomplished in

accordance with the work package instructions. The electricians

performing the work were knowledgeable of how to perform the activities.

The tagout for the work was adequate.

11

Ml.4 Containment Radiation Monitor Testing

a . Inspection Scope ( 61726)

The inspectors observed portions of the performance of procedure O-PT-

26.6V. "Victoreen Radiation Monitoring Equipment Background. Heat Trace

Flow Fault Checks and Filter Replacement." Revision 7.

b.

Observations and Findings

The inspectors observed surveillance activities associated with Unit 1

containment radiation monitor RM-159.

The inspectors observed

activities locally at the detector and in the control room.

The

surveillance was conducted in accordance with procedure O-PT-26.6V and

the instrumentation and control technicians performing the surveillance

activity were knowledgeable of the procedure requirements.

c.

Conclusions

Surveillance activities for a containment radiation monitor were

performed in accordance with procedure requirements and the

instrumentation and control technicians performing the procedure were

knowledgeable of the procedure requirements.

Ml.5

Improper Torque Applied to Safety Injection Check Valves

a.

Inspection Scope ( 62707)

The inspectors reviewed the application of improper torque values to

safety injection check valves 1-SI-130 and l-SI-145.

b.

Observations and Findings

During the Unit 1 maintenance outage conducted in late March. the

licensee performed maintenance on the lC safety injection accumulator

discharge check valve. l-SI-145. to correct a longstanding back-leakage

condition. This maintenance. which involved internal repairs to the

valve. was to be performed in accordance with work order 00365452-01 and

procedure O-MCM-0417-25. "Darling Swing Check Valve Inspection and

Overhaul Model S 350W SC," Revision 6.

Following the completion of the

maintenance activity, the maintenance department determined that a

possibility existed that the valve bonnet hold down fasteners (studs and

nuts) had been tightened to an excessive torque.

Based on this, the

fasteners were removed with the breakaway torque being measured during

removal. which in turn confirmed the over-torque condition.

The

fasteners were removed. replaced with new studs and nuts, and tightened

to the correct torque.

During the same maintenance outage, an inspection of valve 1-SI-130, the

18 safety injection accumulator outlet to the B cold leg check valve.

revealed a body to bonnet leak.

The licensee performed an inspection of

a fastener in the vicinity of the leakage to determine if any bolt

12

wastage had occurred. This inspection revealed that the leakage had

caused some bolt wastage and a decision was made to replace all of the

valve bonnet hold down fasteners. Maintenance personnel replaced all of

the hold down fasteners in accordance with work order 00386551-01 and

procedure O-MCM-1001-01. "Stud Replacement." revision 0.

Based on the

over torque condition discovered on 1-SI-145. the licensee questioned

the possibility of the hold down fasteners on 1-SI-130 being tightened

to an excessive torque.

The fasteners on 1-SI-130 were removed and

their breakaway torque also revealed an over torque condition.

The

fasteners were removed, replaced with new studs and nuts. and tightened

to the correct torque.

The licensee's investigation iDto this matter revealed that the cause of

the over torque condition was the use of an incorrect pressure/torque

conversion chart for the torque head that was used to tighten the

fasteners.

This resulted in the fasteners being tightened to a torque

of approximately 4500 foot-pounds in lieu of the procedurally specified

value of approximately 2600 foot-pounds.

This condition was applicable

to both the 1-SI-130 and 1-SI-145 valves.

To correct this matter. the licensee:

1) Installed new fasteners

tightened to the correct torque, 2) Initiated two deviation reports to

document the occurrence. 3) Pressure/torque conversion charts have been

attached to each torque head. and 4) Craft personnel were briefed on

this matter and informed of the requirement to use only the charts

attached to the torque head.

During the inspectors review of the

matter. no documentation could be located which described the magnitude

of the over torque condition or the acceptability of the threads in the

valve body.

Component engineering personnel informed the inspectors

that a sample of the threads in the 1-SI-145 valve body had been.

inspected and found acceptable.

During the removal and installation

process. the fasteners on 1-SI-130 and l-SI-145 were noted to turn in

and out freely. Additionally, an informal calculation was done to

demonstrate the acceptable affects of the over torque on the valve body.

Based on the inspectors questions. the licensee stated that a more

formal evaluation and documentation of these over torque conditions

would be performed.

The application of the incorrect torque to 1-SI-130 and 1-SI-145 is a

violation of technical specification 6.4.A.7 and 6.4.D.

This non-

repetitive. licensee identified and corrected violation is being treated

as a Non-cited Violation (NCV) consistent with Section VII.B.1 of the

NRC Enforcement Policy. This matter is identified as NCV 280/98004-04.

c.

Conclusions

A non-cited violation was identified for application of a higher than

specified torque for the body to bonnet fasteners on two safety

injection check valves.

An incorrect pressur~/torque conversion chart

for the torquing device was used to apply an approximate torque valve of

4500 foot-pounds in lieu of the specified 2600 foot-pounds of torque.

13

II I. Engineering

El

Conduct of Engineering

El.1 Reactor Coolant Pump (RCP) Thermowell Temporary Modification (TM)

a.

Inspection Scope (37551)

The inspectors reviewed Temporary Modification Sl-98-07, "1-RC~P-18

Lower Bearing Thermowell Plug."

b. Observations and Findings

During the Unit 1 maintenance outage water was found in the B RCP radial

bearing Resistance Temperature Detector (RTD) thermowell. Analysis

determined that the leakage was primary coolant.

The thermowell is 47

inches long and is part of the RCS pressure boundary.

Based on the fact

that replacement of the thermowell would require pump removal and

disassembly, the licensee decided to remove the RTD and plug the

thermowell.

The licensee plans to repair the leaking thermowell at the

next scheduled refueling outage.

The inspectors reviewed TM Sl-98-07, associated Safety Evaluation 98-

0040, and Engineering Transmittal 98-0058, "1-RC-P-lB Pump Bearing RTD

Thermowell Repair." that provided the instructions to plug and seal the

thermowell.

The inspectors determined that the TM. Safety Evaluation

and Engineering Transmittal adequately justified implementation of the

TM to remove the RTD and plug the B RCP radial bearing RTD thermowell.

c.

Conclusions

Safety Evaluation 98-0040 and Engineering Transmittal 98-0058 adequately

justified a temporary modification to plug a leaking reactor coolant

pump thermowell.

EB

Miscellaneous Engineering Issues (92903)

EB.1

(Open) Violation 50-281/96001-01: Failure to revise steam flow

calorimetric computer program.

The inspectors determined that all the

corrective actions identified have not been completed.

The licensee has

two Commitment Tracking System (CTS) items left to complete prior to

closure of the concerns identified in the violation.

The CTS items

involved resolution of procedural and engineering discrepancies.

The

present scheduled completion date documented in the CTS tracking system

is May 31, 1999.

The inspectors discussed the remaining open CTS items

with licensee personnel.

The open items were considered low priority

items by the licensee.

The inspectors expressed concern that the

corrective actions had not been completed.

The inspectors determined

that the items are being reviewed and engineering is providing some

attention to the remaining items. This item will remain open pending

additional review of the licensee's actions .and their progress to

complete the remaining items.

14

IV. Plant Support

Rl

Radiological Protection and Chemistry Controls (71750)

On numerous occasions during the inspection period. the inspectors

reviewed Radiation Protection (RP) practices including radiation control

area entry and exit. survey results. and radiological area material

conditions.

No discrepancies were noted. and the inspectors determined

that RP practices were proper.

Sl

Conduct of Security and Safeguards Activities (71750)

On numerous occasions during the inspection period. the inspectors

performed walkdowns of the protected area perimeter to assess security

and general barrier conditions.

No deficiencies were noted. and the

inspectors concluded that security posts were properly manned and that

the perimeter barrier's material condition was properly maintained.

V. Management Meetings

Xl

Exit Meeting Summary

The inspectors presented the inspection results t6 members of licensee

management at the conclusion of the inspection on May 13. 1998.

The

licensee acknowledged the findings presented.

The inspectors asked the licensee whether any materials examined during

the inspection should be considered proprietary.

No proprietary

information was identified.

PARTIAL LIST OF PERSONS CONTACTED

M. Adams. Superintendent. Engineering

R. Allen. Superintendent. Maintenance

R. Blount. Manager. Nuclear Safety & Licensing

D. Christian. Site Vice President

M. Crist. Superintendent. Operations

E. Collins, Director. Nuclear Oversight

B. Shriver. Manager. Operations & Maintenance

T. Sowers. Superintendent. Training

B. Stanley, Supervisor, Licensing

W. Thorton. Superintendent. Radiological Protection

15

IP 37551:

INSPECTION PROCEDURES USED

Onsite Engineering

IP 40500:

Effectiveness of Licensee Controls in Identifying, Resolving, and

Preventing Problems

IP 61726:

IP 62707:

IP 71707:

IP 71750:

IP 92901:

IP 92903:

Surveillance Observation

Maintenance Observation

Plant Operations

Plant Support Activities

Followup - Plant Operations

Followup - Engineering

ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

50-280/98004-01

50-280/98004-02

50-280/98004-03 *

50-280/98004-04

Closed

50-280/98004-03

50-280/98004-04

50-280, 281/96011-01

IFI

VIO

NCV

NCV

NCV

NCV

VIO

Review of the licensee's RHR

system failure analysis

(Section 01.2).

Inadequate revision to

procedure l-GOP-1.2 (Section

01. 3).

Failure to follow procedures

by performing preventive

maintenance work on the wrong

B charging pump valve

(Section Ml. l).

Improper Torque Applied to

Safety Injection Check Valves

(Section Ml.5)

Failure to follow procedures

by performing preventive

maintenance work on the wrong

B charging pump valve

(Section Ml. l).

Improper Torque Applied to

Safety Injection Check Valves

(Section Ml.5)

Spent fuel pit cooling valve

out of position

( Sect i on 08 . 1) .

50-280, 281/96012-01

Discussed

50-281/96001-01

16

VIO

VIO

Inadequate ACC diesel

generator return to service

  • procedure (Section 08.2).

Failure to revise steam flow

calorimetric computer program

(Section E8 .1).