ML18152A265

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Insp Repts 50-280/95-16 & 50-281/95-16 on 950806-0902.No Violations Noted.Major Areas Inspected:Plant Status, Operational Safety Verification,Maint & Surveillance Insps, on-site Engineering Review & Plant Support
ML18152A265
Person / Time
Site: Surry  Dominion icon.png
Issue date: 09/28/1995
From: Belisle G, Branch M
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18152A266 List:
References
50-280-95-16, 50-281-95-16, NUDOCS 9510100215
Download: ML18152A265 (17)


See also: IR 05000280/1995016

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W., SUITE 2900

ATLANTA, GEORGIA 30323-0199

50-280/95-16 and 50-281/95-16

Licensee:

Virginia Electric and Power Company

Innsbrook Technical Center

5000 Dominion Boulevard

Glen Allen, VA

23060

Docket Nos.:

50-280 and 50-281

License Nos.:

DPR-32 and DPR-37

Facility Name:

Surry 1 and 2

Inspection Conducted:

August 6 through September 2, 1995

Lead Inspector:

Inspector

Other Inspectors:

D. M. Kern, Resident Inspector

W. K. ~o~rtn~, Res\\9ent Inspector

f;rc1 L5 &7:;/c,,;-

Approved by:

G. ..\\. Be 1 is 1 e, <s ti on Chief

Reactor Projects Section 2A

Division of Reactor Projects

SUMMARY

Scope:

D

This routine resident inspection was conducted on site in the areas of plant

status, operational safety verification, maintenance and surveillance

inspections, on-site engineering review, plant support, and action on previous

inspection items.

Inspections of backshift and weekend activities were

conducted.

Results:

Plant Operations

In mid-August, Hurricane Felix approached the North Carolina and.Virginia

coastlines.

An initiative to review industry hurricane response programs

resulted in several improvements to the Virginia Power Hurricane Response

Plan.

Licensee preparations for the potential on-site hurricane arrival were,

9510100215 950928

PDR

ADOCK 05000280

G

PDR

2

good.

Station management's close control over maintenance activities

demonstrated a strong safety perspective (paragraph 3.1).

Unit I control room annunciator panels A-E were inoperable from August 22-25

due to failed power supplies. This event was similar to a July 1995 problem

with the Unit I annunciator system. Operators implemented appropriate

compensatory measures.

Root cause evaluation remained in progress at the

close of this report period (paragraph 3.2).

Licensee actions associated with restoring redundant pressurizer heater

capacity powered from separate emergency buses were appropriate and

demonstrated a proper safety perspective (paragraph 3.3).

A deficiency report review identified a negative trend in operator performance

associated with human error and inattention to detail (paragraph 3.4).

Maintenance

Maintenance performed to support the Unit 2 core uprate was generally

performed in a quality manner (paragraph 4.2).

Test equipment unavailability for two safety-related maintenance activities

prolonged the period during which the safety-related equipment was either

unavailable or degraded.

This was considered a weakness in the maintenance

program (paragraph 4.3).

Increased online maintenance was noted prior to the Unit I shutdown for

refueling (paragraph 4.4).

Engineering

Marine fouling repeatedly degraded Component Cooling (CC) Heat Exchanger (HX)

and emergency service water pump performance during the summer months.

Component performance trending was beneficial, but was not fully effective in

maintaining CC HX availability. A recent bromine injection modification was a

positive action to improve CC HX performance (paragraph 5.1).

Management's decision to test emergency service water pump IA promptly

following indicated flow degradation on emergency service water pump IC

demonstrated an appropriate concern for common mode failure (paragraph 5.2).

Plant Support

Scaffolding erection for the upcoming Unit I outage was well managed

(paragraph 6).

Security personnel actions did not fully address the degraded conditions of a

vital area/fire barrier/pressure boundary door (paragraph 6).

REPORT DETAILS

1.

Persons Contacted

Licensee Employees

  • W.

H.

  • R.
  • D.

J.

D.

  • B.

R.

B.

  • D.

C.

  • J.
  • S.

R.

  • B.
  • K .
  • E.

T.

  • B.
  • J.
  • N.

Benthall, Supervisor, Licensing

Blake, Jr., Superintendent of Nuclear Site Services

Blount, Superintendent of Maintenance

Christian, Station Manager

Costello, Station Coordinator, Emergency Preparedness

Erickson, Superintendent of Radiation Protection

Garber, Licensing

Garner, Outage and Planning

Hayes, Supervisor, Quality Assurance

Hayes, Supervisor of Administrative Services

Luffman, Superintendent, Security

McCarthy, Assistant Station Manager

Sarver, Superintendent of Operations

Saunders, Vice President, Nuclear Operations

Shriver, Assistant Station Manager

Sloane, Superintendent of Outage and Planning

Smith, Site Quality Assurance Manager

Sowers, Superintendent of Engineering

Stanley, Supervisor, Procedures

Swientoniewski, Supervisor, Station Nuclear Safety

Urquhart, Supervisor, Training

Other licensee employees contacted included plant managers and

supervisors, operators, engineers, technicians, mechanics, security

force members, and office personnel.*

NRC Personnel

M. Branch, Senior Resident Inspector

  • D. Kern, Resident Inspector
  • K. Poertner, Resident Inspector
  • Attended Exit Interview

Acronyms used throughout this report are listed in the last paragraph.

2.

Plant Status

Unit 1 operated at power the entire reporting period.

The unit

commenced the reporting period in an end of cycle coastdown at 97%

power.

The unit was at 58% power with the A condenser waterbox removed

from service for cleaning at the end of the report period.

Unit 2 operated at power the entire reporting period.

On August 26, th~

unit reduced power to 83% for core uprate implementation and to remove

- -

=--=---==- -

-

~

2

the C waterbox from service for cleaning.

The unit returned to full

power on August 31.

3.

Operational Safety Verification (71707, 40500)

The inspectors conducted frequent tours of the control room to verify

proper staffing, operator attentiveness and adherence to approved

procedures.

The inspectors attended plant status meetings and reviewed

operator logs on a daily basis to verify operational safety and

compliance with TSs and to maintain overall facility operational

awareness.

Instrumentation and ECCS lineups were periodically reviewed

from control room indications to assess operability.

Frequent plant

tours were conducted to observe equipment status, fire protection

programs, radiological work practices, plant security programs and

housekeeping.

Deviation reports were reviewed to assure that potential

safety concerns were properly addressed and reported.

3.1

Hurricane Preparations

In mid-August, Hurricane Felix approached the North Carolina and

Virginia coastlines. The projected hurricane path included the

vicinity surrounding Surry Power Station. The licensee

implemented the Hurricane Response Plan at Surry Station and the

corporate offices. Region based specialists helped the resident

inspectors to provide continuous site inspection coverage while

the hurricane was a threat.

In addition, the NRC established a

mobile satellite communications link for use in the event that

normal off-site communication capabilities were disrupted.

The Virginia Power Hurricane Response Plan, revision 1, was

upgraded in early August to incorporate improvements identified

during a review of industry hurricane response programs.

The

licensee implemented hurricane preparations in accordance with the

plan, including OC-21, Severe Weather Checklist and AP-37.01,

Abnormal Environmental Conditions, revisiori 5.

The inspectors

performed periodic plant walkdowns including the electrical

distribution switchyard, the high and low level intake structures,

and the protected area. Hurricane preparations were good.

A continuous on-site Station Hurricane Coordinator was assigned

and watchbills were developed to staff th~ Station Hurri~ane

Response Center located in the TSC.

The TSC was partially staffed

when the storm track appeared most threatening.

The inspectors

reviewed NUREG 1474, Effect of Hurricane Andrew on the Turkey

Point Nuclear Generating Station from August 20-30, 1992, and

determined that licensee preparations for the hurricane were

consistent with the lessons learned from that event.

Station and corporate personnel closely tracked the storm's

position using real time national meteorological resources. Surry

county declared a hurricane watch, but did not escalate to a

hurricane warning which would the be *entry criteria for a NOUE.

~-=~:---=-=-==--=-~=--------------------------------- ---

- - --- -

3.2

3

The inspectors observed that station personnel were aware of

projected weather conditions, including projected high tide

surges.

High tide surges are important because they pose a flood

threat to the CW and ESW pump motors which pump water to fill the

ultimate heat sink.

The highest projected tide surge, in the

event that the hurricane reached Surry Station, was 9 feet above

MSL.

This was below the NOLIE entry condition of 12 feet above

MSL.

Operators demonstrated a clear understanding of the bases

for emergency entry conditions for tide height.

The inspectors questioned how operators measured and assessed tide

height for emergency event classification.

No control room

indications or local measuring instruments at the low level intake

structure exist. The SS informed the inspectors that outside tour

operators are trained to monitor for abnormal tide conditions and

inform the control room when unusually high or low tide conditions

are observed.

The SS then directs operators to monitor tide

height in relation to the top of the CW pump pits.

Emergency

event classification assessment is then made based upon water

height proximity to the CW or ESW pump motors.

Loss of CW and ESW

pumps are the bases for NOLIE and ALERT event declarations.

The

inspectors concluded that the stated method of assessing tide

height for event classification was adequate .

Station management directed that no maintenance on safety-related

equipment, other than that to provide operability, be performed

while the hurricane was a threat. Maintenance personnel stopped

inprogress work and returned components to service accordingly.

On August 17, the hurricane changed course away from land and

moved further out to sea. Management then permitted safety-

related maintenance to continue on a limited basis (e.g., 8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />

restoration requirement)._ Storm warnings for Virginia were

canceled and the licensee secured from the Hurricane Response Plan

at 2:00 pm on August 18.

The inspectors concluded that

management's close control over maintenance activities

demonstrated a strong safety perspective.

Unit 1 Control Room Annunciator Failure

On August 22, 1995, at 11:00 pm several alarms on the A-E control

room alarm panels annunciated for no apparent reason.

The A-E

panels comprise 50 percent of the Unit 1 control room alarms.

Operators saw light smoke and smelled a slight burned odor.

Initial inspection identified a blown fuse to one of nine

annunciator power supplies.

Further investigation confirmed that

the audible alarm, flashing light, and lock-in annunciator

features were not functioning properly. Control room instrument

indicators continued to indicate normally.

Operators initiated

abnormal procedure O-AP-10.13, Loss of Main Control Room

Annunciators, revision 0.

3.3

4

Operators promptly established compensatory actions which included

(1) stationing an additional RO in the control room to

continuously monitor control board indications, (2) implementing

supplemental plant tours at two-hour intervals to verify specific

safety-related equipment status for equipment with degraded

control room alarms, and (3) monitoring the Emergency Response

Facility computer display in the control room as an alternate

indication of important safety-related parameter alarm conditions.

The inspectors accompanied operators on supplemental plant tours

and observed augmented monitoring in the control room.

Operators

were knowledgeable of plant conditions and generally attentive

while performing assigned control board monitoring duties.

The

inspectors observed that some operators had difficulty maintaining

continuous close attention to control board indications for a

prolonged period and*discussed this observation with the SS.

Operations management took subsequent action to rotate the control

board monitoring duties more frequently among qualified ROs.

The

inspectors concluded that operations personnel properly

implemented compensatory actions in response to the inoperable

Unit 1 annunciators.

These same annunciators had been degraded from July 20-23, 1995.

Three of nine power supplies were determined to have failed during

that occurrence.

The root cause and corrective actions were not

fully developed at the time of the August loss of annunciators.

Troubleshooting and corrective maintenance activities for the

August 22-25 event are discussed in paragraph 4.1.

SNS engineers prepared SE 95-102 and JCO Sl-95-002 to assess

continued power operation with degraded control room annunciators.

The licensee determined that the UFSAR accident analysis credited

control room annunciators for mitigation of one accident, the

boron dilution accident. Unit 1 was at O ppm RCS boron

concentration due to end of fuel cycle coastdown when the A-E

annunciators failed. Therefore the boron dilution accident was

not considered credible. Additional compensatory actions were

identified in specific detail. The inspectors reviewed SE 95-102

and JCO Sl-95-002 and observed the SNSOC's safety review.

The

inspectors concluded that the licensee thoroughly evaluated the

loss of annunciator condition and implemented appropriate

compensatory actions.

The licensee replaced or rebuilt eight

power supplies.

The annunciator system was satisfactorily post

maintenance tested and returned to operation on August 25.

Following a 24-hour power supply burn in period, operators secured

the compensatory actions listed above.

Unit 1 Pressurizer Heaters

On August 24, operations found the electrical breaker to

pressurizer heater groups 11, 34 and 63 on the A pressurizer

heater bank tripped. Another group of 3 heaters on bank A was

already out of service and this left the bank with approximately

5

100 KW rated heater capacity available. Technical Specification 3.1.5.a requires that 125 KW of pressurizer heaters be available

and the TS Bases requires that the heaters be capable of being

supplied electrical power from an emergency bus.

Heater Bank A is

powered from the J emergency power bus.

The operators determined

that full heater capacity (250KW) existed on heater bank E powered

from the H emergency power bus and determined that a TS LCO did

not exist for pressurizer heater availability.

On August 25, troubleshooting commenced on heater groups 11, 34

and 63.

The licensee determined that the electrical fault causing

the breaker trip was located inside containment.

Based on this

information, the licensee implemented a temporary modification to

power a group of bank Cheaters from the supply breaker on the J

emergency power bus.

The temporary modification was completed on

August 28, and increased the available heater capacity powered

from the J emergency power bus to 150KW.

The inspectors monitored licensee actions and reviewed the

temporary modification package and associated 50.59 evaluation.

The inspectors determined that the temporary modification package

adequately addressed the safety concerns associated with

implementing the temporary modification.

In particular, the

inspectors verified that the modification package addressed diesel

generator loading requirements.

The inspectors reviewed the licensing requirement associated with

pressurizer heater capacity.

NUREG 0737, Clarification of TMI

Action Plan Requirements, Item II.E.3.1, Emergency Power Supply

For Pressurizer Heaters required that redundant heater capacity be

provided and that each redundant heater or heater group have

access to only one emergency power supply.

The TMI action item

also required that TSs be submitted to address pressurizer heater

capacity. This requirement was implemented to establish

sufficient pressurizer heater capacity to. maintain natural

circulation at hot shutdown conditions following a loss of offsite

power.

TS Amendment 93 contained requirements to have at least 125 KW

pressurizer heater capacity available.

Prior to this amendment,

pressurizer heater operability was not addressed in the TS.

This

amendment was issued after th~ NUREG 0737 requirements were

established and the TS amendment was determined to be acceptable

by the NRC.

Review of NRC correspondence prior to issuance of the

TS amendment determined that the NRC found the licensee's

pressurizer heater power supply design met the requirements of the

TMI Action Item (e.g., redundant heater groups powered from

separate emergency power supplies).

UFSAR Section 4.2.2.2,

Pressurizer, states that two backup heater groups rated at 250 and

200 KW and their associated controls are energized from redundant

emergency buses.

6

The inspectors discussed the apparent disconnect between the TMI

action item and the present TS with the licensee. The licensee

stated that the requirements of TS were met.

The temporary

modification would restore sufficient heater capacity to meet the

TMI action item.

The licensee also provided an engineering

analysis that determined 60 KW of pressurizer heater capacity

would be adequate to maintain natural circulation. The licensee

is presently reviewing the issue to determine if administrative

guidance should be provided to address loss of redundant heater

capacity.

The inspectors determined that the licensee met the

present licensing requirement for pressurizer heater capacity and

considered that the actions associated with restoring redundant

125 KW pressurizer heater capacity powered from separate emergency

buses demonstrated an appropriate safety perspective.

3.4

Deviation Report Review

During the report period the inspectors reviewed the following

DRs:

DR S-95-1596, Spent Fuel Pool Cooling Improperly Aligned

DR S-95-1667, SI Accumulator Inleakage During Recirc and

Sampling Evolutions

DR S-95-1675, AFW Pump Full Flow Recirc Valve Not Open Prior

To Pump Start For Testing

DR S-95-1780, Flow Inadvertently Aligned Through Deborator

While Flushing Ion Exchanger

DR S-95-1808, Containment Chiller Service Water Drain Valves

Not Open As Required By Tag Out

These DRs covered the period July 6 through August 9, 1995.

Each

DR addressed personnel errors by the operations staff. The

inspectors determined that on an individual basis these items did

not constitute a significant safety concern but that they

indicated a negative trend in operator performance and inattention

to detail by the operating crews.

The inspectors discussed these

items with station management and the operations superintendent.

The inspectors determined that the licensee was aware of the trend

and has taken actions to improve performance in this area.

The

actions included briefing all operations personnel on the

particular events and issuance of a station alert policy change.

The inspectors will continue to review this area and will review

operator performance during the upcoming Unit 1 refueling outage

to determine if corrective actions are effective in reversing the

negative trend in operator performance indicated by the above DRs .

Within the areas inspected, no violations or deviations were identified.,

7

4.

Maintenance and Surveillance Inspections (62703, 61726)

During the reporting period, the inspectors reviewed the following

maintenance and surveillance activities to assure compliance with the

appropriate procedures and TS requirements.

4.1

Troubleshooting and Restoration of Failed Unit 1 Control Room

Annunciators

The inspectors observed corrective maintenance ac.t i vi ti es

associated with WO 00324601, Troubleshoot/Repair Annunciator Power

Supplies (see paragraph 3.2). Initial troubleshooting efforts

conducted on August 23 by Virginia Power maintenance personnel,

determined that 4 of the 8 operable power supplies for annunciator

panels A-E were inoperable (1 additional power supply was

previously inoperable prior to the maintenance activity). The

licensee removed the 4 inoperable power supplies from service and

returned annunciator panel E {The First Out Panel) and

approximately 56 other alarms located on panels A-D to service

based on the number of operable power supplies. Subsequent to

returning the selected alarms to service all the operable

annunciators alarmed and then cleared without operator action. A

subsequent alarm test conducted by operations personnel determined

that the annunciators would not alarm and the annunciators on

panels A-E were declared totally inoperable at 7:58 pm on August

23.

On August 24, a vendor representative arrived on site to assist in

the troubleshooting efforts and repair of the power supplies.

The

troubleshooting activities conducted determined that all the power

supplies were degraded/inoperable and also found that the A-E

annunciator panel flashing card was bad.

As a result of this

determination the licensee replaced 3 of the failed power supplies

with new power supplies, the vender repaired the remaining power

supplies onsite (except for the previously inoperable power

supply), and the annunciator flashing card was replaced with a new

card. Annunciator panels A-E and 8 power supplies were returned

to service on August 25.

Power supply voltage readings were

monitored hourly for the 24-hour period following their return to

service to ensure proper operation.

The licensee plans to replace

the remaining inoperable power supply during the upcoming Unit 1

refueling outage.

The licensee is presently performing a Root

Cause Evaluation to determine why the power supplies failed.

The

inspectors will review the root cause determination when

completed.

The inspectors observed maintenance activities conducted in the

field and held discussions with the system engineer and vendor.

The activities observed were conducted appropriately and in

accordance with guidance provided by the work document.

8

4.2

Unit 2 Core Power Uprate

4.3

The Unit 2 core power uprate was performed August 24-31, 1995.

Numerous instrument control and protective setpoints were revised

to correspond to the uprated condition.

The inspectors closely

observed several maintenance activities during which the following

procedures were used:

-

2-IPT-CC-RC-T-412, Delta T and Tavg Loop T-412 Channel

Calibration, revision 14.

-

2-IPT-CC-RC-T-422, Delta T and Tavg Loop T-422 Channel

Calibration, revision 10.

-

2-IPT-CC-RC-T-432, Delta T and Tavg Loop T-432 Channel

Calibration, revision 11.

-

2-IPM-AMS-PNL-002, AMSAC Calibration, revision 4.

-

2-IPM-AMS-PNL-001, AMSAC Functional Test, revision 2.

-

2-IPT-CC-MS-P-446, Turbine Load Loop P-2446 Channel

Calibration, revision 1.

-

2-IPT-CC-MS-P-447, Turbine Load Loop P-2447 Channel

Calibration, revision 1.

Instrumentation technicians demonstrated strong procedural

knowledge and understood why each was being performed.

Communications between the control room and instrumentation rack

test locations were clear. Test equipment used for each procedure

was within specified calibration periodicity and in good working

condition. Technicians performed the maintenance successfully,

and closely followed procedures.

During 2-IPM-AMS-PNL-001, the SG B level

~ Channel II trip and

reset voltages were inconsistent. Technicians repeated the

applicable procedure steps and confirmed that the trip response

was unacceptable. Technicians halted the procedure, informed

management, and met with corporate engineers to further evaluate

the failure.

The licensee concluded that.an analog input module

had failed.

The inspectors observed module replacement and

recalibration. A corporate engineer closely supported the

technicians during these activities and noted that the calibration

procedure specified incorrect PLC monitor register points. After

a procedure revision, AMSAC calibration and functional testing

were successfully completed.

The inspectors concluded that this

maintenance activity was performed in a quality and timely manner.

Test Equipment Unavailable for Maintenance

The inspectors noted two instances during which properly

functioning test equipment was not available for technicians to

complete planned maintenance on safety-related equipment.

Technicians were not able to return charging pump 2-CH-P-lC to

service on August 17 because neither of the two pressure

calibration instruments functioned properly.

One instrument had a

damaged internal component and the second instrument was not

9

sufficiently charged.

Management had directed that 2-CH-P-IC be

restored early from planned maintenance due to an impending ..

hurricane.

The charging pump remained out of service until August

19.

On August 21, technicians were unable to begin corrective

maintenance, an equalizing charge, on station battery IA because a

calibrated DC ammeter was not available.

Each case prolonged the

period during which safety-related equipment was either

unavailable or in a degraded condition.

The Maintenance

Superintendent informed inspectors that tighter controls were

temporarily placed upon calibration equipment while previously

identified programmatic problems were corrected.

The Maintenance

Superintendent expected the actions to be complete in the near

future and improve calibration equipment availability by the

beginning of the Unit 1 refueling outage in September 1995.

The

inspectors considered unavailability of test equipment for

maintenance to be a weakness.

4.4

Online Maintenance

During the inspection period the inspectors reviewed*the safety

related online maintenance activities conducted on Unit 1 for the

period August 1 through September 1.

The most significant online

maintenance activity was conducted on the #1 EDG.

This activity

was scheduled to be completed within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> and maintenance

crews were scheduled to support the maintenance activities on all

three shifts. However, problems were encountered and the diesel

was out of service for approximately 128 hours0.00148 days <br />0.0356 hours <br />2.116402e-4 weeks <br />4.8704e-5 months <br />.

During the period

reviewed, 11 online maintenance activities were scheduled that

required entry into TS LCOs on Unit 1.

The vast majority of the

maintenance items were scheduled to remove the equipment from.

service for less than a shift and in all cases the maintenance

window scheduled did not exceed 50% of the allowed LCO time.

The

inspectors noted that online maintenance activiti~s appeared to

increase prior to the Unit 1 shutdown for refueling.

The inspectors determined that online maintenance activities are

routinely conducted by the licensee and that the licensee has

established guidance on the conduct of online maintenance.

If the

outage time will exceed 50% of the allowed LCO, additional

management approval is required prior to scheduling the

maintenance activity.

The inspectors also determined that the licensee is in the process

of implementing a maintenance rule pilot program.

This program

establishes performance and monitoring criteria for plant systems,

structures, and components based on their risk significance and

importance to safety. The program establishes out-of-service

criteria based on a twelve month rolling average and a report is

presently issued monthly.

The licensee plans to fully implement

the program by July 10, 1996.

The inspectors will continue to

monitor licensee activities in this area. *

10

4.5

Emergency Service Water Pump Testing

On August 31, the inspectors observed operators perform procedure

O-OPT-SW-002, Emergency Service Water Pump 1-SW-P-lB, revision 5.

The procedure provides instructions for operability testing the lB

emergency service water pump.

During procedure performance, the

pump did not develop sufficient flow to meet the acceptance

criteria contained in the procedure.

To investigate the low flow

condition, a work order was initiated to inspect/clean the flow

element annubar.

The annubar was inspected and no obvious

obstructions or clogging were observed.

However, any obstruction

could have been removed when the pump was secured due to backflow

or when the annubar was removed from the system.

The test was

reperformed and indicated pump flow increased by 1000 gpm.

Based

on the increased flow indication, the pump met the acceptance

criteria contained in the procedure and the pump was declared

operable.

The inspectors determined ihat the test was performed

in accordance with the controlling procedure and that the actions

taken to resolve the indicated low flow conditi-0n were adequate to

resolve pump operability concerns.

Within the areas inspected*, no violations or deviations were identified.

5.

On-Site Engineering Review (37551)

5.1

Component Cooling Water Heat Exchanger Marine Fouling

Heavy rains and excessive ambient temperatures during the June and

July timeframes created conditions for significant CC HX marine

fouling.

The inspectors observed maintenance activities, revtewed

maintenance records, and discussed CC HX performance with system

engineers to determine wheth~r the licensee had established

appropriate controls to ensure adequate CC HX operability.

Surveillance procedures are performed weekly on each CC HX to

measure and assess macrofouling blockage.

In late June and early

July, significant hydroid and seaweed blockage was identified.

Each CC HX was determined to be inoperable between one and four

times during a two week period. Engineers noted that the A & CCC

HXs were the most frequently effected due to system configuration.

The inspectors verified that each time a CC HX was identified as

degraded (Alert Condition) or inoperable, the CC HX was promptly

cleaneq, tested, and returned to service.

The number of operable

CC HXs satisfied TS requirements.

The inspectors questioned whether surveillance and cleaning

intervals were adequate to identify and correct CC HX degradation.

The Shift Operations Supervisor informed the.inspectors that the

surveillance frequency would be increased as necessary to improve

reliability.

For two weeks, the A & CCC HXs were tested every

two days.

By mid-July a reliable data trend was observed and the

l

11

weekly test interval was reestablished.

In addition, a PM

schedule item was established to clean the A & CCC HX weekly

until performance improved significantly. The inspectors

determined that these actions were appropriate.

In early 1995, system engineers developed a trending data base to

assess CC HX performance. This analysis helped differentiate

between CC HX tube microfouling and CC HX tube~heet macrofouling.

This tracking provided useful insight to assist maintenance

technicians in determining whether tube scraping and/or tubesheet

cleaning was appropriate.

The inspectors noted, however, that the

engineering assessment of the trend data was not fully effective

in maintaining CC HX availability.

No increased surveillance or

cleaning intervals were recommended when the_C CC HX failed two

consecutive weekly surveillances in June.

The CCC HX also failed

a third consecutive surveillance prior to establishing the

increased monitoring and cleaning schedule.

Engineers informed the inspectors that bromine injection to the B

CC HX had proven effective in reducing marine fouling over a test

period.

In July the licensee began bromine injection to all four

CC HXs.

CC HX performance has been good during this inspection

period.

The inspectors concluded that the bromine injection

modification was a positive action to improve CC HX performance.

5.2

Emergency Service Water Pump Marine Fouling

Based on marine fouling problems identified earlier in the summer,

a three week preventive maintenance interval was established to

clean the lA & lC ESW pump suction bells. The lB ESW pump suction

bell was previously coated with an antifouling material.

On

August 22, ESW pump lC failed its monthly performance test due to

low flow.

This was unanticipated due to the increased cleaning

interval in effect. Operators declared the pump inoperable and

entered a seven day LCO in accordance with TS 3.14.B.

ESW pump lC

was cleaned, retested, and restored to service on August 23.

Divers found a three-inch hydroid growth on the pump endbell which

is not typically sufficient to cause the flow degradation which

was observed.

Based upon the three week cleaning interval and

periodic performance trending, engineers proposed that the annubar

flow instrument may have been fouled, thereby indicating lower

than actual flow.

Management directed that ESW pump lA be tested

immediately to verify pump operability. The inspectors determined

this action was appropriate since marine fouling is a potential

common mode failure mechanism for ESW pumps.

On August 23, ESW pump lA failed its performance test due to low

flow.

The pump suction bell and flow instrument were cleaned, the

pump successfully retested, and returned to service on August 24.

The inspectors questioned whether common mode failure had made two

ESW pumps inoperable at the same time.

Engineering evaluation ET,

CME 95-0070, revision O concluded that although the pumps had

12

failed the ISI test criteria, available ESW flow was sufficient to

meet design accident analysis. The inspectors reviewed ErtME 95-

0070 and determined that the licensee's evaluation was technically

sound.

Licensing personnel initiated a review to assess 10 CFR

50.72 reporting applicability.

Engineers recommended that the pump endbell cleaning frequency be

further increased to every two weeks for the July - September

period.

Long term recommendations included applying an

antifouling coating on the IA & IC ESW pump suction bells,

revising test procedures, and conducting an engineering study to

evaluate potential flow instrument modifications.

The inspectors

concluded that the engineering recommendations were technically

sound.

The recommendations were under management review at the

close nf the inspection period.

Within the areas inspected, no violations or deviations were identified.

6.

Plant Support (71707, 71750)

The inspectors conducted facility tours, work activity observations,

personnel interviews, and documentation reviews to determine whether

licensee programs met regulatory requirements in the areas of

radiological protection, security, and fire protection. Radiological

areas were properly posted. A large number of scaffolds were erected in

preparation for the upcoming Unit 1 refueling outage.

Workers used

appropriate care when erecting scaffolding near equipment which could

cause a plant trip. Security force members ensured proper visitor

escort practices during site family visit tours in late August.

During backshift tours the inspectors noted that a vital area door,

which was also a fire barrier and controlled area pressure boundary, did

not reliably close.

The inspectors found the door closed and latched,

but the door failed to return to the closed position following entry

into the vital area. Security personnel had identified the degraded-

condition three days earlier and initiated corrective action which

addressed the door's security function.

The inspectors determined that

the corrective actions did not fully address the door's degraded

condition and that station operations personnel were not aware of the

degraded fire and pressure boundary door.

The inspectors informed the

SS of the degraded door.

The SS initiated prompt corrective action

which restored the door's operability. The inspectors questioned why

security had not informed the operations staff of the degraded door.

The Security Operations supervisor subsequently issued a memo to

security personnel which adequately clarified management's expectation

that security inform the operations SS whenever a vital door, fire

barrier, or pressure boundary door becomes degraded.

Within the areas inspected, no violations or deviations were identified.

~---------- ---


---

7.

13

Action on Previous Inspection Items (92901)

7.1

(Closed) VIO 50-280/94-08-01, Failure To Open The Unit .I 8 Loop

Hot Leg Stop Valve Within 2 Hours

On March 1, 1994, Unit 1 RCS loop 8 was filled in accordance with

procedure l-OP-RC-002, RCS Fill, revision 3, and the loop was

declared full at 8:40 am.

The loop 8 hot leg stop valve was

opened at 10:50 am.

TS 3.17.5.c required that the loop 8 hot leg

stop valve be opened within 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> after filling the loop.

Failure to open the loop 8 hot leg within 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> as required by

TS was identified as a violation.

This item was also addressed in LER 50-280/94-04 and corrective

actions included revising procedures l/2-0P-RC-002, Reactor

CooJant System Fill, counseling of the personnel involved in the

event, and inclusion of the LER in the required reading program.

The inspectors reviewed the correcti~e actions and verified that

procedures l/2-0P-RC-002 had been revised to provide adequate

guidance for the control of the evolution.

7.2

(Closed) VIO 50-281/94-17-0l, Failure To Close Unit 2 Makeup Water

Isolation Valve Within 15 Minutes After Makeup

7.3

On June 17, 1994, following a makeup evolution to the RCS, the

primary water isolation valve was not secured closed within 15

minutes following the makeup evolution as required by TS 3.2.f.

The valve was left open for a period of 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> and 8 minutes

following the makeup evolution.

This item was also addressed in LER 50-281/94-03 and the

licensee's immediate corrective actions were discussed in

inspection report 50-280, 281/94-17.

Long term corrective actions

included establishing procedural controls to ensure that the

isolation valve will be secured within 15 minutes and the LCD

clock tracked upon completion of makeup activities. Training

Functional Implementation Guideline 15 was also revised to provide

clearer guidance for control of RO/SRO license class inplant

periods.

The inspectors verified that the above actions had been

completed and reviewed the procedure revisions establishing the

procedural controls..

(Closed)

VIO 50-280,281/93-26-03, Failure To Design The ESW Pump

House Doors' Seal Plates Watertight

.

-

This item identified that measures were not established to assure

that the ESW pump house removable seal plates would be watertight

if installed. Corrective actions included performing_ an

engineering evaluation to determine if the seal plates were

required to be watertight, revision of the UFSAR to.document that

the seal plates were not required to be watertight, and revising

the procedure for abnormal weather conditions to reference a

14

maintenance procedure that was implemented to provide the

necessary instructions to ensure that the seal plate installation

restricts inleakage to acceptable limits. The inspectors verified

that the above actions had been completed.

The inspectors also

verified that the seal plate installation was accomplished per the

maintenance procedure during the preparations for hurricane Felix.

Within the areas inspected, no violations or deviations were identified.

8.

Exit Interview

The inspection scope and findings were summarized on September 6, with

those persons indicated in paragraph 1.

The inspectors described the

areas inspected and discussed in detail the inspection results addressed

in the Summary section and those listed below.

Item Number

VIO 50-280/94-08-01

Status

Closed

Description/(Paragraph No.)

Failure To Open The Unit 1 B

Loop Hot Leg Stop Valve Within

2 Hours (paragraph 7.1).

VIO 50-281/94-17-01

Closed

Failure To Close Unit 2 Makeup

Water Isolation Valve Within

15 Minutes After Makeup

(paragraph 7.2).

VIO 50-280,281/93-26-03

Closed

Failure To Design The ESW Pump

House Doors' Seal Plates

Watertight (paragraph 7.3).

Proprietary information is not contained in this report. Dissenting

comments were not received from the licensee.

9.

Index of Acronyms

AFW

AMSAC

AP

cc

CFR

cw

DR

ECCS

EDG

ESW

GPM

HX

ISi

JCO

LCO

AUXILIARY FEEDWATER

ANTICIPATED TRANSIENT WITHOUT SCRAM MITIGATION SYSTEM

ACTUATION CIRCUIT

ABNORMAL OPERATIONS PROCEDURE

COMPONENT COOLING

CODE OF FEDERAL REGULATIONS

CIRCULATING WATER

DEVIATION REPORT

EMERGENCY CORE COOLING SYSTEM

EMERGENCY DIESEL GENERATOR

EMERGENCY SERVICE WATER

GALLONS PER MINUTE

HEAT EXCHANGER

INSERVICE INSPECTION

JUSTIFICATION FOR CONTINUED OPERATION

LIMITING CONDITIONS OF OPERATION

15

LER

LICENSEE EVENT REPORT

MSL

MEAN SEA LEVEL

MW

MEGAWATTS

NOUE

NOTIFICATION OF UNUSUAL EVENT

NRC

NUCLEAR REGULATORY COMMISSION

OC

OPERATIONS CHECKLIST

PLC

PROGRAMMABLE LOGIC CONTROLLER

PM

PREVENTIVE MAINTENANCE

PPM

PARTS PER MILLION

RCS

REACTOR COOLANT SYSTEM

RO

REACTOR OPERATOR

SE

SAFETY EVALUATION

SG

STEAM GENERATOR

SI

SAFETY INJECTION

SNS

STATION NUCLEAR SAFETY

SNSOC

STATION NUCLEAR SAFETY AND OPERATING COMMITTEE

SRO

SENIOR REACTOR OPERATOR

SS

SHIFT SUPERVISOR

TMI

THREE MILE ISLAND

TS

TECHNICAL SPECIFICATION

TSC

TECHNICAL SUPPORT CENTER

UFSAR

UPDATED FINAL SAFETY ANALYSIS REPORT

VIO

VIOLATION

WO

WORK ORDER