ML18152A250

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Insp Repts 50-280/93-24 & 50-281/93-24 on 931003-1106.No Violations Noted.Major Areas Inspected:Plant Status, Operational Safety Verification,Maintenance & Surveillance Insp,Previous Insp Items & Emergency Response Training
ML18152A250
Person / Time
Site: Surry  Dominion icon.png
Issue date: 11/30/1993
From: Belisle G, Branch M, Tingen S, York J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18152A251 List:
References
50-280-93-24, 50-281-93-24, NUDOCS 9312140051
Download: ML18152A250 (19)


See also: IR 05000280/1993024

Text

4,

I

.

Report Nos. :

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W., SUITE 2900

ATLANTA, GEORGIA 30323-0199

50-280/93-24 and 50-281/93-24

Licensee: Virginia Electric and Power Company

5000 Dominion Boulevard

Glen Allen, VA

23060

Docket Nos.:

50-280 and 50-281

License Nos.:

DPR-32 and DPR-37

Facility Name:

Surry 1 and 2

Inspection Conducted: October 3 through November 6, 1993

Inspectors:

Inspector

J~ ~ort!R7menf'I~or

Approved by:

SUMMARY

Scope:

1/*Jtr f'3

Date Signed

1/-..Jer-f~

Date Signe

/l-~-13

Date Signed

This routine resident inspection was conducted on site in the areas of plant

status, operational safety verification, maintenance inspections, surveillance

inspections, balance of plant inspection, action on previous inspection items,

emergency response training for off-site support groups and engineered safety

feature system walkdown.

While performing this inspection, the resident

inspectors conducted reviews of the licensee's backshifts, holiday or weekend

operations on October 12, 21, 26, 30, 31 and November 1, 2, and 3, 1993.

. . .

2

Results:

In the Operations area, the following items were noted:

Measures implemented to compensate for reactor coolant system leaking

into the Unit I B safety injection accumulator did not prevent the boron

concentration in the accumulator from decreasing below the Technical

Specification (TS) minimum requirements on two occasions (paragraph

3.e).

The initial Station Nuclear Safety and Operating Committee screening of

the deviation report documenting that boron concentration in the Unit I

B safety injection accumulator was below TS minimum requirements

categorized the event as not reportable. After additional engineering

review, the event was considered reportable. A licensee event report

will be written (paragraph 3.e).

Although the licensee had recently completed a component relabeling

program, seven components in the Unit I and 2 charging pump service

water support systems were not labeled with the new label plates

(paragraph 9).

In the Maintenance/Surveillance area, the following items were noted:

During the period, two Unit I rod control system problems occurred that

resulted in rod control system urgent failure alarms (paragraphs 3.a and

4.c).

During summer months, recurring operational problems with the 555-ton

mechanical chiller condensers continued to cause entry into TS action

statements for containment partial pressure. This challenged operators

unnecessarily (paragraph 3.f).

The licensee's temporary leak sealant program was identified as a

strength (paragraph 4.a).

During the previous Unit 2 refueling outage, a new type of packing was

installed in the auxiliary feed water pumps that required special

installation and run-in instructions. The packing was installed

correctly but the process could have been done more efficiently

(paragraph 4.e).

The use of the motor operated valve diagnostic equipment for

troubleshooting the reactor trip bypass breaker was innovative, provided

the licensee with additional diagnostic information, and was considered

a strength (paragraph 4.b).

During reactor protection system logic testing, the inspectors observed

good communication between all parties, as well as, good self checking

techniques by the personnel manipulating the test switches. This was

considered extremely important since the procedure directed

approximately 500 various switch operations (paragraph 5).

,.

',

3

In the Engineering/Technical Support area, the following item was identified:

The licensee's ability to utilize advanced metallurgical analysis

techniques for failure analysis cases, such as the cast aluminum-bronze

service water valves, was a continuing strength (paragraph 3.b).

In the Plant Support area, the following item was noted:

The licensee was proactive in working with the state and local

governments in resolving Federal Emergency Management Agency emergency

exercise items (paragraph 8).

  • REPORT DETAILS

1.

Persons Contacted

Licensee Employees

W. Benthall, Supervisor, Licensing

  • R. Bilyeu, Licensing Engineer
  • H. Blake, Jr., Superintendent of Nuclear Site Services
  • R. Blount, Superintendent of Maintenance

D. Christian, Assistant Station Manager

J. Costello, Station Coordinator, Emergency Preparedness

  • J. Downs, Superintendent of Outage and Planning
  • D. Erickson, Superintendent of Radiation Protection

A. Friedman, Superintendent of Nuclear Training

B. Hargrave, Nuclear Materials

  • M. Kansler, Station Manager
  • C. Luffman, Superintendent, Security
  • J. McCarthy, Assistant Station Manager (Acting)
  • A. Price, Assistant Station Manager
  • K. Sloane, Superintendent of Operations (Acting)
  • M. Small, Senior Reactor Operator
  • E. Smith, Site Quality Assurance Manager
  • D. Souza, Senior Reactor Operator
  • T. Sowers, Superintendent of Engineering

J. Swientoniewski, Supervisor, Station Nuclear Safety

NRC Personnel

  • M. Branch, Senior Resident Inspector
  • S. Tingen, Resident Inspector
  • J. York, Resident Inspector
  • Attended Exit Interview

Other licensee employees contacted included control room operators,

shift technical advisors, shift supervisors and other plant personnel.

Acronyms and initialisms used throughout this report are listed in the

last paragraph.

2.

Plant Status

Unit 1 operated at full power for the majority of this inspection

period.

On November 4, the unit began a power coast down.

At the end

of the inspection period the unit was at 98% power.

Unit 2 operated at approximately 98% power throughout the period in

order to minimize level oscillation in the C SG .

j

3.

2

Operational Safety Verification (71707, 42700)

The inspectors conducted frequent tours of the control room to verify

proper staffing, operator attentiveness and adherence to approved

procedures.

The inspectors attended plant status meetings and reviewed

operator logs on a daily basis to verify operational safety and

compliance with TSs and to maintain overall facility operational

awareness.

Instrumentation and ECCS lineups were periodically reviewed

from control room indications to assess operability.

Frequent plant

tours were conducted to observe equipment status, fire protection

programs, radiological work practices, plant security programs and

housekeeping.

Deviation reports were reviewed to assure that potential

safety concerns were properly addressed and reported.

a.

Unit I Control Rod Drive System Urgent Failure Alarms

At 6:24 a.m., on October 13, a Unit 1 rod control system urgent

failure alarm was received.

By design, an urgent failure locks up

the rod control system and prevents normal rod motion.

It does

not prevent rods from tripping into the core if a protective

actuation was initiated. A two hour TS action statement to clear

the alarm was entered in accordance with TS 3.12.C.3. At 8:24

a.m., the two hour action statement was exited and a six hour

action statement to HSD was entered.

The rod control internal

alarm was reset and the urgent failure alarm cleared.

The cause

for the urgent failure alarm was not determined.

Procedure

l-PT-6, Control Rod Assembly Partial Movement, was satisfactorily

performed and the six hour action statement was exited.

On October 21, another rod control system urgent failure alarm

occurred in Unit I. This event is discussed in paragraph 3.d and

4.c.

b.

Through-Wall Leaks in SW Valve Bodies

On October 12, the licensee documented a deficient condition on DR

S-93-1350 which involved several valves in the SW system used for

charging pump lube oil and seal cooling.

The DR described a

condition where SW was seeping through what appeared to be

porosity in the cast valve bodies.

Eleven valves from each unit

exhibited some degree of corrosion attack, from weepage to visual

corrosion products present on the outside of the valves.

The portion of the SW system with the leaking valves provided

cooling water to the charging pump lubricating oil and seal cooler

heat exchanger.

These leaking Jamesbury ball valves provided

maintenance isolation capability. This low pressure system

(approximately 45 psi) normally flows approximately 50 gpm and

varies on a seasonal basis.

The flow velocity is sometimes as low

as two to three feet per second.

Flow below approximately five

feet per second lends the system to the potential to fouling which

can promote the formation of MIC nodules.

3

The SW valves in question are cast aluminum-bronze, alloy C 95400.

After discovering the problem, the licensee replaced several

valves that exhibited through-wall leakage. Originally, this

system was constructed of plastic components.

In 1986 because of

Appendix R considerations, the components were changed to

aluminum-bronze.

The valves that were removed were taken to the site metallurgical

laboratory for determining the failure mechanism. A chemical

analysis of one of the cast valves showed that the chemical

composition requirements in ASTM B 148, Standard Specification for

Aluminum-Bronze Sand Castings, were met.

Cross sections of leaking areas {under MIC nodules) revealed that

the aluminum rich phases had been leached out leaving a porous

structure through which the weeping/leaking occurred. Also, this

examination showed that the through-wall dealloying did not exceed

25 percent of the circumference for any given cross section.

Corrosion product analysis on the outside of the valves showed a

large percentage of aluminum thus confirming the dealloying

process.

Some sections from the first valve removed were used to perform

tensile tests. Samples were taken from the unaffected, as well

as, the dealloyed sections of the cast material. The visual and

metallographic evaluations, along with the tensile tests results,

were used as the basis for the licensee's evaluation that the

valves would maintain their structural integrity in the identified

degraded condition until they could be replaced.

Discussions between the licensee and the NRC concluded that the

licensee needed to request relief from the ASME Section XI Code in

order to continue to operate without immediate repair of the

defects. This determination was consistent with the guidance

contained in GL 91-18 and 90-05.

The licensee indicated that they

disagreed with the NRC's interpretation on addressing operational

leakage under the ASME Code.

However, after determining

structural integrity of the valves in question, the licensee

indicated that they would comply with the NRC's interpretation for

this case and on November 2, a relief request was submitted for

NRC's review.

The licensee indicated that they plan to address

this issue further and have requested a meeting with the NRC to

present their position.

The inspectors are following the licensee's actions to evaluate

the root cause of the material failure, the reportability of the

issue, and replacement of the defected valves. At the end of the

inspection period, the licensee had replaced some of the SW valves

that were subject to through-wall leakage and were developing

plans for replacing the remaining valves.

The licensee's ability

to utilize advanced metallurgical analysis techniques for failure

4

analysis cases, such as the cast aluminum-bronze service water

valves, is a continuing strength.

c.

Unit 2 C SG Special Test

Since Unit 2 startup in May of 1993, the C SG has experienced

level oscillation whenever attempts were made to increase reactor

power to 100%.

Consequently, the unit operated at a reduced power

of approximately 98%.

The licensee's original investigation

centered around FW flow control. Gain adjustments were made to

the C FWRV in an attempt to dampen the SG level oscillations. The

adjustments to the FWRV controls did slow down the valve's

response to level oscillations; however, it was unsuccessful in

resolving the level oscillations to a point that power could be

increased back to 100%.

The licensee contracted a failure analysis expert in an attempt to

find other possible causes for the level oscillations.

Additionally, the licensee held discussions with their NSSS and SG

supplier to determine if other plants had experienced this type of

SG level phenomenon.

There were several possible causes discussed

which refocused the licensee's attentions to possible mechanical

or thermodynamic changes internal to the SG.

The possible

internal causes included damage to the feedwater "J-Tube", or

sludge buildup in the upper tube support region of the SGi

During a forced shutdown in August 1993, the licensee performed a

limited visual inspection of the internals of the C SG through

restrictive openings and no obvious defects were identified.

The inspectors reviewed the safety evaluation {93-196) that

supported the special test {2-ST-306) and attended the pre-shift

operating crew briefing. The scope and precautions contained in

the test procedure were discussed in detail and questions were

directed to the test director who resolved them in an acceptable

manner.

The test entailed raising the C SG program level from the normal

44% to 49% and monitoring the SG for level oscillations, both at

the existing 98% reactor power and at 100% power.

The test

directed holding at this new SG level for 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> and then

raising the program level to 54% and monitoring the resultant

plant response for an additional 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br />.

At the 98% reactor power, the level oscillations in the C SG

appeared to have stabilized after the program level was increased

to 49%.

However, when reactor power was increased to 100%, the

maximum level {on the narrow range instrumentation) oscillation of

+/- 20% magnitude was experienced.

The operators stabilized the

SG level in accordance with the precautions of the special test

procedure and the test was suspended at the direction of the SS

and test director. After reviewing the test results, plant

management directed that the.C SG level setpoint be returned to

d.

e.

5

the 44% value and that reactor power be controlled to minimize

level oscillations.

The C SG level setpoints were returned to the 44% value and

reactor power was lowered to 98%, and level oscillation was

reduced to the pre-test value.

The inspectors continued to

monitor the licensee's corrective actions in this area and will

review any C SG planned outage related activities.

Notice of Enforcement Discretion

On October 21, the NRC granted Enforcement Discretion to TS 3.12.C.3 for Unit 1 only.

On October 21, the Unit 1 Bank D

control rod assemblies became inoperable when a rod control system

urgent failure alarm occurred when operators were performing l-PT-

6, Control Rod Assembly Partial Movement.

TS 3.12.C.3 requires

that inoperable control rod assemblies be restored to operable

status within 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> or that the plant be put into a hot shutdown

condition within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />.

The discretion permitted

continued operation of Surry Unit 1 in Power Operation for a

period of 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> versus the 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> specified in TS 3.12.C.3.

This additional time was projected to allow troubleshooting and

possible repairs to the Control Rod Drive System.

Although the

Bank D control rod assemblies were immovable on demand from the

Control Rod Drive System, the ability of the control rod

assemblies to perform their intended safety function (trip into

the core) when a safety system setting was reached was not

effected. A blown fuse was identified as the cause of the rod

control system urgent failure alarm which resulted in the

immovable Bank D control rod assemblies.

The fuse was replaced

and the control rods were satisfactorily tested in accordance with

l-PT-6.

The Control Rod Drive System was returned to operable

status approximately one hour after the Notice of Enforcement

Discretion as verbally approved by the NRC.

Since rod control system failures appear to be a continuing

problem, the NRC requested the licensee discuss their assessment

of previous failures with NRC management.

The inspectors continue

to monitor the licensee's rod control system reliability

improvement activities and are currently reviewing the RCM study

of that system and the status of implementing any recommended

corrective actions.

Unit 1 B Accumulator In-Leakage

On October 9 and 15, 1993, sample analyses from the Unit 1 B

accumulator revealed that the boron concentration was less than

the minimum required by TS.

It was suspected that back leakage

from the RCS through the accumulator check valves diluted the

boron concentration in the accumulator.

TS 3.3.B states that any

one of the following SI components may be inoperable at any one

time and that if the condition is not restored within the allowed

6

time period then the unit must be placed in hot shutdown within 6

hours.

TS 3.3.B.l states that one accumulator may be isolated for

a period not to exceed 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />.

On both occasions when the boron concentration was out of

tolerance, the licensee declared the B accumulator inoperable in

accordance with TSs 3.3.B and 3.3.B.l and entered a four hour

action statement to restore the accumulator to an operable status.

On both occasions, the boron concentration was restored within

four hours.

The accumulator was not isolated at any time during

these evolutions. The inspectors discussed the licensee's

interpretation of TS 3.3.B.l with the NRC staff and concluded that

the licensee correctly interpreted the TSs.

Although the boron

concentration was low, it was still significantly higher than RCS

boron concentration and could have discharged into the RCS if

needed.

This condition was more conservative than a condition

where the accumulator would have been isolated and not available.

SI accumulator levels are logged every shift. The inspectors

reviewed the logs for the B SI accumulator level from July 1

through November 1, 1993, and concluded that around September 1

levels began to increase due to leakage into the accumulator.

Prior to September 1, coolant was leaking out of the accumulator

and the accumulator had to be filled approximately every 10 days.

After September 1, small amounts of water were drained from the

accumulator to reduce level approximately every three to four

days.

The inspectors concluded that measures implemented to

compensate for leakage of reactor coolant into the Unit 1 B safety

injection accumulator did not prevent the boron concentration in

the accumulator from decreasing below the TS minimum requirements

on two occasions.

The inspectors also reviewed the licensee's reportability

determination for this event. VPAP-1501, Station Deviation

Reports, Revision 3, states that the SS makes the initial

reportability determination and this determination is reviewed by

the Superintendent of Operations, SNS supervisor, and SNSOC.

The

inspectors reviewed DR S-93-1372. This DR documented that on

October 15 the boron concentration in the Unit 1 B SI accumulator

was below the minimum TS requirements.

The inspectors noted that

this event was initially categorized as not reportable.

The

inspectors and other station personnel questioned if the boron

concentration was less than required by TSs for a period greater

than fours hours allowed by the licensee's TS interpretation

discussed above.

Engineering reviewed this event and concluded

that the boron concentration was less than required by TS for a

period greater than four hours.

The licensee subsequently

identified that this event was reportable by an LER .

At the end of the inspection period, the licensee was preparing an

LER and was evaluating corrective action to reduce leakage into

the Unit 1 B SI accumulator.

The licensee was also sampling the B

g.

7

accumulator every two. days to verify proper boron concentration.

The inspectors will review the licensee's LER on this issue to

determine if any additional actions are necessary.

f. Containment Partial Pressure Less Than 9.0 PSIA

TS Figure 3.8.1 requires that containment partial air pressure be

maintained greater than or equal to 9.0 psia.

TS 3.8.D.l.a

specifies that if containment partial air pressure is less than

9.0 psia then containment air partial pressure must be restored to

within acceptable limits within one hour or be in at least hot

shutdown within the next six hours.

The inspectors noted, and the licensee's trending programs

confirmed, that in the summer months a one-hour action statement

had been entered in accordance with TS 3.8.D.l.a on numerous

occasions in both units because indicated containment partial air

pressure fell below 9.0 psia.

In 1992 and 1993 there were at

least six and fourteen DRs, respectively, written to document that

a one hour action statement was entered because containment

partial air pressure was less that 9.0 psia.

Operational problems with the 555-ton mechanical chillers which

normally are used only during the summer months cause indicated

containment partial air pressure to decrease below 9.0 psia. The

licensee has appointed a task team and initiated a station Level I

action item to improve the operation of the 555-ton mechanical

chillers; however, operators have been routinely challenged to

restore containment partial *air pressure on a recurring basis

during the summer months.

The inspectors are continuing to follow

this issue.

Air Leak on EOG #1

During a backshift tour on November 2, the inspectors noted that

air was blowing by the seat of valve l-EG-18.

The valve is a

manual strainer blowdown valve on one of the two banks of EOG

starting air. The air accumulator pressure was normal and no low

pressure alarms were lit. The inspectors notified the SS and an

operator was dispatched to investigate.

The operator checked the

valve closed and then attempted to blow any trash from the seat by

cracking open the valve.

The low pressure alarm was actuated

during the blowdown and the operator reclosed the valve and

allowed the compressor to recover pressure above the alarm

setpoint. The blowdown reduced the leakage somewhat; however, the

valve continued to leak and WR 027327 was initiated to repair the

valve.

Within the areas inspected, no violations were identified .

j

4.

8

Maintenance Inspections (62703) (42700)

During the reporting period, the inspectors reviewed the following

maintenance activities to assure compliance with the appropriate

procedures.

a.

Inspection of Leak Sealant Practices

The site utilized contractors to repair leaks with temporary leak

sealant. Temporary leak sealant has been used to repair a variety

of leaks. The process involves drilling and tapping a valve

bonnet, flange, manway cover or packing gland, and installing

injection adapters.

An injection gun is utilized to inject leak

sealant into the adapter and the desired area.

In other

instances, a box is built around a leak and the box is injected

with leak sealant or sealant can be utilized to plug a valve that

has excessive seat leakage.

Temporary leak sealant can be

utilized on safety and non-safety systems; however, the use of

temporary sealant on safety systems is minimized.

Generally a

rubber based sealant is utilized on systems less than 460 degrees

F and a synthetic fiber based sealant utilized on systems up to

1000 degrees F.

Whenever a temporary leak sealant is utilized to

repair a leak, a WR is processed to restore the component back to

original specifications during the next scheduled outage of

sufficient duration.

Generic procedure O-MCM-1918-01, On-Line Leak Repairs, provides

guidelines for the temporary leak sealant of components in safety

and non-safety related systems.

This procedure was approved by

SNSOC and required that engineering approve using a temporary leak

sealant for repair. Engineering is extensively involved when a

temporary leak sealant is used.

Design Engineering is required to

evaluate stress, seismic calculations, the need for additional

supports, and design pressure when utilizing a temporary leak

sealant. System Engineering evaluates the impact of repair on

system operation, potential for blockage, and the affect of

intrusion of sealant into the system being injected.

Engineering

is also required to perform a safety evaluation screening for the

temporary repair in order to determine if the evolution is a

modification.

Engineering is required to specify any post

maintenance testing that may be required and evaluate if repair

meets ASME specifications. Generally the temporary leak sealant

contractor calculates the injection pressure and the amount of

sealant to inject. This calculation is reviewed by engineering.

Personnel cannot inject more sealant than specified for the job.

Normally injecting temporary sealant to repair a leak is

considered maintenance and not a modification.

Procedure O-MCM-

1918-01, Step 6.1.11, required that the SNSOC review and approve

each work package for the repair of a leak with a temporary leak

sealant when the leak is located inside containment with the unit

operating.

Work packages for injecting sealant into components

located outside of the containment did not require SNSOC review

9

and approval.

The QA department reviewed the work package prior

to performance and specified hold point requirements.

There have been no recent issues or problems due to the

inappropriate use of sealant for temporary leak repairs. The

inspectors were informed that in the 1970s and early 1980s there

was a issue associated with contaminates in the sealant which

contributed to bolting failures on the main steam trip valves and

main feedwater regulating valves which were resolved.

The

licensee's temporary sealant program was identified as a strength.

b.

Unit 1 B Reactor Trip Bypass Breaker Troubleshooting

C.

On October 15, while the licensee was performing l-PT-8.1, Reactor

Protection System Logic, for the B RPS train, the closed indicator

light for the B RTBB went out after the breaker was closed for

testing purposes.

The licensee's investigation identified that a

10 amp fuse in the circuit had blown.

The fuse was subsequently

replaced and it blew again after the breaker was closed.

The RTBB

was opened after the main RTB was verified closed and the licensee

initiated troubleshooting to determine the cause of the blown

fuse.

The RTBB is normally open and is used solely for testing

purposes and when closed its safety function is to open if a RPS

signal is received.

The inspectors witnessed some troubleshooting and subsequent

testing of the breaker after repairs. The troubleshooting had

indicated that the closing solenoid coil was drawing excessive

current because it was kept energized longer than designed.

The

licensee used test equipment normally used for MOV testing to

monitor and record the current being drawn by the closing coil.

Using this equipment allowed the licensee to determine that the

control (X) relay that deenergizes the closing coil solenoid was

not actuating as required.

The mechanical linkage (relay release

arm) between the closing coil solenoid push rod and the relay was

not properly adjusted.

The licensee replaced the closing coil

solenoid, the X relay, and adjusted the linkage prior to breaker

reinstallation and successful retesting.

The use of the MOV diagnostic equipment for troubleshooting the

RTBB was innovative and provided the licensee with additional

diagnostic information and was considered a strength.

Troubleshooting the Rod Control Syitem Urgent Failure Alarm

On October 21, the licensee, while performing a periodic test,

received a rod control system urgent failure alarm when moving

control D bank.

The failure was determined to be in the

01-RD-CAB-lBD power cabinet. The inspectors observed technicians

performing troubleshooting which included electrical measurements

in the affected cabinet.

From the readings taken, it was

suspected that the B phase fuse on the supply power lines to the

10

movable coil circuit was blown.

The licensee requested

enforcement discretion, which was discussed in paragraph 3.d, in

order to proceed with the fuse replacement and testing in an

orderly manner.

At the conclusion of the troubleshooting the

licensee processed a WO and the blown fuse was replaced.

Procedure IMP-C-EPCR-46, Maintenance of Rod Control System, dated

December 22, 1992 was used to control the work.

Periodic test

l-PT-6 was performed on the D control bank and the rod control

system was returned to service.

Good coordination between the two

maintenance groups was noted and no problems were identified by

the inspectors.

d.

Fuse Schedule Inspection

The inspectors reviewed l-DRP-002, Instrument Fuse Schedule,

Revision 5 and 2-DRP-015, Power Fuse Schedule, Revision 0.

The

purpose of these procedures is to provide a fuse control program

for the most critical fuses in the units.

When replacing a fuse

or when obtaining fuse reference data, these procedures are to be

used in lieu of electrical drawings.

If a fuse schedule does not

contain a specific fuse, then the information is obtained from an

electrical drawing or engineering.

Fuse schedules are generally not utilized when isolating

electrical components.

The locations of fuses required to be

removed for isolation are generally obtained from drawings and the

same fuses are reinstalled when returning the component/system

back to service. Through discussions with operators and

electricians the inspectors were informed that as a good working

practice, personnel routinely inspect fuses that are removed to

verify that the fuse specifications are the same as the

specifications on the drawing.

Any discrepancies are resolved.

During the EDSFA conducted by the licensee, the following concerns

were identified with the fuse schedules:

Not all fuses in the fuse schedules were analytically

verified against design basis.

The fuse schedules were not complete in that they did not

contain all critical plant fuses and in some instances did

not specify all fuse data for a specific fuse.

Electrical department personnel were not aware that the

power fuse schedule was an approved document.

There were inconsistencies between fuse schedules and ESK

drawings.

Training was provided to ensure personnel were knowledgeable of

the fuse schedules.

The remaining concerns have not been fully

J

11

resolved but are scheduled to be resolved during future EDSFA

followup inspections performed by the licensee.

e.

Unit 2 A Auxiliary Feed Pump Repack

On October 29, the inspectors witnessed the licensee repacking AFW

pump 2-FW-P-3A.

WO 274804 and procedure O-MCM-0131-01, General

Pump Packing, Revision 0, were utilized to accomplish this

maintenance.

The inspectors reviewed the work package at the job

site while the mechanics were repacking the pump.

The mechanics

received guidance from maintenance engineering personnel. After

maintenance was completed and the pump was returned to service,

the inspectors reviewed the work package a second time. During

the second review, the inspectors noted that the work package

contained additional instructions for repacking the pump and

running the new packing that were added after the pump was

repacked. The additional instructions were provided in an

Information Transmittal Record from maintenance engineering.

The inspectors questioned why these instructions were not on the

job site when the work was accomplished.

The inspectors were

informed that during the previous Unit 2 RFO a different type

packing was installed in the AFW pumps.

The new packing required

different installation and run in methods than the previous

packing.

The inspectors were informed that prior to repacking the

pump on October 29, maintenance personnel were briefed on the

installation and run in methods for the new packing and

maintenance engineering subsequently documented what was done in

the Information Transmittal Record.

The inspectors concluded that the packing was properly installed

in the A AFW pump; however, this maintenance would have been

accomplished more efficiently if mechanics or procedures

recognized the special instructions associated with the new type

of packing.

The need for an Information Transmittal Record

indicated that the work package/training provided for the

mechanics was lacking all the necessary information to accomplish

the maintenance and maintenance engineering support was required

to augment the work package.

Within the areas inspected, no violations were identified.

5.

Surveillance Inspections (61726, 42700}

During the reporting period, the inspectors reviewed surveillance

activities to assure compliance with the appropriate procedure and TS

requirements.

On October 15, the inspectors witnessed the licensee performing l-PT-8.1

for the B RPS train. This testing was being performed as additional

testing for the repairs of the B RTBB discussed in paragraph 4.b to

verify that the protective logic was not affected by the breaker

I

I

I

I

I

_.

12

repairs. The inspectors monitored activities at the test panel in the

protection racks.

Communications between the I&C technicians at the

RTBB, in the control room, and at the test panel were also monitored.

The inspectors observed good communication between all parties, as well

as, good self checking techniques by the personnel manipulating the test

switches.

The inspectors considered this to be extremely important

since the procedure directed approximately 500 various switch

operations.

Within the areas inspected, no violations were identified.

6.

Balance Of Plant Inspection (71500)

The inspectors conducted tours of portions of the TB and other plant

areas susceptible to flooding.

During these tours, the inspectors

verified the availability of the non-safety related TB sump pumps.

The

licensee relies on these pumps to mitigate certain flooding scenarios.

Additionally, the inspectors were sensitive to any work activities that

would increase -the possibility of TB flooding such as openings in the

condenser waterboxes or piping systems.

a.

Hole In Unit 2 D CW Discharge Piping

During the plant tour on October 13, the inspectors became aw~re

of a one-inch diameter hole in the 96-inch CW discharge piping

from the Unit 2 D waterbox.

This non-safety related piping was

designed to AWWA specification and it is isolable from the gravity

flow intake canal by closing the 96-inch safety-related waterbox

inlet MOV.

The condition of the waterbox discharge piping for all

four Unit 2 waterboxes was observed by the inspectors. There was

evidence of previous welded overlay plate repairs to several of

the pipes.

The area where the hole was discovered was rusted

through and crumbled further when probed by the inspectors.

Although no leakage was noted, the C waterbox discharge piping

appeared to be corroded in the area near the floor level where

standing water had previously accumulated.

The inspectors discussed the observed conditions with the system

engineer and reviewed the Surry IPE for sensitivity of a possible

failure of the 96-inch waterbox discharge piping.

The pipe in

question is not routinely inspected.

Five of the eight CW supply

pipes are currently being inspected as part of the licensee's SW

system inspection developed as part of GL 89-13, SW System

Problems Affecting Safety-Related Equipment.

The three CW supply

pipes currently not routinely inspected do not supply the SW

system and were not included in the program.

The inspectors' IPE finding review concluded that a catastrophic

failure of the outlet piping was not considered since the inlet

MOV should close and isolate the leak. The licensee's IPE

considered the condenser waterbox as the weak-link for an isolable

failure.

The IPE described the probability of the inlet MOV not

13

closing and when multiplied by the probability of a waterbox

failure, the results were within acceptable IPE values.

The

licensee's IPE personnel indicated that even with the observed

conditions of the discharge piping, the probability of a

catastrophic failure would still be bounded by the weak-link

analysis. They further stated that it would not be valid to

multiply the probability of a MOV failing to close times a

probability of 1 for the discharge piping failure.

The inspectors discussed the IPE issue with regional personnel and

concluded that the licensee's PRA evaluation of the impact of the

observed condition of the discharge piping was reasonable.

b.

Water Bubbling From Floor Near Unit 2 D CW Pipe

On October 26, DR S-93-1394 documented a condition where the

operators identified that water was bubbling up through a crack in

the floor near the Unit 2 D CW supply line to the condenser.

DR

S-93-1394 indicated that the water was sampled and determined to

be greater than 5000 ppm sodium {similar to raw river water). The

inspectors walked down the area. Water was bubbling from two

locations in a concrete expansion joint approximately two feet

from where the D CW supply line penetrated the floor.

The leakage

rate was difficult to estimate. It was estimated to be one gpm.

The inspectors were initially concerned because the sodium

concentration in the sample indicated that the water may have been

CW which also contains approximately 5000 ppm sodium.

Subsequent

samples indicated that the water was substantially less than 5000

ppm sodium.

The inspectors witnessed personnel collecting water

bubbling from the expansion joint and also observed chemistry

department personnel analyze the sample for sodium.

A Flame

Emission Spectrometer was used to analyze the sample.

The sample

results indicated that it contained 1020 ppm sodium.

The

inspectors also observed personnel analyze a sample of CW for

sodium concentration.

The results of the CW sample indicated that

it contained 5400 ppm sodium.

It was undetermined why the sodium

concentration in the first water obtained from the expansion joint

was higher than the samples obtained later.

Per the licensee, ground water samples obtained just outside of

the turbine building contained approximately 500 ppm sodium.

The

inspectors concluded the water bubbling through the turbine

building floor appeared to be a mixture of ground water and CW due

to the elevated concentration of sodium.

The source of the CW is

unknown.

The inspectors considered the possibility that the leakage was

from the underground D CW supply line which is ASME code class Ill

piping.

The inspectors reviewed CW piping drawing 11548-FC-2C and

verified that the 96-inch carbon steel CW piping beneath the

turbine building floor was enclosed in 18 inches of concrete.

The

14

drawing also depicted mechanical transition joints between the

concrete intake structure piping and the 96-inch steel inlet

piping which the licensee indicated could also be the source of

the leakage.

The inspectors were informed that previous

inspections of the interior of this piping have not revealed

through wall defects. At the end of the inspection period the

licensee was evaluating methods to determine the source of the

leakage.

Within the areas inspected, no violations were identified.

7.

Action on Previous Inspection Items (92701,92702)

(Closed) VIO 50-281/91-20-01, Interval Between Surveillance of Unit 2

Hot Channel Factors Exceeded TS Requirements.

TS 3.12.B.2 requires that

hot channel factors be determined every EFPM and TS 4.0.2 allows a 25%

tolerance. The Unit 2 hot channel factors were determined on July 18

and September 4, 1990. This violation was identified because the

interval between these hot channel factors was 1.44 EFPM which exceeded

the allowable 1.25 EFPM.

In a letter dated October 16, 1991, the

licensee responded to this violation. The licensee determined that the

cause of the violation was improper interpretation of TS grace period

tolerances and that administrative limits to clearly define allowed

grace period limitations were implemented as corrective action. The

inspectors reviewed VPAP-1102, Periodic Testing, Revision 0, and

verified that administrative limits for specifying TS grace period

limitations were clearly defined.

The inspectors also reviewed

procedures that performed hot channel factors for Units 1 and 2 during

1993 and verified that the hot channel factors were performed within the

specified TS intervals.

Within the areas inspected, no violations were identified.

8.

Emergency Preparedness Training For Off-Site Support Groups

Throughout 1993 Virginia Power has provided emergency preparedness

training for state and local government personnel.

On October 26, the

inspectors witnessed several traintng sessions where Virginia Power

personnel instructed personnel from Surry, Newport News, Isle of Wight,

Richmond, Hampton, Smithfield and Petersburg in the areas of

radiological contamination, personal dosimetry and exposure control.

Areas emphasized during these training sessions included training in

corrective actions for previously identified FEMA items.

The inspectors

concluded that the licensee was proactive in working with state and

local governments in resolving FEMA emergency exercise items.

Within the areas inspected, no violations were identified.

9.

ESF Walkdown (71710)

The inspectors walked down the Unit I and 2 charging pump/HHSI SW

support systems. These systems provide cooling water to each

15

charging/HHS! pump lube oil cooler and to the intermediate seal coolers.

Drawings 11448-FM-071B, Revision 30 and 11548, Revision 31, were

utilized for the system walkdown.

During the walkdown the inspectors noted that the following components

were missing the new style label plates:

Duplex strainers 2-SW-S-2A, l-SW-S-2A and l-SW-S-2B.

Valves 2-SW-438, 2-SW-170 and l-SW-271.

Check valve 2-SW-130.

The inspectors concluded that although the licensee had recently

completed a component relabeling program, seven components in the Unit 1

and 2 charging pump SW support systems were not labeled with the new

label plates. This issue was discussed with the licensee.

The remaining deficiencies noted during the walkdown were previously

identified by the licensee and were annotated with WR tags. The

inspectors also noted that there was through-wall weepage on some of the

valves in the system. This issue was discussed in paragraph 3.b.

Within the areas inspected, no violations were identified.

10.

Exit Interview

The inspection results were summarized on November 9, 1993, with those

individuals identified by an asterisk in Paragraph 1.

The inspectors

described the areas inspected and discussed in detail the inspection

results listed below and in the Results section. Dissenting comments

were not received from the licensee. Proprietary information is not

contained in this report.

Item Number

Description

(Paragraph No.)

VIO 50-281/91-20-01

Status

Closed

Interval Between Surveillance

of Unit 2 Hot Channel Factors

Exceeded TS Requirements

(paragraph 7).

  • 11.

Index of Acronyms and Initialisms

ASTM

-

AFW

AMP

ASME

-

AWWA -

BOP

cw

DR

ECCS -

EOG

AMERICAN SOCIETY FOR TESTING AND MATERIALS

AUXILIARY FEEDWATER

AMPERE

AMERICAN SOCIETY OF MECHANICAL ENGINEERS

AMERICAN WATER WORKS ASSOCIATION

BALANCE OF PLANT

CIRCULATING WATER

DEVIATION REPORT

EMERGENCY CORE COOLING SYSTEM

EMERGENCY DIESEL GENERATOR

EDSFA -

EFPM -

ESF

ESK

F

FEMA -

FW

FWRV -

GL

GPM

HHS! -

HSD

I&C

IPE

LER

MIC

MOV

NRC

NSSS -

PPM

PRA

PSI

PSIA -

PT

QA

RCM

RCS

RFO

RPS

RTB

RTBB -

SG

SI

SNS

SNSOC -

ss

SW

TB

TS

VIO

VPAP

WO

WR 16

ELECTRICAL DISTRIBUTION SYSTEM FUNCTIONAL ASSESSMENT

EFFECTIVE FULL POWER MONTH

ENGINEERED SAFETY FEATURE

ELECTRICAL SKETCH

FAHRENHEIT

FEDERAL EMERGENCY MANAGEMENT AGENCY

FEEDWATER

FEEDWATER REGULATING VALVE

GENERIC LETTER

GALLONS PER MINUTE

HIGH HEAD SAFETY INJECTION

HOT SHUTDOWN

INSTRUMENTATION AND CALIBRATION

INDEPENDENT PLANT EVALUATION

LICENSEE EVENT REPORT

MICROBIOLOGICAL INDUCED CORROSION

MOTOR OPERATED VALVE

NUCLEAR REGULATORY COMMISSION

NUCLEAR STEAM SUPPLY SYSTEM

PARTS PER MILLION

PROBABILISTIC RISK ASSESSMENT

POUNDS PER SQUARE INCH

POUNDS PER SQUARE INCH ABSOLUTE

PERIODIC TEST

QUALITY ASSURANCE

RELIABILITY CENTERED MAINTENANCE

REACTOR COOLANT SYSTEM

REFUELING OUTAGE

REACTOR PROTECTION SYSTEM

REACTOR TRIP BREAKER

REACTOR TRIP BYPASS BREAKER

STEAM GENERATOR

SAFETY INJECTION

STATION NUCLEAR SAFETY

STATION NUCLEAR SAFETY AND OPERATING COMMITTEE

SHIFT SUPERVISOR

SERVICE WATER

TURBINE BUILDING

TECHNICAL SPECIFICATION

VIOLATION

VIRGINIA POWER ADMINISTRATIVE PROCEDURE

WORK ORDER

WORK REQUEST