ML18152A248

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Insp Repts 50-280/93-22 & 50-281/93-22 on 930809-0904. Violation Noted.Major Areas Inspected:Plant Status, Operational Safety Verification,Hurricane Emily Response, Maint Insps & Employee Concerns Program Questionnaire
ML18152A248
Person / Time
Site: Surry  Dominion icon.png
Issue date: 09/29/1993
From: Belisle G, Branch M, Tingen S
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18152A249 List:
References
50-280-93-22, 50-281-93-22, NUDOCS 9310120016
Download: ML18152A248 (21)


See also: IR 05000280/1993022

Text

'

Report Nos.:

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W., SUITE 2900

ATLANTA, GEORGIA 30323-0199

50-280/93-22 and 50-281/93-22

Licensee: Virginia Electric and Power Company

5000 Dominion Boulevard

Glen Allen, VA

23060

Docket Nos.:

50-280 and 50-281

License Nos.:

DPR-32 and DPR-37

Facility Name:

Surry 1 and 2

lnspect;on Conducted:~ 9, 1993,

Inspectors:

~~~

through September 4, 1993

M. W. Branch Senior Resident

Inspector

~s;d:it'1'nspector

Approved by: fl~

G.

.Beli,Section Chief

Division of Reactor Projects

SUMMARY

Scope:

i/2.9/q 3

Date Signed

~/1...1/ Cf>

Date Signed

~d

This routine resident inspection was conducted on site in the areas of plant

status, operational safety verification, Hurricane Emily response, maintenance

inspections, employee concerns program questionnaire and fibrous material in

containment.

During the performance of this inspection, the resident

inspectors conducted reviews of the licensee's backshifts, holiday or weekend

operations on August 9, 16, 18, 19, 22, 24, 25, 30, 31 and September 1, 1993.

Results:

One violation discussed below was identified.

In the operations area, the following items were noted:

The failure to adequately evaluate and investigate the Unit 1 reactor

coolant system leakage was identified as Violation 50-280/93-22-01

{paragraph 3.c).

The conduct of unit startups from Hot Shutdown to 2% reactor power with

the controls invoked by Virginia Power Administrative Procedure-0108 was

considered a strength {paragraph 3.e).

2

In the plant support (radiation protection) area the following items were

noted:

The failure to properly post a surface contamination area in violation

of plant procedures was identified as Non-cited Violation

50-280/93-22-02 (paragraph 3.d).

Weaknesses associated with improper use of yellow and magenta rope

normally used for Health Physics posting was noted in several areas of

the station (paragraph 3.d).

In the maintenance area, the following items were noted:

A weakness was identified with the adequacy of the licensee's startup

assessment.

It involved not evaluating the need to inspect the Unit*2

steam generator drain assembly welds while the plant was in cold

shutdown (paragraph 3.c).

The licensee's investigation of how the degraded Train B master safety

injection relay caused the August 27 reactor trip was timely.

The

investigation would have been more complete if the source of the 38

volts that caused the relay to chatter would have been identified

(paragraph 5.a).

An Unresolved Item was identified associated with Emergency Service

Water building degraded flood barriers (paragraph 5.b) .

REPORT DETAILS

1.

Persons Contacted

Licensee Employees

  • W. Benthall, Supervisor, Licensing
  • R. Bilyeu, Licensing Engineer
  • H. Blake, Jr., Superintendent of Nuclear Site Services
  • R. Blount, Superintendent of Maintenance
  • D.\\ Christian, Assistant Station Manager
  • J. Downs, Superintendent of Outage and Planning
  • D. Erickson, Superintendent of Radiation Protection
  • A. Friedman, Superintendent of Nuclear Training
  • B. Hargrave, Nuclear Materials
  • M. Kansler, Station Manager
  • C. Luffman, Superintendent, Security
  • J. McCarthy, Superintendent of Operations
  • A. Meekins, Supervisor of Administrative Services
  • A. Price, Assistant Station Manager
  • V. Shifflett, Licensing
  • B. Shriver, Director, Corporate Nuclear Safety
  • E. Smith, Site Quality Assurance Manager
  • D. Sonvners, Corporate Licensing
  • J. Swientoniewski, Supervisor, Station Nuclear Safety
  • E. Turko, Superintendent of Engineering

NRC Personnel

  • M. Branch, Senior Resident Inspector
  • S. Tingen, Resident Inspector
  • Attended Exit Interview

Other licensee employees contacted included control room operators,

shift technical advisors, shift supervisors and other plant personnel.

Acronyms and initialisms used throughout this report are listed in the

last paragraph.

2.

Plant Status

Unit 1 operated at or about 100% power until it was shutdown to repair a

suspected SG primary manway cover leak on August 21.

As discussed

below, an UE was declared at 4:43 a.m., on August*21 when it was

determined that the RCS leakage was from a non-isolable pipe weld joint

on the B SG channel head drain assembly instead of the SG manway.

The

unit was returned to power on August 30 and was at full power at the end

of the inspection period .

Unit 2 began the reporting period in a forced outage to repair leaking

pressurizer safety valves. The unit was returned to power on August 19

2

and operated until August 23 when it tripped from approximately 98%

power as a result of a failed main generator voltage regulating circuit.

The unit was returned to power on August 25 and tripped again on August

27 as a result of a degraded Train B SI master relay. The unit was

returned to power on September 3 and at the end of the inspection period

the unit was operating at 97.5% power.

3.

Operational Safety Verification (71707, 42700)

The inspectors conducted frequent tours of the control room to verify

proper staffing, operator attentiveness and adherence to approved

procedures.

The inspectors attended plant status meetings and reviewed

operator logs on a daily basis to verify operational safety and

compliance with TSs and to maintain awareness of the overall operation

of the facility. Instrumentation and ECCS lineups were periodically

reviewed from control room indication to assess operability. Frequent

plant tours were conducted to observe equipment status, fire protection

programs, radiological work practices, plant security programs and

housekeeping.

Deviation reports were reviewed to assure that potential

safety concerns were properly addressed and reported.

a.

Licensee 10 CFR 50.72 Reports

1).

August 17 NOUE, (Loss of Emergency Monitoring Equipment).

On August 17, the licensee made an emergency one hour 10 CFR

50.72 call to report a NOUE declaration due to a loss of

power to the primary and backup meteorological towers.

The

UE was declared at 6:35 a.m., and was terminated at 10:44

a.m., on the same day when power was restored to the primary

and backup meteorological towers.

The power loss occurred

when a large bird struck the power lines in circuit 448

causing a phase-to-phase short and circuit 448 to

deenergize.

Power restoration was accomplished after the

damaged power lines in circuit 448 were repaired.

At the time of this event, circuit 448 was the sole power

source to the primary and backup meteorological towers.

The

alternate power supply was unavailable due to maintenance

activities.

During this event several small brush fires occurred outside

the PA when attempts were made to reenergize circuit 448.

The brush fires were immediately extinguished.

2).

August 21 NOUE (Unit 1 Shutdown for RCS Leak).

At 4:43 a.m. on August 21, 1993, the licensee declared a

NOUE based on non-isolable RCS pressure barrier leakage

requiring a plant shutdown per TS 3.1.c.4. The UE was

terminated at 2:43 a.m., on August 22, 1993, after RCS

3).

4).

3

temperature was reduced below 200 degrees F.

This event is

described in detail in paragraph 3.c.

August 23 Unit 2 Reactor Trip

On August 23 the licensee made a non-emergency four-hour 10

CFR 50.72 report due to a Unit 2 automatic reactor trip

caused by a turbine generator trip. The automatic reactor trip occurred at 5:19 a.m. from 97.5% power.

The turbine

generator experienced an excitation loss of power which

resulted in tripping the turbine generator due to loss of

electrical field. All ESF performed as designed and the

plant's response was as expected. All rods inserted into

the core.

The IRPI for rod M-10 initially indicated 35

steps after the reactor trip but drifted to O steps within

approximately twenty minutes.

The slow response of rod M-10

IRPI is a recurring problem.

This is also discussed in

IR93-20.

The minimum RCS pressure and temperature achieved

during the trip was 1840 psi and 530 F respectively. All

AFW pumps automatically started on low-low SG level. The

MSTVs remained open during the event and decay heat was

removed by the main steam dump valves via the main

condenser.

The inspectors were notified by the licensee of the trip and

reported to the site. The inspectors verified that the

plant had responded as discussed above and observed selected

recovery activities.

Subsequent troubleshooting identified a faulty phase shifter

card in the turbine generator excitation circuit which

caused the turbine generator to trip. The phase shifter

card was replaced and satisfactorily tested. Unit 2 was

returned to service on August 25.

August 27 Unit 2 Reactor Trip

On August 27 the licensee made a non-emergency four-hour 10

CFR 50.72 report due to a Unit 2 automatic reactor trip.

The automatic reactor trip occurred at 5:41 p.m. from 97%

power.

Technicians were in the final stages of completing

SI Train B logic testing when the reactor trip occurred.

All ESF performed as expected and the plant's response was

as expected. Automatic SI initiation did not occur during

the trip nor was it required to initiate. The inspectors

were notified by the licensee of the trip and reported to

the site. The inspectors verified that AFW had

automatically initiated on low-low SG level and operated

until SG levels were recovered.

Following the Unit 2

reactor trip RCS temperature and pressure decreased to 530

degrees F and 1840 psig respectively and were stable.

No

primary safety valves, primary PORVs, secondary safety

b.

c.

4

valves, or secondary PORVs opened during the event.

Decay

heat was removed by the main steam dump valves via the main

condenser.

All rods inserted into the £ore, however,

individual rod position for rod M-10 slowly drifted to zero

following the trip. This has occurred during previous Unit

2 reactor trips.

Troubleshooting indicated that the Train B SI master relay

was defective causing the unit to trip. Troubleshooting the

defective relay is further discussed in paragraph 5.a. The

relay was replaced and the unit was returned to power on

August 30.

5).

August 31 NOUE for Hurricane Emily

At 6:10 a.m., on August 31 the licensee declared a NOUE in

accordance with their emergency plan when the National

Weather Service issued a hurricane warning for Surry County

and coastal areas.

The UE remained in effect until 5:13

a.m., on September 1 at which time the hurricane warning was

canceled.

The response to Hurricane Emily is described in

paragraph 4.

Unit 2 Startup on August 19

On August 19, the inspectors observed the Unit 2 startup and

placing the unit on line. The inspectors noted that briefings for

the startup were thorough and emphasized recent problems.

Specifically, due to recent problems experienced during startups

with maintaining steam generator water levels stable (see IR 93-

20), increased emphases was placed on level control.

On several

occasions during the startup the SRO had the operators maintain

the plant in a stable condition to allow a review and brief of the

next step of the startup. Management involvement and oversight

were evident. Overall the inspectors considered that the

evolution proceed cautiously with no problems.

Co11111unications was

generally good with excellent use of repeat backs.

However, the

inspectors did note that during certain evolutions that required

coordination between several operators, no one person was in

charge.

For example when bypassing steam around the MS isolation

valves and when increasing turbine load, several different

operators gave orders to the valve and turbine operators

respectively.

The licensee does not use a designated phone talker

in the control room to conmunicate with auxiliary operators in the

field during startups. These observations were discussed with the

licensee and the licensee stated that they would perform a review.

Unit 1 Shutdown to Repair RCS Leakage

At 9:00 p.m., on August 20, 1993, a normal Unit 1 shutdown from

100% power co11111enced to repair a leak that appeared to be coming

from a mechanical joint on the B SG primary side manway cover.

5

The leak was detected on June 25, 1993, by an increase in

containment radiation monitor readings.

The RCS leakage was

subsequently classified as a 0.2 gpm identified leak based on a

limited visual observation that was restricted due to radiation

levels in the area and the presence of mirror insulation. The

licensee monitored the leak with closed circuit TV after it was

identified. A slight increase in leakage was noted by the close

circuit TV monitor on August 15 and preparations to shutdown the

unit were initiated. The licensee was originally scheduled to

take the unit off-line for repairs on July 10, 1993 but elected to

maintained it operating due to the hot weather load demands

followed by an unscheduled Unit 2 shutdown.

Unit 2 was shutdown

on August 6, 1993, to correct problems with Pressurizer Safety

Valves.

Following the repairs and the return of Unit 2 to

commercial operations on August 19, 1993, the licensee elected to

shut down Unit l for repairs.

Unit l was shutdown on August 21, and radiation levels were

reduced after the shutdown. A closer visual inspection of the

leakage was performed after the mirror insulation was removed.

The leakage was determined to be coming from a non-isolable leak

in a 3/4-inch weld joint on the SG channel head drain valve

assembly.

This drain valve assembly was in close proximity to the

SG manway and the leakage was directed to the SG manway and

escaped around the insulation seams.

At 4:43 a.m., on August 21 the licensee declared an UE based on

non-isolable RCS pressure barrier leakage requiring a plant

shutdown per TS 3.1.c.4. The UE was terminated at 2:43 a.m. on

August 22 after RCS temperature was reduced below 200 degrees F.

A few drops of leakage continued as the licensee preceded with

closing the loop stop valve and draining the loop for repairs.

The licensee inspected the failed weld. A preliminary failure

analysis indicated that the crack was attributable to

transgranular stress corrosion. The weld was repaired and the SG

was returned to service.

The drain valve assemblie~ on the other

two Unit l SGs were inspected by LPT and determined to be

acceptable. Since the failure of the Unit l drain valve assembly

weld could be a generic issue, the licensee considered what

actions would be necessary to evaluate similar Unit 3 weld joints.

After the Unit 2 August 23 reactor trip, the drain valve

assemblies on all three Unit 2 SGs were dimensionally checked and

examined for gross leakage.

No signs of leakage were observed.

However, the insulation covering the potentially effected weld

joints was not removed to allow a visual examination since the

licensee considered that the insulation removal and reinstallation

was too hazardous with the plant in hot shutdown.

The Unit 2

piping and the SG shell wall temperatures were approximately 540

degrees F.

It was not possible to perform LPT weld inspections.

Based on the size of this piping (i.e. 3/8 and 3/4 inch) these

welds were not required to be included in the ISi program.

The

6

licensee is continuing to evaluate the event for possible future

long term corrective actions.

The licensee's basis for not removing the Unit 2 insulation to

perform a visual inspection or LPT was that the temperature of the

SG was too hot.

However, the licensee did not perform any

additional verification of the acceptability of the Unit 2 welds

even though the unit was subsequently cooled to less than 200

degrees F to perform PMT for the failed relay as discussed in

paragraph 5.a. Managements' failure to recognize or evaluate the

need to perform the inspections while the unit was cooled down was

considered a weakness.

There was no commitment tracking item

assigned to ensure that during forced outages or mode changes the

inspections would be performed.

The inspectors reviewed the above events and monitored the

licensee's Unit 1 shutdown activities.

TS 3.1.c.4 required that

the reactor shall be brought to a cold shutdown condition and

corrective action taken prior to resumption of unit operations if

it is determined that leakage exist through a non-isolable fault

which has developed in a RCS component body, pipe wall, vessel

wall, or pipe weld.

TS 3.1.c.l required that any indication of

possible RCS leakage be investigated and evaluated.

The licensee

evaluated the leakage and categorized it as identified leakage

although the insulation covering the weld was not removed to allow

positive leak site identification.

As a result, Unit 1 operated

at power outside TS 3.1.c.4 from 12:52 p.m., on June 25, 1993,

through 2:38 a.m., on August 21, 1993, for a total of 57 days,

with non-isolable leakage in a RCS pipe weld on the B SG channel

head drain assembly.

The failure to adequately investigate and

evaluate the RCS leakage is identified as Violation 50-280/93-22-

0l, Failure to Properly Investigate and Evaluate RCS Leakage.

d.

Improperly Controlled Contaminated Area

During a routine tour on August 16, the inspectors noted a rope

and radiological sign posted across the normal access to the Unit

1 valve pit 12 foot elevation indicating a contaminated area.

There were two additional access points to get into the areaj

although they were not convenient due to piping obstructions. A

radiological boundary was not installed at these other two

accesses.

The inspectors reviewed the survey map which indicated

that there were several places in the area that were contaminated

(1000-3000 DPM) and a radiological boundary was installed to

prohibit general access into the area.

The inspectors notified

the HP supervisor of this condition and a proper boundary was

installed to prevent inadvertent access to the area.

RPR 93-79

was issued by HP documenting that a contaminated area boundary was

not properly posted on all sides to prevent inadvertent access.

Section 6.2.4.a.2 of HPAP-1061, Radioactive Contamination Control,

revision 1, required barrier materials be used as required to

clearly designate a contaminated area boundary.

The failure to

7

properly post the contaminated area in the Unit 1 valve pit 12

foot elevation was identified as NCV 50-280/93-22-02.

This NRC

identified violation is not being cited because criteria specified

in Section VII.B of the NRC Enforcement Policy were satisfied.

This event was fully discussed with HP personnel and procedure

changes are being considered.

During the inspection period the inspectors noted several

instances where yellow and magenta radiological barrier rope was

not appropriately used.

In both instances the rope was being used

for purposes other than a radiological barrier.

In one instance

the rope was utilized to secure a fire hose.

The other instance

involved securing a drain hose.

Station procedures do not

specifically prohibit the use of yellow and magenta rope for non-

radiological purposes but the inspectors consider it is prudent to

restrict use of the rope to radiological purposes.

The inspectors

discussed the issue with the RP Superintendent and during

subsequent tours noted that yellow and magenta rope was being

appropriately utilized as a radiological barrier.

The use of

yellow and magenta radiological barrier rope for purposes other

that a radiological barrier was identified as a weakness.

The

licensee agreed that using yellow and magenta rope for non-

radiological barrier purposes was inappropriate.

e.

Unit 2 Startup on August 25

The inspectors monitored portions of the August 25 Unit 2 startup.

The startup was performed in accordance with 2-GOP-1.4, Unit

Startup, HSD to 2% Reactor Power.

Starting a unit from HSD and

increasing power to 2% was considered an infrequently conducted or

complex evolution which required that additional controls be

invoked in accordance with VPAP-0108, Infrequently Conducted or

Complex Test or Evolutions.

Examples of controls invoked by VPAP-

0108 are that a senior operations manager monitor the evolution

and that a senior operation manager brief the personnel involved

on managements' expectations for accomplishing the evolution.

This evolution was thoroughly briefed by the unit SRO and a senior

operations manager.

During the briefing, safe operation was

emphasized as the top priority. It was evident that the unit SRO

was in charge of the evolution and this portion of the startup

progressed slowly and smoothly.

The conduct of unit startups from

HSD to 2% reactor power along with the additional controls invoked

by VPAP-0108 was considered a strength.

At approximately 2% reactor power operators transitioned from 2-

GOP-1.4 to 2-GOP-1.5, 2% Reactor Power to Max Allowable Power.

The remainder of the startup was not considered a complex or

infrequently conducted evolution and was conducted in a less

formal manner than the portion of the startup where the reactor is

taken critical. Issues associated with command and control was

discussed in IR93-15 and paragraph 3.b of this report.

4.

8

Within the areas inspected, one violation and one NCV were identified.

Hurricane Emily Response (93702)

As discussed above at 6:10 a.m. on August 31 Surry declared an UE when

hurricane warnings were issued for Surry County and coastal areas.

Station personnel had been preparing for the hurricane for several days

in advance of its approach.

The licensee had initiated O-AP-37.01,

revision 2, Abnormal Environmental Conditions and Associated Operations

and Corporate checklist. The AP provided instructions for preparing the

units and station for abnormal environmental conditions.

Included in

the AP were instructions to increase surveillance and monitor status if

hurricane force winds were expected within 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />. Additionally, the

AP required shutting down one unit and then the second unit 24 and 12

hours, respectively, prior to the hurricane arriving onsite. The

licensee never officially anticipated that the hurricane would affect

the site based on their meteorological monitoring and the hurricane's

projected path.

The inspectors reviewed the licensee's response to the hurricane warning

and conducted walkdowns of the plant and surrounding areas.

The results

of that walkdown along with plant design information germane to flooding

and possible wind damage is as follows:

Walkdown results

Inside the PA, the area was generally clean.

However, there were

racks of gas bottles stored outside and there were miscellaneous

large construction materials such as welding machines, plate

steel, pipe, grating, etc., that had been tied with rope.

The switchyard was not designed to withstand hurricane force

winds.

In the area between the switchyard and the intake canal

there were sheet metal cable tray covers that were loosely

fastened that would probably come loose under high winds.

The roofs throughout the plant were generally clear of loose

material. However, several of the roofs were constructed of

loosely fitted concrete tiles that would probably become missiles

under design basis hurricane force winds of greater than 137 mph.

The licensee considered these to be acceptable.

In the event of

high winds creating missile hazards, safe shutdown emergency

equipment would function as designed.

Design Information

Buildings design information and a list of equipment and buildings

susceptible to damage from high winds were discussed in section 3

of IR93-15 .

5.

- - - - ~ ~

9

Flood information is described in section 2.3 of the UFSAR with

critical equipment in the service water pump house being at the 18

foot above mean sea level elevation.

Service water canal level requirements for inventory are 28-30

feet and are based on two concerns; low water in the James River,

which would cause problems in making up water to the intake canal,

and high water in the James (i.e., no DP for SW gravity flow).

The Regional IRC was activated on August 30 at 4:40 p.m., to monitor the

status of the hurricane.

Two NRC regional inspectors and a supervisor

were dispatched to the site with emergency supplies and communication

equipment.

The two regional inspectors remained at the site to aid the

resident inspectors and the regional supervisor reported to the Virginia

Power Corporate EOF.

The three resident inspectors also reported to the

site. The site was continuously manned by NRC personnel from 6:45 a.m.,

on August 31 to 3:00 p.m., on September 1.

The Regional IRC was

deactivated at 9:30 a.m., on September 1.

The site TSC and OSC and corporate EOF were manned from 10:00 p.m., on

August 31 through 5:30 a.m. on September 1.

In addition, the site was

manned with extra security personnel during this time period.

Within the areas inspected, no violations were identified *

Maintenance Inspections (62703) (42700)

During the reporting period, the inspectors reviewed the following

maintenance activities to assure compliance with the appropriate

procedures.

a.

Bench Testing Unit 2 Train B Master SI Relay

As previously discussed in paragraph 3.a(4), the Unit 2 automatic reactor trip that occurred on August 27 was attributed to the

Train B master SI relay, 02-RP-REL-SIAB, being degraded.

The

reactor trip occurred when I&C technicians were in the final

stages of completing a monthly Train B SI logic test. Following

the trip, the inspectors walked down the SI cabinets with the I&C

technicians who performed the SI logic testing. At the time of

the trip, the SI cabinet doors were open and an l&C technician

observed the Train B SI master relay move.

This relay was a

Westinghouse model MG-6 relay.

The degraded relay was original

equipment.

The degraded SI master relay was removed and bench tested. The

inspectors witnessed the bench tests. The relay is normally

deenergized and when a SI signal is generated, the relay energizes

and changes state. Bench testing results identified that the

relay was cycling (chattering) at approximately 38 volts. The

inspectors witnessed the relay chattering at approximately 38

volts when tested. This relay is a 120 volt ac relay that

b.

10

normally changes state at approximately 70 volts. Eight new MG-6

relays were similarly tested and the new relays did not chatter

prior to changing state at 70 volts. It was concluded that the

relay was degraded in that it chattered at 38 volts prior to

changing states at 70 volts.

As previously discussed the I&C

technician observed the relay move when the trip occurred which

indicated that the relay was chattering. The licensee attempted

to determine the source of the 38 volts that caused the relay to

chatter but was unable to identify the source.

The relay has three sets of NO contacts, each set of contacts

actuates an SI slave relay. The SI master relay was actuated and

the time for each contact to close was monitored.

Testing results

indicated that contacts 3-6 closed first. Contacts 3-6 closure

opens the reactor trip breakers. Other SI components actuate when

contacts 3-6 close. These components were already in their SI

position or state when the reactor trip occurred.

For example,

when contacts 3-6 closed, an automatic start signal was sent to

the C HHSI/charging pump.

However, when the reactor trip occurred

the C HHSI/charging pump was already operating.

The licensee

concluded that when the Train B SI master relay chattered contacts

3-6 were the only contacts on the relay that latched and opened

the reactor trip breakers. This explained why other SI component

actuations did not occur when the relay chattered and the unit

tripped.

The inspectors concluded that the licensee's investigation was

thorough and timely in identifying why the degraded Train B master

SI relay caused the August 27 reactor trip breakers to open

without subsequent actuations of other safety equipment.

However,

the investigation would have been more complete if the 38 volt

source that caused the relay to chatter would have been

identified. The inspectors also walked down Unit 1 and 2's SI

cabinets in the switchgear room and noted that in Unit 1 there

were six WR tags installed on the cabinets documenting that

specific relays had chattered. Approximately half of the WRs

stated that relays were chattering when SI test switches were

operated. There were no WR tags on the Unit 2 SI cabinets for

chattering relays.

ESW Pump House Hurricane Flooding Protection Equipment

Section 2.3.1.2.2 of the UFSAR states that in the event of a

hurricane, the ESW pump building is protected against flooding by

installing watertight seal plates (stop logs) in front of the

doors and watertight wells over the louver openings on the side of

the building.

In preparation for hurricane Emily, these stop logs

and watertight wells were installed on August 31.

The inspectors

walked down the ESW building after the stop logs and watertight

wells were installed. The inspectors noted that the watertight

wells would not have prevented flood water from leaking into the


----

- - - -

11

building. There was a gap around the perimeter of each well where

it butted up against the building. Also, all bolts that secure

the wells to the building were not installed. The inspectors

noted that the stop logs for the doorways did not fit securely in

the opening and questioned if they could prevent flood water from

leaking into building.

On September 1, the inspectors monitored the licensee removing the

stop logs and water tight wells and noted the following

deficiencies:

The gaskets on the watertight wells were deteriorated and

appeared to be dry rotted.

Many bolt holes on the watertight wells did not match up to

the bolt holes on the building.

The louvers had a grating welded over the opening. This

grating prevented a watertight seal between the building and

well.

Maintenance personnel documented the deficiencies noted with

installing the watertight wells and stop logs in a memorandum

dated September 2 and in a DR.

The inspectors questioned whether

the ESW pump building would have been adequately protected against

flooding caused by a hurricane with the deficiencies noted. Until

the licensee completes their evaluation of this issue, this is

identified as URI 50-280,281/93-22-03.

c.

MOV 1-SI-MOV-18628 Deferred Maintenance

During a Unit 1 valve pit walkdown, the inspectors noted a WR tag

installed on the declutch lever for MOV l-SI-MOV-18628.

The WR

was annotated that the MOV would not automatically return to the

electrical mode of operation after the handwheel was declutched

and manually operated. This condition was identified during the

Unit 1 spring 1992 RFO and the maintenance to repair the MOV was

deferred to the upcoming 1994 spring RFO.

DR S-92-0740 dated

April 24, 1992, was issued when the condition was first

identified.

Valve l-SI-MOV-18628 is the 8 LHSI pump suction from the RWST.

The valve is normally open.

On low RWST level, the valve

automatically shuts when LHSI pump suction realigns to the

containment sump.

The inspectors were concerned that if the 1-SI-

MOV-18628 declutch lever was inadvertently moved, the MOV would

declutch and not operate electrically when required.

The

inspectors discussed this concern with the licensee. The licensee

considered the MOV fully operable in that the MOV has been

satisfactorily stroke tested every quarter and that the chances of

12

the declutch lever being inadvertently moved are remote because

the MOV is located in a secluded area.

At the end of the inspection period the inspectors requested the

licensee to operate the declutch lever on 1-SI-MOV-1862B with the

inspectors present in order to determine if it is possible to

inadvertently declutch the MOV.

The inspectors will followup on

this issue during the next inspection period.

Within the areas inspected, a URI was identified.

6.

Employee Concerns Program Questionnaire (TI 2500/028)

7.

The inspectors conducted a survey of the licensee's program associated

with raising safety concerns.

The survey results are contained in

Attachment 1 to this report. The format of the TI survey was modified

slightly for clarity.

Within the areas inspected, no violations were identified.

Fibrous Material In Containment (Bulletin 93-02)

The inspectors reviewed the licensee's actions taken to address NRC

Bulletin No. 93-02, Debris Plugging of Emergency Core Cooling Suction

Strainers.

The bulletin required the licensee to identify fibrous air

filters or other temporary sources of fibrous material not designed to

withstand a LOCA, which are installed or stored in containment.

The licensee responded to this bulletin in a letter dated June 9, 1993.

The response stated that temporary fibrous material is not stored or

utilized in either containment while a unit is operating. The response

also stated that permanent fibrous material installed inside the

containments was evaluated to not block or clog ECCS suction strainers.

The NRC's evaluation of the acceptability of the licensee's responses

was documented in a letter dated July 27, 1993.

The inspectors reviewed EWR 93-032, RS Review of NRC Bulletin Number 93-

02/Surry/1&2, dated May 21, 1993, and verified that temporary and

permanent fibrous material in the containments were evaluated.

EWR 93-

032 did identify that during outages, temporary fibrous material is

utilized in the containments. Temporary filters are installed in the

suction containment air recirculation coolers. The licensee revised 1,2

GOP-1.1, Unit Startup, RCS Heatup From Ambient to 195 degrees F, to

strengthen controls to ensure that these temporary filters or any other

temporary fibrous material were removed prior to startup. The

inspectors reviewed the revised procedures and verified that controls

were adequate.

The inspectors also walked down the Unit 1 containment

during the inspection period and did not identify any temporary fibrous

material or any permanent fibrous material concerns that were not

already addressed by EWR 93-032.

13

Within the areas inspected, no violations were identified.

8.

Exit Interview

The results were summarized on September 8, 1993, with those individuals

identified by an asterisk in Paragraph 1.

The following summary of

inspection activities was discussed by the inspectors during this exit:

Item Number

Status

Description

(Paragraph No.)

VIO 50-280/93-22-01

Open

Failure to Properly

Investigate and Evaluate RCS

Leakage (paragraph 3.c).

NCV 50-280/93-22-02

Closed

Failure to Properly Post the

Contaminated Area in the Unit

1 Valve Pit 12 foot Elevation

(paragraph 3.d).

URI 50-280,281/93-22-03

Open

ESW pump building with the

degraded flood barriers

(paragraph 5.b).

Proprietary information is not contained in this report. Dissenting comments

were not received from the licensee.

9.

Index of Acronyms and Initialisms

AFW

AP

CFR

DP

DPM

ECCS

-

EOF

ESF

ESW

EWR

F

GPM

HP

HHS!

-

HSD

I&C

IR

IRC

!RPI -

ISI

LHSI

-

AUXILIARY FEEDWATER

ABNORMAL PROCEDURES

CODE OF FEDERAL REGULATIONS

DIFFERENTIAL PRESSURE

DISINTEGRATIONS PER MINUTE

EMERGENCY CORE COOLING SYSTEM

EMERGENCY OPERATIONS FACILITY

ENGINEERED SAFETY FEATURES

EMERGENCY SERVICE WATER

ENGINEERING WORK REQUEST

FAHRENHEIT

GALLONS PER MINUTE

HEALTH PHYSICS

HIGH HEAD SAFETY INJECTION

HOT SHUTDOWN

INSTRUMENTATION AND CALIBRATION

INSPECTION REPORT

INCIDENT RESPONSE CENTER

INDIVIDUAL ROD POSITION INDICATION

INSERVICE INSPECTION

LOW HEAD SAFETY INJECTION

LOCA -

LPT

MDV

MSTV -

NCV

NDE

NO

NOUE -

NRC

osc

PA

PORV

PMT

PSIG -

PT

RP

RCS

RFO

RWST -

SG

SI

SRO

SW

TI

TS

TSC

UE

UFSAR -

URI

VIO

WR 14

LOSS OF COOLANT ACCIDENT

LIQUID PENETRANT TEST

MOTOR OPERATED VALVE

MAIN STEAM THROTTLE VALVE

NON-CITED VIOLATION

NON-DESTRUCTIVE EXAMINATION

NORMALLY OPEN

NOTICE OF UNUSUAL EVENT

NUCLEAR REGULATORY COMMISSION

OPERATIONS SUPPORT CENTER

PROTECTED AREA

POWER OPERATED RELIEF VALVE

PREVENTIVE MAINTENANCE TEST

POUNDS PER SQUARE INCH

PERIODIC TEST

RADIATION PROTECTION

REACTOR COOLANT SYSTEM

REFUELING OUTAGE

REFUELING WATER STORAGE TANK

STEAM GENERATOR

SAFETY INJECTION

SENIOR REACTOR OPERATOR

SERVICE WATER

TEMPORARY INSTRUCTION

TECHNICAL SPECIFICATION

TECHNICAL SUPPORT CENTER

UNUSUAL EVENT

UPDATED FINAL SAFETY ANALYSIS REPORT

UNRESOLVED ITEM

VIOLATION

WORK REQUEST

ATTACHMENT 1

EMPLOYEE CONCERNS PROGRAM SURVEY

PLANT NAME: SURRY UNITS 1&2

LICENSEE: VEPCO

DOCKET I: 280,281

A.

PROGRAM:

B.

SCOPE:

1.

Does the licensee have an employee concerns program?

(No)

2.

C011111ents:

The licensee does not have a formal employee

concerns program (ECP) program with dedicated staff and

budget. However,

the licensee has implemented an effective

10 CFR 50 Appendix *e* program that is independent of

productive pressures. Elements of this QA program includes

problem identification, resolution, and root cause

determinations that may involve employee interviews.

Additionally, Industrial Safety Reporting and the licensee's

Human Resource programs including grievance, employee exit

interviews, and Employee Assistance Program (EAP) allows an

employee an avenue to identify problems and discuss

differing opinions/views *

Has NRC inspected the program?

(No) Report# N/A

1.

Is it for:

a.

Technical? (Yes, See #A.l Coanent above)

b.

Administrative? (Yes, See #A.1 C011111ent above)

c.

Personnel issues? (Yes, See #A.1 Conment above)

2.

Does it cover safety as well as non-safety issues?

(Yes)

3.

Is it designed for:

4.

a.

Nuclear safety? (See #A.1 COIIID8nt above)

b.

Personal safety? (See #A.l Conment above)

c.

Personnel issues - including union grievances?

(Yes, See #A.l Conment above)

Does the program apply to all licensee employees?

(Yes)

2

5.

Contractors?

(Yes)

Conwnent:

Contractors are covered under the plant qual;ty

assurance (QA) adm;n;strative control program.

However, the

Gr;evance process and Ex;t Interview process is not extended

to contractors.

6.

Does the licensee require its contractors and their subs to

have a similar program?

(No)

7.

Does the licensee conduct an exit interview upon terminating

employees asking if they have any safety concerns?

(Yes)

Coment:

The licensee's exit interview is directed at

f;nd;ng out why the employee is terminating and does not

specifically ask about safety concerns.

C.

INDEPENDENCE:

I.

What is the title of the person in charge?

N/A

2.

Who do they report to?

N/A

3.

Are they independent of line management?

(The VP Human Resources who is responsible for the

grievance, personnel, and EAP is independent of Nuclear

Operations)

4.

Does the ECP use th;rd party consultants?

N/A, C011111ent:

The licensee's EAP uses a third party

consultant.

5.

How is a concern about a manager or vice president followed

up?

Although not formalized, the licensee indicated that

information would be passed up to the next higher level for

disposition *

3

D.

RESOURCES:

1.

What is the size of staff devoted to this program?

Co11111ent:

The licensee's Station Nuclear Safety group who

administer the deficient report (DR} process and Human

Performance Evaluation System is comprised of 19 people.

There is one industrial safety coordinator and one personnel

supervisor as well.

2.

What are ECP staff qualifications (technical training,

interviewing training, investigator training, other)?

N/A

E.

REFERRALS:

1.

Who has followup on concerns {ECP staff, line management,

other)?

The individual or department responsible for the program

under which the concern was processed would have the

responsibility for followup and resolution.

F.

CONFIDENTIALITY:

1.

Are the reports confidential?

Coament: This itea is not applicable since there is no

formal program.

However, based on recent examples and

discussion with the licensee, all personnel related issues

are handled in a confidential manner, with only the

appropriate level of management involved with resolution}.

2.

Who is the identity of the alleger made known to (senior

management, ECP staff, line management, other)?

C011111ent:

This item is not applicable. However, in

resolution of concerns identified through the programs

discussed above, the licensee has indicated that information

is shared on a need to know basis and than only to senior

management.

3.

Can employees be:

a.

Anonymous? (Yes}

b.

Report by phone? (Yes)

G.

4

FEEDBACK:

1.

Is feedback given to the alleger upon completion of the

followup?

(Co11111ent:

The licensee's DR system ask whether the

originator request feedback as to resolution. The licensee

also indicated that feedback is generally provided to a

known alleger when practical.

2.

Does program reward good ideas?

The licensee has an employee suggestion system, which

evaluates ideas and reward employees if they are

implemented.

3.

Who, or at what level, makes the final decision of

resolution?

Final resolution is decided, for the most part by Station

Management with DR resolution being reviewed by the Station

Nuclear Safety and Operating Conaittee.

4.

Are the resolutions of anonymous concerns disseminated?

If determined to be beneficial to other employees.

5.

Are resolutions of valid concerns publicized (newsletter,

bulletin board, all hands meeting, other)?

Resolutions are publicized if appropriate and practical.

H.

EFFECTIVENESS:

1.

How does the licensee measure the effectiveness of the

program?

DR tracking and trending is performed but for the 110st part

there is no formal ECP and this item is not applicable.

5

2.

Are concerns:

a.

Trended?

Yes, The issue itself is if documented on a DR.

b.

Used? (N/A)

3.

In the last three years how many concerns were raised?

Through the HPES 20 concerns were raised and closed and 17

were substantiated.

Through the grievance process 42 concerns were raised, 22

were closed with 5 being substantiated.

4.

How are followup techniques used to measure effectiveness

(random survey, interviews, other)?

Trending of DRs and grievances are used as well as randoa

HPES interviews.

5.

How frequently are internal audits of the ECP conducted and

by whom?

N/A

I.

ADMINISTRATION/TRAINING:

I.

Is ECP prescribed by a procedure?

No, Conments:

As stated earlier, the licensee does not have

a formal EC program.

The DR, Safety, and personnel process

described above are prescribed by policies or procedures

2.

How are employees, as well as contractors, made aware of

this program {training, newsletter, bulletin board, other)?

The above process are discussed in general through employee

training or brochures.

ADDITIONAL COMMEHTS:

NONE

(Including characteristics which make the program

especially effective or ineffective.)