ML18152A246

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Insp Repts 50-280/93-13 & 50-281/93-13 on 930502-0605.No Violations Noted.Major Areas Inspected:Plant Status, Operational Safety Verification,Maint,Surveillance,Safety Assessment & Quality Verification & Licensee Event Review
ML18152A246
Person / Time
Site: Surry  Dominion icon.png
Issue date: 06/25/1993
From: Belisle G, Branch M, Tingen S, York J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18152A247 List:
References
50-280-93-13, 50-281-93-13, NUDOCS 9307220061
Download: ML18152A246 (18)


See also: IR 05000280/1993013

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W .

. ATLANTA, GEORGIA 30323.

Report Nos.:

50-280/93-13 and 50-281/93-13

Licensee: Virginia Electric and Power Company

5000 Dominion Boulevard

Glen Allen, VA

23060

Docket Nos.:

50-i8o and 50-281

License Nos.:

DPR-32 and DPR-37

Faci 1 i ty Name:

Surry 1 and 2.

Inspection Conducted:

May 2 through June 5, 1993.

Inspectors:

Approved by:

Scope:

//_ ~

z%:-::

~ork~~Inspector

S. G. Tinge~ Inspecto

. . 71;{ [I ~lV(~ .

G. A. Belisle, Section Chief

Division of Reactor Projects

SUMMARY

  • 0¢--'

Da

Si ed

_

o~/iiJ

  • ~~3

D e Si ned

._

t/15/13

Date Signed

This routine resident inspection was conducted on- site in the *areas of plant

status, operational safety verification, maintenance, surveillance, safety

assessment and quality verification, licensee event review, and action on

previous inspection items. During the performance of this inspection, the

resident inspectors conducted reviews of the licensee's backshifts, holiday or

weekend operations on May.2, -16, -23, 27-, and--29.

Results:

In the operations area, the following item was noted:

The use of an operations review board to review, answer, and maintain

status of open deviations report action items,-commitment tracking

9307220061 * 930625 -~

PDR -ADOCK 05000280

G

PDR:;:*.

t~

2

system items, and quality assurance findings assigned to oper~tions was

identified as a strength (paragraph 3.b).

In the maintenance/surveillance area, the.following items were noted~

The maintenance associated with the replacement of 1-VS-S-IA was well

planned and conducted.

The installation of this new strainer improved

the material condition of the plant (paragraph 4.a).

From April 1992 through the present inspection period, the number of

non-outage corrective maintenance work orders decreased by approximate.ly

one-half and the average age of these work orders also decreased by

approximately one-half (paragraph 4.b).

From January.1992 through the present inspection period, the Cause

Determination Evaluation (CDE) backlog has been reduced to 21 CDEs which

is a reduction of approximately 95%.

The licensee's action of assigning

additional engineers to the maintenance engineering department and

establishing CDE backlog goals has*been effective in.reducing the CDE

. backlog (paragraph 4.c).

The present Technical Procedure Upgrade Program schedule calls for

approximately 39QO*upgraded*procedures to be issued and-only 2888 have

been issued. At the present upgraded procedure issuance *rate, the. 1996

target date for program completion will not be met.

The Licensee has *

added additional staff to support this procedure upgrade effort

(paragraph 4.d).

The PASSPORT Maintenance Management System is in the process of being

implemented.

The main purpose of this* new program is to improve *

accessibility to the engineering data base required to plan work orders

(paragraph 4.f).

In the engineering/technical support area, the following item was noted:

Non-cited violation 50-280,281/93-13-0l was identified for failure to

adequately control revised motor operated valve setpoints (paragraph

6.a).

-

REPORT DETAILS

1.

Persons Contacted

Licensee Employees

R. Allen, Supervisor, Operations

W. Benthall, Supervisor, Licensing

  • R. Bilyeu, Licensing

H. Blake, Superintendent of Site Services

  • R. Blount, Superintendent of Engineering:
  • D. Christian, Assistant Station Manager
  • J. Downs, Superintendent of Outage and Planning
  • D. Eritkson, Superintendent of Radiation Protection

A. Friedman, Supervisor, Nuclear Training

  • R. Gwaltney, Superintendent of Maintenance
  • R. Hayes, Quality Assurance

M. Kansler, Station Manager

A. Meekins, Supervisor, Administrative Services

  • J. McCarthy, Superintendent of Operations

J. O'Hanlon, Vice President, Nuclear Operations

  • A. Price, Assistant Station Manager

E. Smith, Site Quality Assurance Manager

  • J. Swientoniewski, Supervisor, Station Nuclear Safety
  • W. Woodzell, Senior Instructor

NRC Personnel

M. Branch, Senior Resident Inspector

j_ York, Resident Inspector

  • S. Tingen, Resident Inspector
  • Attended Exit Interview

Other licensee emplojees contacted included control room operators,

shift technica.l advisors, shift supervisors *and other plant personnel.

Acronyms and initialisms used throughout this report are listed in the

last paragraph:

2.

Plant Status

Unit 1 began the reporting period in power operation. The Unit was at

power at the end of the inspection period, day 115 of continuous

operations.

Unit 2 began the reporting period in hot shutdown, day 58 of a RFO.

The

unit was returned to power on May 6 and operated at power until May 31.

On May 31, the unit was taken off-line but remained critical in order to

balance the turbine generator.

On June 1, the unit was returned to

power and operated at power for the remainder of the period.

.

3.

2

Operational Safety Verification (71707, 42700)

The inspectors conducted frequent tours of the-control room to verify

proper staffing, operator attentiveness and adherence to approved

procedures.

The inspectors attended plant status meetings and reviewed

operator logs on a daily basis to verify operations safety and

compliance with TSs and to maintain awareness of the overall operation

of the facility.

Instrumentation and ECCS lineups were periodically

reviewed from control room indication to assess operability. Frequent

plant tours were conducted to observe equipment status, fire protection

programs, radiological work practices, plant security programs and

housekeeping.

Deviation reports were reviewed to assure that potential

safety concerns were properly addressed and reported.

a.

Design Basis Documentation Project Update

A meeting was held in Region II on May 3, 1993, to review the

status of the DBD Program and to address concerns expressed in

North Anna NRC IR 50-338, 339/92-32, and Surry NRC IR

50-280, 281/93-07, regarding the review of open items identified

by this program.

The licensee discussed their evaluation of

design basis documents, the 1dentification and resolution of

engineering issues, and the review and classification of items

opened as a result of the DBD Program.

Further NRC review of the

disposition of open items will be conducted in a future

inspection.

b.

Activities of the Operations Review Board

The inspectors attended a meeting of the ORB on May 28.

This

board consists of two to three operators that are usually

nonlicensed (currently has one licensed RO), the Superintendent of

Operations, one or more shift representatives, and a special

projects representative.

The ORB was formed by the Superintendent

of Operations in September 1992 and is responsible for reviewing,

answering, and tracking all deviations, conunitment tracking system

items, and QA items that are assigned to operations. Requests for

engineering assistance from the operations group and assisting in

resolving items of inunediate concern are handled by this group.

This board has removed some of the administrative burden from

operations management and decreased the backlog of QA items,

deviations, and CTS items assigned to the operations department.

Besides the previous accomplishments-of the ORB, the experience

gained in working on problems and interacting with other

departments is very valuable in training the current and future

ROs and SROs.

Since each of the permanent members are rotated,

this experience will be distributed throughout the operations

department in the future.

The formation and functioning of the

ORB is identified as a strength.

c.

--~-----

3

Emergency TS Change to Operate Unit 2 at Reduced Power

  • On April 29, 1993, during the hydroslati.c test of Unit 2 following

the RFO, RCS leakage past the pressurizer A and/or~ s~fety valves

was observed. The leakage was attributed to loss of the water in

the loop seal upstream of the safety valves which affected the

valve seat leakage.

The hydrostatic test was terminated and the

RCS,pressure reduced to prevent further leakage through the safety

valves.

To complete the ASME required hydrostatic test and to

prevent further leakage past the safety valves, _the valves were

gagged which was discussed in NRC IR 50-280, 281/93711.

After the gagging devices were removed, the A pressurizer safety-

valve continued to leak by the seat. _ The RCS pressure was reduced

to.1800 psig and slowly repressurized to 2135 psig. The safety

valve did not leak at 2135 psig.

By letter dated May 4, 1993, the

licensee requested and was granted enforcement discretion to _

operate Surry, Unit 2 at reduced nominal operating pressure, 2135.

psi g, until an emergency TS change could be submitted.

By letter

dated May 6, 1993, the licensee requested an emergency-TS

amendment to allow operation at a reduced pressure of 2135 psig in

lieu of 2235 psig un~il the next scheduled RFO.

In a letter dated

May 14, 1993, the NRC approved the emergency TS amendment to al)ow

operation at reduced pressure.

4.

Maintenance Inspections (62703) (42700)

During the reporting period, t~e inspectors reviewed the following

maintenance activities to assure compliance with the appropriate

procedures.

a.

Replacement of Strainer 1-VS-S-lA

On May 13, mi nor flooding was reported in MER 4 due to a hole in* a

carbon steel flush line (SW system) for strainer l~VS-S-lA.

The

SW system was realigned and the leak was isolated. The inspectors

observed the replacement of the leaking pipe and the upgrade of

the material condition of the system at the same time.

The

upgrade consisted of replacing the motorized strainer, two valves,

and piping.

The inspectors observed the pre-job briefing and prestaging of the

strainer, valves, gaskets; bolts, etc. Several procedures were

used to rep 1 ace the* components: *procedure O-MCM-1801-01,

Piping/Components Repair/Replacement, dated May 6, 1993; procedure

0-MCM-1001-01, Stud Replacement, dated October 5, 1990; procedure

O-MCM-1401-01, Flange Gasket Replacement, dated June 14, 1991.

Work orders 3800131336 and 3800135428 were used to perform_the

maintenance.

Some of the removal and replacement activities were observed

including torquing, grouting of new studs, and post maintenance

. *~ ....

4

testing (uncoupled run of the strainer motor).

The use of

procedures and sign offs was observed during the operation~

The

maintenance activity was* well planned and conducted and no

discrepancies were noted.

b.

Corrective Maintenance WO Backlog

The inspectors reviewed the distribution of open WOs for the

period ending May 23.

There were a total of 3507 open SR and NSR

WOs for both units. Of these WOs, 1012 were classified as outage

WOs, and 2495 were classified by the licensee as non-outage WOs.

Of the 2495 non-outage WOs, 166 were classified as CM work orders

with an average age of 46 days.

The licensee's goal for 1993 is

to maintain less than 250 non-outage CM WOs with an average age of

45 days or less.

-

The inspectors also reviewed the distribution of open WOs for the

period ending April 5, 1992. There were a total of 5947 open SR

and NSR WOs.

Of these WOs, 3063 were classified by the licensee

as outage WOs, and 2884 were classified as non-outage WOs.

Of the

2884 non-outage WOs, 406 were classified as CM work orders with an

average age of 90 days.

The licensee's goal for 1992 was to

maintain less than 350 non-outage CM WOs with an average age of 45

days or less.*

The inspectors contluded that from April 5, 1992, through the

present inspection period the number of non-outage CM WOs

decreased by approximately one-half and the average age of these

WOs also decreased by approximately one-half.

  • -

c.

CDE Backlog

d.

The inspectors reviewed the status of the CDE backlog. During the

previous SALP assessment periods, the backlog of CDEs increased.

At the beginning of the present SALP assessment period there was a

backlog ~f over 400 CDEs.

Throughout the present SALP assessment

period, the CDE backlog has been reduced to 21 CDEs which is a

reduction of approximately 95%.

The inspectors concluded that the

licensee's actions of assigning additional engineers to th~

maintenance engineering department and establishing CDE backlog

goals have been effective in reducing the CDE backlog.

Station Technical Procedure Upgrade Program

The inspector reviewed the station Procedure Groups 1992 and 1993

status reports. These reports indicated that the licensee had

exceeded their yearly goals for issuing upgraded procedures.

The

goal for 1992 was to issue 600 upgraded procedures and

approximately 625 procedtires were issued.

The goal for 1993 is to

issue 800 upgraded procedures and approximately 400 procedures

have been issued.

5

The present target end date for the TPUP is scheduled for December

1996 and 6639 procedures have been identified for upgrading.

In

order to meet the target date of December, 1996, the TPUP plan

calls for 150 upgraded procedures to be issued every month.

The

inspectors noted that the 1992 and 1993 goals of 600 and 800

issued upgraded procedures do not meet the TPUP plan of 150

procedures per month.

The present TPUP plan calls for

approximately 3900 upgraded procedures issued and only 2888 have

been upgraded. *The inspectors concluded that at the present

upgraded procedure issuance rate the 1996 target date wil 1 not be

met.

The TPUP is divided into electrical, mechanical, I&C, operations,

and other areas.

Each area- is assigned a goal for the number of*.

upgraded procedures to be issued * .In 1992 all departments met or

came very close in meeting their goals. It appears that all

departments with the exception of I&C will meet or exceed their

1993 goals for number of upgraded procedures issued. A goal of

174 I&C upgraded procedures has been established for 1993 and 23

were issued in the first four months.

The delay is due primarily

for critical process loop data and scaling factors.

The licensee

has recognized that I&C upgraded procedures are behind ~chedule

and have implemented corrective actions. A person has been added

to the procedure writers group to determine scaling factors and

additional procedure writers have been assigned to the I&C area~

In addition, engineering has been assigned the responsibility to

  • provide critical p~ocess loop data in a manner to support the

procedure upgrade efforts.

The licensee monitors the number of pro~edural changes made to

upgraded and non-upgraded procedures.

Upgraded procedures

required approximately one third fewer changes than non-upgraded

procedures ..

During the previous SALP assessment period problems were

i dent if fed with procedures for repair of AOVs.

During this SALP *

assessment period, sixteens AOV upgraded procedures have been

issued.

NRC IR 50-280, 281/93-05 identified problems with MS PORV

repair procedures and these procedures are presently being

upgraded.

e.

Troubleshootin~ of the Unit 1 Rod Control System

On June 3*Unit !*experienced problems with the Rod Control system_

while performing the bi-weekly rod exercise test as required by

TS.

When the operator was inserting the* A shutdown bank of rods, *

the group 1 rods inserted ten steps and the group 2 rods did not

move as indicated by IRPI.

The operator also noted that rods in

the A control bank had moved in approximately ten steps even

though that bank of rods was not selected~

By design this

condition did not cause a rod drive urgent failure alarm even

though the failure caused non-selected rods to move.

6

The inspectors monitored the licensee's troubleshooting activities

associated with the rod control failure. The troubleshooting was

controlled by an emergency WO which included i~~tructicins for

u~ing the vendor manuil. The technicians replaced several power

supply cards which were suspected of being defected but the

problem was not resolved.

The old cards were reinstalled and

after the cards were wiggled the problem was resolved. This

indicated to the licensee that either a loose card or dirty

contacts was the problem.

The licensee repeated the rod exerci~e

test as discuss~d in section 5.c of this report and after

satisfactory results were aihieved, declared the system fully

operable. However, several days later the problem reappeared and

after additi-0nal troubleshooting, the licensee replaced a

stationary firing card, performed the rod exercise test and

verified that proper rod motion was achieved.

During the troubleshooting on Ju~e 3, the inspectors noted that

-the vendor manual being used was -in complete disarray with pages

torn out of the book .. In addition, the drawings were also removed

from the book.

The inspectors also noted that the craft personnel

were using uncontrolled drawings and training material in

conjunction with the vendor manual.

The inspectors questioned the

use of the uncontrolled material and held discussions with

maintenance management personnel. The-licensee pointed out that

in the area of troubleshooting, administrative procedure

VPAP-0601, Document Distribution and Control, had been recently

modified through the issuance of PAR PS-01 dated April 29, 1993,

to allow the use of information copies of drawings and training

material to supplement the working copy.

The inspectors noted

that other administrative procedures VPAP-0801, Maintenance*

Program, Revision 2, and MDAP-0002, Conduct of Maintenance,

Revision 0, indicate that only controlled information be used for

the conduct of safety related maintenance. A review of the PAR to

VPAP-0601 indicated that the use of supplemental information in

.conjunction with controlled information for troubleshooting

activiti~s did not violate the other procedures.

However, in the

case of emergency work being performed under a short TS outage

time window it was not clear to the inspectors that only

controlled information would be used.

The inspectors will monitor

additional troubleshooting activities in the future to ensure that

the work is properly controlled.

The inspectors noted that a recent rod control event occurred at

/ '-~nether station as indicated in IN 93-46, Potential Problems With

,.,-

Westinghouse Rod Control System And Inadvertent Withdrawal Of A

Single Rod Control Cluster Assembly.

Surry personnel were aware

of and are following the event that is described in the IN.

They

have been in contact with Westinghouse and are evaluating the rod

system failure described above as to similarity and significance *

The failure of the control rod system is described in Chapter

14.2.4 of the UFSAR which indicates that misalignment of rods are

indicated by asymmetric power distribution as seen on the ex-core

-- 'I

7

Nis or a rod deviation alarm. The UFSAR further indicates that

protection.is afforded by the.reactor protection system in the

form of low or high power reactor trips .. Additional followup of

  • rod control problems by the licensee will be monitored by the.

inspectors.

f.

PASSPORT/Maintenance Management System

In January 1993 the licensee initiated a pilot program, PASSPORT,

for processing WOs whi_ch is scheduled to fully_ implemented by

July 31, 1993. * The main purpose of the new program is to improve

accessibility to the engineering data base required to plan WOs.

Information required for planning a mainten_ance item such as,

safety category, prints, pro.cedures, EQ classification, drawings,

technical m~nuals, and parts will be specified in bne area iri lieu

of ciifferent areas*. This new program will also simplify the WO_

planning process and improve WO history traceability.

Within the areas inspected, no violati6ns were identified.

5.

Surveillance Inspections (61726,-42700)

During the r~porttng period, the inspectors reviewed surveillance

activities to assure tompliance with the appropriate procedure and TS

requirements.

a.

Unit 2 Containment Sump Inspection

TS 4.5.D requires a visual inspection of the containment sump, IRS

pump wells and the engineered safeguards suction inlets be *

performed at least once each refueling period and/or after major

maintenance activities in the containment.

The inspection should

verify that the containment sump and *pump wells are free of debris

that*could degrade system operation and that the sump components

are properly installed and show no sign of .structural distress or

excessiv~ corrosion.

The inspectors reviewed the results of 2-MPT-1205-01, Unit 2

Containment Sump Inspection and Test Setup, dated January 21,

1993*. This procedure was accomplished during the Unit 2 RFO and

one of the purposes of this procedure is to perform the visual

inspections required by TS 4.5.D. During these inspections,

  • foreign material was found inside the ORS and LHSI p*umps

.

containment sump cross connect suction piping.

The following was

found in the ORS pumps sump cross connect suction piping which is

12 inches in diameter and approximately 25 feet long:

2-5/8 inch SS nuts

1-5/8 inch ss steel washer

1-3/8 inch SS washer

I-1/4 inch SS tubing, 1/4 inch long

1-allen wrench, #6

8

1-3/16 inch drift punch, 8 inches long, 1/2 inch diameter *

body

3-3/32 inch diameter tig wires, two were 18 inches and the

third one was 3 inches long.

2-1/8 inch diameter tig wires, 9 and 14 inches long

1..:s/8 inch diameter SS stud, 2 inches long

I-bracket, 2 inches by I inch with a key hole

I-welding rod, 1/16 inch diameter and 2 inches long

8-pieces of SS wire, 1/16 inch diameter and 1/2 inch long

IS-carbon steel sections 1/2 inch by 1/8 inch by I inch

The following foreign material was found in the LHSI pump sump

cross connect piping which is 12 inches in diameter and

approximately 11 feet long:

1-3/16 inch diameter wire, six inches long

1-3/8 inch SS nut

2-welding rod stubs

The licensee concluded that the foreign material was introduced

prior to 1988.

Engineering concluded that the size of some of the

debris could have potentially caused degradation of an ORS pump

but neither of the pumps were considered to be inoperable.

Both

LHSI pumps were also.considered operable with the foreign material

in the system.

In 1988, foreign material was identified in the IRS an LHSI pump

suction piping at. the Units I and 2 containment sump.

The cause

of the foreign material in containment sump piping was identified

as inadequate contra l of foreign material during the perform*ance

of maintenance or introduced during initial construction.

As a

result of inadequate control of foreign material, a civil penalty

w_as issued.

As corrective action, the licensee inspected the

containment sumps piping. Also the licensee implemented a program

to inspect the containment sumps and piping every RFO.

TSs were

changed to require this inspection.

The inspectors reviewed the procedures that were used to inspect

the containment sump ORS and LHSI pump suction piping in 1988 and

during the subsequent RFOs for both units and concluded that the

piping was inspected with remote optical inspection equipment.

In

1993, the licensee utilized more sophisticated remote optical

inspection equipment to inspect Unit 2 ORS and LHSI containment

sump cross connect suction piping and identified the presence of

some foreign material.

In order to retrieve the foreign material

mop heads were tied together and pulled through the piping.

During this process, more foreign material was identified in the

piping and maintenance personnel continued to pull mop heads

through the piping until no foreign material was present.

Afterwards the piping was reinspected with remote optical

inspection equipment and no foreign material was identified.

9

The -inspectors questioned why the optical equipment utilized to

accomplish the visual inspections did not identify all the foreign

material in the piping.

The inspectors .were informed that at the

bottom of the piping there was a layer of black soft silt. The

foreign material noted above*was contained in the silt at the

bottom of the piping and, therefore, not identified by the remote

optical inspection equipment.

The inspectors concluded that the requirements of TS 4.5.D were

adhered to.

b.

. Unit 2 CROM Coil and Insulation Checks

The inspectors reiiewed the results of EMP-C-EPCR-16, Connecting

Reactor Head Control Rod Drive and Positions Indication, dated

August 6, 1992. This procedure was performed during the Unit 2

1993 RFO.

One of the purposes of this procedure was to obtain

bridge and meggar readings on the CROM stationary, lift, and

movable coils. All measured readings were within the procedure's

acceptance criteria.

On three separate occasions in 1991 and 1992, individual rods

dropped into the core in Units 1 and 2.

The cause of the dropped

rods was attributed to degraded control rod drive coil stacks.

The licensees routinely performs EMP-C-EPCR-16 each RFO in order

to identify degraded coil stacks. Also the licensee has improved

the material condition of the containment ventilation system that

provides cooling for the CRDMs.

Individual Rods have not dropped

in either unit since January 1992.

c.

Unit 1 Control Rod Assembly Testing

On June 3, 1993, Unit 1 experienced problems with the Rod Control

system while performing the bi-weekly rod exercise test l-PT-6.0,

Control Rod Assembly Partial Movement, dated February 23, 1993.

This event was previously discussed in paragraph 4.e. After

indication that the rod control system problem had cleared, l-PT-

6.0 was performed to verify operability of the rod control system.

The inspectors witnessed the performance of this test and reviewed

the test data.

No discrepancies were identified.

Within the areas inspected, no violations were identified.

6.

Safety Assessment and Quality Verificati~n (40500)

a.

Review of Deviation Report S-93-0741

  • On June 2 the licensee identified via DR S-93-0741 that during the*

Unit 2 RFO, 17 MOVs were tested and left with thrust values

outside of values specified in Design Reference Procedure 2-DRP-

007, MOV Setpoints, dated August 20, 1991.

The DR stated that the

MOVs were returned to service without properly documenting that

10

the as-left thrust values were not in accordance with 2-DRP-007.

The DR stated that although the MOVs were not set in accordance

with 2-DRP-007, they were evaluated as operable with the as-left

settings.

The iispectors discussed this DR with the MOV coordinator and

reviewed 2-DRP-007; SSES 3~03, Controlling Procedure for Providing

Guidelines for the Responsibilities of MOV Engineer, dated January

16, 1992; O-ECM-15090-1, VOTES MOV Testing, dated April 9, 1993;

EWR 93-004, Evaluation of MOV Setpoints, dated April 20, 1993; EWR 93-011, MI Valves Thrust Bands/Surry/1&2, dated March 22, 1993;

and Engineering Transmittal Records dated March 25 and April 19,

1993.

The revised MOV setpoints were not being adequately

controlled in that:

1.

Station personnel did not submit DRs when allowable thrust

limits were exceeded. Step 6.4 of SSES 3.03 states that

when a MOV allowable thrust limit is exceeded, the MOV

cannot be returned to service unless a DR is submitted and

.evaluated. Maintenance personnel verbally notified

engineering or recorded the condition on the WO, notified

operations that the VOTES testing was satisfactorily

completed and the MOV would be returned to service.

2.

Different documents specified different MOV settings for the

same MOV.

The*purpose of 2-DRP-007 is to specify MOV

setpoints. These setpoints are consistently under revision

due to extensi.ve MOV research and testing that is presently

underway.

EWRs and maintenance transmittals were used to

revise setpoints in lieu of revising 2-DRP-007.

The *

inspectors reviewed the required setpoints for specific MOVs

and noted that 2-DRP-007, EWRs, and maintenance transmittals

would specify different setpoints for the same MOV.

The licensee is in the process of correcting these discrepancies

in accofdance with their corrective actions program.

10 CFR 50, Appendix B, Criterion III, Design Control, requires

that measures be established to assure design basis for components

are correctly translated into procedures and instructions. These

measures shall include provisions to assure that appropriate

quality standards are specified and included in design documents

and that deviations from such standards are controlled. Failure

to adequately control MOY setpoints was identified as a violation,

NCV 50-280, 281/93-13-01. This violation will not be subject to

enforcement action because the licensee's efforts in identifying

and correcting the violation meet the criteria specified in

Section VII.B of the Enforcement Policy~

Within the areas inspected, one NCV

was identified.

. 7.

8.

11

Licensee Event Review (92700)

The inspectors reviewed the LERs listed below.and evaluated the adequacy

of the corrective action.

The inspectors' review also tncluded followup

of the licensee's corrective action implementation.

(Closed) LER 50-281/91-010, Loss of Containment Integrity Caused by

Failure of Main Steam Trip Valve Bypass Valve.

During a startup of Unit

2 on October 31, 1991, the C SG MSTV manual bypass valve, 2-MS-155,

became stuck in the mid position. Containment isolation valve, 2-MS-

155, could not be closed, and a loss of containment integrity was

dee la red. A six hour LtO to Hot Shutdown was entered. The valve was *

closed using a hydraulic jacking device, mechanically blocked closed,

  • and the six hour LCO was exited.

As corrective action, the valve was

repaired during a subsequent outage and a CDE was performed on the

failed components.

The inspe*ctors reviewed CDE 119254 which concluded

that the failure was due to inadequate stem lubrication, which ~aused

heavy friction on the stem, and event~al yoke sleeve failure.

The CDE

stated that similar type failures had occurred previously.

As

corrective action, a PM item was implemented to periodically lubricate

the stem on 2-MS-155 and other similar MS valves.

The inspectors

verified that stem lubrication was present on all valves inspected and

that the licensee had developed a PM to periodically lubricate the

applicable MS valves.

The PM requires the stems to be lubricated every

other RFO and will be implemented during the 1994 Fall Unit 1 RFO.

(Closed) LER 50-280/92-05, Loss of Refueling Integrity Due to Inadequate

Procedures and Work Practices. Violation 50-280/92-07-02 was issued as

a result of this event.

Corrective actions will be reviewed when the

violation is closed out.

(Closed) LER 50-280/92-08, Unit 1 Charging/HHS! SI Pump Configuration

Outside Plant Design Basis Because of Inadequate Procedure Change

Implementation. Violation 50-280/92-12-01 was issued as a result of

this event. Corrective actions were reviewed as part of the violation

closed out as *described in paragraph 8 below.

Within the areas inspected, no violations were identified.

Action on Previous Inspection Items (92701,92702)

(Closed) VIO 50-280, 281/91-24-02, Failure to Comply With tbe

Requirements of TS 3.3.B.2 With the A HHSI Pump Inoperable. Since 1981,

both units operated with one of three HHSI pumps in PTL, and under

certain HHSI pump electrical configurations, the A HHSI pump would

Operator

action would have been required to manually start the A pump.

This use

of manual operator action to start a HHSI pump during an accident

condition was not part of the plant's licensing basis and therefore

considered a violation of TS 3.3.B.2 which required two HHSI pumps be

operable when critical.

In letters dated November 20 and December 20,

1991, the licensee re~ponded to this violation and in these letters

12

stated that the following corrective actions would be implemented to

prevent reoccurrence:

  • Revise ~rocedures to ensure that the HHSI pumps are aligned in a

corifiguration where automatic HHSI* pump actuation capability is

maintained.

Review EOPs in order to determine if other major plant components

require manual operator action which is not consistent with design

basis op~ration.

Develop a policy with regard to acceptable operator manual*

intervention which is consistent with the TS definition of

operability.

. .

Issue an Engineering Technical Bulletin to engineering personnel

describing the event and emphasizing the need to ensure solutions

to design issues do not inappropriately substitute manual operator

actions for automatic design functions.

The inspectors reviewed procedures l-OP-CH-002,003, and 004, Charging

Pump A, B, and C Operations, dated July 2, 1992, and October 8, 1992,

and verified that these procedures contained appropriate instructions

for configuring HHSI pumps when a HHSI ~ump is taken out of service.

The licensee has modified HHSI pump configuration such that all three

pumps in each unit are aligned for automatic start during normal

operation.

In this configuration, no operator intervention is required

to mitigate the initial phase of an accident~

The licensee reviewed EOPS to determine if other major plant components

require manual operator action which is inconsistent with design basis.

This review identified no additional concerns.

The policy developed by the licensee with regard to acceptable operator

manual intervention that is consistent with the TS definition of

operability was previously reviewed by the inspector and considered

adequate. This was discussed in NRC IR 50-280, 281/92-23.

{Closed} VIO 50-281/91-21-01, Failure to Maintain RMT Interlocks

Operable.

TS 3.3.A.6 requires that with the reactor critical, all

valves, piping, and interlocks associated with the RWST and high and low

head SI pumps that are required to operate under accident conditions be

operable. This issue involved the licensee violating TS 3.3.A.6 by

placing the RMT key switches in the refueling position and bypassing the

automatic mode of operation.

In a letter dated October 15, 1991, the

licensee responded to this violation.

In the letter, the licensee

stated that TSs would be revised to add explicit operability

requirements for the RMT system and the use of administrative control

would be reviewed to ensure that manual operator actions are not

inappropriately substituted for automatic actions required by TSs.

On

August 7, 1992, the licensee submitted a TS change to the NRC for

' ;

9 .

13

approval.

The inspectors reviewed the proposed change-and concluded

that RMT automatic mode of operation was adequately addressed~

The

inspectors also have routinely monitored the licensee's use of

administrative controls and have noted that manual operator actions have

not been inappropriately substituted for automatic action.

(Closed) VIO 50-280, 281/92-04-01, Failure to Implement Adequate

Corrective Actions to Prevent Repetitive HHSI Pump Lube Oil TCV

Failures.* This issue involved inadequate corrective actions which

resulted in reoccurring HHSI pump lube oil TCV failures. The licensee

responded to this violation in letters dated April 27, and September 22;

1992~

In these letters, the licensee stated that six TCVs would be

replaced with an improved design as a long term corrective action. The

inspectors reviewed DCP 92-27-03, Charging Pump SW TCV Replacement,

dated April 28~ 1992, and verified that the TCVs were replaced with.new

globe valves d~signed to be less *susceptible to clogging from debris in

the SW system.

(Closed) VIO 50-280/92-12-0l, Failure to have HHSI Pumps Operable in

Accordance With TS 3.3.B.2. This issue is similar to VIO 50-280,281/91-

24-02 in that HHSI pumps in-unit 1 were configured such that operator

action would have been required to start*a HHSI pump under certain

accident scenarios which is not in accordance with the facility design

basts. Although these violations were similar, they were attributed to

different root causes.

The first violation occurred because manual

operator intervention was accepted as an alternative to automatic

action, and the second violation occurred due to inadequate development

and implementation of a procedure change.

In a letter dated August 12,

1992, the licensee responded to VIO 50-280/92-12-01.

In this letter,

the licensee stated that station processes which change or modify *

procedures, programs or plant systems would be reviewed to ensure that

change control or process was properly managed.

A task team, led by the

Assistant Station Manager, O&M, was formed to review this area. The

task team concluded that the procedures and program change processes

were adequate, but that the station processes for modifying plant

systems needed enhancement. There was not adequate accountability for

changes and too many modifications were being implemented to effectively

manager As a result, the engineering modification backlog was reviewed

- and reduced from 333 proposed modifications to 162 proposed

modifications.

The backlog was reduced by canceling modifications or

scheduling modifications for completion. Other enhancements were made

in the areas of preparation of modification procedural changes and in

training plant personnel on plant modifications. Meetings were held

with station personal emphasizing accountability.

Within the areas inspected, no violations were identified.

Exit Interview

The results were summarized on June 9, 1993, with those individuals

identified by an asterisk in Paragraph 1. The following summary of

inspection activity was discussed by the inspectors during this exit:

Item Number

NCV 50-280,281/93-13~01

LER 50-281/91-010

LER 50-280/92-05

LER 50-280/92-08

VIO 50~280,281/91-24-02

VIO 50-281/91-21-01

VIO 50-280,281/92-04-0l

VIO 50-280/92-12-01

14

Status

Closed

Closed

Closed

Closed

Closed

Closed

Closed

Closed

Description

(Paragraph No.)

Failure to Adequately Control

- Revised MOV Setpoints

(paragraph 6.a).

Loss of Containment Integrity

Caused by Failure of Main

Steam Trip Valve Bypass Valve

(paragraph 7). _

Loss of Refueling Integrity

Due to Inadequate Procedures

and Work Practices {paragraph

7).

Unit 1 Charging/HHS! SI Pump

Configuration Outside Plant

Design Basis Because of

Inadequate Procedure Change

Implementation (paragraph 7)'.

Failure to Comply With the

Requirements of TS 3.3.B.2

With the A HHSI Pump

Inoperable (paragraph 8).

Failure to Maintain RMT

Interlocks Operable (paragraph

8).

Failure to Implement Adequate

Corrective Actibns to Prevent

Repetitive HHSI Pump Luba Oil'

TCV Failures {paragraph 8)~.

Failure to have HHSI Pumps

Operable in Accordance With TS 3.3.B.2 {paragraph 8).

Proprietary information is not contained in this report. Dissenting conunents

were not received from the licensee.

15

10. . Index of Acronyms and I nit i a 1 isms

AOV

ASME -

CDE

CM

CTMT -

CROM -

DBD

DCP

ECCS -

EOPS -

EQ

ESGR -

EWR

HHS!

-

IN

IR

!RPI -

IRS

I&C

LCO

LHSI

-

LER

MER

MS

MSTV

NCV

NI

NRC

NSR

ORB

ORS

PORV -

PSIG -

PTL

UFSAR -

RCS

RFO

RHR

RMT

RO

RSD

RWST

SALP. -

SG

SR

ss

SW

TCV

TPUP -

AIR OPERATED VALVE

AMERICAN SOCIETY OF MECHANICAL ENGINEERS

CAUSE DETERMINATION EVALUATION

CORRECTIVE MAINTENANCE

CONTAINMENT

CONTROL ROD DRIVE MECHANISM

DESIGN BASIS DOCUMENTATION

DESIGN CHANGE PACKAGE

EMERGENCY CORE COOLING SYSTEM

EMERGENCY OPERATING PROCEDURES

ENVIRONMENTAL QUALIFICATION

EMERGENCY SWITCHGEAR ROOM

ENGINEERING WORK REQUEST

HIGH HEAD SAFETY INJECTION

INFORMATION NOTICE

INSPECTION REPORT

INDIVIDUAL ROD POSITION INDICATION

INSIDE RECIRCULATION SPRAY

INSTRUMENTATION AND CALIBRATION

LIMITING CONDITION FOR OPERATION

LOW HEAD SAFETY INJECTION

LICENSEE EVENT REPORT

MECHANICAL EQUIPMENT ROOM

MAIN .STEAM

MAIN STEAM TRIP VALVE

NON-CITED VIOLATION

NUCLEAR INSTRUMENT

NUCLEAR REGULATORY COMMISSION

NON SAFETY RELATED

OPERATIONS REVIEW BOARD .

OUTSIDE RECIRCULATION SPRAY

POWER OPERATED RELIEF VALVE

POUNDS PER SQUARE INCH GAUGE

PULL TO LOCK

.

UPDATED FINAL SAFETY ANALYSIS REPORT

REACTOR COOLANT SYSTEM

REFUELING OUTAGE

RESIDUAL HEAT REMOVAL

REFUELING MODE TRANSFER

REACTOR OPERATOR

REFUELING SHUTDOWN

.

REFUELING WATER STORAGE TANK

SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE

STEAM GENERATOR

SAFETY RELATED

STAINLESS STEEL

SERVICE WATER

TEMPERATURE CONTROL VALVE

TECHNICAL PROCEDURE UPGRADE PROGRAM

~-

TS

VIO

WO 16

TECHNICAL SPECIFICATION

VIOLATION

WORK ORDER