ML18152A220

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Resident Insp Repts 50-280/88-28 & 50-281/88-28 on 880703- 30.Violations Noted.Major Areas Inspected:Licensee Action on Previous Enforcement Matters,Plant Operations,Plant Maint, Plant Surveillance & Plant Startup from Refueling
ML18152A220
Person / Time
Site: Surry  Dominion icon.png
Issue date: 08/25/1988
From: Cantrell F, Holland W, Larry Nicholson
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18152A221 List:
References
50-280-88-28, 50-281-88-28, IEB-85-003, IEB-85-3, NUDOCS 8809140384
Download: ML18152A220 (17)


See also: IR 05000280/1988028

Text

Report Nos.:

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W.

ATLANTA, GEORGIA 30323

50-280/88-28 and 50-281/88-28

Licensee:

Virginia Electric and Power Company

Richmond, Virginia

23261

-Docket Nos.:

50-280 and 50-281

Facility Name:

Surry 1 and 2

License Nos.:

DPR-32 and DPR-37

Inspection Conducted:

'lh :;L

Date Signed rr)

<g' - fJ 5'---o o

L. E.

Date Signed

?Thsko-

trate S'i gned

SUMMARY

Scope:

This routine resident inspection was ~ondu2ted on site in the areas

of licensee action on previous enforcement matters, plant operations,

plant maintenance, plant surveillance, and plant startup from

refueling.

Results:

The following items were identified in this inspection report.

One apparent violation (paragraph 3) was identified for failure to

provide adequate procedures, and/or to follow

procedures

for

cleanliness and foreign material exclusion with regard to maintenance/

modifications on safety-related systems (280; 281/88-28-01).

One unresolved item (paragraph 5) was identified for evaluation and

review of the emergency diesel generator room louvers (280;

281/88-28-02).

One inspector followup item (paragraph 5) was identified involving a

test to demonstrate adequate service water flow to the component

coo 1 i ng water heat exchanger ( CCWHX) without the vacuum priming

system in service (280; 281/88-28-03).

One unresolved item (paragraph 7) is identified for additional review

of the original modification package, and the subsequent safety

reviews associated with the modification of the reactor trip breakers

which allow for remote connection of test equipment (280/88-28-04).

8809140384 880830

PDR

ADOCK 05000280

G

PNU

1.

Persons Contacted

Licensee Employees

REPORT DETAILS

J. Bailey, Superintendent of Operations

D. Benson, Station Manager

H. Blake, Superintendent of Site Services

R. Blount, Superintendent of Technical Services

  • R. Cramer, Superintendant of Projects, Site Services
  • E. Grecheck, Assistant Station Manager
  • R. Johnson, Operations Supervisor
  • R. MacManus, Supervisor, Surveillance and Test Engineering

G. Miller, Licensing Coordinator, Surry

  • H. Miller, Assistant Station Manager
  • J. Ogren, Superintendent of Maintenance
  • J. Price, Site Quality Assurance Manager

S. Sarver, Superintendent of Health Physics

  • Attended-exit meeting.

Other licensee employees contacted included control room operators,

shift technical advisors, shift supervisors and other plant personnel.

The NRC Region II Section Chief, F. Cantrell, visited the Surry Power

Station on July 12 and 13, 1988.

Mr.

Cantrell 1 s tour included all

accessable

uncontaminated areas of Unit 1 including the auxiliary

building, safeguards areas, control room, and emergency diesel generator

rooms.

Unit 1 was heating up from cold shutdown to hot shutdown in

preparation for restart during the tours.

On July 28, 1988, the NRC systematic assessment of licensee performance

(Inspection Report 280; 281/88-05) for the period of September 1, 1986, to

April 30, 1988, was presented to Virginia Power management and discussed

at the Surry Power Station.

The presentation was conducted by C. Hehl,

Deputy Director, Division of Rear.tor Projects (DRP), RII.

Other NRC

personnel that were in att~ndance are listed below. *

M. Ernst, Deputy Regional Administrator, RII

H. Berkow, Director, Project Directorate II-2, NRR

B. Wilson, Chief, Projects Branch 2, DRP, RII

C. Patel, Project Manager, Surry, NRR

W. Holland, Senior Resident Inspector, Surry, DRP, RII

L. Nicholson, Resident Inspector, Surry, DRP, RII

L. Engel, Project Manager, North Anna, NRR

2.

Plant Status

Unit 1

2

Unit 1 began the reporting period in cold shutdown (day 87 of a

maintenance/refueling outage). During this period, the unit completed all

outage-related work and commenced heatup above 200 degrees Fon July 9;

however, when the unit rea~hed approximately 500 degrees Fon July 10,

leakage was identified through a containment isolation valve in the

containment spray system.

The unit entered a 30 hour3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br /> LCD to cold shutdown

in order to repair the leaking valve.

The unit returned to cold shutdown

on July 11.

Repairs were accomplished on the leaking valve, and heatup was

resumed on July 12.

The reactor was taken critical on July 14.

An

i~advertent boration during physics testing on July 14 caused the reactor

to go subcri ti cal; therefore, the contra l rods were admi n i strati ve ly

tripped.

The unit restarted on July 15.

Physics testing was completed

late on that same day.

The final testing of the turbine driven auxiliary

feedwater pump was completed after emergency repairs were made on July 18,

and the unit returned to power operation on the same day.

(Auxiliary

feedwater pump repairs are addressed in paragraph 6.) The unit operated

at power for the remainder of the inspection period.

Unit 2

Unit 2 began the reporting period at power.

The unit operated ~t power

for the duration of the inspection period.

3.

Licensee Action on Previous Enforcement Matters

(92702)

(Closed) Unresolved Item 280; 281/88-26-02, Review of the licensee's

program for control of cleanliness and foreign material exclusion in

safety-related systems or components.

This issue was identified in

inspection report 280; 281/88-26.

In that report, the inspector reviewed

selected administrative procedures relating to cleanliness which were used

by licensee personnel and contractor personnel.

The inspector then

reviewed selected plant work orders and design change packages, and

determined that in several instances, appropriate documentation was not

available in those packages to ensure that cleanliness, or foreign material

exclusion was being maintained during the maintenance activities.

During this inspection period, the inspector continued with his review.

The inspector reviewed the Virginia Power Topical Report, VEP l-5A dated

June, 1986.

In that report, the licensee stated "Cleanliness will be

maintained, consistent with the work being perfor~ed, so as to prevent the

entry of foreign material into safety-related systems. This will include,

as a minimum, documented cleanliness inspections which will be performed

prior to system closure .

11

The inspector discussed this requi rern:ent with

the licensee, and requested that the licensee provide additional

information with regards to other administrative procedures that implement

this position.

3

The inspector continued his inspection with review of the following

administrative

procedures that were

in effect during the Unit 1

refueling/maintenance outage that was completed during this inspection

period.

SUADM-M-02, PLANT HOUSEKEEPING, dated April 30, 1985.

This procedure

provides for guidance with regard to cleanliness and accountability

in critical areas (i.e., reactor cavity when reactor vessel is open,

refueling areas, fuel building, containment, safety-related work

areas, etc.). The inspector considers that this procedure implements

the requirements of the topical report referenced above.

SUADM-M-16, OPERATION OF THE MAINTENANCE DEPARTMENT, dated March 3,

1988.

This procedure provides requirements with regard .to procedural

control of safety-related maintenance activities. The procedure also

defines minor maintenance, as maintenance of a simp1e nature that can

be safely performed without the use of a safety committee approved

procedure.

After review of the above procedures, the inspector reviewed work orders

that were accomplished in the Unit 1 containment

sump

prior to

identification of the inside recirculation spray pump problems which were

discussed in inspection report 280; 281/88-26.

The work orders reviewed

were:

Work Order Job Number (WOJN) 3800062569,

REMOVE

RS SUMP GRATING,

dated 04/18/88.

WOJN 3800062573, INST RS SUMP BLNK (SUMP) PT-16.4, dated 04/18/88.

The inspector noted that both of the above work orders were on a safety-

related system.

However, neither job appeared to have been worked using a

procedure. Also, no documentation was available to identify cleanliness

and foreign material exclusion requirements.

The inspector did note that

WOJN 3800062573 did identify procedure number MMP-C-G-201, CMP FOR FLANGED

JOINTS IN GENERAL, as the procedure which should be used to perform this

work.

However, an add it i ona 1 note on the work order stated that no

procedure was needed.

The inspector reviewed the referenced procedure,

and noted that even if that procedure had been used, no requirements for

system cleanliness or foreign material exclusion were listed, nor would

any

11 as left

11 conditions with regard to cleanliness hav~ been documented.

The

inspector then

reviewed

Design

Change

(DC)

88-01-1,

INSIDE

RECIRCULATION SPRAY PUMP FULL FLOW TEST LINE/ SURRY/ Unit 1, which was

approved for installation by the station safety committee on March 31,

1988.

The inspector specifically looked for cleanliness/foreign material

exclusion controls in the procedure and noted the following:

4

Step 3.5 of the precautions portion of the procedure required that

system cleanliness must be maintained in accordance with ANSI N45.2.l

for a class B system.

The step also required that extreme care

should be exercised when cutting and welding piping to prevent the

introduction of foreign material into the inside recirculation spray

system.

Section 4 of the procedure was the ar.tual work performance section.

In this section, initial engineering inspections and evaluations were

accomplished, the test sump was fabricated, the discharge piping

modifications were accomplished, the pump test piping was fabricated,

and the test 1 ines were installed as required to support testing.

The inspector noted that no steps in this section documented any

cleanliness or foreign material exclusion conditions during, or after

the work was performed.

The inspector discussed the findings with

licensee endineering and management, and concluded that although the

procedure

precaution

(step 3.5

above)

identified

cleanliness

requirements, no procedural requirements were in place to document

actual conditions.

Technical Specification 6.4 requires that detailed written procedures with*

appropriate check-off lists and instructions be provided for preventive

and corrective maintenance operations which would have an effect on the

safety of the reactor, and that these procedures be followed.

The inspector identified two examples (WOJNs of previous page) of failure

to follow procedure with regard to performance of safety-related work

during the Unit 1 outage in April, 1988, as required by SUADM-M-16.

Also,

four examples of failure to follow procedure or inadequate procedure were

identified in' inspection report 280; 281/88-26 with regard to performance

of safety-re 1 ated work during the Unit 2 refue 1 i ng outage in October/

November, 1986.

In addition, documentation of cleanliness controls was

not accomplished as required by administrative procedure (SUADM-M-02).

The inspector also identified three examples of inadequate procedure in

the plant modifications area in that DC' 88-01-1, DC 86-13-1, and DC

87-22-1, were accomplished on safety-related systems during the Unit 1

outage, without documenting cleanliness or foreign material exclusion

conditions prior to system closure as required by the topical report.

In

addition, the inspector determinP-d that the engineering and construction

administrative procedures do not require documentation as stated in the

topical report.

Add it i ona 1 ex amp 1 es of inadequate procedure were i dent i fi ed when the

licensee attempted to test the lA inside recirculation spray pump, and

found foreign material (nuts, bolts, washers, welding rod, etc.) in the

discharge strainer on the test line.

Subsequent inspections of both the

Unit 1 and 2 containment sumps revealed additional foreign material in the

suction

piping

for

other

safety-related

systems

(i.e.,

outside

recirculation spray and

low head safety injection systems).

This

condition was reported to the NRC in licensee event report (LER) 280/88-17

5

(an additional example of failure to follow procedure is identified in

Section 7).

With regard to containment pump cleanliness problems, the licensee's

Engineering Work Request ( EWR)88-247 of June 16, 1988, evaluated the

material found in the Unit 2 pump and its impact on Unit 2 pumping systems

(inside recirculation spray, outside recirculation spray, and low head

safety injection) and the systems' operability.

For Unit 2, the licensee

concluded that there was a low probability of the material in the sump

affecting the ab1lity of any of these pumps to perform their function to

mitigate the consequences of an accident.

The inspectors examined a list

with a description of debris found in the Unit 1 sump.

An EWR for Unit 1

was not completed during this reporting period. Additional discussion of

sump cleanliness and pump operability are scheduled during an enforcement

conference on September 16, 1988.

From

the

information

provided

above

and

in

Inspection

Report

50-280;281/88-26,

it is apparent that foreign material exclusion/

cleanliness was not being implemented as described. by the topical report.

These problems were programmatic in nature with at least one specific

example (the two containment sump problems predominant).

The fact that

the containment sumps were not adequately maintained free of foreign

material has the potential to jeopardize the operation of safety related

systems which can mitigate the consequences of a major accident.

It is

noted that cleanliness problems associated with the safety related pumps have

been addressed by the licensee.

Both containment sumps were cleaned. The

results of the initial flow test of the Un1t 1 inside recirculation spray

pumps were marginal.

Both pumps were rebuilt, and retest results met

requirements before restart of the unit.

Failure to provide an adequate procedure, and/or to follow that procedure

for cleanliness/foreign material exclusion with regard to maintenance or

modifications

on

safety-related

systems

is

a

violation

(280;

281/88-28-01).

The above examples of the violation were discussed with station management

on several occasions during this inspection period.

The discussions with

quality assurance (QA) management provided information which indicated

that the licensee's QA performance evaluation program observations early

in the Unit 1 outa~e were identifying material control and system cleanli-

ness problems.

These QA observations were presented to station management

on May 10, 1988, well in advance of the identification of the containment

sump foreign material/cleanliness problems.

However, it should be noted

that the inspectors' findings were not as a result of the QA observations.

The inspector also was informed near the end of the inspection period that

corrective actions for the noted conditions were being implemented.

The

inspector reviewed Maintenance Department Standing Order No. 88-1 dated

July 29, 1988, and noted that the standing order provided specific

instructions to department personnel with regard to ensuring that foreign

6

material exclusion is practiced during maintenance activities. Also, the

inspector reviewed a memorandum from the site services superintendent to

station management dated July 29, 1988, that identified specific actions

relating to cleanliness inspection and protection for safety and

non-safety related systems that was in the process of being implemented by

site services.

However, the inspection period ended prior to being able

to observe any results of the above directives.

Within the areas inspected, one apparent violation was identified.

4.

Unresolved Items

Unresolved items are matters about which more information is required to

determine whether they are acceptable, or may involve violations or

deviations. * One new unresolved item (paragraph 5) was identified for

review of the licensee evaluation and corrective actions of the emergency

diesel generator r6om louvers. Also, one new unresolved item (paragraph 7)

was identified for additional review of the original modification package,

and subsequent safety reviews associated with the modification of the

reactor trip breakers which allows for remote connection of test

equipment.

5.

Plant Operations

Operational Safety Verification

(71707)

The inspectors conducted daily inspections in the following areas:

control room staffing, access, and operator behavior; operator adhererice

to approved procedures, technical specifications, and limiting conditions

for operations; examination of panels containing instrumentation and other

reactor protection system elements to determine that required channels are

operable; and review of control room operator logs, operating orders,

plant deviation reports, tagout logs, jumper logs, and tags on components

to verify compliance with approved procedures.

The inspectors conducted weekly inspections in the following areas:

verification of operability of selected ESF systems by valve alignment,

breaker positions, condition of equipment or component(s), and operability

of instrumentation and support items essential to .system actuation or

performance.

Plant tour.s included observation of general plant/equipment conditions,

fire protection and preventative measures, control of activities in

progress, radiation protection controls, physical security controls, plant

housekeeping conditions/cleanliness, and missile hazards.

The inspectors

routinely monitor the temperature of the auxiliary feedwater pump

discharge piping to ensure steam binding is prevented.

The inspectors conducted biweekly inspections in the following areas:

verification review and walkdown of safety-related tagout(s) in effect;

review of sampling program (e.g., primary and secondary coolant samples,

7

boric acid tank samples, plant liquid and gaseous samples); observation of

control room shift turnover; review of implementation of the plant problem

identification system; verification of selected portions of containment

isolation lineup(s); and verification that notices to workers are posted

as required by 10 CFR 19.

Certain tours were conducted on backshi fts or weekends.

Backs hi ft or

weekend tours* were conducted on July 4, 7, 9, 10, 11, 13, 14, 15, 16, 17,

18, and 29.

I_nspections included areas in the Units 1 and 2 cable vaults,

Unit 1 containment, vital battery rooms, steam safeguards areas, emergency

switchgear rooms,

diesel

generator rooms,

control

rooin,

auxiliary

building,

cable penetration areas,

independent spent fuel

storage

facility, low level intake structure, and the safeguards valve pit and

pump pit areas. Reactor coolant system leak rates were reviewed to ensure

that detected or suspected leakage from the

system was

recorded,

investigated, and evaluated; and that appropriate actions were taken, if

required.

The inspectors routinely independently calculated RCS leak

rates using the NRC Independent Measurements Leak Rate Program (RCSLK9).

On a regular basis, radiation work permits (RWPs) were reviewed, and

specific work activities were monitored to assure they were being

conducted per the RWPs.

Selected radiation protection instruments- were

periodically checked, and equipment operability and calibration frequency

were verified.

In the course of monthly activities, the inspectors included a review of

the licensee 1 s physical security program.

The performance of various

shifts of the security force was observed in the conduct of daily

activities to include:

protected and vital areas access controls;

searching of personnel, packages and vehicles;

badge

issuance and

retrieval; escorting of visitors; and patrols and compensatory posts.

On July 10, the inspector monitored Unit 1 heatup evolutions that were in

progress from the control room.

Earlier that morning, with heat up in

progress, and temperature greater than 400 degrees F, it was noted that

containment sump inleakage was greater than normal.

Station management

realized that a potential containment integrity issue could be developing,

and instructed operations to begin investigating. At 0900 hours0.0104 days <br />0.25 hours <br />0.00149 weeks <br />3.4245e-4 months <br />, a shift

supervisor log entry was made stating that it appears that one of the

discharge valves to a containment spray pump was

leaking through.

Operations personnel systematically investigated the_problem, and at 0930

hours it was

determined that containment

spray discharge

valve

l-CS-MOV-1018 (which indicated closed), was allowing water to leak from

the refueling water storage tank (RWST) into containment,

and was

collecting in the containment sump.

Control room operators subsequently tried to cycle and reseat the valve,

but sump inleakage remained at an elevated rate.

The inspector witnessed

the ensuing control room discussion between the shift supervisor, two

additional senior reactor operators (SRO),

and the Unit 1 reactor

operator.

The discussion concluded that the valve was in fact leaking an

8

unknown

amount,

and

as

such constituted a potential violation of

containment integrity.

At 1035 hours0.012 days <br />0.288 hours <br />0.00171 weeks <br />3.938175e-4 months <br />, the SRO responsible for Unit 1

ordered the plant heatup stopped at just below 500 degrees F, and started

a 30-hour clock (limiting condition for operation, LCD) to cold shutdown

in accordance with Technical Specification (TS) 3.0.1 due to a potential

violation of containment integrity.

Station management was informed of the shift supervisor's decision to

enter the LCD, a~d stop the heatup based on leakage past the containment

isolation valve.

The inspector monitored the station management briefing

of this situation and observed senior station management state that the

heatup should continue while at the same time remaining in the LCO to cold

shutdown.

A call was then made to the control room stating that the

Station Nuclear Safety and Operating Committee (SNSOC) had agreed that the

plant heatup should continue while a test was being developed to quantify

the leakage.

This decision was reversed, and the unit ultimately placed

in cold shutdown following further discussions between the resident

inspectors, station management, and the unit SRO.

It is important to note that the ultimate decision made by management was

not to resume heatup after entering the LCO, after the inspectors

discussed this sequence of events with station management, and expressed

concern about the message that may be conveyed to the licensed operators

when management directs them to continue with plant startup while in a

Technical Specification Action Statement that requires the unit to go to

cold shutdown.

Although station management was concerned about the

integrity of containment*, and felt that more time for evaluation was

needed to better understand if a true containment integrity problem did

exist, the order to continue heatup while in the LCO, although legally an

option, appeared to be a nonconservative approach.

On July 12, the inspector witnessed the Unit 1 heatup past 350 degrees F,

and independently verified that all engineered safety equipment required

to be operable to exceed 350 degrees F was in fact returned to service.

This review included both a procedural audit, and control board walkdown

of applicable switches and relays.

Procedure adherence was adequate with

no discrepancies noted.

The inspectors performed an operational assessment of the cooling air

supply to the emergency diesel generators (EOG) during this inspection

period.

The EOGs are completely enclosed in rooms, and depend on air

entering the room through the room's intake louvers for combustion and

cooling air. Heat is removed from the EOG cooling water by forcing air

over a radiator and exhausting out of the room.

The inspectors expressed

concern regarding the operation of the room louvers that must open to

allow air into the EOG rooms.

After identification of the issue by the

inspectors, the station secured the air supply to the louvers, causing

them to remain open, until an evaluation of the concern could be

performed .

9

The main air intake louvers are located at the top of each diesel room,

and consist of ten pane 1 s conected in pairs to five actuators.

Each

actuator requires station service air to compress a spring to keep the

louvers closed.

The station service air is supplied through two parallel

solenoid valves that reposition and vent the supply air to the actuators

on a start signal from the EOG.

The air system, valves and louvers were

not procured as safety related equipment and are not seismically

qualified.

Review of licensing documentation did not specifically

disclose safety-related considerations for this system.

Engineering Work Request (EWR)88-296 documented the station evaluation of

the concerns relating to this issue.

The inspector reviewed the EWR and

discussed the following items w1th station management and staff:

It takes a calculated differential pressure across the louvers equal

to one and one-half inches of water to force them open against the

normal pressure of service air.

Since the louvers open into the

room, the measured differential pressure of 2.6 inches across the EOG

fan should be adequate to open the louvers even if the service air

system failed to isolate and vent.

This fact was not included in the

original EWR but was stated by the licensee.

The diesel requires 35,500 CFM of air for starting and cooling.

Each

of the ten panels per diesel allows 13,500 CFM of air to enter the

rooms, thus requiring three of the ten panels to open.

A periodic verification that the louvers are functioning properly is

indirectly performed each time the EOG is started per operating

procedure 1-0P-6.1.1, No. 1 Emergency Diesel Generator, Exercise

Start From MCR.

The inspector commented that the step that checks

the louvers could easily be confused with a check of the engine

radiator louvers.

Station engineering had initiated an effort to replace the existing louver

system with an upgraded system prior to this inspection. This effort is

currently in the initial design and planning stage.

The inspectors noted

the importance of these louvers, and offered the following comments:

Field verification that the louvers will in fact open with a complete

failure of the service air system to isolate and vent off pressure

has not been performed.

Although calculations indicate that the_

differential pressure across the louvers with the EOG running should

must open for the EDGs to perform their safety function; thereby,

preventing this louver system from being an entirely passive system.

The fact that the louvers are not classified as safety related has

contributed to a lack of appropriate attention being placed on their

maintenance and upkeep.

This condition was demonstrated on July 6,

1988, when the air system was isolated from all the louvers and 11 of

the 30 panels failed to function properly.

10

The licensee agreed with the above comments and stated that the louver

system would remain in the present failed open condition until the system

is either removed, rep 1 aced, or restored to a fully operab 1 e status.

In

any case, an evaluation will be performed by the licensee to determine if

any portion of the louver system should be safety related. The licensee

stated that they will defer any decision on testing of the presently

in sta 11 ed system unt i 1 a permanent course of action is d_etermi ned.

The

inspectors will review the licensee cictions,

and final

resolution

regarding the adequacy of the louver system and its safety classification.

This item is identified as an unresolved item (URI 280; 281/88-28-02)

pending licensee actions, and the inspector's completion of these reviews.

On July 14, the inspector witnessed Unit 1 return to criticality after

completion of a three month refueling/maintenance outage.

The inspector

reviewed the procedures associated with the startup, and monitored pulling

of the control rods until the reactor was critical.

No discrepancies were

noted.

During last month

1 s exit interview with station management on July 5,

1988, the l1censee agreed to conduct a test of the component cooling water

heat exchanger (CCWHX) service water system in order to verify satisfac- *

tory operation through the CCWHX without the use of vacuum priming.

This

test will be conducted after the start of the Unit 2 refueling/maintenance

outage which is scheduled to commence in September 1988.

Prior to

testing, the licensee has agreed to maintain intake canal level at or

above 27 feet.

This test is identified as an inspector followup item (IFI

280; 281/88-28-03).

Engineered Safety Feature System Walkdown

(71710)

The inspector performed a walkdown of the containment isolation system for

Unit 1.

This verification also included the following: confirmation that

the licensee

1 s system lineup procedure matches plant drawings and actual

plant configuration; hangers and supports are operable; housekeeping is

adequate; valves and/or breakers in the system are installed correctly and

appear to be operable; fire protection/prevention is adequate; major

system components are properly labeled and appear to be operable;

instrumentation is properly installed, calibrated, and functioning; and

valves and/or breakers are in correct position as required by plant

procedure and unit status.

Within the areas inspected, no violations or deviations were identified.

6.

Maintenance Inspections (62703)

During the reporting period, the inspectors reviewed maintenance

activities to

assure

compliance with

the appropriate

procedures.

Inspection areas included the following:

OVERHAUL OF TURBINE DRIVEN AUXILIARY FEEDWATER PUMP (l-FW-P-2)

11

On July 15, the licensee attempted to run the Unit 1 turbine driven

auxiliary feedwater pump in order to verify operability as required by

technical specifications prior to the unit exceeding 10 percent power.

During the initial start attempt, the pump indicated initial flow, then

stopped running for some unknown reason.

A licensee evaluation concluded

that the pump was locked up by an internal obstruction.

The unit

operators logged this condition, and a 1 so, 1 ogged the technical specif i-

cat ion requirement that the pump must be proven operable within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />

after the unit was taken critical, or the unit must return to hot shutdown

within the next 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />.

In the next 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br />, the licensee disassembled

the pump, inspected the pump internals and made repairs to the parts which*

caused the pump to lock up, reassembled the pump, and verified operability

in accordance with the 72-hour technical specification requirements.

The inspectors monitored the licensee actions during initial pump testing

which identified the problem, during pump repair evolutions, and during

final operability testing.

The repairs were.accomplished using mechanical

maintenance procedure MMP-C-FW-092 dated October 23, 1987.

The inspector

noted'that although the procedure did provide for a cleanliness inspection

of the lower casing prior to reassembly, it did not maintain foreign

material exclusion control through rotor installation and upper casing

placement.

The licensee also noticed this condition, and during pump

closeout, quality control inspectors were assigned to provide appropriate

coverage for foreign material exclusion during final assembly steps and to

document these cleanliness inspections.

No discrepancies were noted.

The inspectors conducted a comprehensive review of all safety related work

orders that remained outstanding on Unit 1 following the return to full

power operations.

This review also included witnessing select SNSOC

meetings that approved deferral, or recommended completion of work items

prior to leaving the refueling outage.

The inspectors found the overall

process to be adequate, but did note that 19 outstanding work orders

remained unworked which involved safety-related motor operated valves

drawing in excess of 25 percent of ful 1 1 oad amperage.

An Engineering

Work request (EWR 88-266) documented the evaluation, and conclusion that

the elevated supply voltage was the principal cause for the high current

reading on the Limitorque motor operator~.

The engineering report further

stated that although the high current readings could be a indicative of a

problem with the motor operator, a determination should be made on a case

by case basis.

The inspectors discussed the EWR with engineering and.

electricians, and reviewed supporting field data and test results.

In

addition, the EWR recommended a program be established to obtain motor

performance curves, and deve 1 op app 1 i cab 1 e acceptance criteria. * The

licensee incorporated. these recommendations into their committment

tracking system for action; therefore, the inspectors will continue to

monitor progress in this area as a part of their routine inspection

effort.

No discrepancies were noted.

Within the areas inspected, no violations or deviations were identified.

' .

12

7 .. Surveillance Inspections (61726)

During the reporting period, the inspectors reviewed various

surveillance activities to assure compliance with the appropriate

procedures as follows:

Test prerequisites were met.

Tests were performed in accordance with approved procedures.

Test procedures appeared to perform their intended function.

Adequate coordination existed among personnel involved in the test.

Test data were properly collected and recorded.

Inspection areas included the following:

TESTING OF THE UNIT 1 INSIDE RECIRCULATION PUMP (1-RS-P-lA)

On July 5, the inspector witnessed testing of 1-RS-P-lA in accordance with

special test 1-ST-214, Operability of IRS Pumps.

The stated purpose of

this test was to prove operability of the inside recirculation spray

pumps, and to establish reference values for inside recirculation spray

pump testing in accordance with ASME Section XI, Subsection IWP.

This

test was being accomp 1 i shed after overhaul of the pump; when, during an

earlier run the test data could not confirm that the pump met a 11

operational requirements.

The inspector reviewed the test procedure prior

to test performance, and observed the testing of 1-RS-P-lA from inside

containment.

The following items were noted by the inspector.

The test procedure was used by the craft as the working procedure to

install and remove system/test spoolpieces.

The inspector observed

the system spoolpiece on the discharge side for 1-RS-P-lA laying on

t_he deck during testing.

The flange ends were not blanked as

required by the procedure to maintain cleanliness and no steps in the

procedure-verified that cleanliness or foreign material exclusion was

maintained during the reassembly of the system to its norma 1

configuration. This is an additional example of appare_nt violation

280; 281/88-28-01.

between

room was poor:in that

time

during

testing.

containment

environment

inspectors.

the operator in containment and the control

communication was lost for short periods of

Communications

problems

in

the

noisy

Communication

has

been

frequently

noticed

by

the

Based on his observations, the inspector concluded that the testing was

accomp 1 i shed in accordance with procedure ( except as noted above), and

that results were adequate to evaluate pump operability.

i3

REACTOR PROTECTION LOGIC TESTING

On July 13, the inspector witnessed testing of the rector protection logic

system for Unit 1 in accordance with 1-PT-8.2, dated July 5, 1988, Reactor

Protection Logic.

This test is to ensure the operability of the rector

trip portion of the reactor protection system, * and is required to be

performed at the conclusion of each refueling outage.

Included in this

test are individual tests of train

11A

11 and train

11 B

11 logic channels with

their associated alarms and interlocks that are required to function

during restart and normal operations.

The inspector 'Jbserved a problem with step 5.17 of the above test

procedure that times the reactor trip relays from initiation of a trip

signal in the protection cabinets until the trip breaker ope~s.

The trip

breaker appeared to be opening correctly, but the timer used for this test

was not stopping when the breaker tripped.

The instrument technicians

performing the test repeated the step several times, and concluded that

the wiring in the breaker cubicle must be incorrect.

The problem was then

turned over to the electricians for resolution.

The electricians corrected the wiring discrepancy in the reactor trip

breaker cubicles, and the breakers were subsequently tested satifactorily.

However, the determination and retermination of the two wires inside the

breaker cubicl~ was not specified on either a work order or detailed in

any way in a procedure.

An incorrect assumption was made that the

outstanding work order that installed the breakers (WO# 68076), and the

maintenance procedure invoked by that work order (PC-DB-E/Rl, Reactor Trip

And Bypass Breaker Maintenance) contained the necessary steps to perform

the desired work.

The subject w1r1ng is connected to one of three identical relay terminals

mounted on the breaker that provides breaker status to the various logic

and interlock circuits.

Each relay has ten terminals that are wired to

the various circuits. The wiring that was incorrectly landed connects to

terminals 5 & 6 on the upper relay and runs to a test jack mounted on the

side of the breaker cubicle, thus requiring disconnecting and reconnecting

each time the breaker is removed.

The breakers were removed from their

cubicles and refurbished during the refueling outage.

The inspector

expressed concern that the wiring had previously been connected and

reconnected without

a. written procedure each ti me the breakers were

removed.

The significance of this item was amplified when the inspector obs~rved

the numerous wires connected to the terminals, and the functions the

terminals perform.

Although it is important to recognize the extensive

1 ong-range project to imp rove the procedures currently underway, the

failure to identify a procedure inadequacy and correct the situation on a

component such as the reactor trip breakers is a concern, as wel 1 as the

failure to properly recognize and change the necessary procedure when. the

wiring modification was originally installed.

The inspection period ended

14

prior to the inspector completing his review of these concerns.

This item

is identified as an unresolved item (280/88-28-04) pending completion of

additional reviews of the original modification package, and subsequent

safety reviews associated with this modification.

On July 14, the inspector witnessed testing of the main steam isolation

valves in accordance with test procedure 1-PT-14.2, Main Steam Trip Valves

and Main Steam Non-Return Valves.

This test is required by technical

specifications to ensure that the steam isolation valves will close in a

specified period of time.

The valves functioned as required with no

discrepancies noted in either the test results or the manner in which the

test was conducted.

Within the areas inspected, no violations or deviations were identified.

8.

Plant Startup from Refueling

(71711)

During this inspection period, the inspectors conducted a walkdown of the

Unit 2 containment prior to restart to independently ascertain that

a pp r o p r i a t e p o rt i o n s o f the react o r coo l a n t , rec i r c u l at i o n s p ray , a n d

auxiliary feedwater systems had been properly returned to service and that*

general

containment cleanliness was

adequate.

The

inspect~rs also

witnessed selected portions of the Unit 1 restart including the monitoring

of the following tests:

On July 13, the inspectors witnessed initiation and testing of the

Shutdown Bank A control rods in accordance with 1-PT-7.2, HOT ROD

DROPS.

The inspector noted that the test was

being properly

contra 11 ed by the senior reactor operators in compliance with the

Technical Specification.

No discrepancies were noted.

The inspectors witnessed testing and monitored activities associated

with periodic test 1-PT-28.11, Start-Up Physics Testing.

This

procedure is the contra 11 i ng procedure for several start-up tests

required to be performed at low power levels following refueling.

The inspectors witnessed pretest briefings, verified that specified

conditions were met, and witnessed portions of the following tests:

Reactivity Computer Accuracy Determination

This test determines the reliability range* of the reactivity computer

that is used in subsequent testing by inserting and withdrawing rods

to add or subtract reactivity, and measuring the resulting flux

halving or doubling.

The computer was determined to be accurate

within plus or minus 40 pcm.

No discrepancies were noted.

Isothermal Temperature Coefficient

This test involves measuring the moderator temperature coefficient by

determining the effects of plant temperature changes on reactivity

while maintaining constant rod position and boron concentration.

15

During the initial temperature swing from 546 degrees to 543 degrees,

the reactor went subcritical when

an inadvertant boration of

approximately 30 ppm boron occurred.

The boration was determined to

be from an apparent combination of operator error and leakage past a

boric acid isolation valve.

The SNSOC was convened, and the decision

was made to manualiy trip the control rods and restart the reactor.

A second reactor startup was commenced at 0109 hours0.00126 days <br />0.0303 hours <br />1.802249e-4 weeks <br />4.14745e-5 months <br /> on July 15, but

had to be stopped when an urgent rod failure occurred at 0111 hours0.00128 days <br />0.0308 hours <br />1.835317e-4 weeks <br />4.22355e-5 months <br />.

Two circuit cards were replaced in the power cabinets, and the urgent

failure alarm was cleared at 0235 hours0.00272 days <br />0.0653 hours <br />3.885582e-4 weeks <br />8.94175e-5 months <br />.

A third reactor startup was

comme~ced at 0257 hours0.00297 days <br />0.0714 hours <br />4.249339e-4 weeks <br />9.77885e-5 months <br /> with a return to criticality at 0329 hour5.

The * boron endpoint was redetermined and an average temperature

coefficient of -3.22 pcm/degree F was .measured.

The inspector witnessed the inadvertant boraticn and preperations for

return to power, and commented that communications between the test

group and the reactor operator could be improved.

The licensee

agreed with this comment and stated that the outage coordinator had

submitted a similar comment.

No

discrepancies in the actual

performance of this test were noted.

Rod Swap Reference Bank Measurement*

This test a 11 ows for measurement of the rod worth ( pcm) of the

reference bank (Control Bank B) when fully inserted from 225 steps to

0 steps.

The inspector witnessed selected portions of this test.

No

discrepancies were noted.

Integral Rod Worth Measurements Using the Rod Swap Technique

This test allows for determination of the differential rod worth of

the reference bank (Control Bank B) when one of the remaining control

rod banks is fully inserted into the core.

The inspe~tor witnessed

this portion of testing when the test bank used was Control Bank C.

No discrepancies were noted.

Additional inspection of startup testing was accomplished by a regional

based inspector during the week of July 18, 1988.

This inspection is

discussed in inspection report 280; 281/88-29.

In the areas inspected, no violations or deviations were identified.

9.

Followup on IE Bulletins (92703)

(Open) IE Bulletin 85-03. As requested by action item e. of Bulletin

85-03, Motor-Operated Valve Common Mode Failures During Plant Transients

Due to Improper Switch Settings, the licensee identified the selected

safety-related valves, the valves' maximum differential pressures, and the

licensee's program to assure valve operability in their letters dated

May 13 and October 17, 1986, and February 24, 1987.

16

Review of these responses indicated the need for addition information

which was contained in Region II letter dated August 18, 1987.

Review of the licensee's September 18,

1987, and January 5, 1988,

responses to this request for additional information indicates that the

licensee's selection of the applicable safety-related valves to be

addressed and the valves'

maximum differential pressures meet the

reqtii rements of the bul 1 et in, and that the program to assure valve

operability requested by action e. of the bulletin is now acceptable.

The results of the inspections to verify proper implementation of this

program, and the review of the final response by action f. of the bulletin

will be addressed in subsequent inspection reports.

This item remains

op~n.

10.

Exit Interview

The inspection scope and findings were summarized on August 3, 1988, with

those individuals identified by an asterisk in paragraph 1. The following

new items were identified by the inspectors duriTig this exit.

One apparent violation (paragraph 3) was identified for failure to provide

adequate procedures and/or to follow procedure for cleanliness and foreign

material exclusion with regard to maintenance/modifications on safety-

related systems (280; 281/88-28-01).

One unresolved item (paragraph 5) was identified for review of the

license~ evaluation and actions regarding the emergency diesel generator

room louvers (280; 281/88-28-02).

One inspector followup item (paragraph 5) was identified involving a test

to demonstrite adequate service water flow to the component cooling water

heat exchanger (CCWHX) without the vacuum priming system in service (280;

281/88-28-03).

One unresolved ftem (paragraph 7) is identified for additional review of

the original modification package, and the subsequent safety reviews

associated with the modification of the reactor trip breakers which allow

for remote connection of test equipment (280/88-28-04).

The licensee acknowledged the inspection findings with no dissenting

comments.

The licensee did not identify as proprietary any of the

materials provided to, or reviewed by the inspectors during this

inspection.