ML18152A210

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Insp Repts 50-280/97-12 & 50-281/97-12 on 971116-1227. Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support
ML18152A210
Person / Time
Site: Surry  Dominion icon.png
Issue date: 01/26/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18152A211 List:
References
50-280-97-12, 50-281-97-12, NUDOCS 9802040061
Download: ML18152A210 (21)


See also: IR 05000280/1997012

Text

Docket Nos:

License Nos:

Report*No:

Licensee:*

Facility:

Location:

Dates:

Inspectors:

Approved by:

9802040061 980126

PDR

ADOCK 05000280

8

PDR

U.S. NUCLEAR REGULATORY COMMISSION

REGION II

50-280-. 50-281

DPR-32, DPR-37

.. 50-280/97-12. 50-281/97-12

Virginia Electric and Power Company (VEPCO)

Surry Power Station. Units 1 & 2

5850 Hog Island Road

Surry, VA 23883

November 16 - December 27. 1997

R. Musser. Senior Resident Inspector

K. Poertner. Resident Inspector.

D. Jones. Senior Radiation Specialist. (Sections Rl.2.

Rl.3 and Rl.4)

H. White_ner. Reactor Inspector. (Sections Ml.2 and

Ml.3)

W. Miller. Reactor Inspector. (Section F8.1)

R. Haag. Chief. 'Reactor Projects Branch 5

Division of Reactor Projects

Enclosure 2

EXECUTIVE SUMMARY

Surry Power Station. Units 1 & 2

NRC Inspection Report Nos. 50-280/97-12. 50-281/97-12

This integrated inspection included aspects of licensee operations.

engineering, _maintenance. and plant support. The report covers a 6-week

period of resident inspection and includes the~results of:announced

inspections by a regiona-1 radiation specialist and a regional reactor

inspector .. In addition,. the report includes the results of an inoffice review

by a regional: reactor inspector.

Ope rat i ans*

,

A violation was identified for the failure to have appropriate

i nstructi ans aya_i 1 ab] E\\'tq ** return the Alternate Alternating Current

Diesel Generator to service following maintenance activities. This

condition resulted in the generator being unavailable to auto_matically

connect to the station electrical busses for a period of approximately

36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br /> (Section 01. 2).

'

A violation was identified involving the failure to proper.ly perform the

verification that the Alternate.Alternating Current Diesel Generator

breaker control switches were in the Auto-after-Trip position as *

..

required by operator logs (Section 01. 2).

. .

While returning the Alternate *Alternating Current Diesel Generator to

service. the operating crews demonstrated a willingness to accept

inadequate instructions and exhibited a lack of attention to detail and

questioning attitude. This evolution also revealed a weakness in the

control of trainees by qualified watchstanders (Section 01.2).

The plant response to a Unit 2 manual reactor trip was normal except for

a problem with control rod indications. With the unit stabilized at hot

shutdown. inattention of the operating crew to plant conditions resulted

in steam generator power operated relief valve actuations. Maintenance

items identified following the trip were corrected prior to restart of

the unit (Section 01.3).

The shift brief prior to startup and operator performance while taking

the Unit 2 reactor critical were excellent (Section 01.3).

Management's decision to hold Unit 2 power at approximately 35% while

resolving issues with an Anticipated Transients Without Scram Mitigating

System Actuation Circuitry setpoint and with the Turbine Driven

Auxiliary Feedwater Pump was conservative and demonstrated a good safety

perspective (Section 01.3).

Maintenance

A violation was identified for failure to perform post maintenance

testing which was specified in work instructions for the Unit 2 Turbine

Driven Auxiliary Feedwater Pump governor replacement (Section Ml.I) .

2

Maintenance activities involving. emergency diesel generator radiator

louvers. control room chiller. and the screen wash system were completed

in a -thorough and professional *manner.

Maintenance personnel were

knowledgeable of the assigned tasks. procedures were detailed and

_actively used on the job. and cooperation and coordination between

various plant groups were good (Section Ml.2).

Surveillance activities involving the control room chillers. ~n

emergency servicewater pump. and the turbine driven auxil.iary.feedwater

pump were completed in a thorough and professional manner.

Maintenance

  • .personnel were knowledgeable .of the assigned tasks. :procedures were

detailed and actively used on the job. and cooperation and coordination

between various plant groups were good (Section Ml.3).

A non-cited violation was identified for failing to test the remote

manual undervoltage.trip prior toplacing,the reactor trip bypass

breakers inservice as required by Technical Specifications

(Section MB.1).

The operating experience review staff failed to r~cognize the

applicability of improper reactor trip bypass breaker testing to Surry

after this issue was i denti fi ed *in October 1996 at the licensee* s North

Anna Station (Section MB.1).

Engineering

The total number of temporary modifications. four on Unit 1 and none on

Unit 2 .. indicated a willingness to correct problems in an expeditious

manner.

The temporary modifications had safety evaluations which were

completed prior to installation (Section El.1).

Plant Support

Health physics practices were observed to be proper (Section Rl.l).

The licensee's program for transportation of radioactive materials had

been effectively implemented pursuant to Department of Transportation

and NRC regulations.

Enhanced procedures for shipping radioactive

materials were found to be a program strength (Section Rl.2).

The licensee's water chemistry control program for monitoring primary

and secondary water quality had been implemented in accordance with the

Technical Specification requirements and industry guidelines for

pressurized water reactor water chemistry (Section Rl.3).

The licensee had implemented and maintained a program for obtaining and

analyzing samples of reactor coolant and containment atmosphere under

accident conditions in accordance with Technical Specification

requirements and Updated Final Safety Analysis Report commitments

(Section Rl.4) .

3

Security and material condition of the protected area perimeter barrier

were acceptable (Section Sl).

Report Details

Summary of Plant Status

Unit 1 operated at power the ent~re reporting period.

Unit 2 operated at power until December 2 when the unit was manually tripped

by the operating crew (See Section 01.3). The:unit was returned to service on

December 3 and achieved 100 percent power on December 6.

The unit-operated at

or near power for the remainder of the inspection period.

I . Ope rat i ems

01

Conduct of Operations

'

.

.

.

01.1 General Comments (40500. 71707)

The inspectors conducted freque*nt control room tours to verify proper

staffing, operator attentiveness. and adher~nce to approved procedures.

The inspectors attended daily plant status meetings to maintain

awareness of overall facility operations and reviewed operator logs to

verify operational safety and compliance with Technical Specifications

(TSs).

Instrumentation and safety system lineups were peri odi ca 11 y

reviewed from control room indications to assess operability. Frequent

plant tours were conducted to observe equipment status and housekeeping.

Deviation Reports (DRs) were reviewed to assure that potential safety

concerns were properly reported and resolved.

The inspectors found that

daily operations were generally conducted in accordance with regulatory

requirements and plant procedures.

01.2 Inoperable Alternate Alternating Current (AAC) Diesel Generator (DG)

a.

Inspection Scope (71707)

The inspectors reviewed the circumstances surrounding a failure to

ensure that the AAC DG was properly aligned following return to service.

b. Observations and Findings

On November 25: the AAC DG was tagged out for preventative maintenance

activities on the associated electrical busses and breakers.

On

November 26. at 10:30 p.m .. maintenance activities were completed. the

associated tagout was cleared and the AAC DG was returned to service in

accordance with Procedure O-MOP-AAC-002. "Return to Service of the AAC

Diesel Generator." Based on the maintenance activities performed the

licensee determined that an AAC DG run was not required to return the

diesel to an operable status.

On November 28. during the performance of the quarterly AAC DG test. six

breaker control switches were found in the Pull-to-Lock (PTL) position.

With the switches in the PTL position the AAC DG would not have

automatically aligned to the associated station busses.

The switches

were returned to Auto-after-Trip and the quarterly AAC DG test was

subsequently performed satisfactorily.

2

Although not addressed in TS. the AAC DG was installed to meet

regulatory requirements.

Consequently, the licensee has established a

14 day administrative limit for the allowed outage time of the AAC DG.

The 14 day administrative limit was not exceeded during the time frame

that the AAC DG was inoperable.

The*switches found

0in the ,PTL position were not addressed in Procedure

O-MOP-AAC-002.

The tagout associated with the maintenance activity

(S0-97-AAC-006) had a hand written note in the comments section that

stated "ensure all switches that have a Pull-to-Lock position are

left in auto after clearing tagout. This applies to 0-AAC-BKR-Ml..

Q.:.AAC-'-BKR-'-M2.' O-AAC.,BKR-M3. O-MC-BKR-L2. O-AAC-'BKR-L3. they are *not

addressed by MOP."

The switches were* not *included in the actual tagout

portion of the clearance.

The tagout comment listed. by equipment

number. the breakers that are controlled by the switches. but did not

provide the applicable switch equipment numbers.

The tagout comment did

not mention that the actual switches which had the PTL feature were

located on a panel that was separate from the actual breakers listed in

the tagout comment.

In addition. the tagout comment did not identify

a 11 the switches . that were subsequently .. found out . of pas it ion.

The

operators performing the return to service did not have a good

understanding of the AAC DG and associated system controls. The

operators did not question that the test switches they verified (located

on the breakers and referenced in the comments section of the tagout)

did not contain a PTL position. This discrepancy was not *identified to

the operator's supervisor.

While returning the AAC DG to service the

operators did not check the control switches with the PTL feature that

were located on another panel.

Technical Specification 6.4.A.7 requires that detailed written

procedures with appropriate check-off lists and instructions be provided

for preventive or corrective maintenance activities which would have an

effect on the safety of the reactor. Procedure O-MOP-AAC-002 and Tagout

S0-97-AAC-006 did not contain appropriate check-off lists and

instructions to return the AAC DG to service following maintenance

activities. The failure to have detailed written procedures and

appropriate check-off lists to return the AAC DG to service is

identified as Violation 50-280. 281/97012-01.

The inspectors reviewed the operator logs associated with the AAC DG.

Procedure "Outside Log" required that the fo 11 owing switches be verified

in the Auto-after-Trip position on a daily basis: O-AAC-1-05M3. O-AAC-1-

05L2. O-AAC-1-05L3. O-AAC-1-05Ll. and O-AAC-1-05Ml.

The operator logs

performed on November 27 did not identify that the switches were in the

PTL position. Discussions with the Operations Department determined

that.the AAC DG logs were taken by a trainee on November 27 with a

qualified operator present. The qualified operator was in the room but

did not directly observe the trainee when the logs were taken.

If the

operator had properly performed his log taking responsibilities the

inoperable AAC DG would have been identified on November 27.

The

failure to follow the requirements of Procedure "Outside Log" is

identified as Violation 50-280. 281/97012-02.

J

3

The licensee initiated a Category 2 Root Cause Evaluation following

discovery of the mispositioned switches.

The licensee had not completed

the evaluation by the end of the inspection period.

c. Conclusions

.

,

-

,,

A violation was identified for the.failure to have appropriate

instructions available to return the Alternate Alternating Current

Diesel Generator to service following maintenance activities. This

condition resulted i~the generator being unavailable to automatically

connect to the station electrical busses for a period of approximately

36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />,

A violation was identified involving the failure to properly perform the

verification that the Alternate Alternating Current Diesel Generator

breaker control switches were in the Auto-after-Trip position as

required by operator logs.

While returning the Alternate Alternating Current Diesel Generator to

service. the operating crews demonstrated a willingness to accept .

inadequate instructions and exhibited a lack of attention to detail and

questioning attitude. This evolution also revealed a weakness in the

control of trainees by qualified watchstanders.

01.3 Unit 2 Reactor Trip and Restart

a.

Inspection Scope (71707)

The inspectors reviewed the activities associated with a Unit 2 manual reactor trip.

b. Observations and Findings

On December 2. Unit 2 was manually tripped from 100 percent power when

Annunciator H-A-8, "Main Steam Trip Valve Closed." was received in the

control room and the reactor operator observed that the "A" Main Steam

Trip Valve (MSTV) indicated an intermediate position. The unit was

stabilized at hot shutdown.

During the reactor trip, six control rods

did not indicate less than 10 steps as required by Emergency Operating

Procedures (EOPs) and the Reactor Coolant System (RCS) was borated an

additional 1100 gallons as required by the EOPs.

All six control rod

indications drifted to zero steps following the reactor trip. Both

source range instruments automatically energized as designed when power

decreased into the source range.

Following the unit stabilization at hot shutdown. the "A" and "B" Steam

Generator Power Operated Relied Valves (PORVs) opened automatically due

to a RCS temperature increase. The operators lowered RCS temperature to

terminate the PORV actuations. Through interviews with the operators.

the inspectors determined that inattention of the operating crew to

4

plant conditions and equipment status caused the unintended RCS

temperature increase and resulting steam generator PORV actuations.

The "A" MSTV did not close during the event.

Inspection of the "A" MSTV

determined that the open limit switch arm was displaced below the valve

position arm resulting in an intermediate indication in the control room

and the annunciator alarm.

When the limit switch was reset. the limit

switch arm and valve position arm had marginal overlap. Prior to

returning the unit to service. the limit switch mounting was modified to

provide more contact area.

The reason the switch became disengaged from

the valve position arm could not be determined.

However. insulation

work_ on,the '.',A" MSJV wa.s Jhought to _be a potential contributor to the

malfunction.

The six rod position indicators that did not indicate less than 10 steps

following the reactor trip were calibrated prior to restart of the unit.

The unit was returned to service at 11:42 p.m. on December 3.

The

inspectors observed the reactor startup. The shift briefing prior to

startup and operator performance while taking the reactor critical were

excellent. Following the return to service of the unit. power was

maintained at approximately 35 percent to resolve an issue with the

Anticipated Transients Without Scram Mitigating System Actuation

Circuitry (AMSAC).

AMSAC is not required below 40 percent reactor

power.

The licensee had previously identified that the system may not

automatically enable prior to 40 percent reactor power based on the fact

that the enable setpoint actuates off turbine first stage pressure.

This item was discussed in more detail in NRC Inspection Report Nos. 50-

280. 281/97-10.

The licensee lowered the AMSAC enable setpoint to

ensure that the system would enable pri.or to 40 percent reactor power.

While the unit was holding at 35 percent power to resolve AMSAC enable

setpoint concerns. the Turbine Driven Auxiliary Feedwater Pump (TDAFWP)

was tested as required by the TS.

During the test. the turbine tripped

on overspeed.

The licensee decided to maintain power at 35 percent

power until the cause of the turbine overspeed was identified and

corrected. The TDAFWP trip is discussed in more detail in Section Ml.1.

The unit was returned to 100 percent power on December 6. following the

replacement of the TDAFWP governor.

c. Conclusions

The plant response to a Unit 2 manual reactor trip was normal except for

a problem with control rod indications. With the unit stabilized at hot

shutdown. inattention of the operating crew to plant conditions resulted

in steam generator power operated relief valve actuations. Maintenance

items identified following the trip were corrected prior to restart of

the unit.

The shift brief prior to startup and operator performance while taking

the reactor critical were excellent.

. -

5

. Management's decision to hold power at approximately 35% while resolving

issues with an Anticipated Transients Without Scram Mitigating System

Actuation Circuitry setpoint and with the Turbine Driven Auxiliary

Feedw.ater Pump was .conservative and demonstrated a good safety

perspective:

08

Misce.llaneous*Operations tssues (90712)

08.1 (Closed) Licensee Event Report (LER) 50-280. 281/97010-00: Missed fire

protection survei 11 ance due to personnel.error. .This event-was

.

discussed in NRC Inspection Report Nos. 50-280 .. 281/97.-10 :and resulted

iri the issuance of a Non-cited Violation; The. inspectors reviewed the

LER and determined that the report adequately described the event ~nd

a-ssoci ated corrective actions.

II. Maintenance

Ml

Conduct of Maintenance

Ml.1 Unit 2 Turbine Driven Auxiliary Feedwater Pump CTDAFWP) Overspeed Trip

a .. Inspection Scope (61726) (62707}

The inspectors reviewed a overspeed trip event of the Unit 2 TDAFWP

  • during testing.

b. Observations and Findings

On December 4. following the return of Unit 2 to operational status. a

TDAFWP performance test was conducted in accordance with Procedure

2:..oPT-FW-003. "Turbine Driven Auxiliary Feedwater Pump 2-FW-P-2." The

Unit 2 TDAFWP operated normally for approximately one minute. and then

began to experience divergent speed oscillations which resulted in an

overspeed trip.

Subsequent to the TDAFWP trip. the licensee started the TDAFWP several

times. and no overspeed trips occurred.

However. computer traces of the

TDAFWP's speed indicated an instability in the operation of the TDAFWP

governor as indicated by convergent oscillations at low speeds.

The

licensee replaced the TDAFWP governor and tested the TDAFWP

satisfactorily on December 6.

An in depth review by the licensee revealed that the Unit 2 TDAFWP

governor had been r-eplaced during the October 1997 Refueling Outage.

The governor was replaced in accordance with Work Order 00310109-01

and-Procedure O-MCM-1403-01. "Terry Turbine Overhaul. 1-FW-T-2 and

2-FW-T-2," Revision 8.

An examination of the maintenance documentation

revealed that Section 6.12 (Governor Post-Maintenance and Operational

Checks) of Procedure O-MCM-1403-01 had not been performed although it

was designated as a post maintenance test requirement in Work Order 00310109-01. Specifically, Section 6.12 of Procedure O-MCM-1403-01

provided instructions to perform final tuning/adjustment of the governor

6

following installation and/or maintenance.

These instructions had been

added earlier as corrective actions for previous problems experienced

with the TDAFWP governors.

The Unit 2 TDAFWP- was tested s.atisfactorily following the October 1997

Refueling Outage.

An examination of the speed traces taken during this

test did not reveal a governor- malfunction. :on December 2. during the

manual reactor trip from 100 percent power.* the TDAFWP automatically

started -.and i nJected as expected.

Based on the.inspectors

1 and

licensee:s review- ofcthese circumstances. past inoperability (from the

refueling outage, until the December" 4,TDAFWP trip) could not.be

cone l us i ve l y demonstrated. : * :

The failure to perform adjustments to the Unit.2 TDAFWP governor in

accordance with Section 6.12 of Procedure O-MCM-1403-01 prior to

returning the machine to :service is* a failure to follow safety related

work procedures. This is a violation of TS 6.4.A.7 and will be tracked

as Violation 50-281/97012-03.

c. Conclusions

A violation wa?_ i_dentified.for-faHure* to**perform post maintenance

testing which was specified in work instructions for the .Unit 2 Turbine

Driven Auxiliary Feedwater Pump governor replacement.

Ml.2 Maintenance Observations

a.

Inspection Scope (62707)

The inspectors observed all or portions of and/or reviewed documentation

for the Work Orders (WOs) and the Design Change Packages (DCPs)

discussed below.

b. Observations and Findings

Emergency Diesel Generator (EOG) No. 1 Radiator Louvers

The inspectors*observed the licensee initiate a troubleshooting process

in accordance with WO 003730130. Troubleshoot/Repair East Louver

Control.

The WO contained very specific instructions from the system

engineer for the troubleshooting process. The process was performed in

accordance with O-ECM-0701-01. "Emergency Diesel Generator Maintenance."

Revision -4.

The inspectors reviewed the WO and procedure which were

present and followed at the jobsite. The system engineer was present to

support maintenance and observe work progress. The inspectors observed

that the craft were methodical and professional in performance of their

duties and coordination between maintenance. engineering and operations

was good.

The problem was identified as a feedback circuit in the

actuator. A new actuator was tested and installed. Subsequently, the

east EDG radiator louvers functioned correctly during the post-

maintenance test.

7

In conjunction with the above maintenance activities. the licensee

implemented DCP 94-011.27 using WO 00377350-01. WO 00377350~02 and a

generic procedure. "Standing MI Low Voltage Modifications -Surry/Units

1&2." The inspectors reviewed portions of the design package and

determined that the safety evaluation was appropriate.

The modification

involved the removal of a capacitor in the louver control circuit which

was, initially intended to act as an arc suppressor.

The vendor

indicated that arc suppression was not needed and the capacitors might

cause harm to internal switches. The vendor. Barber-Colman. recommended

removal of the capacitors.

Control Room and Emergency Switchgear Room Chillers

The inspectors observed Preventative Maintenance (PM) activities

performed-on Control Room Chiller 1-VS-E-4B.

The PM was performed in

accordance with WO 00373029-01 and Procedure O-MCM-0814-01. "Control

Room Chiller Maintenance." Revision 1. The PM involved the change out

of compressor oil. inspection and cleaning of oil and suction strainers.

and cleaning of the reservoir.

The inspectors determined that the

procedure was at the jobsite and was followed. the procedure

instructions were thorough. and the technicians were knowledgeable of

the assigned task. Also. foreign material exclusion control was

maintained while the chiller was open.

Screen Wash Pump 2A Discharge Check Valve

The inspectors observed maintenance personnel replacing a check valve in

the discharge piping of Screen Wash Pump 2A.

The check valve was stuck

open causing Pump 2A to spin backwards when parallel Pump 2B was

operated.

The job was performed in accordance with WO 00373932.

The

valve was a flanged connection and involved removal of eight bolts in

each flange and a spool piece between the pump expansion joint and the

valve.

Work instructions were adequate and followed. personnel were

knowledgeable of the task and engineering support was evident from valve

specifications and torque tables being included in the work package.

Screen Wash Pump 2A Motor Replacement

The inspectors observed replacement of the Screen Wash Pump 2A Motor

which had shorted out when the licensee attempted to run the motor after

the maintenance on the discharge check valve.

The licensee stated that

there was not an apparent connection between the failure and the

previous maintenance.

The work was performed in accordance with Urgent

WO 00379533-01 and Electrical Corrective Maintenance Procedure O-ECM-

1404-02. "Low Voltage Motor Maintenance." Revision 1. The work package

was maintained at the jobsite and was followed.

Good coordination was

noted between electrical and mechanical groups.

Welders were available

as needed to remove the pump to motor coupling.

The job was difficult

due to severe corrosion resulting from the salt water environment but

was thoroughly performed.

8

Replace High Level Intak~ Structure Level Probe

The inspectors observed the licensee change out the high level intake

structure level probe in accordance with WO 00376855-01.

Previous

failures of these probes due to biofouling resulted in the licensee

changing out the Unit 2 probe to monitor probe function and the degree

of biofouling. The response time of the old probe was measured at 31

seconds before removal. After installation. the new probe's response

time was 26 seconds.

The acceptance limit for response time was less

than. 66 seconds.

  • *

The inspectors observed that safety measures and foreign material

exclusion control were. in force at;_.the jobsite. Change-out of the

probes involved sending divers into high level screen wash well 2A to

remove the bottom bracket of the probe and sending a technician into the

well to remove the upper bracket. Communication was maintained with

these personnel at all- times and appropriate safety lines were *used. :

Tools used in the well were tethered and an inventory maintained. Also.

a guard was posted at the entrance to the well while the floor grating

was removed.

The various groups involved in the job were well

coordinated and knowledgeable of their assigned tasks. The inspectors

verified that procedures were at the jobsite and followed.

c. Conclusions

Maintenance activities involving emergency diesel generator radiator

louvers. control room chiller. the screen wash system. and the high

level intake structure level probe were completed in a thorough and

professional manner. Maintenance personnel were knowledgeable of the

assigned tasks. procedures were detailed and actively used on the job.

and cooperation and coordination between various plant groups were good.

Ml.3 Surveillance Observation

a.

Inspection Scope (61726)

The inspectors observed all or portions and/or reviewed documentation

for the surveillance activities discussed below.

b. Observations and Findings

Control Room Chiller Performance Tests

The inspectors observed performance testing of Control Room Chillers

1-VS-E-4B and 1-VS-E-40 in accordance with Procedure O-MPM-0210-01.

This procedure provided instructions for verifying chiller and service

water temperature and pressure parameters and is performed three times a

week for early indication of chiller problems.

The procedure was

thorough and provided acceptable ranges for the various parameters.

This test also served as a post maintenance test for the chiller PM.

The inspectors observed that the procedure was at the jobsite and was

9

followed. technicians were knowledgeable of their assigned tasks and

results were documented.

Emergency Servi*ce Water Pump Diesel

-

The inspectors observed the check out of the diesel for Emergency

Service Water Pump 1-SW-P-lC iri accordance with Procedure O-MCM-0703-01.

This test was a combined effort by Operations. Electrical and Mechanical

Maintenance .. and the vendor representative. The inspectors observed *

erigine preparation for start-up, inspection of the engine after start.

adjustment of the idle* speed. -veri fi cation of valve clearance and *.

verification that the ,air shutdown valve would manually trip. the engine.

The test was thorough and -we 11 moni tared. Personnel .were knowledgeable

of the task. and coordination between groups was good.-

Auxiliary Feedwater System

The inspectors observed the functional checkout of the TDAFWP in

accordance with Procedures l-OPT-FW-003 and l-OPT-FW-007.

The

inspectors attended the pre-job briefing and determined that the

briefing was thorough and complete.

Procedures were walked through and

responsibilities were identified. The inspectors observed the periodic

testing of the TDAFWP including verification of steam supply check valve

full flow and backseating, the stroke time of the steam admission

,

valves. vibration measurements and pump flow and pressure measurements

using the recirculation flow path. All parameters were in the

acceptable range and the test was successfully completed. Coordination

between various plant groups was good.

c.

Conclusions

Surveillance activities involving the control room chillers. an

emergency service water pump. and the turbine driven auxiliary feedwater

pump were completed in a thorough and professional manner.

Maintenance

personnel were knowledgeable of the assigned tasks. procedures were

detailed and actively used on the job, and cooperation and coordination

between various plant groups were good.

MB

Miscellaneous Maintenance Issues (92700)

M8.l (Closed) LER 50-280. 281/97011: Improper bypass breaker testing due to

inadequate definition of "in service.* This LER reported the failure to

perform a surveillance test required by TS 4.1.A and TS Table 4.1-1.

item 36.

More specifically, the licensee was not testing the remote

manual undervoltage trip prior to placing the reactor trip bypass

breakers in service as required by TS. Rather. the licensee was testing

the remote manual undervoltage trip after placing the breaker(s) in

service. This matter was discovered at a Management Safety Review

Committee Meeting during a discussion of a similar matter related to an

occurrence at the licensee's North Anna Power Station (Reported to the

10

NRC in LER.338. 339/96009).

The* operating experience review staff

failed to recognize the applicability of improper reactor trip bypass

breaker testing to Surry after this issue was identified in October 1996

at the licensee's North Anna Station.

As corrective action for this matter. the licensee performed the

following;

1) a station deviation report was issued to document the

matter. and 2) the surveillance testing -procedures (for both Unit 1 and

2) were revised to provide.instructions to-test the remote manual

undervoltage trip*prior to placing the reactor trip bypass breaker(s) in

service, The inspectors*observed*the testing-of the Unit 1-reactor trip

bypass breakers fo 11 owing. the revision of the survei 11 ance testing

procedwre.

The remote manual undervoltage trip was tested prior to

placing the reactor tri'p bypass breakers in service.

Failure to test the remote manual undetvoltage trip prior to placing the

reactor *trip bypass breakers inservice is a violation of TS 4.1.A. Table

4.1-1. item 36. This non-repetitive. licensee identified and corrected

violation is being treated as a Non-cited Violation (NCV) consistent

with Section VII.B.l of the NRC Enforcement Policy. This matter is

identified as NCV 50-280, 281/97012~04.

El

Conduct of Engineering

El.l Temporary Modifications

-a.

Inspection Scope (37551)

III. Engineering

The inspectors reviewed the active Unit 1 and Unit 2 Temporary

Modifications (TMs).

b. Observations and Findings

At the end of the inspection period Unit 1 had four active TMs installed

and Unit 2 had no active TMs.

The inspectors verified that safety

evaluations had been performed and approved for all the active TMs prior

to installation of the TM and that the operators were aware of the

i nsta 11 ed TMs .

c. Conclusions

The total number of temporary modifications. four on Unit 1 and none on

Unit 2. indicated a willingness to correct problems in an expeditious

manner.

The temporary modifications had safety evaluations performed

prior to installation .

. ~

11

IV. Plant Support

Rl

Radiological Protection and Chemistry Controls

Rl.1 General Comments (71750)

On numerous occasions <luring the inspection period. the inspectors

reviewed Radiation Protection (RP) practices including radiation control

area entry and exit. survey results. and radiological area material

condi ti ans . * No discrepancies were noted .. and the inspectors determined

that RP practices were proper ..

'

.

Rl.2 Transportation of*Radioactive Materials

a.

Inspection Scope *(86750)

The inspectors reviewed selected elements of the licensee's program for

transportation of radioactive materials to determine whether the

licensee properly processes. packages. stores. and ships radioactive

materials and whether the changes to the Department of Transportation

(DOT) and NRC regulations. which became effective on April 1.1997. had

been implemented.

The review included records for training of personnel

on the changes to the regulations. procedures for prepari.ng radioactive

material for shipment. and shipping papers for selected recent

shipments.

Those procedures and records were evaluated for consistency

with the requirements delineated in 49 CFR Parts 170 - 179. 10 CFR Part

20. and 10 CFR Part 71 for licensed material transported outside the

confines of the plant.

b.

Observations and Findings

The inspectors reviewed the training records for selected individuals

authorized to sign shipping papers and determined that training on the

changes to the regulations had been provided during February, June and

August 1996. i.e .. prior to the effective date of the changes.

The

selected individuals included two *Health Physics (HP) area supervisors

and two HP technicians. The manuals for the above training were also

reviewed and found to have specifically addressed the new rules for the

following topics: Low Specific Activity (LSA) and Surface Contaminated

Object (SCO) hazards. definitions. and requirements; placarding.

labeling. and marking of vehicles and packages; use of Systems

Internationals (SI) units on shipping papers. labels. and emergency

response instructions; package selection; waste classification; shipping

papers; and receipt procedures and surveys. The inspectors reviewed HP

Procedures HP-1071.021. 1071.030. 1071.040. 1072.010. 1072.020.

1072.030. 1072.040. 1072.050. and 1072.060 and determined that the

instructions therein were consistent with applicable DOT and NRC

requirements for selection of an acceptable container for various types

of materials. LSA and SCO classifications. vehicle placarding, package

marking and labeling, use of SI units. contamination and radiation

levels. shipping papers. vehicle inspection. driver's instructions.

emergency response information. and material receipt. The inspectors

' -

12

noted that the procedures included attachments for specific types of

shipments which delineated the pertinent requirements applicable to the

material and/or~hipment type and checklists for assuring that each of

the requirements were met.

The licensee indicated those attachments

were d~veloped to provide the individuals involved in the preparation of

shipments with a readily available listing of the applicable

-

requirements.-

Imp 1 ementat ion of enhanced procedures for shipping

radioactive materials was deemed by the inspectors to be a program

strength.

The licensee used computer programs (RADMAN) for guidance in preparing

radioactive materials for shipment and for generating shipping papers.

~hose programs included libraries of A1 and A v~lues. i.e .. radio

nuclide activity levels used for selection of proper shipping packages.

The inspectors verified that the A1 and A2 values for five selected

radio nuclides listed in those libraries were accurate.

The licensee's shipment logs indicated that. as of mid-November. the

licensee had made 78 shipments of radioactive material this year.* The

inspectors reviewed the shipping papers for four recent shipments

consisting of: liquid waste shipped to a licensed waste processor: dry

active waste shipped to a licensed waste processor for volume reduction:

a cask of resin shipped for disposal: and contractor owned outage

related tools returned as SCOs.

The information on the shipping papers

was found to be consistent with applicable DOT and NRC requirements and

the licensee's procedures.

The inspectors toured interior and exterior storage areas used for

temporary storage of packaged low'."level radwaste awaiting shipment.

radwaste awaiting further processing. or slightly contaminated equipment

held for reuse.

The inspectors noted that the containers were

appropriately labeled.

During the inspection the inspectors called the

emergency response telephone number listed on the shipping papers for a

shipment which was currently in transit and determined that emergency

response and incident mitigation information was readily available.

c.

Conclusions

The licensee had effectively implemented a program for transportation of

radioactive materials pursuant to DOT and NRC regulations.

Enhanced

procedures for shipping radioactive materials was found to be a program

strength.

Rl.3 Water Chemistry Controls

a.

Inspection Scope (84750)

The inspectors reviewed implementation of selected elements of the

licensee's water chemistry control program for monitoring primary and

secondary water quality.

The review included examination of program

guidance and implementing procedures. and analytical results for

selected chemistry parameters. Those procedures and data were compared

13

to the requirements in TSs 3 .1 0-. 3 .1. F and 4 .1 C for monitoring

specific primary coolant chemistry parameters and to the programmatic

requirements. delineated in License Condition 3.K. for monitoring

secondary water chemistry.

b.

Observations and Findings

The inspectors reviewed Virginia* Power Administrative Procedure (VPAP)

2201. "Nuclear Plant Chemistry Program". Revision No. 2. and determined

that. it included provisions for sampling and analyzing reactor coolant

at the prescribed frequency for the parameters required to be monitored

by the TSs.

The procedure also included provisions for monitoring

primary and secondary water quality based on established industry

guidelines and standards. Although the licensee's procedure did not

specifically indicate that their program included implementation of the

Electric Power Research Institute (EPRI) guidelines. for Pressurized

Water Reactor (PWR) primary and secondary water chemistry. the

inspectors used those guidelines as references for evaluating the

effectiveness of the licensee's program. The inspectors noted that VPAP-

2201 listed the sampling frequency and typical values for each parameter

to be monitored. Action levels applicable to various operational modes

were given where appropriate. Guidance was also provided for actions to

be taken if analytical results exceeded prescribed limits. The

inspectors determined that the above guidance and procedures were

consistent with the applicable TS requirements and. with a few minor

exceptions for good cause. the EPRI guidelines.

The inspectors also reviewed records of analytical results for selected

parameters generated during the period September through November 1997.

The parameters selected included dissolved oxygen. chloride. fluoride.

pH, and dose equivalent iodine-131 in reactor coolant; copper and

hydrazine in feedwater; sodium in steam generator blowdown; and

ethanolamine in condensate. Those parameters were maintained well

within the relevant TS limits and within the EPRI guidelines for power

operations. The inspectors noted that the dose equivalent iodine-131 in

the Unit 1 reactor coolant was approximately an order of magnitude

higher than that of Unit 2 due to a leaking fuel rod in Unit 1.

c.

Conclusions

Based on the above reviews. the inspectors concluded that the licensee's

water chemistry control program for monitoring primary and secondary

water quality had been implemented in accordance with the Technical

Specification requirements and industry guidelines for pressurized water

reactor water chemistry.

Rl.4 Post Accident Sampling

a.

Inspection Scope (84750)

The inspectors reviewed implementation of the licensee's program for

obtaining and analyzing samples of reactor coolant and containment

14

atmosphere under accident conditions.

The review included examination

of procedures and records for operation of the High Radiation Sampling

System (HRSS). training of personnel on operation of the system. and

calibration of the system's in-line analytical instrumentation.

The

procedures and records were evaluated for consistency with the

programmatic requirements specified in TS 6.4.M and with the design

bases for system capabilities as described in Section 9.6 of the Updated

Final Safety Analysis Report (UFSAR).

b .. Observattons 1and Findings

The inspectors reviewed 13 procedures pertaining to operation. training.

and calibration of the HRSS.

The procedures included provisions for

operating the system on a monthly basis. alternating between units. for

the purposes of verifying the functionality of the equipment and to

provide continuing on-the-job tratning of personnel in the use of the

equipment. Acceptance criteria were specified for comparison of the

analytical results from the HRSS to results from the routine sampling

methods.

The procedures also provided for weekly calibration of the in-

line analytical instrumentation.

The inspectors determined that the

licensee's procedures were consistent with TS 6.4.M and UFSAR Section

9.6.

The licensee's records for the monthly operational tests of the

HRSS during the period May through October 1997 and the weekly

calibrations of the HRSS in-line analytical instrumentation during the

period September through October 1997 were reviewed by the inspectors.

The records indicated that the tests and calibrations had been performed

at the prescribed frequency and that the results were generally

satisfactory. During October 1997. the licensee had experienced

problems with the apparatus for in-line measurement of pH and boron

concentration of reactor coolant samples.

Work requests were promptly

issued for repair of the equipment.

The inspectors noted that the HRSS

included equipment for collecting diluted and undiluted grab samples for

analysis by onsite or offsite laboratories if necessary.

c. Conclusions

Based on the above reviews and observations. the inspectors concluded

that the licensee had implemented and maintained a program for obtaining

and analyzing samples of reactor coolant and containment atmosphere

under accident conditions in accordance with Technical Specification

requirements and Updated Final Safety Analysis Report commitments.

Sl

Conduct of Security and Safeguards Activities (71750)

On numerous occasions during the inspection period. the inspectors

performed walkdowns of the protected area perimeter to assess security

and general barrier conditions.

No deficiencies were noted and the

inspectors concluded that security posts were properly manned and that

the perimeter barrier's material condition was properly maintained .

  • -

F8

15

Miscellaneous Fire Protection Issues (71750)

F8.l Fire Protection Predecisional Enforcement Conference

On December 4, 1997. an open predecisional enforcement conference was

held to discuss_the results of an NRC inspection conducted durin~ the

period-of August -24 through October 4. 1997.

The inspection-results

-were documented in NRC Inspection Report Nos. 50-280. 281/97-09 which

were se~t to the licensee by letter dated October 30. 1997.

Four

apparent violations were identified in this report.

EEI 50.:280, 281/97009-03, Failure to meet the requirements of Appendix R

for vital bus isolation.

EEI 50-280; 281/97009-04: Failure to meet the requirements of Appendix R

for circuit breaker coordination.

, .

EEI 50-280. 281/97009-05: Failure to promptly correct licensee

identified Appendix R fire protection discrepancies.

EEI 50-280, 281/97009-06: Fai*lure to report Appendix R fire protection

discrepancies which were outside the design basis of the plant.

Based on information developed during the inspection and information

provided during the predecisional enforcement conference. the NRC

determined that violations of NRC requirements had occurred. Apparent

violations EEI 50-280. 281/97009*-03. and EEI 50-280. 281/97009-05 were

identified as Violations (VIOs) 50-280. 281/EA 97-474 01013 and 50-280.

281/EA 97-474 01023 which constituted a Severity Level III problem.

Apparent violation EEI 50-280, 281/97009-06 was identified as a Severity

Level IV violation. VIO 50-280. 281/EA 97-474 02014.

Apparent Violation EEI 50~280, 281/97009-04. has been re-characterized

as a deviation from a commitment in UFSAR Section 9.10. This deviation

is identified as DEV 50-280. 281/97009-09.

V. Management Meetings

Xl

Exit Meeting Summary

The inspectors presented the inspection results to members of licensee

management at the conclusion of the inspection on January 7, 1998,

The

licensee acknowledged the findings presented.

The inspectors asked the licensee whether any materials examined during the

inspection should be considered proprietary.

No proprietary information was

identified.

PARTIAL LIST OF PERSONS CONTACTED

M. Adams. Superintendent. Engineering

R. Allen. Superintendent. Maintenance

..

16

R. Blount. Assistant Station Manager. Nuclear Safety & Licensing

D. Christian. Station Manager

E. Collins. Director. Nuclear Oversight

M. Crist. Superintendent. Operations

B. Shriver. Assistant Station Manager. Operations & Maintenance

T. Sowers*. Superintendent.* Training

B. Stanley .. Supervi so*r. Licensing

_

W. *Thornton. ~uperintendent. RadiologicaJ Protection

IP 37551:

IP 40500:

IP 61726:

IP 62707:

IP 71707:

IP 71750 :.

IP 84750:

IP 86750:

IP 90712:

IP 92700:

Opened

INSPECTION PROCEDURES USED

I ~

Onsite Engineering

Effectiveness of Licensee Controls in Identifying, Resolving, and

Preventing Problems

Surveillance Observation

Maintenance.Observation

Plant *operations

Plant Support Activities

Radioactive Waste Treatment. and Effluent and Environmental*

Monitoring

. ..

.

..

Solid Radioactive Waste Management and Transportation of

Radioactive Materials

Inoffice Review of Written Reports of Nonroutine.Events at Power

Reactor Facilities

Onsite Followup of Written Reports of Nonroutine Events at Power

Reactor Faciliti.es

ITEMS OPENED AND CLOSED

50-280. 281/97012-01

VIO

Failure to have appropriate

procedures/checklists to return the AAC

diesel generator to service following

maintenance activities (Section 01.2)

50-280. 281/97012-02

VIO

Failure to properly perform operator logs

(Section 01. 3).

50-281/97012-03

VIO

Failure to follow work instructions

related to the Unit 2 TDAFWP governor

replacement (Section Ml.1).

50-280. 281/97012-04

NCV

Improper bypass breaker testing due to

inadequate definition of "in service*

(Section M8.1).

50-280. 281/EA 97-474 01013

VIO

Failure to meet the requirements of

Appendix R for vital bus isolation

(Section F8 .1).

~ -

17

50-280. 281/EA 97-474 01023

VIO

Failure to promptly correct licensee

identified Appendix R fire protection

discrepancies (Section FB.1)~

50-280, 281/EA 97-474 02014

VIO

Failure to report Appendix R fire

protection discrepancies which were

outside the design basis of the plant

(Section FB.1).

50-280. 281/97009-09

DEV

Failure to meet the commitments to

Appendix R for circuit breaker

coordination (Section FB.1).

Closed

50-280. 281/97010-00

LER

Missed fire protection surveillance due to

personnel error (Section 08.1).

50-280, 281/97012-04

NCV

Improper bypass breaker testing due*to

inadequate definition of "in service"

(Section MB .1).

50-280, 281/97011-00

LER

Improper bypass breaker testing due to

inadequate definition of "in service"

(Section MB.1).

50-280, 281/97009-03

EEI

Failure to meet the requirements of

Appendix R for vital bus isolation

( Sect i on FB. 1) .

50-280, 281/97009-04

EEI

Failure to meet the requirements of

Appendix R for circuit breaker

coordination (Section FB.1).

50-280, 281/97009-05

EEI

Failure to promptly correct licensee

identified Appendix R fire protection

discrepancies (Section FB.1).

50-280, 281/97009-06

EEI

Failure to report Appendix R fire

protection discrepancies which were

outside the design basis of the plant

(Section FB.1).