ML18152A195

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Insp Repts 50-280/96-07 & 50-281/96-07 on 960616-0727.No Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support
ML18152A195
Person / Time
Site: Surry  
Issue date: 08/26/1996
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18152A196 List:
References
50-280-96-07, 50-280-96-7, 50-281-96-07, 50-281-96-7, NUDOCS 9609100167
Download: ML18152A195 (26)


See also: IR 05000280/1996007

Text

U.S. NUCLEAR REGULATORY COMMISSION

REGION I I

Docket Nos:

License Nos:

Report Nos:

Licensee:

Facility:

Location:

Dates:

Inspectors:

Approved by:

9609100167 960826

PDR

ADOCK 05000280

G

PDR

50-280, 50-281

DPR-32, DPR-37

50-280/96-07, 50-281/96-07

Virginia Electric and Power Company (VEPCO)

Surry Power Station, Units 1 & 2

5570 Hog Island Road

Surry, Va 23883

June 16 - July 27, 1996

M. Branch, Senior Resident Inspector

D. Kern, Resident Inspector

W. Poertner, Resident Inspector

R. Chou, Reactor Inspector (Sections El.I and

El. 2)

L. Garner, Project Engineer (Sections M8.2,

M8.3, M8.4, M8.5, M8.6 and EB.I)

R. Gibbs, Reactor Inspector (Section Ml.3)

E. Testa, Senior Radiation Specialist (Sections

Rl. 1, R2. 1, R2. 2, R3 . 1 and RB. 1)

G. Belisle, Chief, Projects Branch 5

Division of Reactor Projects

Enclosure

EXECUTIVE SUMMARY

Surry Power Station, Units 1 & 2

NRC Inspection Report Nos. 50-280/96-07, 50-281/96-07

This integrated inspection included aspects of licensee operations,

engineering, maintenance, and plant support.

The report covers a six-week

period of resident inspection; in addition, it includes the results of

announced inspections by four regional inspectors.

Operations

Licensee actions with regard to Hurricane Bertha demonstrated a good

safety perspective and ensured that important systems were fully

operable and that the site area was prepared for severe winds

(Section 01.2).

A Unit 1 power reduction to less than 50 percent power was initiated on

July 17 due to failure of a moisture separator reheater stop valve to

reopen following testing.

The valve was repaired/retested and the unit

was returned to full power on July 18 (Section 01.3).

Maintenance

Failure to apply anti-corrosion coatings to the station and emergency

diesel generator battery intercell connections during refueling outage

maintenance had minor safety significance and was treated as a Non-Cited

Violation.

The licensee initially considered the condition acceptable

until the inspectors informed them that the Technical Specifications

(TSs) required the coating to be applied at a refueling outage frequency

(Section Ml.l).

Maintenance personnel properly evaluated and repaired a leak on valve

2-FW-10.

Procedure revisions were initiated to strengthen oversight

controls on the amount of injection material used.

The leak repair crew

was knowledgeable and the prejob briefing effectively addressed

communications, radiation protection escort coverage, stay time, and

radiation work permit requirements (Section Ml.2).

The preventive maintenance program for the low head safety injection

system was found to be comprehensive and was adequately implemented.

No

deficiencies in the program or implementation of the program were

observed (Section Ml.3).

Preventive maintenance activities performed on the Unit 1 C charging

pump were performed in accordance with the procedure requirements

(Section Ml.4).

Number 1 emergency diesel generator testing was satisfactorily

accomplished (Section Ml.5).

Performing preventive maintenance activities on the wrong containment

spray pump had low safety significance and was treated as a Non-Cited

Violation (Section Ml.6).

2

LER 50-280, 281/96006 description scope was incomplete.

It did not

address that TS 4.0.3 was entered for not completing TS surveillance

requirements on station battery 2B (Section MS.I)~

Engineering

The procedures and calculations generated to support heavy load

operations including spent fuel cask operations were adequate to provide

the details for conducting heavy load operation.

The engineers were

knowledgeable in preparing the procedures, calculations, analyses, and

dispositioning the deviation reports.

The crane operator training and

qualification were adequate (Sections El.I and El.2)

Design Change Package 95-019, Normal Switchgear Air Conditioning

Upgrade/Surry/Unit 1&2, was effectively implemented to establish

adequate environmental conditions for control rod drive cabinet

circuitry. Station management's decision to augment normal switchgear

room heating, ventilation and air conditioning with temporary spot

coolers through the summer was prudent (Section E2.l).

Emergency diesel generator fuel oil configuration and existing

operational practices assured that required fuel oil inventories were

being maintained (Section E2.2).

Plant Support

The program for shipping radioactive materials was effectively

implemented (Section Rl.1).

No concerns were identified during review of radiation monitor

calibration and alarm setpoints (Section R2.1).

Housekeeping and the control of contaminated and radioactive material

within the Auxiliary Building, radioactive waste warehouse, scrap

storage areas, and Fuel Handling Building were acceptable (Section

R2.2).

The inspectors concluded that the licensee had implemented and

maintained an effective program to monitor and control liquid and

gaseous radioactive effluents. The projected offsite doses resulting

from those effluents were well within the limits specified in the TSs,

Offsite Dose Calculation Manual, and 40 CFR 190 (Section R3.1).

The licensee had implemented water chemistry control programs in

accordance with the TS requirements.

The licensee was aggressively

sampling and monitoring the primary and secondary water chemistry

parameters (Section RS.I).

Report Details

Summary of Plant Status

Unit 1 operated at approximately 100 percent power until July 17 when power

was reduced to 49 percent to repair the 1 C reheat stop valve (Section 01.3).

The unit was returned to 100 percent power on July 18.

Unit 2 operated at approximately 100 percent power the entire reporting

period.

I. Operations

01

Conduct of Operations (40500, 71707)

01.1 General Comments

The inspectors conducted frequent control room tours to verify proper

staffing, operator attentiveness, and adherence to approved procedures.

The inspectors attended. daily plant status meetings to maintain

awareness of overall facility operations and reviewed operator logs to

verify operational safety and compliance with Technical Specifications

(TSs).

Instrumentation and safety system lineups were periodically

reviewed from control room indications to assess operability.

Frequent

plant tours were conducted to observe equipment status and housekeeping.

Deviation Reports (DRs) were reviewed to assure that potential safety

concerns were properly reported and resolved.

The inspectors found that

daily operations were generally conducted in accordance with regulatory

requirements and plant procedures.

01.2 Hurricane Bertha Preparations

a.

Inspection Scope

During the week of July 8, the inspectors monitored the licensee's

actions regarding preparations for Hurricane Bertha.

The inspectors

reviewed the Updated Final Safety Analysis Report (UFSAR) and the

Virginia Power Hurricane Response Plan, revision 2.

Additionally, on

July 12, the inspectors toured the outside and roof areas of the plant

looking for loose or unsecured items.

b.

Observations and Findings

During the week of July 8, Hurricane Bertha approached the U.S. coast.

The licensee monitored the storm track and implemented severe weather

preparations in accordance with Operations Checklist (DC) - 21, Severe

Weather.

The licensee's hurricane response is triggered by the

prediction of hurricane force winds on-site by the Virginia Power

Weather Center.

Hurricane force winds were not predicted during the

approach of Hurricane Bertha; however, the licensee did implement the

plan on July 12 as a precautionary measure when the storm was predicted

to pass through the area.

The inspectors reviewed the licensee's

c.

01.3

2

preparations, reviewed the status of important systems, and monitored

the storm progress.

The outside and roof areas inspected were clean and

the minor unsecured articles noted were immediately corrected by the

licensee. Maintenance and surveillance activities performed by the

licensee were minimized during the approach of the storm, the shift

operating crew was augmented prior to the arrival of the storm, and all

safety systems were fully operable.

Hurricane force winds were not

observed onsite and the Surry hurricane response plan was terminated at

5:00 a.m. on July 13 when the storm exited the area.

Conclusions

The licensee's actions with regard to Hurricane Bertha demonstrated a

good safety perspective and ensured that important systems were fully

operable and that the site area was prepared for severe winds.

Unit I Power Reduction

On July 17 at 3:12 p.m., during performance of procedure l-OSP-TM-001,

Turbine Inlet Valve Freedom Test, revision 7, the IC Moisture Separator

Reheater (MSR) stop valve did not reopen following close testing.

The

procedure required that power be reduced to less than 50 percent if a

reheat stop or intercept valve failed to reopen.

The required power

reduction reduces stresses on the MSR caused by increased flow rates and

moisture loading. A power reduction was commenced and power was

stabilized at 49 percent at 2:46 p.m., on July 17.

The valve was

repaired, retested and the unit was returned to 100 percent power on

July 18 at 8:20 p.m.

II. Maintenance

Ml

Conduct of Maintenance

Ml.I

Missed Emergency Diesel Generator and Station Battery Surveillance Tests

a.

Inspection Scope (92902)

On June 19 station management determined that anti-corrosion coating had

not been applied to the 18 and 28 station batteries and the No. 1, 2,

and 3 Emergency Diesel Generator (EOG) battery interconnectors within

the period specified in TS.

Operators entered a 24-hour Limiting

Condition of Operation (LCO) in accordance with TS 4.0.3 for failing to

perform the TS required surveillance. Priority I Work Orders (WOs)

were issued, anti-corrosion coating was applied to the battery

interconnections listed above, and the LCO was exited at 5:15 p.m.

The

inspectors reviewed this event to determine the cause and safety

significance of the missed surveillance, and to evaluate the licensee's

corrective actions.

3

b.

Observations and Findings

TS 4.6.C.l.f requires that an anti-corrosion coating be applied to

station battery cell interconnections during refueling outages.

Station

procedures require that the existing anti-corrosion coating be

inspected, but do not specify coating application unless bare metal is

exposed.

While processing a Preventive Maintenance (PM) deferral

request for the 28 station battery, maintenance personnel noted that

refueling outage battery inspection procedures did not require a coating

application.

DR S~96-1379 was initiated to determine whether current

maintenance practices satisfied TS requirements for the station

batteries.

Initial licensee DR review determined that the TSs were

satisfied.

The NRC reviewed the issue and informed station management that failure

to apply the anti-corrosion coating violated the Surry Station TSs.

In

addition, the inspectors informed the licensee that TS 4.6.D.l.e, which

requires anti-corrosion coating be applied to the EOG batteries each

refueling outage, was not satisfied. A TS surveillance requirement

validation project, performed in 1993-1994, had overlooked this same

discrepancy due to personnel error.

The inspectors noted that the TS

surveillance validation project was effectively implemented and

considered this an isolated discrepancy.

Station management directed

appropriate immediate corrective action for this event as discussed in

paragraph (a) above.

The station and EOG batteries remained able to perform their function

during this event.

Battery intercell connection resistance and anti-

corrosion coating condition were consistent with vendor's

recommendations and industry standards.

The inspectors reviewed

ANSI/IEEE STD 450-1987, IEEE Recommended Practice for Maintenance,

Testing, and Replacement of Large Lead Storage Batteries for Generating

Stations and Substations, and EXIDE 58.00, Instructions for Installing

and Operating Stationary Batteries, and concluded that the failure to

reapply the anti-corrosion coating did not adversely impact battery

operability.

The event was reported in Licensee Event Report (LER) 50-280, 281/96006

(Section MS.I) as required by 10 CFR 50.73(a)(2)(i)(B).

The licensee

intends to submit a TS amendment request to revise EOG battery and

station battery refueling cycle surveillance requirements to be

consistent with standard TSs.

Part of this change would remove the

requirement to reapply anti-corrosion coating when the existing coating

was satisfactory.

The revision would also implement a cell

tightness/resistance check similar to that described in standard TS.

The inspectors discussed the intended TS amendment request with

licensing and system engineers.

In addition, schedulers intend to add

anti-corrosion application battery PMs to the upcoming Unit I work scope

pending approval of the TS amendment request.

The inspectors concluded

that the planned corrective actions were appropriate .

':ii

4

c.

Conclusions

Ml.2

a.

b.

Failure to apply anti-corrosion coatings to the station and EOG battery

intercell connections during refueling outage maintenance is a violation

of TS 4.6.C.l.f and 4.6.0.1.e.

The discrepancy had low safety

significance and was initially identified by the licensee in DR S-96-

1379.

This failure constitutes a violation of minor significance and is

being treated as a Non-Cited Violation (NCV), consistent with Section IV

of the NRC Enforcement Policy. This item is identified as NCV 50-280,

281/96007-01.

Feedwater Injection Check Valve Seal Injection Leak Repair

Inspection Scope (62703)

On July 18, operators identified leakage from the Unit 2 feedwater check

valve 2-FW-10 during the monthly containment walkdown.

Feedwater check

valve 2-FW-10 is a containment isolation valve on the C feedwater line

inside containment.

The inspectors monitored repair activities to

determine whether appropriate reactor and personnel safety

considerations were addressed.

Observations and Findings

Mechanics promptly determined the leak was from the valve body to bonnet

at approximately 100 cubic centimeters per minute.

Engineering and

maintenance personnel developed a good repair plan in a timely manner.

The inspectors reviewed Engineering Transmittal (ET) S96-0217, FW Check

Valve Leak Sealing (2-FW-10) Surry Power Station-Unit 2, revision 0, and

associated WO 344933-01.

ET S96-0217 was technically sound.

The WO

provided generally good work instructions.

However, controls to limit

the amount of injection material used were very limited.

The inspectors

determined that a vulnerability for sealant over injection existed.

The inspectors observed that maintenance personnel primarily relied on

vendor experience to limit the maximum amount of sealant injected.

Although the void volume was calculated, neither implementing procedure

O-MCM-1918-01, On-Line Leak Repairs, revision 7, nor the WO specified

the maximum amount of sealant material to be injected.

The inspectors

discussed this observation with maintenance and engineering personnel

who initiated action to strengthen controls on the amount of injection

material to be used.

The inspectors attended the prejob briefing. Operations, maintenance,

and radiological aspects were briefed in excellent detail.

Previous

communications, radiation protection escort coverage, stay time, and

radiation work permit briefing weaknesses were completely addressed.

The inspectors discussed this repair evolution with the work crew and

determined that the crew was knowledgeable and knew the correct amount

of injection material to use for this repair.

The leak repair was

successfully completed on July 25.

5

c.

Conclusions

Maintenance personnel properly evaluated and repaired a leak on 2-FW-10.

Procedure revisions were initiated to strengthen oversight controls on

the amount of injection material used.

The leak repair crew was

knowledgeable.

The prejob briefing effectively addressed

communications, Radiation Protection (RP) escort coverage, stay time,

and Radiation Work Permit (RWP) requirements.

Ml.3

Preventive Maintenance (PM)

a.

Inspection Scope (62700)

This portion of the inspection was conducted to assess the licensee's

preventive maintenance program.

In order to accomplish this effort the

PMs conducted on the Unit 2, Train A, Low Head Safety Injection (LHSI)

system were selected for review.

The inspection included: verification

that all major equipment in the system was subjected to some kind of PM,

review of a sample of all of the latest PMs completed on the system for

technical adequacy (including comparison of the PMs to the applicable

vendor technical manuals for the equipment), review of the adequacy of

the technical justifications for all PM deferrals written on the system

since 1994, and review of the adequacy of the scheduling of future PMs

based on the specified frequency and the latest PM completion date.

In

addition, information in the applicable portions of section 6.2 of the

UFSAR were reviewed for inconsistency with other information reviewed

during the inspection.

The specific components reviewed during the

inspection were as follows:

Flow Transmitter 2-SI-FT-2945: WO 321113-01 (18 month calibration)

and vendor manual 38-R711-00001

Motor Operated Valve 2-SI-MOV-2860A: WOs 332985-01 & 04, 293332-

01, and 294124-01 (electrical and mechanical inspection); vendor

manuals 38-L553-01 (motor), 38-L553-01 (operator), and 38-C473-04

(valve)

Motor Operated Valve 2-SI-MOV-2862A: WOs 332863-01, 333510-01, and

333509-01 (mechanical inspection, electrical inspection, VOTES

testing, respectively), and vendor manual 38-L553-0l (motor), 38-

L553-02 (operator), 38-T459-02 (valve)

Motor Operated Valve 2-SI-MOV-2863A: Inspector verified scheduling

only

Motor Operated Valve 2-SI-MOV-2864A: Inspector verified scheduling

only

Motor Operated Valve 2-SI-MOV-2890C: Inspector verified scheduling

only

6

LHSI Pump 2-SI-P-lA: WO 303989-01 (electrical inspection), vendor

manual 38-W893-49 (motor), and 38-8940-02 (pump)

Pressure Indicator 2-SI-PI-2943: WO 335777-01 (18 month

calibration); no vendor manual available

Relief Valve 2-SI-RV-28458: WO 295137-01 (RV set point check) and

vendor manual 38-C515-00010

Check Valves 2-Sl-243, and 2-Sl-85: WOs 332163-01, 332157-01, and

341826-01 (acoustic testing, full flow testing, and seat leak

check); vendor technical manual not reviewed

Motor Control Center for Valve 2860A, 2-EP-BKR-2Hl-2NlB: WO 293797-01 (Clean, inspect and electrical test of MCC electrical

components); vendor technical manual not reviewed

The inspectors also reviewed 12 PM deferrals.

b.

Observations and Findings

The PM program on the LHSI system was found to be comprehensive and

provided adequate coverage for the important components in the system

that were reviewed by the inspectors.

No technical deficiencies were

noted during the review of the PM work packages, and no deviations from

vendor recommendations concerning periodic maintenance were observed.

PM deferrals were found to be based on sound engineering principles, and

the scheduling of future PMs was accurately reflected in the scheduling

computer data base.

c.

Conclusions

The licensee's PM program for the LHSI system was found to be

comprehensive and was adequately implemented.

No deficiencies in the

program or implementation of the program were observed.

No deficiencies

were noted during the UFSAR review.

Ml.4 Charging Pump 1 C Motor Service and Inspection (62703)

On July 23, the licensee performed a scheduled PM on the 1 C charging

pump.

The inspectors monitored activities in progress to verify proper

implementation of the maintenance program.

The maintenance activity was

accomplished in accordance with WO 00337622 and procedure O-ECM-1412-01,

Charging Pump Motor Maintenance, revision I.

The maintenance activity

consisted of a motor inspection and cleaning, oil flush, and coupled run

to monitor vibration, motor amps, and bearing temperatures.

The

inspectors monitored activities in progress, verified proper isolation,

and verified adequate post maintenance testing was implemented following

the maintenance activity.

The 1 C charging pump maintenance activity

was accomplished in accordance with the WO and maintenance procedure

requirements.

7

Ml.5

Emergency Diesel Generator (EOG) Testing (61726)

The inspectors observed portions of the performance of procedure l-OPT-

EG-001, Number 1 Emergency Diesel Generator Monthly Start Exercise Test,

revision 7, conducted on July 9.

The inspectors reviewed the procedure

and verified that the procedure acceptance criteria was satisfied.

No

discrepancies were noted during the portions of the procedure observed.

Ml.6

Work Performed on Wrong Component (62703)

a.

Inspection Scope

On July 16, a PM was commenced on the Unit 2 B containment spray pump

instead of the Unit 1 B containment spray pump as required by the WO.

The inspectors reviewed the circumstances surrounding the work activity

and the licensee root cause analysis.

b.

Observations and Findings

At 6:00 a.m., on July 16 containment spray pump l-CS-P-18 was tagged out

to perform a lubrication PM activity per WO 340622.

At 8:40 a.m. an

operator performing normal rounds observed a maintenance mechanic

working on containment spray pump 2-CS-P-18.

The pump coupling guard

had been removed and a grease gun was installed. The operator

recognized that work was being performed on the wrong component, stopped

further work activities by the mechanic, and then notified the control

room.

The pump was placed in pull-to-lock at 8:44 a.m., the coupling

guard was reinstalled and the pump was returned to service at 9:04 a.m.

The maintenance activity performed would not have prevented the pump

from operating if a start signal had been received.

The licensee

performed a category 2 root cause analysis.

The inspectors reviewed the

root cause analysis and agreed with the conclusions reached.

c.

Conclusions

Failure to implement the requirements of WO 340622 is a violation of

station administrative procedures.

The discrepancy had minor safety

significance and was identified by the licensee using the DR process.

This.licensee identified and corrected violation is being treated as a

NCV, consistent with Section VII.8.1 of the NRC Enforcement Policy.

This item is identified as NCV 50-280, 281/96007-02.

MB

Miscellaneous Maintenance Issues (92700, 92902)

MB.I

(Closed) LER 50-280, 281/96006:

Failure to Apply Anti-Corrosion Coating

to EOG and Station Batteries. This event is discussed in paragraph

Ml.I.

The inspectors noted that the event description scope was

incomplete in that TS 4.0.3 was entered for not completing TS

surveillance requirements on station battery 28 in addition to station

battery 18 and EOG batteries l, 2, and 3 listed in the LER.

The

licensee intends to submit an LER update to correct this discrepancy.

8

M8.2

(Closed) LER 50-280/94003: Hole in Recirculating Spray Heat Exchanger

Service Water Outlet Piping.

The hole resulted from corrosion at a

point on the outlet piping elbow where the original coal tar epoxy

coating failed.

Immediate corrective actions included replacing the

elbow and verifying that minimum wall thickness existed on similar

piping on the other trains.

Long term corrective actions included:

cleaning by sandblasting, inspections, weld repairs as needed, and

recoating with a new type epoxy.

The inspectors reviewed the work

documentation for the activities completed during the recent Unit 2

outage.

No concerns were identified.

The inspectors verified that the

pipe sections discussed in the LER and which remain to be recoated were

planned to be completed during each unit's next scheduled refueling

outage.

M8.3

(Closed) LER 50-280/94002: Three of Fifteen Main Steam Safety Relief

Valves (SRVs) out of Tolerance due to Minor Setpoint Drift.

(Closed) LER 50-281/95002: Two Main Steam and Two Pressurizer (PZR) SRVs

as Found Lift Setting Out of Tolerance.

The two PZR SRVs as found lift

settings were within+/- 3 percent tolerance as specified in TS

Amendment 207, dated December 28, 1995 and thus would no longer be

required to be reported.

However, PZR SRVs with as found setting

outside the+/- 3 percent tolerance band are discussed in Section M8.5.

Records document that the main steam SRVs, which were found out of

tolerance, were repaired and tested three times to verify that they

would lift within+/- 1 percent of thecTS specified value.

Main steam

SRV as found and as left test data for the period 1988 to 1996 was

reviewed.

During this interval, testing was either performed in place

using Trevitest equipment or the main steam SRVs were sent to Wyle

Laboratory for testing. Testing using Trevitest equipment was

discontinued in 1993.

On Unit 1 there were 9 as found failures out of

55 tests conducted and on Unit 2 there were 3 as found failures out of

74 tests conducted.

The same main steam SRV never experienced two

consecutive as found test failures.

The as found main steam SRV

failures appeared to be random except that all as found failures

occurred after a change in testing equipment, e.g., Trevitest testing

performed after Wyle Laboratory testing. Whether this was coincidence

or indicative of a minor problem with one or both of the test methods

could not be determined.

Due to wear, whenever main steam SRVs were tested at Wyle Laboratory,

they are refurbished.

The inspectors concluded that present testing

practices and the refurbishment program was adequate.

M8.4

(Closed) Violation 50-280, 281/94028-01:

Failure to Stop Work When Work

Instructions Could not be Followed.

The response to the Notice of

Violation (NOV), dated December 27, 1994, identified that additional

guidelines would be provided to ensure adequate implementation

instructions are provided prior to implementing Design Change Packages

(DCPs) and guidelines would include management's expectations when work

instructions cannot be followed.

The inspectors verified that

M8.5

M8.6

9

guidelines were appropriately incorporated into procedures and training

was provided to maintenance and outage and planning personnel as

committed in their NOV response.

(Open) LER 50-281/96003: One PZR SRV as Found Lift Setting Out of

Tolerance.

(Closed) LER 50-280/95008:

One PZR SRV as Found Lift Setting Out of

Tolerance.

This item is being closed for administrative purposes since

it is similar to LER 50-281/96003 which remains open to track this

issue.

The inspector reviewed the documentation associated with the PZR SRVs

repair and subsequent satisfactory tests.

The inspectors had no

questions concerning the repairs performed.

However, an abnormality in

the test data was noted.

For six valves tested, the difference between

the second as found lift setting and the first as found lift setting was

approximately 2 percent greater (three valves), approximately 4 percent

greater (one valve) and less than 1 percent lower (two valves).

The

second as found test was performed immediately after the first test

without any adjustments to the SRVs.

Having four out of six SRVs open

at approximately 2 percent or higher on their second opening seems

unusual.

This observation was discussed with the maintenance engineer

who indicated that the subject had already been discussed with the

vendor.

The cause for this behavior is not known .

There is little industry operational experience with these new style

valves.

The SRVs were procured from Crosby and shop tested by Crosby in

1993.

The Unit 1 SRVs were removed and tested in September 1995.

The

Unit 2 SRVs were removed and tested in February 1995 and May 1996.

Pending review of additional test data associated with these new style

SRVs, this LER will remain open.

(Open) Violation 50-280, 281/94017-02:

Failure to Implement Corrective

Actions to Preclude Repetition of Foreign Material Exclusion (FME)

Deficiencies.

The inspectors verified that the corrective actions

described in the NOV response dated August 17, 1994, were implemented.

Review of audits and quarterly DR trend reports revealed that problems

in the FME area continue to exist.

The quality assurance Foreign Material Exclusion Follow-Up Assessment,

dated August 30, 1995, concluded that FME program requirements were not

consistently applied for work activities for open systems and

contributors to industry events exist at Surry.

The inspectors verified

.that the issues were addressed by the Maintenance Department.

The Third Quarter 1995 Station Deviation Trend Report recommended that a

FME task team be formed to review activities and past assessments and

report the results to management.

Although no task team was formed,

actions were taken to improve FME controls .

10

Nuclear Oversight finding 96-06-02S, Operations/Refueling Activities,

was issued concerning FME problems encountered during Unit 2 refueling

activities in June 1996.

The inspectors observed that the number of DRs associated with FME

problems decreased from six per quarter in mid-1995 to only one or two

during recent quarters. There appears to be no one single cause for the

continuing FME deficiencies.

Based upon documentation reviews and

interviews with station personnel, FME problems areas include personnel

that infrequently implement FME controls and a sensitivity to adversely

affecting surrounding equipment while performing work.

An example from

finding 96-06-02S was greasing the Fuel Building Crane drive wheel

assembly while it was positioned over the Spent Fuel Pool.

Although recognizing the improving trend in this area, problems do

continue. This violation will remain open pending additional inspection

activities to monitor progress in this area.

III. Engineering

El

Conduct of Engineering

El.I Heavy Load Program

a.

Inspection Scope (37700)

The inspectors examined the licensee's responses to the Generic Letters

(unnumbered) dated December 22, 1980, Control of Heavy Loads and 81-07,

Control of Heavy Loads; reviewed the adequacy of the heavy load program

to assure that it was prepared in accordance with regulatory

requirements, appropriate industrial codes and standards; and verified

through record review that the crane operators received proper training

and were qualified to perform the heavy load lifting operations.

The inspectors reviewed a Nuclear Standard for heavy loads, the

licensee's Phase I and Phase 2 responses to NUREG 0612, Control of Heavy

Loads at Nuclear Power Plants, and eight procedures which implement the

licensee's program.

The inspectors reviewed the codes and standards

that were listed as references in the licensee's heavy load program.

The inspectors examined Westinghouse Technical Report WCAP-9198, Reactor

Vessel Head Drop Analysis, revision 0, and three calculations that were

completed to support the responses sent to the NRC for Generic Letter 81-07.

The inspectors' review included the assumptions, theory, and

codes used.

The inspectors also reviewed the records for the training,

qualification, and requalification for 12 crane operators in order to

verify compliance with ANSI codes and the licensee procedure

b.

11

requirements.

The inspectors also reviewed licensee DRs in order to

determine the adequacy of resolution and corrective actions.

Observations and Findings

Inspection of the licensee's responses to the NRC and application of the

requirements and standards provided by the documents listed above

including the associated licensee's procedures indicated that the

licensee was committed to NUREG 0612.

The inspectors verified through

review of programs, procedures, calculations, and records that the

requirements of Phase I based on NUREG 0612 were met.

The seven

requirements are listed below:

Define the safe load paths

Develop load handling procedures

Establish periodic inspection and testing of cranes

Establish training and qualification for crane operators

Special lifting devices should satisfy the guidelines of ANSI

N14.6.

Standard lifting devices should be installed and used in

accordance with the guidelines of ANSI 830.9

Design cranes to ANSI 830.2 or CMAA-70.

Procedures GMP-001 and O-MCM-1150-01 were specified to be used to meet

NUREG 0612 for handling heavy load movements over the reactor core and

the spent fuel pool.

The safe load paths were contained in these

procedures.

Procedures GMP-010 and GMP-C-107 were used in the area of

balance of plant. There are approximately 10 additional existing

procedures that are used for crane maintenance and inspection.

The licensee classified the crane operators into four categories as:

1) mobile crane operators; 2) floor operated overhead crane operators;

3) cab operated overhead crane operators; and 4) cab operated polar

crane operators. During the records review for 12 crane operators, the

inspectors questioned training on several operators for overhead and

mobile crane operations.

The licensee presented the course materials

and the inspectors verified that they covered the training for both

overhead and mobile crane operations, even though the certificates only

stated one type of crane operations.

The licensee issued 21 DRs for heavy load movements during the past two

years.

The inspector randomly selected and reviewed five DRs: S-94-

1558, S-94-1928, S-94-2089, S-95-0379, and S-95-0577.

The inspectors

concluded that the resolution and corrective actions were adequate .

12

In the Phase II response to Generic Letter 81-07, the licensee stated

that the load drop analyses would be performed and submitted to the NRC

for review.

The NRC issued Generic Letter 85-11 and canceled the

requirements contained in the Phase II response.

Therefore, the load

drop analyses were not performed by the licensee except for the reactor

vessel head drop.

c.

Conclusions

The inspectors concluded that the program, procedures, and calculations

for heavy load movements were adequate.

The engineers were

knowledgeable in preparing the procedures, calculations, analyses, and

dispositioning the deviation reports.

El.2 Review of Spent Fuel Pool Cask Programs

a.

Inspection Scope (60855)

The inspectors reviewed five licensee procedures and calculations to

determine Spent Fuel Pool Cask Program compliance with the licensee's

commitments, regulatory requirements, and appropriate industry codes and

standards.

b.

Observations and Findings

The licensee generated calculations to support safe operations around

the spent fuel pool area during cask operations in case of an accidental

cask drop.

The licensee did not have any cask drop analysis for the

transfer from the Crane Enclosure (Fuel Handling Building) to the cask

storage area (ISFSI) even though the cask-carrying truck passes over

diesel generator fuel supply pipes during the transfer.

The di~sel fuel

pipes consist of six pipes which are part of a safety related piping

system.

The licensee's engineers gave the inspectors the following

reasons for not generating a load drop analysis:

The cask is being carried not greater than six inches above the

ground.

If the cask drops, the impact load due to the six-inch

drop will be very small.

The chance to hit all six diesel fuel pipes is very small unless

the cask drops directly into the center of the pipe group.

Every

two pipes supplies a diesel generator and each reactor only

requires one diesel generator to supply its electricity.

A station blackout due to the loss of outside (external) power

will require one diesel generator for safe shutdown or removal of

decay heat if both of the reactors are being shut down or both

units are already in shutdown conditions.

The inspectors accepted the licensee's explanation and considered that

the cask drop analysis is not required if the six diesel fuel lines are

the only safety-rela~ed piping or equipment in the outside cask transfer

13

route.

However, the licensee did perform a soil pressure impact check

  • for the cask truck running over the six diesel fuel pipes.

The inspectors informed the licensee's engineers about the hydrogen

explosion on May 28, 1996, at the Point Beach Nuclear Plant, during a

welding operation to seal a cask cover lid.

The licensee's engineers

said that an explosion is unlikely at Surry, in that, the casks they use

are tightened with bolts and there is no welding involved.

c.

Conclusions

E2

E2.l

a .

b.

The inspectors considered that the procedures and calculations were

adequate.

The fact that no cask drop analysis for the transfer of the

cask from the crane enclosure area to the storage facility was

determined to be acceptable. A hydrogen explosion, similar to the May

1996 Point Beach event, is highly unlikelj to occur during the cask

drying process because no welding is involved.

Bolts are used to

tighten the cask cover lid.

Engineering Support of Facilities and Equipment

Normal Switchgear Room Ventilation Upgrade

Inspection Scope (92903)

In May 1995 Surry Unit 2 experienced two reactor trips due to Control

Rod Drive (CRD) circuit card failures.

The licensee determined that the

CRD circuit cards had become degraded from prolonged exposure to

elevated temperatures.

Short term corrective actions were previously

documented in NRC Inspection Reports Nos. 50-280, 281/95-08 and 95-17.

In May 1996 the Unit 1 and Unit 2 normal switchgear room ventilation

systems were upgraded as a long term corrective action.

DCP 95-019,

Normal Switchgear Air Conditioning Upgrade/Surry/Unit 1&2, was developed

to increase the Heating Ventilation and Air Conditioning (HVAC) cooling

capacity sufficiently to assure the normal switchgear rooms can be

maintained below 83°F.

Prior to this DCP, the HVAC system was sized to

maintain the rooms below 104°F.

The inspectors reviewed the ventilation

modification to determine whether corrective actions had been properly

implemented to preclude event recurrence.

Observations and Findings

DCP 95-019 installed larger capacity evaporator coils which nearly

doubled the normal switchgear room cooling capacity, removed ventilation

damper motor operators which had been unreliable, and reduced room heat

load by deenergizing switchgear space heaters.

The inspectors reviewed

DCP 95-019, associated WOs, and toured the normal switchgear rooms

during periods of elevated outside air temperature.

Room temperature

remained below 83°F when outside air temperature approached 100°F.

The

inspectors determined that DCP 95-019, through revision 13, was properly

implemented .

C.

14

Spot coolers, installed as a Temporary Modification in June 1995,

remained in service providing supplemental cooling to the CRD cabinets

following installation of DCP 95-19.

The inspectors questioned

management's intention regarding whether to make the spot coolers a

permanent design change or to close out the TM.

Station management

decided to continue augmenting normal switchgear room HVAC with the

temporary spot coolers through the summer.

Management intends to

reevaluate the TM for closure after the normal switchgear room HVAC

upgrade has demonstrated reliability through the hot summer period.

Conclusions

The inspectors concluded that the HVAC upgrade was an effective long

term corrective action to establish adequate environmental conditions

for CRD cabinet circuitry. Station management's decision to augment

normal switchgear room HVAC with temporary spot coolers through the

summer was prudent.

E2.2

Emergency Diesel Generator (EOG) Fuel Oil Tank Capacity

a.

Inspection Scope (37551)

TSs require each EOG fuel oil day tank to contain at least 290 gallons

and a total on-site fuel supply of at least 35,000 gallons.

The total

on-site fuel oil supply is required to provide sufficient fuel for one

EOG to run fully loaded for a week.

The UFSAR further specifies that

each EOG fuel oil day tank will have the capacity to support

approximately three hours full load operation.

The day tank is further

defined in the UFSAR to include both the EOG base tank and the attached

auxiliary wall tank located within the EOG room.

The inspectors

reviewed the UFSAR, TSs, engineering calculations, operator logs, and

local fuel oil tank indication to verify that a sufficient EOG fuel oil

supply was maintained.

b.

Observations and Findings

Calculation 01039.3410-M-2, EOG Underground Fuel Oil Storage Tank 7 Day

Usable Fuel Oil Supply, revision 0, states that 33,264 gallons are

required to support full load operation for 7 days.

Calculation

01039.3410-M-3, EOG Base and Day Tank 3 Hour Usable Fuel Oil Supply,

revision 0, states that 643 gallons are required to support full load

operation for 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br />.

Both calculations used the correct EOG fuel oil

consumption rate (198 gph) as independently derived by the inspectors

from Surry specification NUS-74 and correctly accounted for unusable

volumes within the tanks. Operator logs assign minimum acceptable fuel

oil tank levels which are above the TS required values.

In addition,

operator logs require a minimum EOG day tank level which is

approximately 100 gallons above the capacity needed for 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> of

15

operation.

The inspectors visually verified that the EDG day tanks were

filled to required levels.

The inspectors observed that operator logs

used different terms to identify the EDG day tanks than contained on the

tank labels, the UFSAR, and the two referenced calculations.

The system

engineer initiated appropriate action to revise the operator logs and

correct this discrepancy.

c.

Conclusions

The inspectors concluded that the EDG fuel oil configuration and

existing operational practices assured that required EDG fuel oil

inventories were being maintained.

EB

Miscellaneous Engineering Issues (92700)

E8.l

(Closed) LER 50-280/95005:

Error in Calculation to Convert TS NaOH

Volume to Level for the Chemical Addition Tank (CAT).

This error was

also addressed as NCV 50-280, 281/95009-01.

The NCV discussed the

acceptability of the immediate and proposed long term corrective

actions.

In this inspection period, the inspectors verified that

applicable engineering and operating procedures were revised and

implemented.

Specifically, a family of curves was provided in the Curve

Book to correlate percent NaOH concentration at various temperatures to

the indicated level needed to ensure that the TS required minimum volume

was met.

While reviewing 01/02-PT-36, Log Readings, revision 20, the inspectors

noted that the minimum allowed indicated level in the CAT was 98

percent, the value corresponding to the TS maximum allowed NaOH

concentration at 40°F.

However, no notation was provided to inform

Operations that with CAT temperatures less than 40°F, a 98 percent

indicated level would not ensure that the TS required minimum volume

would be available, i.e., at low temperatures further evaluation would

be necessary to verify that TS minimum volume requirements were met.

The Operations Manager indicated that the data logging procedure would

be revised to warn operators of this potential problem.

A review of Unit 1 and 2 CAT temperatures and indicated levels during

the period from December 1995 to March 1996 revealed that the minimum

temperature recorded was 42°F (Unit 1 CAT) and indicated level always

exceeded 98 percent. Thus, the TS required minimum CAT volume level

restriction was met during this cold weather period.

In addition, the

inspectors verified that the Unit 2 hand held computerized data logger

acceptance criteria was consistent with 02-PT-36.

RI

Rl.1

a.

16

IV. Plant Support

Radiological Protection and Chemistry (RP&C) Controls

Transportation of Radioactive Material

Inspection Scope (86750, TI 2515/133)

The inspectors evaluated the licensee's transportation and radioactive

materials programs for implementation of revised Department of

Transportation (DOT) and NRC transportation regulations for shipment of

radioactive materials as required by Title 10 Code of Federal

Regulations (CFR) Part 71.5 and 49 CFR Parts 170 through 189.

b.

Observations and Findings

C.

The inspectors selectively reviewed site transportation procedures and

determined that they adequately addressed the loading, shoring and

bracing of radioactive waste shipments to waste processors; placarding

of radioactive material loads; marking, labeling and placarding for

radioactive waste shipments to disposal facilities; radioactive material

shipment documentation; and radioactive waste surveys for shipment to

disposal facilities.

The inspectors witnessed the radioactive waste

shipment no.: 096-16 made on July 25, 1996 .

The inspectors reviewed the licensee's records for the four most recent

shipments that were made in 1996.

The inspector determined the shipping

papers contained the required information.

In addition, the inspectors

determined that the licensee had maintained adequate records of

shipments of licensed material for a period of three years after

shipment as required by 10 CFR 71.9l(a).

Conclusions

The licensee had effectively implemented a program for shipping

radioactive materials.

R2 Status of Radiation Protection Facilities and Equipment

R2.1

Radiation Monitor Calibrations

a.

Inspection Scope (84750, 82701)

b.

The inspectors reviewed selected radiation monitors for calibration and

alarm set points.

Observations and Findings

The inspectors reviewed selected alarm setpoints and calibration data

and determined that radiation monitors were within their calibration

interval and alarm setpoints were correctly set .

17

c.

Conclusions

No concerns with licensee facilities or equipment or analysis were

identified during the inspection.

R2.2 Tours of Licensee Radiological Control Areas CRCAs) (71750. 83750)

During tours of the licensee's facilities; the inspectors selectively

verified that radiological postings and labels were appropriate for the

radiological hazard.

The inspectors also observed that the housekeeping and the control of

contaminated and radioactive material within the licensee's Auxiliary

Building, radioactive waste warehouse, scrap storage areas, and Fuel

Handling Building were acceptable.

R3

RP&C Procedures and Documentation

R3.l

Control of Radioactive Effluents

a.

Inspection Scope (84750)

TS 6.4 for both units required the licensee to establish, implement, and

maintain a program for the control of radioactive effluents

The

program was required to include limitations on the annual and quarterly

radiation doses from radioactive materials in liquid and gaseous

effluents released to unrestricted areas.

TSs 6.6 and 6.8 for both

units described the reporting schedule and content requirements for the

Annual Radioactive Effluent Release Reports.

The reports were required

to be submitted prior to May 1 of each year and to cover the operation

of the facility during the previous calendar year. Summaries of the

quantities of radioactive materials in liquid and gaseous effluents

released from the facility and an assessment of the radiation doses due

to those releases were required to be included in the reports and an

assessment be made to ensure that doses are below

40 CFR 190 limits.

b.

Observations and Findings

The inspectors reviewed the effluent data compiled from the licensee's

effluent release report for the year 1995.

The values used for 1995

annual dose estimates were taken from the licensee's 1995 Annual

Radiological Environmental Operating Report.

The inspectors also

reviewed the supporting data for the effluent release report covering

the year 1995 and discussed the data presented in reports with the

licensee.

The inspectors determined that one effluent monitor instrument was

inoperable for more than 30 days.

The monitor was 02-SW-RM-220, Unit 2

Discharge Tunnel Radiation Monitor.

Coaxial and high voltage cables

were replaced.

During this period once-per-twelve-hour grab samples

18

were obtained in accordance with the Offsite Dose Calculation Manual

(ODCM).

There were no unplanned liquid or gaseous effluent releases classified

according to the criteria in the ODCM.

There were no major changes to

radioactive liquid, gaseous, and solid waste treatment system during

this reporting period.

No gas storage tanks exceeded the limits allowed by TS 3.7 during the

reporting period. Three minor changes were made to the ODCM during 1995

and were implemented in revision 7 dated October 31, 1995 (Procedure

VPAP-2103).

There were no continuous liquid effluent releases above the

lower limit of detection for either Surry Unit 1 or 2 during this

period.

c.

Conclusions

The inspectors concluded that the licensee had implemented and

maintained an effective program to monitor and control liquid and

gaseous radioactive effluents.

The projected offsite doses resulting

from those effluents were well within the limits specified in the TSs,

ODCM, and 40 CFR 190.

RS Miscellaneous Radiation Protection and Chemistry Issues

RB.I

Primary and Secondary Water Chemistry Review

a.

Inspection Scope (86750, TI 2515/133)

The inspectors reviewed and discussed the results of the licensee's

primary and secondary chemistry program.

b.

Observations and Findings

The inspectors reviewed the chemistry results for the TS data associated

with the primary and secondary water chemistry parameters for the period

from January l, 1996 through July 1, 1996, and determined that all

required TS chemistry results were maintained at small percentages of

limits.

c.

Conclusions

The licensee was aggressively sampling and monitoring the primary and

secondary water chemistry parameters.

F8

Miscellaneous Fire Protection Issues (92904)

F8.l

(Closed) Violation 50-281/96003-06:

Failure to Provide a Continuous

Firewatch.

This violation resulted from the failure of the diesel

generator rear exit door to close following exit from the room by plant

personnel due to welding cables blocking the door open.

Corrective

. *

19

actions for this violation included posting the rear exit door as an

emergency exit only and activating alarms on the doors.

The inspectors

verified that the corrective actions had been completed.

20

V. Management Meetings

XI

Exit Meeting Summary

The inspectors presented the inspection results to members of licensee

management at the conclusion of the inspection on August 1, 1996.

The

licensee acknowledged the findings presented.

The inspectors asked the licensee whether any materials examined during the

inspection should be considered proprietary.

No proprietary information was

identified .

.

.

21

PARTIAL LIST OF PERSONS CONTACTED

Licensee

R. Blount, Maintenance Superintendent

D. Christian, Station Manager

J. McCarthy, Assistant Station Manager, Operations & Maintenance

B. Stanley, Director Nuclear Oversight

J. Swientoniewski, Supervisor Station Nuclear Safety

W. Thorton, Superintendent, Radiological Protection

' *

IP 37551:

IP 37700:

IP 40500:

IP 60855:

IP 61726:

IP 62700:

IP 62703:

IP 71707:

IP 71750:

IP 82701:

IP 83750:

IP 84750:

22

INSPECTION PROCEDURES USED

Onsite Engineering

Design Changes, and Modifications

Effectiveness of Licensee Controls in Identifying, Resolving, and

Preventing Problems

Operation of an ISFSI

Surveillance Observation

Maintenance Implementation

Maintenance Observation

Plant Operations

Plant Support Activities

Operational Status of the Emergency Preparedness Program

Occupational Exposure

Radioactive Waste Treatment, And Effluent And Environmental

Monitoring

IP 86750:

Solid Radioactive Waste Management And Transportation Of

Radioactive Materials

IP 92700:

Onsite Followup of Written Reports of Nonroutine Events at Power

Reactor Facilities

IP 92902:

Followup - Maintenance

IP 92903:

Followup - Engineering

IP 92904:

Followup - Plant Support

TI 2515/133:lmplementation of Revised 49 CFR Parts 100-179 AND 10 CFR Part 71

Opened

50-280, 281/96007-01

50-280, 281/96007-02

Closed

50-280, 281/96006

50-280/94003

50-280/94002

50-281/95002

ITEMS OPENED, CLOSED, AND DISCUSSED

NCV

Failure to Apply Anti-Corrosion Coating to EOG

and Station Batteries (Section Ml.l).

NCV

Performing PM on the Wrong Component

(Section Ml.6).

LER

Station and EOG Battery Connections Not Coated

With Anti-corrosion Material Due to Procedural

Error (Section M8.l).

LER

Hole in Recirculating Spray Heat Exchanger

Service Water Outlet Piping (Section M8.2).

LER

Three of Fifteen Main Steam Safety Relief Valves

Out of Tolerance due to Minor Setpoint Drift

(Section M8.3).

LER

Two Main Steam and Two Pressurizer SRVs as Found

Lift Setting Out of Tolerance (Section M8.3).

l

"! .

50-280, 281/94028-01

50-280/95008

50-280/95005

50-281/96003-06

Discussed

50-281/96003

50-280, 281/94017-02

23

VIO

Failure to Stop Work When Work Instructions

Could not be Followed (Section M8.4).

LER

One PZR SRV as Found Lift Setting Out of

Tolerance (Section M8.5).

LER

Error in Calculation to Convert TS NaOH Volume

to Level for the Chemical Addition Tank

(Section E8.l).

VIO

Failure to Provide a Continuous Firewatch

(Section F8.l).

LER

One PZR SRV as Found Lift Setting Out of

Tolerance Section M8.5).

VIO

Failure to Implement Corrective Actions to

Preclude Repetition of Foreign Material

Exclusion Deficiencies (Section M8.6) .