ML18152A141

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Insp Repts 50-280/88-02 & 50-281/88-02 on 880201-05.No Violations or Deviations Noted.Major Areas Inspected: Licensee Practices Re balance-of-plant in Programmatic Areas of Operations & Training & Outstanding Open Items
ML18152A141
Person / Time
Site: Surry  Dominion icon.png
Issue date: 03/08/1988
From: Jape F, Szczepaniec A
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML18152A142 List:
References
50-280-88-02, 50-280-88-2, 50-281-88-02, 50-281-88-2, NUDOCS 8803280076
Download: ML18152A141 (19)


See also: IR 05000280/1988002

Text

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--

Report Nos. :

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W.

ATLANTA, GEORGIA 30323

50~280/88-02 and 50-281/88-02

Licensee:

Virginia Electric and Power Company

Richmond, VA

23261

Docket Nos.:

50-280 and 50-281

Facility Name:

Surry 1 and 2

License Nos.: DPR-32 .and DPR-37

Inspection Conducted:

February 1-5, 1988

Team Leader:

..

?iz,~ * 9-r< .

F. J~e

.

,,

A. Si"ci~i~ bfs'a'/{'feam feader

Team Members:

W. Kleinsorge

R. Perfetti

S. E. Sparks

P . .Taylor

Accompanying Personnel:

A. R. Herdt

Approved by:

~ *

.~

F. Jape,

1e

Test Programs Section

Division of Reactor Safety

SUMMARY

3/f!KI

Date Signed

o~/e'f,~~

>1J11dr

Date Signed

  • scope:

This special, announced inspection was conducted in accordance with

TI 2515/83,

11Balance of Plant Trial Inspection Program (Feedwater System)

11 to

assess the licensee's practices concerning Bala_nce _of_ Plant in programmatic

areas of Operations and Training, Maintenance, Design Control and

Modifications, and Management Support and Quality Assurance.

Outstanding open

items were also inspected.

Results:

In the areas inspected, violations or deviations~were not identified .

8803280076 880315

PDR

ADOCK 05000280

Q

DCD

BACKGROUND

BALANCE OF PLANT INSPECTION

EXECUTIVE SUMMARY

Recent NRC and industry reports analyzing unplanned reactor shutdowns and plant

trips. have indicated that a majority were caused by transients from failures of

BOP systems and components.

The safety significance of BOP failures can be

related to two aspects of challenges to reactor.safety.

The first concerns

challenges to reactor safety systems caused by BOP failure, such as failure of a

feedwater regulating valve.

The second concerns BOP failures that complicate

the ability of operators and.safety systems to control the reactor given that a

challenge to a safety system has already occurred.

An example of. this would be

the failure of turbine bypass valves which could complicate recovery during a

plant transient.

Looked at from a different perspective, the safety significance of BOP failures

can be related to the probability of reactor core damage. This probability can

be directly related to two separate factors .. The first factor is the frequency

or number of challenges to safety systems; the second is the unavailability of

those systems.

Thus, decreasing the frequency of challenges to safety system

from the BOP can.decrease the risk to public health and safety;

NRC' s Temporary Instruction (TI) 2515/83 was developed as a result of the

growing concern for the safety significance of BOP failures.

Similar

inspections have already been performed at Salem Nuclear Generating Station,

6/15-19/87; Edwin I. Hatch Plant, 7/27-31/87; and Zion Nuclear Station,

10/19-23/87.

Due to -the plant operating history and the number of BOP

failures,. the Surry Power Station was chosen as a fourth site for the special

inspection.*

SCOPE

This inspection was not intended to be compliance oriented. This it primarily

due to the absence of prescriptive requirements applicable to BOP systems.

Rather, the intent was to justify to the licensee concerns about design,

modification, maintenance, operations and testing practices for BOP systems,

specifically feedwater and related components.

The team consisted of six

inspectors with one assigned to the different programmatic areas of Operations

and Training, Maintenance, Design Control and Modification, and Modification

and Quality Assurance.

The* most current events, based on licensee event

reports,were selected for initial review.

These events were.revi'ewed for-root

cause determination and corrective act ions. * Each inspector then reviewed the

events for the attributes of each programmatic area as they applied for each*

event.

When _felt' useful, additional events or failures were reviewed to obtain

a clearer understanding of how the attributes are perceived or handled by the

licensee.

Although the feedwater system was the main focus of the inspection,

other BOP systems which would exemplify actions of the licensee were also

reviewed.

The assessment of the licensee's practices were then based on a.

I I

sampling of events arid actions on the part of the -licensee, including

procedures, reports and programs and selected interviews with plant personnel.

RESULTS

The results of the inspection ar~ detailed within the report and are summariz~d

here and classified as strengths or weaknesses.

Other observations which were

not classified as either strengths or weaknesses are discussed in the

report.

Strengths are those items which the inspection team feel make a

considerable positive impact upon the licensee's efforts to increase

BOP /feedwater system re 1 i abi 1 i ty and decrease safety system cha 11 enges. *

Weaknesses are those areas considered to be needing attention Dr correction to

achieve the same results.

a.

Strengths

1)

Simulator training is conducted on a continuing cycle to enhance the

operators abi_ 1 i ty to contra l feedwater during startups and shutdowns.

2)

Self imposed requirements have recently been added to test feedwater

regulating valves at shutdown and prior to startup.

3)

Work progress on BOP equipm~nt proceeds at approximately the same

rate as* safety-related equipment, once the work item ha*s been

identified.

4)

Establishment and active use of a predictive maintenance program and

a maintenance engineering organization.

5)

Establishment and use of the Quality Maintenance Team concept.

6} - Engineering Work Packages and Design Change Packages are handled the

same for BOP systems as for safety-related.

7)

Good communications . exist between_ key personnel in Technical

Services, Operations and Maintenance associated with regard to design

modifications.

8)

The number of BOP related reactor trips has _reduced from 11 in 1984

to two in 1987, and attention continues to be di -rected toward

reducing the number further.

9)

Extensive management involvement/interest in BOP/feedwater system

problems.

10) * Continued allocation of significant funds toward BOP/feedwater

systems .

11)

There appears to be a* concerted effort by, the 1 i censee to upgrade

equipment, whenever poss i b 1 e, in conjunction with modifications.

Examples include the incorporation of upgraded underv~ltage relay

III

models .in the Main Tran~former work request, and the incorp6ration of

rotary screw air compressors in the IA design change.

12)

When a problem arises at one unit and a design change is initiated,

there appears to be a good effort by the 1 i censee to eva 1 uate the *

. app 1i cabi l ity of the change to the other unit and to fo 11 owup

accordingly.

b.

Weaknesses

1)

Lack of formal programs for root cause analysis, documentation,

trending and centralization of information on station, specifically

for BOP /feedwater system.

Reviewed LE Rs have shown 1 ack of

consistency, thoroughness and relationship to previous events.

2)

  • Lack of a formal program for trendin~ BOP deviations, similar to one

in use for safety-related equipment.

3)

Subjective determination of when BOP/feedwater components are to be

repaired, or possibly underg6 design modifications.

This is related

to the lack of formal training and trending programs.

4)

The licensee 1s approach to the repeated problems with the instrument

air system and the main f eedwater va 1 ves appears to be more

prescriptive than preventive.

CONCLUSIONS

Using the guidelines of TI 2515/83, and based upon observations, staff

interviews, and reviews of various_programs, records, procedures, and reports,

the Surry Power Station has been found to have a significant number of the

applicable attributes which are decreasing safety system challenges and

increasing feedwater and their BOP system/component reliability.

L

Persons-Contacted

Licensee Employees

REPORT DETAILS

  • J. A.* Bailey, Superintendent of Operations
  • D. L. Benson, Station Manager*

.

  • R. H. Blount, II, Superintendent of Technical Services
  • D. J. Burke, Superintendent of Maintenance
  • A. H. Friedman, Superintendent of Training
  • E.* S. Grecheck, Assistant Station Manager
  • J. B. Logan, Supervisor, Safety Engineering
  • H. L. Miller, Assistant Station Manager

G. L. Pannell, Director, Safety Evaluation and Control*

Other 1 i censee emp 1 oyees contacted inc 1 uded engineers, technicians,

operators, mechanics, and office personnel.

NRC Resident Inspectors

  • vi. E. Holland

L. E. Nicholson

  • Attended exit interview*

2.

Exit Interview

The inspection scope and findings were summarized on February 5, 1988,

with those persons indicated in Paragraph 1 above.

The inspector

described the . areas inspected and discussed in deta i 1 the inspection

findings. . No dissenting comments were received from the 1 i censee.

The *

licensee did not identify as proprietary any of the materials provided

to or reviewed by the inspectors during this inspection.

NOTE:

A list of abbreviations used in this report is contained in

paragraph 11..

3.

Licensee Action on Previous Enforcement Matters

a.

(Closed) Unresolved Item 281/86-36-03, RTD Ca~ibration Records

This matter was reviewed by the NRC staff and it was concluded that

the method used by the. licensee was adequate.

This UNR is closed .

2

b.

(Closed) Unresolved Item 281/86-36-04, RTD Temperature Map

The temperature prof i 1 e map provided by the 1 i censee fo 11 owing the

inspection was reviewed.

The physical location of data points were

indicated.

This resolves the inspector's concern and the item is

closed.

c.

(Closed) Unresolved Item 281/86-36-05, Revise Procedures

The ILRT procedure was revised to require retention and retrie~al of

raw data used in the acceptance criteria.

Test results were

revalidated, therefore, this item is closed.

4.

Unresolved Items

Unresolved items were not identified during this inspection.

5.

Selected Components and Events

6.

Using the guidelines of TI 2515/83, the inspection team selected the most

current events and component failures on which to begin the inspection.

The concept of the inspection was to then use these events and components

as a starting point for a review of each programmatic area.

Results of

the inspection are therefore not only based upon these LERs, but also upon*

p 1 ant operating hi story, post-trip reports, other se 1 ected LE Rs, and

discussions with plant personnel.

The initial LERs reviewed were:

280/86-001

280/86-005

280/87-019

281/86-003

281/86-007

281/87-003

Reactor trip due to loss of instrument air

Isolated phase bus duct arcing

.Manual reactor trip due to failed relay in main

transformer

Turbine/reactor t~ip from high steam generato.r

l~vel

. . .

. * ..

Manual reactor trip due to high steam generator

level

Reactor trip by turbine generator anti-motoring

The programmatic areas reviewed were Operations and Training, Maintenance,

Design Contra 1 and Modi fi cat ions, and Management Support and Qua 1 i ty

Assurance.

The areas were inspected using the applicable attributes of

TI 2515/83 and the results in each area are presented separately.

Design and Modifications Aspects

An eva 1 uat ion was made of th*e 1 i censee' s fo 11 owup investigations. and .

activities relating to the long-term corrective actions with regard to

design modifications as they applied to the selected components and events

listed in paragraph 5.

3

There were no design medications associated with lER 86-001. _ The root

cause of the reactor trip as outlined in the licensee's LER, appeared to

have been from a -decrease in instrument air *(IA) pressure due to ice

_formation in the condenser-evaporator section of the Unit 1 IA dryer that

resulted in blocking air flow to the IA system.

A hot gas. bypass valve in

the dryer was not properly adjusted to maintain air temperature above

freezing.

Corrective action consisted of proper adjustment of the bypass

  • valve by a service representativeand revision of the turbine building logs

to incorporate IA dryer condenser temperature readings.

No design changes

or modifications were instigated by the licensee as a result of this LER.

LER 86-005 involved the manual tripping of Unit 1 from 42% power due

to .arcing on the A isolated phase bus duct.

The root. cause of the *

duct arcing appeared to have been as a result of corrosion product

buildup on the contact surfaces of the lugs of the ground straps that

were used to bridge butting sections of duct.

(The straps carried

less current which led to the duct arcing).

Corrective action

consisted of replacement of the damaged section of duct by welding to

prevent *possible recurrence and modification to other butting

sect ions of duct by we 1 ding such that the probabi 1 i ty of future

occurrences would be reduced as a result of the e 1 i mi nation of the

grounding straps.

No additional modifications or design changes were_

instigated by the li_censee as a result of this LER.

_

.

.

LER 87-019 involved the manual tripping of Unit 1 from* 98% power due

to 1 ass of cooling and oil fl ow for the

118

11 Main Transformer.

Power.

was 1 ost to the cooling fans and oi 1 ci rcul at i ng pumps when an

undervoltage. relay in -the cooling control circuit failed.

In

addition, the transformer local annunicator * panel had failed to

initiate a TROUBLE alarm on the c*ontrol room annunciator panel.

The

  • failures of the relay and the annunciator panel were attributed to

aging.

As a result of the event, several modifictions to. the Main

Transformers and their associated alarms in the control room were

outlined in

an

engineering work request

(EWR)

for Unit 1.

Modifications included *the addition of a redundant trouble alarm to

prevent future faulty operations, (Winding Temperature High and Total

Loss of Oil Flow Alarm), installation of fault pressure protection -

(Sudden Pressure Relay trip package), -installation on an insulating

barrier behind some of the re 1 ays in the trans former contro 1 pane 1 s,

and e 1 i mi nation of a 11 automatic throw-overs between the 480V sources

within the Transformer cabinets.

The automatic throw-over switch is

undesirable because it has the potential of transferring any trouble

-on the circuit being transferred. to the second circuit causing all

cooling to the lost.

EWR No.87-329 was reviewed to verify that the

modifications were designed, constructed, and tested in accordance

with appropriate portions of non-nuclear codes and standards that

were the. same as those used for the ori gi na 1 components.

(Vi rgi ni a

Power's Transformer Standard Specification is VEP-3700-86-01).

Due

to the unavailability of some of the necessary materials, all

modi fi cat i ans could not be performed during* the December 1987 Snubber

Outage.

However, the licensee's Control_ Operations staff_ discussed

4

the rema1n1ng modifications* to be perforfued, as well

~s * the

additional improvements to the Unit 1 Main Transformer with the NRC

_inspector.

In addition to the modifications to the Unit 1 Main Transformer,.

similar modifications - were performed under EWR No.87-330 for the*

Unit 2 Main Transformer.

This work request also included the

addition of emergency breakers so that one 480vac source could supply

both cooling groups if necessary.

LER 86-003 involved a Unit 2 turbine trip/reactor trip from high

steam generator level in the "8

11 steam generator.

The high steam

_generator 1 evel occurred during rampdown when the

118

11 main feedwater

bypass valve apparently failed to close on demand.

The failure is

believed to have been caused by a blockage in the air pilot relay

which prevented proper air fl ow to the va 1 ve operator. -The b 1 ockage

was dislodged following the trip and the valve cycled satisfactorily.

LER 86-003 stated that an* engineering review to evaluate the most

effective method of contra 11 i ng contaminants in the IA system was

being conducted.

As a result of this review, design change package

(DCP) number 86-03~3 was initiated.

The compressed air system at Surry originally consisted of a service

air subsystem, - an instrument air subsystem, _and a containment air

subsystem for each uriit.

The service air and instrument air subsystems

were supplied by identical positi.ve displacement, reciprocating type

air compressors which had required continua 1 maintenance, thereby *

reducing the reliability of the compressed air system.

During the

licensee's

Steam 'Generator

Replacement

Outage

appr*oximately

1980-1981, an outage service air compressor (originally dedicated as

the so.urce of outage service air inside containment) and a condensate

po 1 is her instrument air compressor were designated as the primary

source for the. instrument .and service air subsystems.

The original

instrument and service air compressors were used to provide backup air. _

While the outage instrument and service air co~pressor and the condensate

polisher instrument air compres~or were more teliable, the compressors

could not meet all df the station's compressed air requirements.

Therefore,

DCP 86-03-3 dated October 26, 1986 proposed to rep 1 ace the original

service air compressors on a one for one basis with* new oil free,

rotary screw air cooled compressors.

The

rotary screw air

_ compressors are. thought to be more reliable than the* reciprocating

. type air compressors throughout the industry.

The new service air compressors which are double the capacity of the

original service air compressors are designated as the normal source

of ser~ice and instrument air for each unit.

The original instrument

air compressors left installed in their original location are

dedicated for emergency standby service.

_

While the upgrade of air compressors for both units shows a concerted

effort by the

1 i censee to increase system re 1 i abi 1 i ty 1 _ the

5

thoroughness and timeliness of the design change is questionable.

This observation stems from the following information.

LER 86-001, which was previously discussed, concerned the events

surrounding a reactor trip* on* Unit 1 due to loss of instrument air.

The root cause cited in the LER was an improperly adjusted hot gas

bypass valve in the dryer that resulted in ice formation which

subsequently blocked air flow to the IA system.

A similar event

occurred on Unit 1 on November 21, 1985, LER 85-022.

At the time of

the initial report, it was only speculated that the cause of the

event was due to a momentary drop in IA pressure.

The LER was updated

on March 26, 1986.

Although the pressure decrease in IA did not

result in a reactor trip, it did present a challenge to the ability

of the plant personnel

to maintain the unit 1s availability.

Corrective action. outlined in

LER 86-001 consisted of proper

adjustment of :the bypass valve and inclusion of lA dryer condenser

temperature readings into the turbine 1 ogs.

Whi 1 e both LER 1 s cite

the root cause as an improperly adjusted bypass valve,* DCP 86-03-3

dated October 28, 1986, appears to cite a different root cause,

specifically,

11The decrease in instrument air header pressure was

attributed to a mechanical failure in the air dryer which caused

moisture in the compressed air to freeze and prevent air.flow.

11

Not

only does this discrepancy question the licensee 1s root cause

analysis, it *also questions the licensee's desire to update the proper

documentation since it would appear that the true root cause would be

cited in the most recent analysis, (DCP 86-03-3 dated October 28,

1986),

thereby, prompting a correction of affected documents,

LER 85-022 and LER 86-001.

Further, it is questionable as to why the

instrument dryers were not upgraded in conjunction with the air

compressors,

since

DCP 86-03-3 *states that,.

11 In addition to

compressor reliability problems, the instrument air dryers (1-IA-0-1

and 2-IA-0-1) have required continual maintenance

11 *.

With regard to the ti me 1 i ness of the design change, it appears as

though the 1 i censee might have precluded at 1 east the two cited

challenges to the safety sytems, had the recognized deficiencies been

modified sooner.

It would appear that the licensee recognized the

problems with the original compressed air system from an early time

period since DCP 86-03-3 states,

11The instrument and service air

  • com~ress,~rs have required cont i n~a 1 mai ~tenan~e and . have. not been

rel 1 ab 1 e!1/~ an.d that a more rel 1 ab 1 e, J ury-r, gged s ubst, tute was

employed after the Steam Generator Outage, approximately in the 1981

time frame.

While the use of the substitute compressors improved the

reliability of the compressed air systems for both units, it is not

evident from the documentation provided for the inspector* s review,

. that the 1 i censee made an effort or commitment to reso 1 ve and modify

the compressed air systems for the station until February 8, 1986,

when a prob 1 em with the IA system resulted in a cha 11 enge to the .

safety systems and a commitment was made to evaluate methods for

contamination in the IA system.

Detai 1 s of this event are out 1 i ned

in LER 86-009, Automatic Start of Auxiliary Feedwater PU.!1JPS, fo.r _

6

Unit 1.

Eight days later, the same problem with IA resulted in a reactor

trip on Unit 2 as previously discussed in LER 86-003.

LER 86-007 details the events surrounding a ~anual reactor trip on Unit 2

due to high steam gene~ator leVel.

The roo~ cause cited in the LER was

failure of Feedwater Control Regulation Valve, FCV-2478 to close.

The

failure was attributed to metal debris between the plug and the valve

seat.

The valve was. disassembled, inspected and the metal debris

preventing the valve closure was removed.

The valve was reassembled,

tested satisfactorily; and returned to.operable status.

the LER concluded

that no further act ion was necessary regarding this event to prevent

recurrences.

The lack of a documented commitment to evaluate possible

methods to prevent this type of FCV failure in the future.as well as other

failure mechanisms might be construed as a weakness in the licensee's

. approach to BOP systems and components given the hi story of the FCV

fai 1 ures for both Units 1 and 2.

During the period from January 1986 to

August 1987, 24 main feedwater control valve failures ,.occured.

(9 for

Unit 1 and 15 for Unit 2).

While some of these failures could be

attributed to poor maintenance procedures and practices, some of these

failures could be attr.ibuted to design weaknesses including (but not

limited to) valve packing._ lifetime, *valve trim (plug and cage or seat)

lifetimes, valve operator adjustment sensitivity, valve operator inability

to withstand their environmental vibration, and valve operator inability

to function with poor quality instrument air.

Design changes initiated to

upgrade the main feedwater control valves (as well as other main feedwater

valves) could be instrumental in making the main feedwater system more

re 1 i able, thereby reducing the probabi 1 i ty of unnecessary cha 11 enges to .

reactor safety systems.

Therefore, the need for possible design changes.

should be evaluated by the licensee.

LER 87-003 details the events surrounding a Unit 2 reactor trip by turbine

trip.

As Unit 2 was ramping down for a maintenance., outage, the turbine

tripped due to a generator anti-motoring s i gna 1 as operators were -

preparing to remove the main generator from service.

The root cause of

the generator anti-motor signal was cited in the LER as leakage past the

governor valves.

The LER committed to inspect the govern valves during

the next outage of sufficient* duration and for repairs to be made

accordingly.

This commitment was verified by the inspector via the

licensee's Commitment Tracking System.

As a result of this event, EWR

No.87-193 was initiated.

The EWR evaluated the need for an instantaneous

alarm circuit to the niain turbine anticipatory motoring trip to possibly

prevent unnecessary reactor trips.

Currently, the main. turbine is

designed to have an anticipatory motoring trip base_d on a low differential

.pressure (LlP) across the High Pressure turbine.

A time delay relay

  • circuit is activated upon sensing low LlP.

If this condition does not

clear withih one minute, there is activation of a turbine trip.

The

annunciator in the control room informs the operator of this trip

mechanism after the one minute delay.

Currently, there is no alarm on the

alerting device on a low LlP across the HP turbine to warn that a turbine trip

will result. in one minute, if this signal does not clear.

Therefore, *EWR

No.87-193 proposed to add an instantaneous alarm_ switch to the trip logic

7

for the main turbine anticipatory motoring trip based on low LlP.

Upon

activation of the one minute time delay relay for low LlP turbine trip, an

annunciator window labeled "Generator Motoring Turbine Low LlP

11 would light

up in the control room and would possibly enable operations time to clear

the condition and prevent unnecessary trips.

The EWR package was reviewed

by the inspector and was found to be in accordance with the 1 i censee I s

Technical Specifications, established QA/QC controls and was consistent

with the Updated. Final Safety Analysis Report and Design Basis Document.

The licensee's unreviewed safety question evaluation.was also reviewed and

was found to be in accordance with the requirements of 10 CFR 50.59.

The

incorporation of the. instantaneous alarm circuit was considered as a

strength by the inspector in terms of the licensee's approach to BOP.

systems and components.

7.

Operations

a.

LER Review

The selected LERs were reviewed to determine the appropriateness of

the licensee's actions from an operational standpoint.

The inspector

verified that the 1 i censee I s LER ope rat iona 1 commitments were being

tracked and documented.

Operating Procedure 2-0P-2.1.2, Decreasing

Power from Existing Power Level to 2%, was reviewed to verify the

revision commitment of LER 86-003 concerning the stroke testing of.the

feedwater bypass valve prior to.use.

The inspector. also reviewed Procedure SUADM-LR-08, Licensee Event

Report System, along with the selected LERs to determine the adequacy

of the licensee's root cause analysis.

The r~view revealed that the

licensee's root cau~e analysis was not documented adequately in the

LERs.

In addition, the licensee failed to discuss, as outlined in

SUADM-LR-08, why prior corrective actions did not prevent recurrence

for LERs86-003 (Unit 2) and 86-005 (Unit 1).

  • b.

System Valve Lineups and Walkdowns

The inspector reviewed the most recent valve lineups performed by.the

licensee as indicated from operating Procedures 2-0P-30.lA,

Condensate Va 1 ve Checkoff, and 2-0P-31. lA, Feedwater Va 1 ye Sheet

Checkoff.

Feedwater and Condensate system valve positions from the

most recent Unit 2 valve lineup were found to be consistent with

as-bui 1t drawings 11548-FM-68A, Rev. 21 (Feedwater system) and

11548-FM-67A,

Rev. 21 (Condensate system).

In addition, the

inspector noted that drawing 11548-FM-67A, Rev.* 21 re.fleeted a recent

modification to the condensate system (per Design Change 85-26) by

the incorporation of Valves 2-CN-540 and 2-CN-541.

The. inspector performed a wa 1 kdown of the Unit 2 Feedwater and

Condensate system~ to check for proper labeling of v~lves, proper

8

valve positioning, and the general. condition of valves and pumps.

The following valves were verified to be in the correct position in

accordance with the specific valve lineups:

MOV-FW-250A

2-FW-106

2-FW-88

2-CN-142

2-FW-110

2-FW-105

HCV-FW-255C

2-CN-138

2-FW-111

2-FW-104

2-CN-540

2-FW-107

2-FW-103

2-CN-541

The inspector found the housekeeping and general condition of the

Fe*edwater and condensate systems to be adequate.

c.

Operational Controls

The inspector held discussions with operations group management,

contra 1 room supervisors and operators to assess the . 1 i censee I s

methods used to provide operational control of BOP components and

equipment.* The administrative controls used for documenting and

working safety related systems equipment problems such as maintenance

requests, equipment tagout, and design change authorization are the

same as .those for BOP equipment. * In addition to these routine

controls, it is essential that the BOP equipment and ~ystems b~ known

to the contra l room personne 1.

The licensee has a program which

requires the control room operators to maintain BOP equipment checklist

forms which provide ready access to the conditions of these systems.

Entries made to the BOP equipment checklist to provide system status

inc 1 ude abnorma 1 1 i neups, degraded conditions, major components

. tagged aod identified problem areas.

Each shift reviews system

status and signs off on identified items when corrected in order to

maintain the system status current and meaningful.

The inspectors

reviewed items listed on the BOP equipment status checklist and found

the status to be current and identified problems being pursued for

corrective action. . The fo 11 owing BOP contra 1 room copy of operating

procedures were reviewed to verify *that they are consistent with the

as-built drawing, reflect vendor manual recommendations, are-control

copies, current and approved for use.

0

0

0

0

0

0

0

0

l-OP-1.3

1-0P-2.1.2

1-0P-30.0

1-0P-30.1

1-0P-31.1.1

1-0P-31.1. 2

AP-21.00

Unit Startup Operations 350/450 psig to* Hot

Shutdown

Increasing Power from 2% to 100%

Placing the Main Condensate System in Service

Removing Main Condensate System From Service

Placing the Main Feedwater System in Service

Placing the Steam Generators in Wet Layup

Loss of Main. Feedwater Flow

Annunciator Acknowledge Procedure:

IF-64, Steam Generator 18 High~Level

IF-67, Steam Generator lC Lo Lo level

d.

9

In addition to thes~ procedures, the inspector noted that in BOP

systems, detailed maintenance operating procedures are used to remove

and restore to service major components such as condensate pumps,

main feedwater pumps, instrument air system compressor.

In addition,

valves and electrical breaker alignment, along with tagout

requirements, are specified in these maintenance procedures.

Operating Experience and Information

The inspectors held discussions with control room supervisors,

operator~, and training supervisors and instructors to dete~~ine the

handling of BOP operating activities and LER related events with

regard to the attention being given to disseminate this information

to plant operators.

The licensee has established procedures

(Administrative Procedure LR-03, Operating Experience Reviews) for

processing operating experience from- several sources such as plant

LERs, NRC notices, bulletins, INPO operating experiences, and North

Anna LERs:

This material is reviewed by the plant training

organization for reviews and inclusions into the licensee's operator

requalification program, system and development training for

non-1 i censed operators.

The inspector examined several 1 es son p 1 ans

for BOP systems and noted the incorporation of the above materials.

In addition to these requirements, the licensee required reading

files for the on-shift operating personnel were examined and noted to.

contain similar material for review.

The licensee has established

procedures requiring post reactor trip review and the dissemination

of this information to the operating staff.

The inspector concluded that the licensee has an adequate program to

ensure event related information is provided to the operating staff.

8.

Maintenance

-

.

The inspectors reviewed procedures and maintenance histories, and

conducted interviews with key plant personnel to assess the licensee's

preventive, corrective, and predictive maintenance programs as they (the

programs) relate to the BOP systems.

a.

The inspectors reviewed the below listed-procedures to assess the

programmatic coverage analyzing, defining, planning, scheduling, *

tracking and implementing co~rective actions for BOP systems.

SUADM-M-02 of

April 30, 1985

SUADM-M-03 of

October 4, 1984

  • SUADM-M-09 of

March 11, 1986

"Station Housekeeping"

11Cleanness Control of Plant Systems and

Components"

"Secondary Repair/Replacement Program"

SUADM-M-27 of

. October 8, 1987

SUADM-M-16 of

October 6, 1987

SUADM-M-10 of

August 2, 1984

SUADM-M-11 of

October24, 1985

SUADM-M-12 of

February 19, 1985

SUADM-M-33 of

October 28, 1986

SUADM-M-42 of

August 25, 1987

SUADM-TR-01

SUADM-SP-02

10

"Requests for Repair or Replacement

Follower"

110peration of the Maintenance Department"

"Work Planning and Tracking System"

"Work Request Systems"

"Work Order Planning"

11Secondary Piping Inspection"

"Lubrication Test Program"

"Qualification and Training"

"Quality Maintenance Team (QMT)"

Relative to the administrative procedures defining the licensee'-s

program for the maintenance effort for BOP systems, the inspectors

noted the following:

0

0

0

The

program

is

implemented

by

"should" . statements

(recommendations) and "may" statements (permission), which makes

the program comp] ete ly subjective and dependent on personne 1

experience and judgement.

The program has many undefined initial isms and acronyms, a

potential area for confusion.

The program has many references to uni dent i fi ed superseded

procedures by number only, a potential area for confusion.

b.

The* inspectors reviewed the below listed LERs and their associated

documentation packages to assess the licensee's practices in

programmatic areas that were found to be contributing. factors to

events or component * failures.

Specific areas examined included

whether:

equipment failures. were evaluated for input to the

preventative maintenance program and possible design modification;

maintenance planning has taken into account the possible safety

consequences of concurrent or sequent i a 1 maintenance or testing

activities; procedural steps that must be accomplished correttly in

proper order to avoid malfunction or failure are highlighted to

maintenance personnel; the preventative maintenance program is

11

adequate for ensuring system/component r*eliability; approved

procedures were employed where the activity exceeded the normal

skills possessed by qualified maintenance personnel; replacement

parts and materials were determined and documented to.be of at least

the same quality as the original parts; post maintenance testing

and/or inspection was specified, correct and complete; measuring and

test equipment used was in calibration; maintenance personnel were

appropriately trained and qualified; and inservice inspection/test

activities were periodically performed as appropriate to ensure their

continu~d availability.

1-86-001

Rx trip on SF/FF Mismatch with Low SIG Level Due to MFRV's

Shutting Due to .Loss of IA Pressure Due to Ice Formation in

the IA Dryer Due to Improper Hot Gas Bypass Valve

Adjustment in the Dryer

1-86-010

Rx Trip on Turbine Trip on High S/G Level Due To Difficulty

Controlling 1C1 MFRV Due to Feedback Cam on Valve Operator

Not Adjusted Following Maintenance

2-86-003

Rx Trip On .Turbine Trip on High

1B' SIG Level Due to MFRV

Bypass Valve Failing to* Close Due To Blockage of.Air Pilot

Relay

2-86-007 Manual Rx Trip on High 'A' SIG Level Due to Failure of MFRV

to Seat Due to Metal Debris Between Plug and Seat

2-86-020

Rx Trip Due to Low Level in 1C1 S/G Due to Shrink Caused by

1 C

11

MSTV Shutting Due to Improper Reassembly Fo 11 owing

Maintenance.

Suction Piping to

1A1 MFWP Ruptured Approx.

40 Seconds After Rx Trip.

2-87-003

Rx Trip on Turbine Anti.:.Motoring Trip* Due to Governor

Valve Leakage

With regard to the above, the inspectors noted the following:

0

Of the six LE Rs examined and eight total LE Rs that reported

reactor trips resulting from BOP component degradation or

failure during the period January 1986 - December 1987, four

LERs were attributed by the 1 i censee to 1 ack of maintenance or

improper maintenance (improper valve adjustment, valve operator

not adjusted following maintenance, valve failing to open due to

blockage, testing before use was needed, and improper valve

reassembly after maintenance).

In all of the above cases, the

licensee determined that the existing maintenance procedures or

testing procedures (that *would initiate maintenance) were

inadequate.

Those procedures were all appropriately revised to

i 11 umi nate the i dent i fi ed inadequacies.

LER No. 2-87-003 was

not considered above because the determination of root cause and

actions to prevent recurrence for LER 2-87-003 as stated by the

r ..

0

12

licensee would require disassembly and inspection at

11the next

outage of sufficient duration

11 (most probably the next refueling

outage}. . It should be noted that of the six LE Rs examined in

this area and the eight total LERs (1-86 to 12-87) that reported

reactor trips caused by BOP component degradation or failure,

all four LERs attributed to inadequate procedures were 1986

events; none in 1987.

LER No. 2-86-007 reported that the Main Feedwater Regulating

Valve (MFRV) failed- to close due to metal dehris between the

p 1 ug and the seat.

The 1 i censee indicated that, based on

rememberances of personnel i nvo 1 ved, the debris was a nut.

However, the licensee indicated that they were unable to show

that any review was made to determine the fa 11 owing:

The source of the nut.

If the nut came from within the system~ whether there were

any other nuts or other parts free or potentially free in

the system that could cause a recurrence of this failure or

  • a failure of the component missing the nuts or other parts.

c.

In early 1986, the license established a maintenance engineering

organization with the_ responsibility for providing engineering

support for the electrical and mechanical maintenance programs.

Within the maintenance. engin_eering organization, the Predictive

Analysis Group was established, early in 1987, with primary attention

being focused on equipment vibration; lube oil monitoring and

analysis and trending of the vibration and oil analysis data.

These

areas were examined.

Section 5.1 of ADM21-04,

11 Policies and

Procedures -

Maintenance Programs

11 , provides the admi ni strati ve

controls for the program.

The vibration spectrum analysis and oil analysis monitoring programs

currently monitor 118 pieces of plant equipment, of which

approximately 50% are within the scope of BOP.

Lube oil samples and

vibration data is collected monthly from each piece of equipment in.

the program.

The* lube oll samples are sent to a contractor, *

Precision Mechanical Analysis of Brandon, Florida, for analysis.

The

tesults of the oil analysis is electronically transmitted to the site

to assure timely data return.

The vibration data is collected by the

licensee with audio recording tape and analyzed on site by computer.

The data can be viewed as a high resolution signal analyzer in

spectrum form or on a CRT monitor in numeri ca 1 value form.

The data

from both the lube oil and vibration spectrum monitoring is trended.

Case histories were reviewed- for equipment that was repaired based *

upon program recommendations prior to failure, avoiding an unexpected

plant outage.

The Predictive Maintenance Program has the elements in it required

fo*r plant availability improvement.

The s~vings from _the program

13

have already justified its cost.

In the long run, the effect should

be to . reduce cha 11 enges to the reactor system caused by preventab 1 e

equipment failures.

9.

Management Support and Quality Assurance

Management support provided to BOP systems and their operations was

inspected using the guidelines and attributes of TI 2515/83.

It was observed that there was extensive management i nvo 1 vement in

responding to BOP problems most evident when those problems affected the

safe, reliable operation of the reactor plant.

The significance of any

pro_b 1 em is determined by its affect upon the opera ti on of the p 1 ant and

not whether it is part of a safety-related or BOP system.

Consequently,

many of the responses to identified problems are applicable to all areas

of the power plant.

Examples of such responsiveness, which are not just

limited to safety-related systems are establishment of the Quality

Maintenance Team concept, the Human Performance Evaluation System, the

corporate. health ~are p~ogram, and the procedure upgrade program.

The

responsiveness, however, is limited to the extent that management is aware

of current pr.ob 1 ems or conditions based on trending reports.

This wi 11 be

evaluated later in the discussion of management involvement.

Responsiveness

has been found to also be prioritized for specific areas of concern.

For

example, a large *effort was expended in solving the feedwater regulating

valve operation problems during startups/shutdowns by. improving such areas

as training, testing; operational control, and maintenance; yet a BOP area

(feedwater heater) where 1/1 logic exists, has not.yet been modified.

Instead of a modification, *controls are being used, such as signs and

procedures, to prevent recurrence.

No recurrence has occurred s i nee the

original trip.

It was also observed that although a prob.lem with the

instrument air system was i dent ifi ed by the 1 i censee, no permanent

corrective action was taken until after an event occurred.

This item is

addressed more completely in paragraph 6.

Success in reducing the number of plant trips is also used as an indicator

of management support.

Reactor trips at Surry have steadily decreased

from 22 in 1984 to five in 1987.

Of these, 11 were BOP re 1 ated in 1984,

and two in 1987.

Neither of the two BOP trips in 1987 were feedwater

related; nor were they recurrences of previous trips.

The amount of resources being allocated towards BOP was also* reviewed.

From a funding perspective, a considerable portion of ~roposed budgets fof

1987, 1988, and 1989 are being allocated to BOP systems, especially when

compared to the r~latively low number of BOP related trips. Within tbe

five. year pl an, 42% of the 1987 budget was a 11 ocated; in 1988 it is 21%

and in 1989, it is 25%.

From the human resources perspective, it is

observed that there is no dedicated organization for addressing BOP, and

therefore, difficult to access.

The dedicated II system engi neer~1 concept

has not been used at Surry, as elsewhere; however, due to the size of the

station s~aff, it may not be desirable,

~----------

-

~~~

14

The licensee has been found to be participating in and utilizing different

industry initiatives in reduction of the number of BOP related trips.

The

two most notable are the Nuclear Performance Reporting Data System

(NPRDS), and the Westinghouse Owners Group (WOG) Trip Reduction Committee.

The licensee provides input into the NPRDS and also generates its 6wn

reports for use by maintenance and planning.

The chairman of the WOG

trip reduction committee is from Virginia Power..

As mentioned .earlier, upper management involvement in addressing ~OP

problems is very extensive. Other than in areas of responsiveness, there

is upper management participation in plant startups and shutdowns, daily

production meetings,, ahd post trip reviews, for BOP matters as well as

safety related.

Management has app 1 i ed the requi.rements for qua 1 i ty and

safety throughout the plant and, other than for regulating requirements,

basically operates the plant without differentiation between BOP and

safety-related systems.

However, a couple of specific areas where

differences do exist were found.

The degree of detail within maintenance

procedures, deviation reporting and deviation trending is much less thah

required for safety related.

Since there is such intensive personal

m~nagement involvement, and the staff appears to work so closely together,

the 1 i censee be 1 i eves the organization can satisfactorily address any

problem that is discovered:

However, since no formalized program exists

for both documenting and determining ~oot cause* on a centralized basis,

the lack of continuity, source of readily available information, and of

consistency may not give management the best information available to

properly respond to ongoing problems.

This can be of value not only f6r

addressing BOP component failures and related events, but also for safety

re 1 ated components and events.

  • .

The management po 1 i ci es and attitudes were found to be understood and

generally implemented at both the worker and first line supervisor levels.

Interviews of plant personnel indicate that an emphas*is on quality of work

is present throughout the station, and that station personne 1 are

responding positively. It was also observed that personnel understand the

importance of finding current root causes of inplant failure an"Cl are

taking the proper steps to prevent recurrence once a root cause has been

properly identified.

In conclusion, it appears that both manag~ment and

the craft share t_he idea of improving quality, determining causes of

problems and preventing recurrences, to keep the plant operating as safely

and reliably_as possible.

Within the Quality Assurance area, no formal program was .found.

specifically for BOP systems.

However, a Quality Assurance review is

required for all procedures, including BOP, prior to procedures

per.formance.

Quality Assurance also reviews all completed work packages.

The emphasis is definitely placed on.safety-related work vice BOP, yet BOP

is not totally ignored.

If there are BOP aspects in an area of a

general periodic audit, these BOP items,are reviewed as we11.

An example

r

15

would be the periodic audit of Mechanical Maintenance and Welding.

A

heavy reliance, however, is placed upon the station personnel and other

programs at the site, such as the Quality Maintenance .Team, to produce

quality work.

10.

Licensee Actions on Previously Identified Inspection Findings (92701)

(Closed) IFI 280, 281/86-40-01, Revise Procedure 112-PT-10 to incorporate

all required parameters.

The subject procedure was revised on October 8, 1987 for Unit 1, and

October 26, 1987 for Unit 2.

The inspector verified that all parameters

have been incorporated into the procedure.

These items are closed.

11.

List of Abbreviations

BOP

CRT

DCP

EWR

IA

INPO

LER

MFRV

MFWP

MSTV

NPRDS

QA

QC

QMT

RX

SF/FF

SIG

TI

WOG

Balance of Plant

Cathode Ray Tube

Design Change Package

Engineering Work Request

Instrument Air

Institute of Nuclear Power Operations

License Event Report -

Main Feedwater Regulating Valve

Main Feedwater Pump

Main Steam Tri~ Valve

Nuclear Performance Rating Data System

Quality Assurance

Quality Control

Quality Maintenance Team

Reactor

Steam Flow/Feed Flow

Steam Generator

-Temporary Instruction

Westinghouse Owners Group