ML18152A089

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Insp Repts 50-280/99-03 & 50-281/99-03 on 990411-0522.Two Violation Noted.Major Areas Inspected:Aspects of Licensee Operations,Engineering,Maint & Plant Support
ML18152A089
Person / Time
Site: Surry  Dominion icon.png
Issue date: 06/18/1999
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18152A090 List:
References
50-280-99-03, 50-280-99-3, 50-281-99-03, 50-281-99-3, NUDOCS 9907070033
Download: ML18152A089 (30)


See also: IR 05000280/1999003

Text

1-

U.S. NUCLEAR REGULATORY COMMISSION

REGION II

Docket Nos.: 50-280, 50-281

License Nos.: DPR-32, DPR-37

Report Nos.: 50-280/99-03, 50-281/99-03

Licensee:

Virginia Electric and Power Company (VEPCO)

Facility:

Surry Power Station, Units 1 & 2

Location:

5850 Hog Island Road

Surry, VA 23883

Dates:

April 11 - May 22, 1999

Inspectors:

R. Musser, Senior Resident Inspector

K. Poertner, Resident Inspector

G. McCoy, Resident Inspector

T. Fredette, Resident Inspector, Plant Hatch (Sections 01.2 and M1.1)

D. Forbes, Radiation Specialist (Sections R1 .2 and R1 .3)

P. Fillion, Reactor Inspector (Sections E1 .3, E1 .4, E1 .5, E8.1 and E8.2)

J. Lenahan, Reactor Inspector (Sections E1 .3, E1 .4, E1 .5 and E2.1)

R. Bernhard, Senior Reactor Analyst (Section E 8.2)

Approved by: R. Haag, Chief, Reactor Projects Branch 5

Division of Reactor Projects

Enclosure

9907070033 990618

PDR

ADOCK 05000280

G

PDR

EXECUTIVE SUMMARY

Surry Power Station, Units 1 & 2

NRC Integrated Inspection Report Nos. 50-280/99-03, 50-281/99-03

This integrated inspection included aspects of licensee operations, engineering, maintenance,

and plant support. The report covers a six-week period of resident inspection; in addition, it

includes the results of announced inspections by a regional radiation specialist and regional

reactor inspectors.

Operations

Operators were attentive to plant conditions during the core off-load and displayed a

safety-conscious awareness and attitude toward critical parameters. However, the

inspectors observed that the licensee's operator communications expectations were not

rigorously implemented (Section 01.2).

The shutdown of Unit 2 for a scheduled refueling outage was well executed and

performed in accordance with approved procedures. The operators appropriately

responded to an erratic source range detector indication and failure of the main turbine

to trip properly (Section 01.3).

Overall condition of the Unit 2 containment, following plant shutdown, was observed to

be good with the exception of the residual heat removal (RHR) pump seals which

  • exhibited signs of previous leakage. When the RHR system was placed in service, seal

leakage was observed on both RHR pumps (Section 01.4).

Reactor coolant system draindown activities to flange level were well controlled and

accomplished in accordance with the procedural requirements (Section 01.5).

Refueling operations were performed in accordance with Technical Specification*

requirements. However, personnel demonstrated a willingness to defuel the reactor with

degraded equipment. A malfunctioning instrumentation cable take up reel caused a

periodic lost of gripper engagement indication which would stop hoist movement. An

operator work around was used to maintain gripper engagement indication (Section

01.6).

During the installation of the reactor vessel upper internals assembly, two fuel alignment

pins were damaged as well as four fuel assembly top nozzles. The licensee removed

and repaired the upper internals and damaged fuel assemblies that were to be reused

  • *(Section 01.7).

The failure to place the automatic load tap changer switch on the A Reserve Station

Service Transformer in the automatic position after a manual adjustment was identified

as a non-cited violation. This matter was the result of operator inattention during

equipment operation (Section 02.1 ).

2

The licensee's preparation of the Unit 2 containment prior to restart from a refueling

outage was satisfactory. Minor deficiencies were identified and corrected prior to

containment closeout (Section 02.2).

The failure to follow procedures to properly de-energize the Unit 2 High (Hi)

Consequence Limiting Safeguards (CLS) logic circuitry during the replacement of a Hi

CLS relay was identified as a non-cited violation. This resulted in an unanticipated

engineered safeguards actuation of the B train of Hi CLS. Operations authorized the

relay replacement under a tagout for the Hi-Hi CLS actuation logic and maintenance

personnel failed to verify the relay was de-energized (Section 02.3).

Maintenance

The licensee's planning for the inspection of low head safety injection check valve was

comprehensive. Coordination between various plant departments was evident.

Appropriate use of mock-ups and As-Low-As-ls-Reasonably-Achievable concepts was

observed. Technical input from craft workers was used extensively in the planning

process (Section M 1.1).

Because of binding problems with two new rotating elements, the licensee was unable to

install a new rotating element in the Unit 2 A motor driven auxiliary feedwater pump. The

original rotating element was visually inspected and reinstalled in the pump (Section

M1.2).

The licensee identified a problem with hold-down spring retaining bolts on several fuel

assemblies present in the Unit 2 core and decided to the repair any potentially

susceptible fuel assembly scheduled to be returned to the core. The top nozzles on 16

fuel assemblies were successfully replaced (Section M1 .3).

Observed maintenance activities were properly performed. Personnel conducting the

activities were knowledgeable and properly followed work package instructions. The

(Section M1 .4).

Five routine periodic tests observed were properly performed. The tests were properly

approved by station management, test procedures were properly followed by

knowledgeable workers and Technical Specification requirements were satisfied

(Section M1.5).

Engineering

The modification to resolve Thermo-Lag issues inside the Unit 1 and Unit 2 containments

has been completed (Section E 1.1 ) ..

The Unit 2 low head safety injection (LHSI) pump recirculation lines were modified to

improve recirculation flow for the weaker pump during parallel pump operation. While

the recirculation flow for the weaker pump increased from previous values, the flow rates

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for both LHSI pumps were below the vendor's recommended values. The licensee

determined the achieved recirculation flow rates were acceptable (Section E1 .2).

The inspectors reviewed a sample of design changes implemented on Unit 2 during the

current refueling outage and concluded that the licensee's design change process met

the requirements in the area of design control (Section E1 .3).

The inspectors reviewed a sample of recently completed safety evaluations performed

pursuant to 1 O CFR 50.59. The safety evaluations reached correct conclusions

concerning whether the proposed change would compromise safety and whether an

unreviewed safety question was involved. Documentation of the safety evaluations was

complete (Section E1 .4).

The inspectors reviewed deviation reports generated during the spring 1999 refueling

outage and concluded that the licensee's corrective action program was meeting the

requirements of 10 CFR 50, Appendix B, Criterion XVI, "Corrective Action" (Section

E1.5).

The licensee's program for maintenance, inspection and repairs to containment coating

was adequate. Containment liner corrosion at the basement slab/liner intersection was

observed (Section E2.1).

Plant Support

The licensee was effectively maintaining controls for personnel monitoring, control of

radioactive material, radiological postings, radiation area controls, and high radiation

area controls as required by 10 CFR Part 20 (Section R1.2).

The licensee was maintaining programs for controlling exposures As-Low-As-ls-

Reasonably-Achievable (ALARA) and continued to be effective in controlling overall

collective dose. All personnel radiation exposures during 1999 to date were below

regulatory limits (Section R1 .3).

Report Details

Summary of Plant Status

Unit 1.operated at power the entire reporting period. Unit 2 operated at power until April 18,

1999, when the unit was shutdown for a scheduled 36 day refueling outage. The unit remained

shutdown for the remainder of the inspection period.

01

01.1

I. Operations

Conduct of Operations

General Comments {71707, 40500)

The inspectors conducted frequent control room tours to verify proper staffing, operator

attentiveness, and adherence to approved procedures. The inspectors attended daily

plant status meetings to maintain awareness of overall facility operations and reviewed

operator logs to verify operational safety and compliance with Technical Specifications

(TSs). Instrumentation and safety system lineups were periodically reviewed from

control room indications to assess operability. Frequent plant tours were conducted to

observe equipment status and housekeeping. Deviation Reports (DRs) were reviewed

to assure that potential safety concerns were properly reported and resolved. The

inspectors found that daily operations were generally conducted in accordance with

regulatory requirements and plant procedures.

01.2

Control Room Observations During Unit 2 Core Offload (71707)

The inspectors monitored control room activities during the initial portion of the Unit 2

core offload. The inspectors observed that, in general, operators were attentive to plant

conditions during this period, maintained communications with personnel on the

containment refueling bridge during fuel assembly movement, and displayed a safety-

conscious awareness and attitude toward critical parameters.

However, the inspectors observed poor operator communication practices as

exemplified by three-part communications in the control room not being consistently

practiced, and in fact, appeared to be the exception rather than the rule. This included

control room operators communicating to each other, as well as, operators giving

direction to non-control room personnel.

The inspectors discussed these observations with licensee management, who

acknowledged that their expectations for three-part communications were not met. The

inspectors concluded that the licensee's operator communications expectations were oot

rigorously implemented.

2

01.3

Unit 2 Shutdown for Refueling Outage

a.

Inspection Scope (71707)

The .inspectors observed and assessed performance.of the operating crew during the

shutdown of Unit 2 for a planned refueling outage.

b.

Observations and Findings

C .

On April 18, the inspectors observed portions of the Unit 2 shutdown for a scheduled

refueling outage. At 12:52 a.m., the unit was removed from the grid and the reactor was

manually tripped at 1 :03 a.m. When the main turbine was tripped from the control room,

the turbine relatched following the trip without operator action. The turbine was retripped

by the operating crew and the turbine remained unlatched. A DR was initiated to

document the relatching of the main turbine following a manual turbine trip. Following

energization of the source range detectors, detector N-32 exhibited erratic indication and

was declared inoperable. The detector was subsequently replaced prior to fuel offload.

Overall, the shutdown was well executed and performed in accordance with approved

procedures.

Conclusions

The shutdown of Unit 2 for a scheduled refueling outage was well executed and

performed in accordance with approved procedures. The operators appropriately

responded to an erratic source range detector indication and failure of the main turbine

to trip properly.

01.4

Unit 2 Containment Walkdown

a.

Inspection Scope (71707)

. The inspectors performed a detailed walkdown of the Unit 2 containment following entry

into the cold shutdown condition.

b.

Observations and Findings

The inspectors performed a detailed walkdown of all major areas of the Unit 2

containment once containment vacuum was broken and cold shutdown was achieved.

system loop .rooms, the pressurizer cubicle, the containment sump, and seal table room.

The overall condition of containment was good in that; 1) Leakage from piping system

mechanical connections was minimal, 2) The sump was free of debris, 3) Material

condition of components was good, and 4) No excess material was located within

containment.

The inspectors did note large accumulations of boric acid on the residual heat removal

(RHR) pumps. The leakage originated from the pump seal area. During subsequent

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C.

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containment inspections when the RHR system was in service, the inspectors noted

active seal leakage for both idle and operating pumps. The amount of leakage was in

the range of multiple drops per minute. This item was discussed with the operations shift

supervisor and the Superintendent of Operations. The licensee had previously identified

seal leakage for the RHR pumps and had initiated work requests to perform repairs

(replace the pump seals). During the current refueling outage, the boric acid deposits

were removed and based upon an evaluation of the seal leakage, the licensee deferred

the planned corrective maintenance to a future outage. The evaluation included the

removal and inspection of a carbon steel fastener on RHR pump 2-RH-P-1 B. Corrosion

on the fastener was within acceptable limits. See Section E2.1 for additional discussion

on the effects of the RHR pump seal leakage.

Conclusions

Overall condition of the Unit 2 containment, following plant shutdown, was observed to

be good with the exception of the residual heat removal (RHR) pump seals which

exhibited signs of previous leakage. When the RHR system was placed in service, seal

leakage was observed on both RHR pumps.

01.5

Unit 2 Draindown to Flange Level

a.

Inspection Scope (71707)

The inspectors observed portions of the activities associated with lowering reactor

coolant system (RCS) water level to allow removal of the reactor vessel head.

b.

Observations and Findings

The inspectors observed control room activities associated with lowering RCS level from

22 percent pressurizer level to flange level to allow removal of the reactor vessel head.

The activity was controlled by procedure 1-0P-RC-004, "Draining the RCS to Reactor

Flange Level," Revision 11. The inspectors reviewed the procedure prior to initiation of

the draindown and verified that the required initial conditions were met. The activity was

well controlled and accomplished in accordance with the procedural requirements.

c.

Conclusions

Reactor coolant system draindown activities to flange level were well controlled and

accomplished in accordance with the procedural* requirements.

01.6

Unit 2 Refueling Observations

a.

Inspection Scope (71707)

The inspectors observed the defueling of the Unit 2 reactor .

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b.

Observations and Findings

C.

Fuel handling evolutions were observed both in the containment and in the fuel building.

Activities were adequately supervised and TS requirements were met. A foreign material

control monitor was posted at the access to the refueling cavity area to ensure all

personnel entering the area were not taking unnecessary items into the area. No

problems were encountered in latching fuel assemblies with damaged hold down spring

retaining bolts. See Section M1 .3 for additional discussion on the damaged hold down

spring retaining bolts.

During the defueling process, the operators encountered problems with the

instrumentation cable take up reel on the manipulator crane. At certain rotational

positions on the take up reel slip ring assembly, the manipulator crane indication for

gripper engagement would be lost while raising or lowering the hoist. When the gripper

indication was lost the hoist would stop. To correct this, the operators mechanically

adjusted the cable to move the take up reel, indication was regained and the hoist

operated normally. This condition deteriorated to the point where the operators would

stop the movement of the take up reel (at a position on the reel where gripper indication

was maintained). Then as the hoist was raised, operators placed the instrument cable

slack on the deck of the manipulator crane. The inspectors viewed this operator work

around as an unnecessary distraction during a critical plant evolution, i.e., movement of

spent fuel. Continuing the core offload demonstrated a willingness by refueling

personnel to defuel the reactor with less than optimal equipment conditions. When a

replacement take up reel assembly became available, it was installed and the remainder

of the core was off-loaded.

Conclusions

Refueling operations were performed in accordance with technical specification

requirements. However, personnel demonstrated a willingness to defuel the reactor with

degraded equipment. A malfunctioning instrumentation cable take up reel caused a

periodic lost of gripper engagement indication which would stop hoist movement. An

informal operator work around was used to maintain gripper engagement indication.

01.7

Damage to the Unit 2 Reactor Vessel Upper Internals Fuel Alignment Pins

a.

Inspection Scope (71707 *. 62707)

b.

The inspectors-reviewed the events surrounding the damage to the Unit 2 reactor vessel

upper internals fuel alignment pins which occurred during upper internals reinstallation.

Observations and Findings

On May 8, following reinstallation of the Unit 2 reactor vessel upper internals, the

licensee determined, through seating verification measurements, that the upper internals

assembly was not fully seated. The following day, the licensee made the determination

that the upper internals would have to be removed and inspected for potential damage to

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both the upper internals and fuel assemblies. The inspectors remotely monitored the

removal of the upper internals and observed that the evolution was carried out in a

careful and deliberate manner. Once removed, an inspection of the upper internals

underside revealed that at least one, and potentially two fuel alignment pins were bent.

An inspection of the fuel top nozzles revealed four assemblies (R-8, R-9, P-8 and M-8)

with some form of damage (rolled/scratched metal) near one of the two S holes in the top

nozzles. Additionally, six assemblies were observed to be slightly misaligned.

The licensee contracted the Nuclear Steam System Supply (NSSS) vendor to repair

(bend back) the damaged upper internals fuel alignment pins. While the. NSSS vendor

was mobilizing, the licensee removed fuel assemblies adjacent to those with damaged

top nozzles so that the fuel assemblies could be visually inspected prior to removal from

the core. Other than the damage noted to the fuel assembly top nozzles, no structural

damage to the fuel assemblies was noted. A total of 18 fuel assemblies were removed

from the core for inspection and/or reconstitution (replacement of the top nozzle). The

final assembly to be removed, at core location R-9, could not be grappled using the

refueling bridge mast grapple due to damage the bundle received through contact with

the upper internals. The licensee obtained an alternate lifting tool (a cruciform shaped

tool known as the SFACHT) from the NSSS vendor which they used to remove the fuel

assembly from core location R-9. The inspectors observed the removal of this assembly

from the reactor and noted that the evolution was performed in accordance with

procedural requirements and in a safe and deliberate manner. The fuel assembly

removed from core location R-9 was not re-used, however, the other three assemblies

with damage to their top nozzles were reconstituted with new top nozzles prior to fuel

reload.

The NSSS vendor verified that there were two bent fuel alignment pins on the underside

of the upper internals corresponding to core locations R-8 and R-9. These pins were

bent back into position. The licensee conducted a root cause investigation to determine

the reasons for the bending of the fuel alignment pins. The root cause evaluation had

not been finalized at the end of the inspection period; however, a preliminary

determination stated that an out of specification gap (high) between the R row of fuel and

the reactor baffle plate caused the misalignment between the alignment pins and the fuel

assembly top nozzles. The licensee verified this gap was in tolerance prior to re-

installing the upper internals.

c.

Conclusions

During the installation of the reactor vessel upper internals assembly, two fuel alignment

pins were damaged as well as four fuel assembly top nozzles. The licensee removed

and repaired the upper internals and damaged fuel assemblies that were to be reused.

6

02

Operational Status of Facilities and Equipment

02.1

Reserve Station Service Transformer Automatic Load Tap Changer

a.

Inspection Scope (71707)

b.

The inspectors reviewed the licensee's actions when the A Reserve Station Service

Transformer (RSST) load tap changer selector switch was found in the incorrect position.

Observations and Findings

The RSSTs are equipped with an automatic load tap changer to maintain a desired

voltage range on the emergency buses during long-term grid voltage transients. At 2:56

a.m. on May 17, Unit 1 operators received an alarm from annunciator 1K-G3, Bus 1J

Overvoltage. They reviewed the Annunciator Response Procedure (ARP) 1 K-G3 "Bus

1J Over Volt," and manually adjusted the A RSST tap changer as described in the ARP.

At 12:33 p.m. on the same day an operator noted during his rounds that the A RSST tap

changer selector switch was in OFF. Subsequent investigation by the licensee

concluded that the operator who had adjusted the tap changer had missed the last step

in ARP 1 K-G3 to place the tap changer selector switch in the AUTO position. The switch

was placed in the proper position and a DR was written. With the load tap changer in the

manual position, no automatic voltage compensation would occur in response to grid

voltage fluctuations and prevent equipment powered from the emergency buses from

operating outside their normal voltage band.

Technical Specification 6.4.A.3 requires detailed written procedures, in part, for actions

to be taken for specific and foreseen malfunctions of systems or components including

alarms. In addition, TS 6.4.D requires that procedures described in Specifications 6.4.A

and 6.4. B shall be followed. The failure to properly follow ARP 1 K-G3 is a violation of TS 6.4.D. This licensee identified Severity Level IV violation is being treated as a Non-Cited

Violation (NCV) consistent with Appendix C of the NRC Enforcement Policy. This

violation is in the licensee's corrective action program as DR S-99-1353 and is identified

as NCV 50-280/99003-01.

c.

Conclusions

The failure to place the automatic load tap changer switch on the A Reserve Station

Service Tr1;1nsformer in the automatic position after a manual adjustment was identified

as-a non-cited violation. -This matter was the*result of operator inattention during

equipment operation.

02.2

Unit 2 Containment Closeout

a.

Inspection Scope (71707)

On May 21, the inspectors performed a containment closeout walkdown to review

containment conditions prior to unit restart.

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b.

Observations and Findings

C.

The inspectors accompanied the plant operators as they performed a walkdown of the

Unit 2 containment prior to the unit restart. A number of items were noted during the

walkdown such as an unsecured trash rack door to the containment sump, tywraps and

small bits of loose wire on the decking. All the large equipment stored inside

containment was adequately secured, and no loose debris was noted inside the

containment sump. The overall condition of the containment was adequate to support

restart of the unit. Responsible licensee personnel were informed of walkdown findings

prior to exiting containment.

Conclusions

The licensee's preparation of the Unit 2 containment prior to restart from the refueling

outage was satisfactory. Minor deficiencies were identified and corrected prior to

containment closeout.

02.3

Unit 2 Engineered Safeguards Feature (ESF) Actuation During High (Hi) Consequence

Limiting Safeguards (CLS) Relay Replacement

a.

b.

Inspection Scope (71707, 62707)

The inspectors reviewed the events and licensee's actions following the receipt of an

unexpected ESF actuation during a relay replacement activity in the Hi CLS system.

Observations and Findings

On April 26, at approximately 8:37 a.m., with Unit 2 in the refueling shutdown mode, a

spurious Hi CLS signal was generated during the replacement of relay 2-CLS-RLY-181

in the B train of the Hi CLS system. The relay was being replaced as a preventive

maintenance activity in accordance with work order 00392317-01 and procedure O-ECM-

1801-01, "Westinghouse Type BF or BFD Relay Replacement," Revision 12. All

components associated with the CLS system, with the exception of 2-RM-TV-2008 and

the Hi CLS actuation logic, were properly tagged out and defeated .. Upon receipt of the

Hi CLS signal, trip valve 2-RM-TV-2008 closed as designed. This isolated the

containment particulate and gaseous radiation monitors.

This event was initially reported to the NRC in accordance with 10 CFR 50.72 as a four

  • hour non-emergency*ESF actuation. Subsequent to this report, the licensee determined

that the event did not meet the criteria for reporting an ESF actuation. Specifically, the

event was determined not to be reportable because the actuation of the Hi CLS logic

was the result of an invalid signal and resulted in the actuation of only one component

which did not mitigate the consequences of the event. On May 21, the licensee

retracted the event report.

,

A review of the event by the inspectors and the licensee revealed that the relay being

replaced was not in the proper configuration for relay removal. Specifically, the Hi CLS

C.

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logic was energized and therefore procedu~e O-ECM-1801-01 requires that a temporary

modification Uumper) be used to properly isolate the relay. Operations personnel

authorized the replacement of relay 2-CLS-RLY-181 and assigned the work to the tagout

for the Hi-Hi CLS actuation logic. In doing so, they failed to recognize or inform

maintenance personnel that Hi CLS relay 2-CLS-RLY-181 would not be de-energized.

Personnel replacing the relay incorrectly assumed, without verifying, that the relay was

de-energized and did not request the use of a jumper. Detailed written procedures for

preventive or corrective maintenance operations which would have an effect on the

safety of the reactor are require by TS 6.4.A. 7. The failure to follow procedures which

are required by TS 6.4.A.7 is a violation of TS 6.4.D. This Severity Level IV violation is

being treated as a NCV, consistent with Appendix C of the NRC Enforcement Policy.

This violation is in the licensee's corrective action program as DRs S-99-1013 and S-99-

1018, and is identified as NCV 50-281/99003-02.

Conclusions

The failure to follow procedures to properly de-energize the Unit 2 High (Hi)

Consequence Limiting Safeguards (CLS) logic circuitry during the replacement of a Hi

CLS relay was identified as a non-cited violation. This resulted in an unanticipated

engineered safeguards actuation of the B train of Hi CLS. Operations authorized the

relay replacement under a tagout for the Hi-Hi CLS actuation logic and maintenance

personnel failed to verify the relay was de-energized.

II. Maintenance

M1

Conduct of Maintenance

M1 .1

Inspection of Unit 2 Safety Injection Check Valve

a.

Inspection Scope (62707, 71750)

b.

The inspectors observed elements of maintenance planning, mock-up training, As-Low-

As-ls-Reasonably-Achievable (ALARA) planning and engineering support for open and

inspection activities of six-inch low head safety injection check valve 2-Sl-79. The valve

had failed a leak test early in the Unit 2 refueling outage.

Observations and Findings

  • The inspectors-attended a series of planning meetings related to the work surrounding

check valve 2-Sl-79, which was projected by health physics (HP) department as a high

radiation dose job, based on historical data and plant conditions. Each meeting was

comprehensive, and attempted to take advantage of "lessons learned" from previous

work activities on a similar check valve (1-Sl-85) conducted during the last Unit 1 outage.

The inspectors observed that ideas were constantly solicited from craft mechanics,

welders, health physics personnel and supervisors on ways to reduce radiation dose

and/or expedite the job. Special attention was given to staging extra tools for valve

disassembly, mechanics practicing disassembly using mock-ups, foreign material

9

exclusion (FME) control and contingencies if inspection of.the valve should determine

that replacement would be necessary.

The inspectors reviewed procedure O-MCM-0417-01, "VELAN Swing Check Valves

Inspection and Overhaul," Revision 6, and accompanied the mechanical maintenance

supervisor in observing the valve inspection from a remote video monitor. The valve

inspection included cover removal and inspection, FME apparatus installation, as-found

visual inspection (VT), hangar and disc removal, and "blue check" of the seating surface.

The inspectors observed that the two mechanics worked expediently, yet were cautious

in following procedural steps. The mechanics were in radio communication with the

supervisor who was also following the procedure. The visual inspection revealed that

the valve seat was severely eroded and that valve cutout and replacement would have to

be accomplished. The effectiveness of preplanning activities was evident in that the

entire inspection activity, from mechanics starting disassembly to installing an FME cover

over the valve body and vacating the valve area, took less than 30 minutes.

c.

Conclusions

The licensee's planning for the inspection of low head safety injection check valve was

comprehensive. Coordination between various plant departments was evident.

Appropriate use of mock-ups and As-Low-As-ls-Reasonably-Achievable concepts was

observed. Technical input from craft workers was used extensively in the planning

process .

M 1.2 Rotating Element Replacement on 2-FW-P-3A

a.

Inspection Scope (62707)

b.

The inspectors observed portions of the planning, replacement, and troubleshooting

efforts during the replacement of the rotating element on Unit 2 motor driven auxiliary

feedwater pump, 2-FW-P-3A.

Observations and Findings

The rotating element for 2-FW-P-3A was scheduled to be replaced in response to

concerns about diffuser cracking and the effect on pump performance. New stainless

steel rotating assemblies (diffuser and impeller assemblies mounted on a common shaft)

had been purchased from the vendor and were going to be used as a one-for-one

  • replacement for the rotating assembly-currently installed in the pump. During the

installation of the new rotating assembly, the mechanics noted that the pump shaft would

not spin without rubbing. The pump was disassembled and inspected. Metal filings and

indications of metal-to-metal rubbing were found inside the rotating assembly. After

consultation with the vendor, the inner diameter of the rotating assembly was machined

to increase the tolerances. When the rotating assembly was installed into the pump

casing for the second time, binding was again noted when the shaft was rotated. A

second rotating assembly was installed in the pump casing and again binding was noted .

The original rotating element was cleaned and reinstalled in the pump. No degradation

C.

10

of the diffuser assembly was noted during visual inspection. The pump was satisfactorily

retested and returned to service. The licensee is investigating the cause of the binding

in the replacement rotating assemblies.

Conclusions

Because of binding problems with two new rotating elements, the licensee was unable to

install a new rotating element in the Unit 2 A motor driven auxiliary feedwater pump. The

original rotating element was visually inspected and reinstalled in the pump.

M1 .3

Fuel Assembly Top Nozzle Replacement

a.

Inspection Scope (62707)

The inspectors observed portions of the inspection and repair of fuel assemblies found to

have damaged hold;.down springs retaining bolts.

b.

Observation and Findings

Prior to the removal of the spent fuel assemblies from the reactor vessel, the licensee

. was informed of problems at other plants which had discovered that certain fuel

assemblies had damaged hold-down spring retaining bolts. Although the specific design

of the fuel assemblies were different at the other plants, bolts from the same lot were

used on 60 assemblies that were present in the Unit 2 reactor core, and 44 of these

assemblies were scheduled to be reloaded during refueling. None of the Unit 1

assemblies had hold-down bolts from the lot in question. Licensee management decided

to replace the top nozzles on any fuel assembly in question which was to be returned to

the core during refueling. During removal of the fuel assemblies from the Unit 2 reactor

core, each assembly was visually inspected. Several of the 60 assemblies were noted to

have enlarged gaps in the top nozzle indicating possible problems with the hold-down

spring bolts. The Unit 2 core was re-designed such that only 16 of 44 fuel assemblies

would be reused in the. upcoming fuel cycle. The top nozzle assembly on each of the 16

fuel assemblies was replaced with a new top nozzle assembly with improved hold-down

springs and bolts from a different lot. No problems were encountered during the

replacement of the top nozzles on the reused fuel assemblies.

c.

Conclusions

  • The licensee identified a problem with hold-down spring retaining bolts on several fuel

assemblies present in the Unit 2 core and decided to the repair any potentially

susceptible fuel assembly scheduled to be returned to the core. The top nozzles on 16

fuel assemblies were successfully replaced.

11

M1 .4

Observation of Maintenance Activities

a.

Inspection Scope {62707)

b.

C.

The inspectors observed portions of the following work orders (WOs):

409702-01

401130-01

404767-01

405974-01

406454-04

375462-01

410971-01

Fuel Assembly Repairs, Surry Unit 2

lnspecUOverhaul Motor Driven Auxiliary Feedwater (MDAFW)

Pump

Protective Relay Maintenance, Reserve Station Service

Transformer B

Functional test of L TC Controller

Freeze Seal downstream of 2-SI-MOV-2869B to Allow Testing

Charging Pump C Normal Feed Breaker PM

Remove/Reinstall Gland Steam Supply Strainer

Observations and Findings

All work had been properly approved by the operations department and was included on

the plan of the day (POD) or the outage schedule. The inspectors found that the work

performed under these activities was professional and thorough. Tagout number 2-99-

FW-0012 for the A MDAFW pump was reviewed and found to be properly prepared and

authorized. The tagged components were in the required positions and the tags were

properly installed. The work was performed with the work package present and in use.

Accompanying documents such as procedures and supplemental work instructions were

properly followed. Personnel were experienced, properly trained and knowledgeable of

their assignments.

Conclusions

Observed maintenance activities were properly performed. Personnel conducting the

activities were knowledgeable and properly followed work package instructions. The

tagout for the A motor driven auxiliary feedwater pump was properly implemented.

M1 .5

Periodic Test (PD Observations

a.

Inspection Scope (61726)

The inspectors observed the performance of the following PTs:

-*

OPT-SW-003

CAL-046

2-0PT-Sl-008

2-0PT-ZZ-002

2-NSP-RX-0014

Emergency Service Water Pump 1-SW-P-1C

Source Range Discriminator Voltage and High Voltage

Determination

Delta P Testing of 2-SI-MOV-2869A

ESF Actuation with Undervoltage and Degraded Voltage-

2J Bus

Rod Exercise Test

E1

12

b.

Observations and Findings

The inspectors verified that the tests were properly approved by management and

included on the POD. The inspectors checked selected components for their pre-test

and post-test positions to ensure that they were properly positioned and no

discrepancies were identified. The inspectors checked test instruments to ensure proper

calibration and that the due dates had not expired. When the tests affected TS

components, the inspectors ensured that appropriate TS action statements were

implemented. The inspectors also reviewed the test acceptance criteria to ensure they

were consistent with TS requirements. The inspectors reviewed selected test data after

the completion of the test to ensure component performance was satisfactory.

During test performance, the inspectors evaluated procedure adherence and worker

knowledge of the assigned activities. The inspectors found the testing work practices to

be satisfactory.

c.

Conclusions

Five routine periodic tests observed were properly performed. The tests were properly

approved by station management, test procedures were properly followed by

knowledgeable workers and Technical Specification requirements were satisfied .

Ill. Engineering

Conduct of Engineering

E1 .1

Unit 2 Containment Thermo-Lag Modification

a.

Inspection Scope (37551)

The inspectors reviewed the implementation of Design Change Package (DCP)98-007,

"Containment Radiant Energy Shields."

b.

Observations and Findings

C.

In correspondence to the NRC, the licensee committed to install non-combustible radiant

energy shields in the Unit 1 and Unit 2 containments during the 1998 Unit 1 refueling

outage and the 1999 Unit 2 refueling outage. The inspectors reviewed the associated

DCP and physically"verified in the field that the licensee installed the modification in Unit

2 during this refueling outage. The modification had previously been completed on

Unit 1 (See Section E1 .1 of NRC Integrated Inspection Report Nos. 50-280, 281/98-09).

Conclusions

The modification to resolve Thermo-Lag issues inside the Unit 1 and Unit 2 containments

has been completed .

13

E1 .2

Low Head Safety Injection (LHSI) Recirculation Line Modification

a.

Inspection Scope (37551)

The inspectors reviewed the implementation of DCP.98-053, "LHSI Recirculation Line

Relocation/Surry/Unit 2."

b.

Observations and Findings

The modification was implemented to address an issue with available recirculation flow

when both LHSI pumps were operating in parallel. Prior to implementation of the

modification, the pump recirculation line originated downstream of the pump discharge

check valve which could result in insufficient flow during periods of parallel operation with

RCS pressure greater than LHSI pump discharge pressure. The modification rerouted

the pump recirculation line upstream of the pump discharge check valve. The

modification also installed a small (~ inch) bypass line with a normally open* isolation

valve around the pump discharge check valve. This line was installed to provide a flow

path to the refueling water storage tank (which had previously existed prior to the

modification) for small amounts of leakage into the LHSI system from the RCS and

thereby preventing system pressurization. The inspectors verified that the

aforementioned bypass isolation valve was added to the system lineup procedure.

The inspectors reviewed the associated DCP and physically verified field implementation

of the modification. The inspectors also observed the post modification testing

associated with completion of the DCP. During parallel operation of the LHSI pumps

after completion of the modification, recirculation flow was below the pump vendors

recommended 150 gpm flow rate per pump. The A pump developed approximately 122

gpm and the B pump developed approximately 148 gpm. Both pumps developed greater

than 150 gpm when not operating in parallel. The licensee determined that the flow rates

achieved were adequate and documented the results in an engineering transmittal. The

inspector's evaluation of the measured flow rates versus the vendor's recommended flow

rate is discussed in section EB.2. The inspectors noted that the modification improved

the pump recirculation flow during parallel operation for the weaker pump and decreased

the flow for the stronger pump. The inspectors questioned whether a future modification

would be considered to improve recirculation flow rates during parallel pump operation

and was informed by licensee management that no further modification would be

considered.

During field observation *of pump performance after implementation of the modification to

the recirculation piping, the inspectors observed and heard vibration in the recirculation

piping. The licensee was aware of the vibration, and made acceleration/velocity readings

at a point having the highest observable amplitudes. The licensee's engineering

mechanical group reviewed the vibration data and concluded that the maximum pipe

stresses were below the endurance limit of the material, with adequate margin for

discontinuities in the piping, such as welds and branch connections. Engineering

concluded that the structural integrity of the piping system would not be challenged by

the observed vibrations. Inspection followup item (IFI) 50-281/99003-03 was opened to

C.

14

review the licensee's structural integrity conclusions concerning vibration of the LHSI

pump recirculation piping.

  • Conclusions

The Unit 2 low head safety injection (LHSI) pump recirculation lines were modified to

improve recirculation flow for the weaker pump during parallel pump operation. While

the recirculation flow for the weaker pump increased from previous values, the flow rates

for both LHSI pumps were below the vendor's recommended values. The licensee

determined the achieved recirculation flow rates were acceptable.

E1 .3

Review of Design Changes

a.

Inspection Scope (37550)

The inspectors reviewed a sample of design changes implemented during the current

refueling outage on Unit 2. The basic requirement applicable to this area of inspection

was 10 CFR Part 50, Appendix B, Criterion Ill, Design Control. Regulatory Guide 1.64,

"Quality Assurance Requirements for the Design of Nuclear Power Plants," (ANSI

N45.2.11) was also applicable.

b.

Observations and Findings

Sixty-seven design changes were implemented on Unit 2 during the current refueling

outage. Thirty of the design changes were classified as safety-related. The following

safety related DCPs were reviewed:

97-030 98-006

98-023 98-044

98-053 98-056

98-092

Residual heat - FCV/HCV support removal

Containment floor plug elimination

Motor operated valve replacement, SW 2048, 204C and 204D

Pressurizer level transmitter spans revised

Turbine driven auxiliary feedwater pumps steam supply valve logic

change

Low head safety injection pumps reroute recirculation piping

Inside recirculation spray pumps and low head safety injection

pump overcurrent trip device replacement and reset

Reactor protection system test circuit surge suppressors

The inspectors found that the safety evaluations for all the design changes reviewed

adequately demonstrated that the changes would maintain the design basis. The

objective of each change was clearly stated in the design change package, and the

inspectors agreed that the changes met the stated objective. The inspectors noted that

the safety evaluations included Year 2000 computer considerations where appropriate.

For one design change, the inspectors confirmed that a relevant 10 CFR Part 21 report

had been evaluated by the licensee. The inspectors observed that the specified post-

modification tests were adequate to demonstrate that the design objectives of the

changes were met and that the systems were operable. Where available during the

'( *

15

inspection, the test data was reviewed and found acceptable. The cognizant engineers

were able to satisfactorily answer questions posed by the inspectors concerning the

design changes. The design changes reviewed were prepared by four different

organizational groups, so they were seen as representing the work of a large percentage

of the engineering organization.

c.

Conclusions

The inspectors reviewed a sample of design changes implemented on Unit 2 during the

current refueling outage and concluded that the licensee's design change process met

the requirements in the area of design control.

E1 .4

Review of Safety Evaluations

a.

Inspection Scope (37001)

b.

The inspectors reviewed a sample of recently completed safety evaluations which had

been prepared pursuant to 10 CFR 50.59, "Changes Tests and Experiments."

Observations and Findings

The licensee submits to the NRC a list of facility, procedure or method of operation

changes each month as part of the Monthly Operating Report. These changes required

licensee evaluations to determine whether they represent an unreviewed safety question

as defined in 1,0 CFR 50.59. The inspectors obtained the lists submitted for the months

of November 1998 through February 1999, and they indicated a total of 46 safety

evaluations had been performed during those months. The inspectors chose the

following safety evaluations for review:

Changes to Electrical Corrective Maintenance Procedure O-ECM-

0103-02, "Station Battery UPS System Maintenance." The

procedure was revised to provide for connecting a test load and

other temporary changes for the purpose of conducting

maintenance tests.

Changes to Operations Procedure 1-0P-RC-001A, "Reactor

Coolant System Valve Alignment." The procedure was changed

to require operating with a certain drain valve closed rather than

  • the open position.-

Evaluate the reduction in containment wall thickness from that

specified in UFSAR, Section 15, while work is in progress to

remove and repair spalled/loose concrete from the Unit 2

containment exterior wall.

The inspectors found that the reviewed safety evaluations addressed whether the

changes would alter the performance or integrity of any structure, system or component

16

important to safety through the answering of detailed questions on the formal evaluation

form. The potential effect of the proposed change on the ability of the operators to

control and monitor the plant was considered. The inspectors found that the safety

evaluations addressed potential failure modes and electrical loading. The inspectors

noted that TS were discussed in relation to each proposed change. The inspectors

observed that any impact on special programs or equipment was considered through a

24-question form. The inspectors noted in particular that the unreviewed safety question

portion of the review specifically discussed the design basis accidents considered in the

review. The inspectors found that the safety evaluations reached correct conclusions

with regard to the considerations mentioned above.

The inspectors examined the work in progress covered by Safety Evaluation 98-124 and

verified that the safety evaluation adequately described the changes to containment wall

thickness while concrete repairs were in progress. The licensee's conclusions in the

safety evaluation were acceptable.

The documentation of the safety evaluations included written statements for all the

considerations mentioned in the previous paragraphs. Documentation included a listing

of all the identified applicable UFSAR sections. The documentation included statements

of limiting conditions and special requirements together with the relevant formal tracking

mechanism. There were signatures by the evaluators of certain individual considerations

such as reactivity, radiation control, emergency preparedness, etc., where those persons

were different than the overall reviewer. The inspectors also noted that the safety

evaluations were readily retrievable from records storage.

c.

Conclusions

The inspectors reviewed a sample of recently completed safety evaluations performed

pursuant to 10 CFR 50.59. The safety evaluations reached correct conclusions

concerning whether the proposed change would compromise safety and whether an

unreviewed safety question was involved. Documentation of the safety evaluations was

complete.

E1.5

Review of DRs

a.

Inspection Scope (37550)

The inspectors reviewed a sample of DRs generated during the current Unit 2 refueling

.. outage and followed up on deficiency DRs discussed in previous inspection reports. The

basic requirement applicable to this area of inspection is 10 CFR 50, Appendix B,

Criterion ~VI, "Corrective Action".

b.

Observations and Findings

As of May 12, 1999, there were about 216 routine level DRs generated during the

current Unit 2 outage and there were 15 potentially significant (i.e. second highest of the

three levels) DRs generated. There were no significant level reports generated. The

.

17

inspectors obtained a summary statement for each DR. The inspectors evaluated,

inspected or discussed with the cognizant engineers all of the potentially significant level

reports. The inspectors reached the conclusion that all of these problems were either

resolved by the licensee or significant progress had been made to give confidence that

the problem would be resolved in a timely manner. The inspectors reviewed the

summary statements for about 30 percent of the routine level DRs. The inspectors found

that all of these had been correctly classified and the initial assessments and corrective

actions were appropriate to the circumstances. DR S-99-1067 documented an

evaluation for a case where the running amperes for a motor operated valve measured

during a routine valve diagnostic test was higher than the criterion in the test process.

The inspectors reviewed this DR in detail, discussing various aspects with electrical

design engineering and the MOV coordinator. The inspectors concluded that the

reasons for accepting the higher than expected current were valid.

NRG Inspection Report No. 50-280/98-09 discussed a case where work scheduling and

planning had not replaced a degraded arcing contact in a safety-related 4160 V circuit

breaker at the earliest opportunity, even though there were two previous opportunities to

do so. During this inspection, the inspectors confirmed that the cracked arcing contact

was replaced by Work Order 395596 on February 16, 1999.

The inspectors reviewed DR numbers S-99-1007, -1033, and -1055. These DRs

addressed testing of the setpoints for the Unit 2 main steam safety relief valves which

were slightly outside the Technical Specification plus or minus 3 percent limits. The test

data were as follows:

Valve Number

TS Limits (psig)

As-found Test Results (psig)

2-MS-SV-203C

1077 - 1143

1143.8

2-MS-SV-201 C

1053 - 1117

1127

2-MS-SV-204C

1087 - 1153

1084

The licensee's corrective actions were to readjust the setpoints for the three valves

which failed the surveillance tests and test the remaining 12 valves. The remaining 12

valves were within the TS acceptance limits. The inspectors determined the resolution

for the three valves which failed the surveillance tests and the expanded test sample size

were acceptable.

DRs S-99-0921, -0982, and -1071 were also reviewed. These DRs were initiated by the

licensee to document and disposition the results of snubber visual inspections which did

not comply with Technical Specification acceptance criteria. DR numbers S-99-0921

and -0982 concerned six snubbers which had low fluid levels in their reservoirs. These

snubbers were functionally tested in accordance with the TS requirements and found to

be operable. DR S-99-1071 was initiated to document that two snubbers on the

feedwater line were found to be fully compressed in their cold set position. The licensee

issued Engineering Transmittal S-99-093 to evaluate this problem. The licensee's

18

engineering evaluation showed that upon piping heatup, the piping would move outward

which would relieve any binding of the snubbers when the snubbers extended.

Therefore the snubbers were operable during plant operation. Additional corrective

adions included -modifications to the pipe support to shorten the snubber support

brackets so that the snubbers would not be fully compressed when they were in the cold

position.

c.

Conclusions

The inspectors reviewed deviation reports generated during the spring 1999 refueling

outage and concluded that the licensee's corrective action program Was meeting the

E2

Engineering Support Of Facilities and Equipment

E2.1

Review of Program for Visual Inspection of the Reactor Containment Structures

a.

Inspection Scope (37500)

The inspectors examined the licensee's program for inspection of the

containment structure.

b.

Findings and Observations

The inspectors reviewed the licensee's in service inspection manual, Section 7 .22,

Revision 1, dated February 1, 1999, for visual inspection of the reactor containment

buildings. This procedure specifies the requirements for performance of visual

inspection of the containment structures in accordance with Article IWE of ASME Section

IX. 10 CFR 50.55a requires the licensee to implement the requirements of IWE Section

IX by September 9, 2001. In preparation for implementation of the containment

inspections, licensee engineers have performed inspections of the containment buildings

to identify and repair deficiencies in protective coatings, the containment building steel

liner, penetration areas, and in other areas in the containment. These visual inspections

have also included the exterior concrete surface of the containments. The inspectors

reviewed the following records which documented the results of the licensee's

inspections:

Summary of results of Unit 1 containment walkdown performed on May 14, 1998.

DR S-98-2606, S-98-2980, and S-99-0955

Summary of results of Unit 2 containment walkdown performed on April 21, 1999.

On May 12, 1999, the inspectors performed a walkdown inspection of the Unit 2

containment building on elevations -27', -3.5', 18.5', and 47'. The inspectors identified

the following deficiencies which the licensee had not identified during their inspections:

19

The coatings on a ventilation duct near Column line 7 at' elevation 9' had loose

(delaminated) coatings. The ventilation duct was in close proximity to the reactor

building sump.

The grating which covers the drain trench in the containment basement (elevation

-27') were not secured in any manner to prevent the gratings from being

dislocated. Several of the gratings were overlapped with other gratings, bent, or

had gaps between adjacent gratings. The concern was that the trench bypasses

the reactor building trash rack and leads to the reactor building sump. If the

grating is dislocated during accident conditions, it would be possible for debris to

bypass the sump trash racks and partially clog the sump screens.

The concrete floor in the area of RHR pump 2-RH-P-18 (elevation -13') has been

damaged by boric acid solution leaking from the pumps and associated piping

and fittings. The cementitious material has been dissolved resulting with an area

approximately 20 to 25 square feet with exposed aggregate. A trench

approximately 8 feet in length, approximately 1 to 1.5 inches deep extends

between the pump and floor drain. The concern is that the concrete reinforcing

steel and embedded plates in the area could be degraded from corrosion caused

by the boric acid.

The licensee initiated DR S-99-1316 to document and disposition the above

discrepancies. Prior to containment closeout the grating which covers the drain trench

was repaired and reinstalled. This resolved the issues of the grating being bent and

having gaps between adjacent sections. The licensee reviewed the design of the trench

grating and determined the grating did not need to be secured to perform its function.

During the walkdown inspection the inspectors also identified the presence of corrosion

on the steel liner plate at the intersection of the concrete.slab and liner at elevation -27'.

The corrosion appears to extend below the concrete slab for an unknown distance.

There is evidence that, although the coatings in this area had been previously repaired,

the coatings are starting to fail in this zone. A similar situation existed in Unit 1

containment and was addressed by DR S-98-2606. Based on the DR evaluation and the

licensee's May 14, 1998, summary of inspection results, the Unit 1 liner was

dispositioned as being adequate. The licensee stated that the Unit 1 disposition also

adequately addressed the Unit 2 liner corrosion. The licensee's inspection results stated

that the gap between the liner and concrete slab was sealed by a "tight" rust scale which

would prevent moisture intrusion and corrosion of the liner plate below the slab.

However, the inspectors questioned the basis*for this conclusion. The presence of the

corrosion will inhibit the application of protective coatings to prevent additional corrosion

of the liner plate. It is well established that the principal purpose of coatings is to seal the

surface of the steel liner and reduce the rate of corrosion of the metal. The presence of

the corrosion will not inhibit additional corrosion, but may actually accelerate the

corrosion rate.

The inspectors noted that licensee inspections performed to comply with Article IWE and

10 CFR 50.55a will require determination of the extent of corrosion (flaw size) by

20

measurement, evaluation of the flaws, and repairs if necessary. The licensee's current

evaluation will not satisfy the requirements of 10 CFR 50.55a and Article IWE which are

effective September 9, 2001. The extent and depth of the corrosion are unknown at this

time. On June 15, 1999, a conference call was held with the inspectors, the licensee and

participants from the Region II office and NRR to further discuss the licensee's actions

on containment liner corrosion. The licensee stated that work orders exist to repair Unit

1 liner corrosion located above the slab and that engineering will examine the condition

of the liner before coatings are reapplied. The licensee is planning to perform a liner

inspection per Article IWE during the next Unit 1 and 2 refueling outages. In addition,

engineering is reviewing their overall effort for resolving liner corrosion to determine if

addition actions are needed and to elaborate on their evaluation which accepted the Unit

1 liner corrosion. Inspection Followup Item 50-280, 281/99003-04 was opened to review

engineering's additional reviews and resulting actions to resolve containment liner

corrosion.

c.

Conclusions

The licensee's program for maintenance, inspection and repairs to containment coatings

was adequate. Containment liner corrosion at the basement slab/liner intersectiqn was

observed. The licensee is continuing to review their efforts to resolve the liner corrosion.

MB

Miscellaneous Engineering Issues (92903)

E8.1

(Closed) IFI 50-280, 281/98201-05: adequacy of 4160 V electrical cables to withstand

fault current. The licensee's rationale for accepting the 4160 V cables, even though they

are undersized in the traditional sense from the short-circuit viewpoint was described in

NRG Inspection Report No. 50-280/99-01, Section E8.1. After further review of the

licensee's rationale, the size of the 4160 V electrical cables is considered adequate.

E8.2

(Closed) IFI 50-281/99001-04: review the acceptability of reduced minimum flows for the

low head safety injection pumps after piping modifications. This item questioned whether

Unit 2 low head safety injection (LHSI) pump recirculation minimum flows would be

sufficient to preclude hydraulic instabilities after a piping modification.

The LHSI pumps are vertical two stage centrifugal pumps manufactured by Byron

Jackson. A letter from Byron Jackson to the licensee dated July 8, 1988, gave the rated

conditions for these pumps as 3000 gallons per minute (gpm). This letter also indicated

that the pumps could be operated at a minimum flow of 150 gpm. The licensee found

  • that themanufacturer*considered*this minimum-flow sufficient to avoid pump damage

due to temperature rise and flashing during continuous operation but that it did not

preclude the possibility of damage due to hydraulic instabilities. Licensee documents

indicated that a minimum flow of about 900 gpm might be needed to preclude damage

due to hydraulic instabilities.

LHSI pump recirculation operation involves two cases. (1) parallel pump recirculation for

a maximum of 30 minutes or (2) single pump recirculation for an estimated 17 hours1.967593e-4 days <br />0.00472 hours <br />2.810847e-5 weeks <br />6.4685e-6 months <br /> plus

24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> in piggyback mode (i.e. feeding the suction of the safety injection charging

e

21

pump). The licensee used pump recirculation flow measurements obtained following the

modification and estimated piggyback flow to evaluate both cases. These flows were as

follows:

Pump

Number

U2-1A

U2-1B

Parallel Pumps on

Recirculation

122 gpm

148 gpm

Single Pump on

Recirculation

171 gpm

217 gpm

Piggyback

Mode

400 gpm

400 gpm

The licensee evaluation found that the flows were adequate in both single and parallel

pump recirculation, as summarized below:

Parallel Pump Operation: The measured flows for the pumps in this operating mode

were below 150 gpm after the modification. Therefore, the licensee evaluated whether

unacceptable temperature rise, flashing, and hydraulic instabilities would result. The

Hydraulic Institute Standard (1994 Edition) indicates that the temperature rise across a

pump should be limited to 15°F and that there should be a safe margin against flashing.

The licensee calculated that the temperature rise would only be 9°F during the 30

minutes of operation and that the outlet temperature would be 53°F, which is well below

the flashing point at the given suction head. With regard to hydraulic instabilities, suction

and discharge recirculation resulting from low flow were of concern. The Hydraulic

Institute Standard indicated that suction recirculation is a potential problem in high-

energy pumps and can cause localized pitting. The licensee noted that the LHSI pumps

are not high-energy pumps, and that any pitting that may occur would be slow and not

cause significant mechanical degradation during the mission time. The standard states

that discharge recirculation can lead to mechanical vibration and bearing failure. The

licensee took vibration readings on the upper motor bearing after the modification, before

declaring the pumps operational. The vibration readings were unchanged from historical

levels, and the licensee concluded that the reduced minimum flow was not at a level that

would result in damaging discharge recirculation. Based on their above evaluations the

licensee concluded that parallel pump recirculation flow following the modification was

adequate.

Single Pump Operation: The single pump operation flows measured by the licensee

after the modification were above 150 gpm, such that ur:iacceptable temperature rise and

flashing were not a concern. However, flow was sufficiently low for possible hydraulic

instabilities. * Based on the vibration measurements referred to in the previous paragraph,

the licensee concluded that the single pump operation flows were adequate.

For both parallel and single pump operation the inspectors concluded that the licensee

had adequately demonstrated the acceptability of recirculation flows through their

evaluations.

In March, 1999, prior to the implementation of the recirculation line modification, the

inspectors performed a review of Engineering Transmittal CME 98-014, "Evaluation of

22

Operation of LHSI Pumps Recirculating to the RWST," Revision 3. The inspectors

generated an inquiry based on questions of lack of inclusion of uncertainty in the

calculation, the age of the test data used, and the validity of using the recent test results

made at a very flat portion of the curve for monitoring flow degradation. In reply the

licensee provided the inspectors with the position paper "Low Head Safety Injection

Pump 2-SI-P-1A Operability, Surry Power Station -Unit 2," a letter from Byron Jackson

dated April 15, 1999, concerning their review of the position paper, and "Virginia Power

Response to NRC Inquiry Regarding Engineering Transmittal CME 98-014," Revision 3.

The responses revisited the operability of the pump considering a dead-headed

condition. The licensee and a manufacturer's representative, based on calculation,

knowledge of pump characteristics, and test data indicated that the pumps are currently

not degrc1ded due to past operation at potential dead-headed conditions. Based on the

new evaluation, and the manufacturer's concurrence, the inspectors operability concerns

with the pump have been addressed.

IV. Plant Support

R1

Radiological Protection and Chemistry Controls

R1 .1

General Observations (71750)

On numerous occasions during the inspection period, the inspectors reviewed radiation

protection (RP) practices including radiation control area entry and exit, survey results,

and radiological area material conditions. No discrepancies were noted, and the

inspectors determined that RP practices were proper.

The plant primary and secondary chemistry logs were reviewed to ensure that plant

chemistry. was within the Technical Specification and procedural limits. No deficiencies

were noted.

On May 21, the inspectors observed the addition of hydrazine to the Unit 2 reactor

coolant system. The evolution was performed in accordance with the requirements

specified in procedure 2-0P-CH-008, "Chemical Addition to the RCS," Revision 5.

R1 .2

Tour of Radiological Protected Areas

a.

Inspection Scope (83750)

The inspectors reviewed implementation of-selected elements of the licensee's radiation

protection program as required by 10 Code of Federal Regulations (CFR) Parts 20.1201,

1501, 1502, 1601, 1703, 1802, 1902, and 1904. The review included observation of

radiological protection activities including control of radioactive material, radiological

surveys/postings, and radiation area/high radiation area controls.

23

b.

Observations and Findings

During tours of the turbine building,' reactor building, auxiliary building, and storage and

handling facilities, the inspectors reviewed survey data and observed activities in

  • progress. Based on these observations the inspectors determined that the licensee had

effectively posted areas where radioactive material was stored and radioactive material

observed was labeled as required. Lock boxes containing keys to Locked High

Radiation Areas and Very High Radiation Areas were inventoried by the inspectors and

all keys were accounted for. During tours the inspectors observed that Locked High

Radiation Areas were locked and controlled as required by licensee procedures.

Radiological surveys reviewed were well documented and areas observed were posted

consistent with the survey documentation. Independent surveys were performed by the

inspectors in selected areas of the auxiliary building to 'verify licensee survey results.

Survey instrumentation and continuous air monitors observed in use within the

radiological controlled areas were operable and currently calibrated. The inspectors

determined the licensee had an adequate number of survey instruments available for

use during the outage and the instruments were being calibrated and source checked as

required by licensee procedures.

Selected radiation work permits (RWPs) were reviewed for adequacy of the radiation

protection requirements based on work scope, location, and conditions. For the RWPs

reviewed, the inspector noted that appropriate protective clothing and dosimetry were

required. During tours of the plant, the inspectors observed the adherence of plant

workers to the RWP requirements during the performance of work.

The inspector reviewed selected personnel contamination events (PCEs) and discussed

contamination control practices for selected outage operations. As of April 26, 1999,.

approximately 30 PCEs, had occurred. This number of PCEs included both particles and

dispersed contamination events for clothing and skin. Based on records reviewed, all

skin doses were well below regulatory limits. During tours of the Unit 2 reactor building

and auxiliary building the inspectors observed adequate contamination control practices.

Contaminated square footage was being maintained less than one percent of the total

RCA during non-outage periods and approximately three percent during the outage.

c.

Conclusions

The licensee was effectively maintaining controls for personnel monitoring, control of

radioactive material, *radiological postings, radiation area controls, and high radiation

area controls as required by 1 O CFR Part 20.

R1.3

Occupational Radiation Exposure Control Program

a.

Inspection Scope (83750)

The inspectors reviewed the licensee's implementation of 10 CFR 20.1101 (b) which

requires that the licensee shall use, to the extent practicable, procedures and

e

24

engineering controls based upon sound radiation protection principles to achieve

occupational doses and doses to members of the public that are ALARA.

b. . Observations and Findings

The inspectors review of the licensee's ALARA program determined the licensee had

established a goal of approximately 97 person-rem for the Unit 2 refueling outage

scheduled for 36 days. At the time of the inspection on April 29, 1999, the licensee was

below target with daily projections based on work scope accomplished.

The inspectors reviewed and discussed ALARA initiatives such as shielding, reactor

coolant system micron filtration, reactor crudburst shutdown activities, use of video

monitoring and teledosimetry, hot spot reduction efforts, and outage planning. The

inspectors observed an ALARA committee meeting to address the replacement of a

safety injection valve. The meeting was well attended by plant management and was

interactive. The inspectors also attended the ALARA pre-job briefing for the safety

injection valve replacement. The pre-job briefing addressed all ALARA concerns and

safety aspects. Based on these discussions and observations, the inspectors

determined the licensee was maintaining programs for controlling exposures ALARA and

continued to be effective in controlling overall collective dose. All personnel radiation

exposures during 1999 to date were below regulatory limits.

c.

Conclusions

The licensee was maintaining programs for controlling exposures As-Low-As-ls-

Reasonably-Achievable (ALARA) and continued to be effective in controlling overall

collective dose. All personnel radiation exposures during 1999 to date were below

regulatory limits.

S1

Conduct of Security and Safeguards Activities (71750)

On numerous occasions during the inspection period, the inspectors performed

walkdowns of the protected area perimeter to assess security and general barrier

conditions. No deficiencies were noted and the inspectors concluded that security posts

were properly manned and that the perimeter barrier's material condition was properly

maintained.

V. Management Meetings

X1

Exit Meeting Summary

The inspectors presented the inspection results to members of licensee management at the

conclusion of the inspection on June 4, 1999. The licensee acknowledged the findings

presented. On June 15, 1999, a conference call was held with the licensee and NRC personnel

from the Region II office and Office of Nuclear Reactor Regulation to discuss containment liner

corrosion and actions the licensee have taken and are planning to take.

'

25

The inspectors asked the licensee whether any materials examined during the inspection should

be considered proprietary. No proprietary information was identified.

  • PARTIAL LIST OF PERSONS CONTACTED

M. Adams, Superintendent, Engineering

R. Allen, Superintendent, Maintenance

R. Blount, Manager, Operations & Maintenance

E. Collins, Director, Nuclear Oversight

M. Crist, Superintendent, Operations

D. Llewellyn, Superintendent, Training

E. Grecheck, Site Vice President

B. Stanley, Supervisor, Licensing

T. Sowers, Manager, Nuclear Safety & Licensing

W. Thornton, Superintendent, Radiological Protection

IP 37001

IP 37550

IP 37551:

IP 40500:

IP 61726:

IP 62707:

IP 71707: *

IP 71750:

IP 83750:

IP 92903

INSPECTION PROCEDURES USED

10 CFR 50.59 Safety Evaluation Program

Engineering

Onsite Engineering

Effectiveness of Licensee Process to Identify, Resolve, and Prevent Problems

Surveillance Observation

Maintenance Observation

Plant Operations

Plant Support Activities

Occupational Exposure

Engineering Follow-up

ITEMS OPENED AND CLOSED

Opened

50-280/99003-01

NCV

Failure to place the load tap changer on the A

Reserve Station Service Transformer in automatic

following manual adjustment (Section 02.1)

50-281 /99003-02

NCV

50-281 /99003-03

IFI

50-280, 281/99003-04

IFI

Failure to properly de-energize the Unit 2 Hi CLS

logic circuitry (Section 02.3)

Review engineering's structural integrity

conclusions concerning vibration of the LHSI pump

recirculation piping (Section E1 .2)

Review engineering's additional reviews and

resulting actions to resolve containment liner

corrosion (Section E2.1)

Closed

50-280/99003-01

50-281 /99003-02

50-280, 281/98201-05

50-281/99001-04

NCV

NCV

IFI

IFI

26

Failure to place the load tap changer on the A

Reserve Station Service Transformer in automatic

following manual adjustment (Section 02.1)

Failure to properly de-energize the Unit 2 Hi CLS

logic circuitry (Section 02.3)

Adequacy of 4160 VAC electrical cables to

withstand fault current (Section E8.1)

Review the acceptability of reduced minimum flows

for the low head safety injection pumps after piping

modifications (Section E8.2)