ML18152A066

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Insp Repts 50-280/96-10 & 50-281/96-10 on 960908-28. Violations Noted.Major Areas Inspected:Maint,Engineering & Plant Support
ML18152A066
Person / Time
Site: Surry  
Issue date: 10/28/1996
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18152A067 List:
References
50-280-96-10, 50-281-96-10, NUDOCS 9611040199
Download: ML18152A066 (34)


See also: IR 05000280/1996010

Text

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U.S. NUCLEAR REGULATORY COMMISSION

REGION I I

Docket Nos:

License Nos:

Report No:

Licensee:

Facility:

Location:

Dates:

Inspectors:

Approved by:

9611040199 961028

PDR

ADOCK 05000280

G

PDR

50-280. 50-281

DPR-32. DPR-37

50-280/96-10. 50-281/96-10

Virginia Electric and Power Company (VEPCO)

Surry Power Station. Units 1 & 2

5850 Hog Island Road

Surry. VA 23883

September 8 - 28. 1996

R. Musser. Senior Resident Inspector

D. Kern. Resident Inspector

W. Poertner. Resident Inspector

P. Kellogg, Reactor Inspector (Sections 08.1.

08.2. Ml.3. MB.4. and M8.5)

W. Miller. Reactor Inspector (Sections Fl.1.

Fl.2. F2.1. F2.2. F3. F5. F6. F7. F8.1. and

FB.2)

N. Salgado. Resident Inspector. Oconee (Section

E4.1)

E. Testa. Senior Radiation Specialist (Sections

Rl.1. R2.1. R2.2. R7. and R8.1)

G. Belisle. Chief. Projects Branch 5

Division of Reactor Projects

Enclosure 2

EXECUTIVE SUMMARY

Surry Power Station. Units 1 and 2

NRC Inspection Report 50-280/96-10 and 50-281/96-10

This integrated inspection included aspects of licensee operations. engineer-

ing. maintenance. and plant support.

The report covers a three-week period of

resident inspection: in addition. it includes the results of announced inspec-

tions by three regional inspectors.

DRerations

The licensee's actions to repair a Unit 2 letdown line leak were appropriate

and accomplished in a methodical manner.

The management decision to

reengineer the configuration of the Unit 2 letdown line and remove the unit

from service to implement the modifications prior to the next scheduled

refueling outage seems appropriate based on the number of recent weld failures

that have occurred on the Unit 2 letdown line piping (Section 01.2).

The decision to test all four Component Cooling Heat Exchangers (CCHXs)

following a failed test on the C CCHX demonstrated an appropriate safety

perspective and sensitivity to potential common mode failure.

Increasing the

testing frequency was successful in preventing entry into a Technical

Specification (TS) Limiting Condition for Operation (LCD) during the remainder

of the inspection period (Section 01.3).

The licensee's actions to investigate and repair the A Unit 1 charging pump

motor failure were appropriate and accomplished in an expedious manner

(Section 01.4).

Issues identified during the service water self-assessment had been thoroughly

investigated and dispositioned by the licensee (Section 08.1).

Maintenance

The Unit 2 blender maintenance activity was accomplished in accordance with

the Work Order (WO) package requirements and approved procedures.

The system

was adequately isolated prior to commencing maintenance (Section Ml.1)

Engineering

Safety Evaluation 96-122 adequately justified the use of alternate boration

and dilution flowpaths and the Station Nuclear Safety Operating Committee

(SNSOC) meeting was professional and resulted in an indepth review of the

subject safety evaluation (Section El.1).

Review of standing DCP scope additions determined that they contained the

appropriate specifications. drawings. system descriptions. and safety

evaluations (Section E4.1).

Plant SURROrt

The licensee effectively implemented comprehensive training programs for the

operation of the Surry Radwaste Facility (SRF) and shipping radioactive


' *


2

materials. The inspectors determined that the revised radwaste shipping

approach. in the May 6. 1996 letter was acceptable (Section Rl.l).

No concerns with the licensee's SRF radiation monitor or calibration and

alarm. set points. equipment or High Integrity Container CHIC) lifting

attachments analysis were identified during the inspection (Section R2.1).

The Independent Spent Fuel Storage Installation (ISFSI) was properly posted

and entrance to the location appropriately controlled by Radiation Work

Permits (RWPs).

Environmental Thermo Luminescent Dosimeters (TLDs) were

verified to be in place. Adequate dose assignment as a result of neutron dose

assessment was taking place.

Surveys were taken as required and results were

selectively spot checked and found comparable.

Smear surveys were counted and

found clean.

Housekeeping was excellent at the ISFSI and low level waste

storage warehouse (Section R2.2).

The licensee was performing self assessments and taking timely and

comprehensive corrective actions.

One Unresolved Item was identified for

improper actions associated with a containment entry. A Noncited Violation

was also identified for respirators issued to nonqualified personnel (Section

R7).

The licensee was aggressively sampling and monitoring the primary and

secondary water chemistry parameters.

Parameters were maintained at a few

percent of TS limits.

The continuing training program appeared comprehensive

and provided adequate training to improve and maintain technician knowledge

and analytical skills (Section RS.l).

Corrective actions to improve RWP comprehension. Radiation Protection (RP)

coverage within containment. and stay time assessment were effectively

implemented (Section RS.2).

The licensee has been pro-active in the resolution of the Thermo-Lag issue.

Completion of the NRC review for the use of Thermo-Lag as radiant energy heat

shields in the containment is the only outstanding Thermo-Lag related issue at

Surry (Section Fl.l).

One fire protection related violation involving the failure to provide

appropriate preventive maintenance for safety related motors was identified

(Section Fl.2).

The spare equipment required for repairs following an Appendix R fire was

properly stored.

However. an Inspection Followup Item was identified for

preventive maintenance requirements on spare safety-related equipment (Section

Fl. 2).

The maintenance records. equipment trending data and inspection of the fire

protection components. indicated that there was no maintenance backlog on the

fire protection systems and. with the exception of the out-of-service fire

suppression systems for the SRF. the maintenance. operability and performance

of these systems were adequate.

The lack ~fa site procedure to establish

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appropriate compensatory measures for degraded fire protection systems and

features not included in the TSs was identified as a weakness (Section F2.1).

Appropriate surveillances and tests were being performed on the fire

protection features and systems (Section F2.2).

The fire protection program implementing procedure met the commitments to the

NRC.

However. the procedure does not require each fir*e brigade member to

participate in at least two drills per year (Section F3).

The fire brigade organization and training met the commitments to the NRC.

Not stipulating a minimum participation of at least two drills per year for

each member of the fire brigade was identified as a weakness (Section F5).

the licensee's commitments to the NRC (Section F6).

The audits and assessments of the facility's fire protection program were

through and appropriate corrective actions were taken to resolve the

identified issues (Section F7) .

1

Report Details

Summary of Plant Status

Unit 1 and Unit 2 operated at power the entire reporting period.

I. Operations

01

Conduct of Operations (71707)

01.1 General Comments (40500)

The inspectors conducted frequent control room tours to verify proper

staffing. operator attentiveness. and adherence to approved procedures.

The inspectors attended daily plant status meetings to maintain

awareness of overall facility operations and reviewed operator logs to

verify operational safety and compliance with Technical Specifications

(TSs).

Instrumentation and safety system lineups were periodically

reviewed from control room indications to assess operability. Frequent

plant tours were conducted to observe equipment status and housekeeping.

Deviation Reports (DRs) were reviewed to assure that potential safety

concerns were properly reported and resolved.

The inspectors found that

daily operations were generally conducted in accordance with regulatory

requirements and plant procedures.

01.2 Unit 2 Letdown Line Leak

a.

Inspection Scope (71707. 40500)

The inspectors reviewed the licensee's actions to repair a leak on the

Unit 2 letdown line inside containment.

b.

Observations and Findings

On September 11. at 2:19 a.m .. Reactor Coolant System (RCS) total

leakage increased to 0.941 gallons per minute (gpm) and unidentified

leakage increased to 0.849 gpm.

Previous total leakage and unidentified

leakage values were 0.139 gpm and 0.033 gpm respectively.

Based on the

increased leakage rate. containment air samples were requested and a

backup leakage calculation was initiated. The backup calculation was

consistent with the previous calculation. A containment entry was made

to try to identify the source of the increased RCS leakage.

The

containment entry identified that a leak existed on the normal letdown

line at a welded coupling downstream of valve 2-CH-HCV-2200B.

Excess

letdown was placed in service and normal letdown was removed from

service to isolate the leaking weld joint. Following isolation of

normal letdown total. leakage decreased to 0.297 gpm and unidentified

leakage decreased to 0.167 gpm.

At no time did the leakage values

exceed the TS allowed values.

C.

2

Station management conducted numerous meetings on this matter to

determine a course of action to repair the leak.

The licensee decided

to repair the leaking weld joint with the unit at power and to cut out

the failed weld so that a failure analysis could be performed.

The

licensee also decided that the unit would be shutdown and the letdown

line would be modified at the earliest opportunity once the root cause

of the weld failure was determined and a corrective action plan

developed.

The decision to shutdown the unit in the future to modify

the letdown line was based on the fact 4 weld leaks had developed in the

letdown line piping within the last 12 months.

The three previous leaks

developed on the piping tee connection immediately downstream of the

leaking coupling.

The failed coupling weld was a shop welded joint

associated with repair activities for a March 1996 letdown line weld

failure.

The licensee removed the failed weld for failure analysis and replaced

the coupling and associated piping.

Normal letdown was returned to

service on September 13 following coupling and pipe replacement

activities. The failure analysis performed on the failed weld

determined that the weld failed as the result of a fatigue crack which

initiated at a lack of fusion discontinuity in the fillet weld between

the 2 inch coupling and schedule 40 pipe.

The failure analysis

determined that the fatigue crack possibly initiated as a relatively low

cycle/high stress process but was predominately propagated as a high

cycle/low stress process.

The licensee was still formulating a

corrective action plan to modify the letdown line piping at the end of

the inspection period.

Conclusions

The licensee's actions to repair the letdown line were appropriate and

accomplished in a methodical manner.

The management decision to

reengineer the configuration of the Unit 2 letdown line and remove the

unit from service to implement the modifications prior to the next

scheduled refueling outage seems appropriate based on the number of

recent weld failures that have occurred on the Unit 2 letdown line

piping downstream of the letdown orifices.

01.3 Component Cooling Heat Exchanger Fouling

a.

Inspection Scope (71707. 40500)

The inspectors reviewed the licensee actions with regard to inoperable

Component Cooling Heat Exchangers (CCHXs).

b.

Observations and Findings

On September 18. at 8:35 p.m .. the C CCHX failed to meet the acceptance

criteria of procedure l-OSP-SW-004. Measurement of Macrofouling Blockage

of Component Cooling Heat Exchanger 1-CC-E-lC. revision 5. due to low

flow.

The C CCHX was declared inoperable.

Based on the low flow

condition operations tested the D CCHX due to concerns with potential


3

common mode failure mechanisms.

The D CCHX also did not meet the

procedure acceptance criteria and was declared inoperable at 9:30 p.m.

With two out of four CCHXs inoperable both units entered a 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />

action statement to return 3 CCHXs to service.

The A and B CCHXs were

tested and met the operability acceptance criteria. The testing of the

A and B CCHXs was completed at 2:30 a.m. on September 19.

The C CCHX was cleaned and returned to service at 1:51 a.m. and the D

CCHX was cleaned and returned to service at 5:58 a.m.

The licensee

increased the CCHX macro fouling testing frequency from once a week to

twice a week based on the increased fouling rate observed.

The

inspectors verified that increased testing was implemented and noted

that as of the end of the inspection period. the increased testing

frequency was successful in preventing entry into a TS Limiting

Condition of Operation (LCD).

c.

Conclusions

The decision to test all four CCHXs demonstrated an appropriate safety

perspective and sensitivity to potential common mode failure.

The

increased testing frequency was successful in preventing entry into a TS

LCD during the remainder of the inspection period.

01.4 Unit 1 Charging Pump Failure

a.

Inspection Scope (71707)

The inspectors reviewed the circumstances surrounding the failure of the

Unit 1 A charging pump.

b.

Observations and Findings

On September 19. at 8:49 p.m .. the Unit 1 A charging pump was started

from the control room to allow the C charging pump to be secured.

When

the pump was started. pump current (amps) pegged high and then returned

to zero.

The operator in the auxiliary building reported a flash of

light. a puff of smoke and a loud noise from the pump cubicle.

The

control room operator immediately secured the pump and placed the

control switch in pull-to-lock to prevent further operation of the pump.

Further investigation by operations found discoloration in the area of

the motor junction box and an instantaneous overcurrent drop on the C

phase at the breaker cubicle.

At the time of the event. the B charging pump was inoperable due to

maintenance activities. The maintenance activities had been completed.

however. post maintenance testing was required to declare the pump

operable and breaker interlocks prevented starting the B pump with the C

charging pump powered from the same electrical bus.

With the A charging

pump inoperable. a 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> LCD was entered due to only one charging pump

being operable and capable of receiving an automatic start signal on an

accident signal.


4

The A charging pump breaker was tagged out at 9:40 p.m .. to allow

electrical maintenance personnel to troubleshoot the problem.

The

troubleshooting determined that the B phase of the motor was

electrically open and that the B phase motor lead had burned through at

the lug connection in the motor junction box.

The pump motor was

meggered with satisfactorily results.

Based on the troubleshooting

activities the licensee decided to replace all the electrical

connections in the motor junction box and test the breaker trip

circuits. The licensee determined that the C phase overcurrent

indication resulted from mechanical agitation when the breaker tripped

open and that a real instantaneous overcurrent condition did not occur

on the C phase.

The electrical connections were replaced and the breaker trip functions

were tested.

No problems were identified during the testing. The

licensee replaced the C phase overcurrent device based on the indication

problem following breaker operation.

The failed connection was saved

and sent offsite for analysis in an attempt to determine the cause of

the failure.

The A charging pump was tested and returned to service at

9:21 p.m. on September 20.

Subsequent to returning the A charging pump

to service. the B charging pump was tested and the 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> LCO was

exited at 11:31 p.m. on September 20.

The inspectors inspected the failed motor lead connection. monitored

licensee corrective actions. and reviewed the event with maintenance

engineering personnel to ensure that the pump breaker protection devices

operated as designed.

c.

Conclusions

The licensee's actions to investigate and repair the A charging pump

motor failure were appropriate and accomplished in an expedious manner.

08

Miscellaneous Operations Issues (92901)

08.1

(Closed) Inspection Followup Item (IFI) 50-280. 50-281/94009-01: follow-

up on Service Water System Operational Performance Assessment (SWSOPA)

corrective actions.

During the Service Water System Operational

Performance Inspection (SWSOPI). several items had been identified that

required additional corrective action or evaluation by the licensee.

These items were as follows:

The assessment identified that Service Water System (SWS) lines of

8 inches or less were not being flow tested. the heat exchanger

performance monitoring did not meet the intent of GL 89-13. and

that the Emergency Service Water (ESW) pump right angle gear

coolers did not receive adequate maintenance.

The inspector

reviewed the licensee's closeout of these assessment items.

The

SWS lines of 8 inches or less are being inspected during component

maintenance activities and during outages.

Heat exchanger

performance had been enhanced by the installation of additional

flow indications.

The right angle gear coolers have flow

5

instrumentation installed which indicates when cleaning of the

coolers is necessary.

Charging pump lube oil cooler temperature control valves had been

down graded inappropriately to non-safety related.

New valves had

been procured as non-safety related.

However. these new valves

had not been installed at the time of the assessment.

The

original disposition of this items was to change the failure mode

of these valves and leave them as non-safety related.

Upon

further review the licensee determined that the valves should be

classified as safety related.

The inspector reviewed the change

documentation to upgrade the valves back to safety related.

The

new valves will be upgraded or safety related valves will be

procured prior to their installation.

The SWS pumps were diesel powered and fuel for their engines was

supplied from a common tank.

The SWSOPA identified that the four

sampling procedures applicable to this tank had inconsistent fuel

oil sampling acceptance criteria. The inspector reviewed the

change to C-93.212. "Diesel Fuel Tank Number 2 [underground

storage tank]: Sampling and Analysis After Fuel Addition." dated

6/28/94. and concluded that the acceptance criteria had been

changed to agree with the other three procedures.

The Updated Final Safety Analysis Report (UFSAR) contained an

incorrect statement. in one section. that indicated that the

containment would return to a subatmospheric condition in less

than 30 minutes.

The correct value is 60 minutes.

The inspector

reviewed the applicable portions of the UFSAR and determined that

the 30 minute error was revised to 60 minutes in revision 23

issued in December 1994.

The licensee's intake canal level probes which are required to

operate to isolate non-safety related loads on the SWS system had

been failing due to macrofouling of the probe tip. Replacement

tips had been response time bench tested and failed the 66 second

response time required for the isolation actuation.

The inspector

reviewed the Performance Test (PT) test. PT-2.21 B. C. Canal

Level. dated 2-24-94. which tests the installed probes.

The PT

had been revised to reduce the setpoint from 300mv to 250mv.

This

reduced the response time of the probes by 10 -15 seconds.

The

response time of the probes was demonstrated to be< 66 seconds on

the last performance of the PTs.

Recirculation Spray Heat Exchanger (RSHX) flow was being monitored

by valve position vice flow indication.

Flow indication existed

but had not been included in the Emergency Operating Procedures

(EOPs) as an indication available to the operators.

The inspector

reviewed the applicable EOPs (1/2-E-O. revision 16. and determined

that the RSHX flow instrumentation had been added to the

procedures in addition to the valve position.

6

The SWSOPA identified discrepancies in operator training modules

NCRODP 12-S and 13 Intake Canal Level and Setpoints. concerning

the low level setpoint of the i~take canal for various functions

and system operating requirements.

The inspector reviewed the

training modules.

The modules had been revised to show the

correct setpoint of 23 feet.

The RSHXs are normally isolated and drained during normal

operation.

The SWSOPA had determined that water had entered one

of the heat exchangers when throttling Circulating Water (CW)

system during cold weather. Administrative procedures were to be

revised to ensure that the RSHXs remained dry.

The inspector

reviewed the operations monthly check for dryness.

The test

procedures had also been revised to note that the isolation valves

are leak tight and to minimize the length of time that water is

against the valves.

The SWSOPA identified that the radiation monitoring equipment on

the SWS discharge piping from the RSHXs may not be operable due to

inadequately sized suction piping.

The suction piping had been

changed from 3/4 inch to 2 inch.

The inspector reviewed the

performance test. 1/2 OPT-RS-066 Radiation Monitor Functional

Test. Dated 8/20/96. This test determines that water pumps

through the detector well. check that static and dynamic pressures

available and that the annunciator circuits function properly.

The test results were satisfactory.

08.2 (Closed) Licensee Event Report (LER) 50-281/96001-00 and Violation (VIO)

50-280. 50-281/96002-02:

loss of containment integrity due to through

wall leak in the Residual Heat Removal (RHR) reactor cavity drain line.

A through wall leak developed due to intergranular corrosion at the

intersection of the pipe seam and an overlapping saddle support weld.

The Unit was brought to cold shutdown and the piping was replaced.

Ultrasonic Testing (UT) of additional piping on Unit 2 did not identify

any additional defects that were beyond code allowable.

The resident inspectors in responding to this event determined that. on

January 16. 1996. written procedures were not followed for corrective

maintenance operations.

The leak on a containment penetration weld

inside the Radiological Control Area (RCA) was not reported to the Shift

Supervisor. and this weld leak was not documented on a Work Request

(WR).

The weld leak was identified on a maintenance Deficiency Card.

Also. this deviation was not reported on a DR.

These failures allowed

Unit 2 to operate at power for approximately five weeks with a degraded

containment penetration. This was identified to the licensee as a

violation in NRC Inspection Report (IR) 50-280. 281/96-06.

As part of followup to the LER the inspector also verified the

licensee's corrective actions for the violation. These corrective

actions included revising procedures VPAP- 1501 and 2002 Deficiency

Reporting revision 5 and 6. to include the necessity of identifying any

7

though wall leak inside the RCA on a WR. and revising the screening

process for Deficiency Cards.

Additionally. the station manager issued

a memorandum to all station personnel discussing the correct programs

for the identification of deficiencies.

The inspectors concluded that

these actions were adequate to preclude recurrence.

II. Maintenance

Ml

Conduct of Maintenance

Ml.1 Unit 2 Blender Repair

a.

Inspection Scope (62703)

The inspectors observed corrective maintenance activities associated

with Work Order (WO) 00351738. Investigate/Repair Valve FCV 1114A.

b.

Observations and Findings

On September 25. the inspectors reviewed the WO package. verified that

the system isolation was adequate to perform the maintenance activity.

and observed portions of the maintenance activity in progress.

The

maintenance activity was initiated due to the inability to achieve

primary grade (PG) water flow to the Unit 2 blender.

The activity

consisted of removing the valve actuator and bonnet to allow inspection

of the valve internals to determine if the valve disc had separated from

the valve stem.

Inspection of the valve internals did not identify any

discrepancies. Subsequent inspection of the piping downstream of the *

valve utilizing a boroscope determined that a spring loaded check valve

was not moving freely.

The check valve was mechanically cycled

internally and proper operation was verified.

The system was returned

to service and proper PG flow was obtained.

c.

Conclusions

The maintenance activity was accomplished in accordance with the WO

package requirements and approved procedures.

The system was adequately

isolated prior to commencing maintenance.

Ml.2 Reactor Protection System Logic Testing

a.

Inspection Scope (61726)

The inspectors witnessed portions of the Unit 2 Reactor Protection

System (RPS) logic testing conducted on September 27.

b.

Observations and Findings

The inspectors witnessed the portion of Unit 2 procedure PT 8.1. Reactor

Protection Logic (for Normal Operations). revision 8. performed on the B

train of the RPS.

The technicians performing the surveillance were

knowledgeable of the procedure requirements and precautions.

The

. *

8

periodic test was accomplished in accordance with the procedure and all

acceptance criteria were met.

c.

Conclusions

The portion of the RPS logic testing witnessed by the inspectors was

accomplished in accordance with the procedure's requirements and all

acceptance criteria were met.

The technicians performing the

surveillance were knowledgeable of the procedure's requirements and

precautions.

Ml.3

Main Steam Safety Valves

a . Inspection Scope

b.

C.

The inspector observed the release nut clearance on both units* main

steam safety valves on September 25. 1996.

Observations and Findings

In May 1996. an event occurred at another reactor where the release nut

cotter pin became disengaged. This allowed the release nut to vibrate

down the valve stem and caused the valve to stick open.

The root cause

of this occurrence appeared to be inadequate maintenance procedures in

that the cotter pin. which was to hold the release nut 1/8 to 1/16

inches above the top lever. was incorrectly installed. The Dresser

model 3700 safety valves are similar in construction to the other

plants. The inspector observed the safety valves in Unit 1 and 2.

Observations confirmed that clearance between the release nut and the

top lever did exist and was greater than 1/8 inch.

The cotter pins

could not be observed.

The cap of the valve covers the top of the

release nut and obscures the area where the cotter pins are installed.

The licensee's system engineer was familiar with the event and had

initiated a change to maintenance procedures MPT-0427-02. Main Steam

Safety Setpoint Verification for both unit3. Additional~y. the system

engineer had initiated a technical manual change to clarify the

installation of the cotter pins.

The system engineer indicated that

only vender personnel had worked on the safety valves and that no

previous problems had been identified in this area.

Conclusions

The licensee was aware of the problem with the main steam safety valve

release nuts and had taken appropriate action by initiating changes to

maintenance procedures to ensure that a similar problem would not occur

at this facility.

MB

Miscellaneous Maintenance Issues (92700. 92902)

M8.l

(Closed) Violation 50-280. 281/95022-01:

missed technical specification

surveillance. This violation was issued Nhen maintenance personnel

failed to perform station battery and smoKe detector surveillances

9

within required periodicities. Root cause evaluation (RCE) 95-09.

Missed Battery Surveillance. revision 1. determined that electrical

supervisors failed to adequately perform technical reviews of completed

surveillances. The licensee attributed the errors to programmatic

issues and weaknesses in personal accountability and supervisory

oversight.

Initial corrective actions were previously documented in NRC

IR 50-280. 281/95-22.

Corrective actions to preclude recurrence included counseling electrical

supervisors regarding their surveillance reviews. procedure revisions to

clarify supervisory review responsibilities and partial surveillance

completion documentation. and one additional person was assigned to the

electrical department to assist in periodic test (PT) scheduling and

tracking.

To further strengthen PT accountability. VPAP 1102. Periodic

Testing. revision 1-PSl. was revised to require administrative and

technical PT reviews to be completed within the PT test interval. The

inspectors reviewed the procedure revisions. interviewed personnel. and

verified that the corrective actions were complete.

No TS surveillances

have been missed since April 1995.

The inspectors concluded that

corrective actions were effectively implemented to address this

violation.

M8.2

(Closed) LER 50-281/95004-00: installation of damaged circuit card

resulted in Unit 2 manual reactor trip.

On May 11. 1995. installation

of a damaged control rod drive (CRD) circuit card caused four control

rods to fully drop into the core with the reactor at 100 percent power.

The event and initial corrective actions were documented in NRC IR 50-

280. 281/95-08. A cracked resistor on the replacement circuit card was

not evident to technicians prior to installation. Corrective actions to

preclude recurrence included several revisions to warehouse receipt.

inspection. and storage practices.

These actions were effectively

implemented promptly after the event.

In addition. the licensee

developed additional preinstallation card testing capabilities. The

inspectors observed the revised circuit card receipt practices and

preinstallation testing.

NRC IR 50-280. 281/95-17 documents some of the

circuit card testing observations.

The inspectors concluded that

corrective actions were properly implemented to preclude the

installation of damaged CRD circuit cards.

M8.3

(Closed) LER 50-281/95005-00: manual trip due to control rods dropping

into reactor core.

On May 21. 1995. four control rods dropped into the

core due to a degraded CRD circuit card.

The event and initial

corrective actions were documented in NRC IR 50-280. 281/95-08.

The

licensee determined that the root cause was an adverse operating

environment (excessive heat and dust) in the vicinity of the CRD

cabinets.

The root cause assessment considered a broad range of causal

factors.

NRC IRs 50-280. 281/95-17. 96-02. and 96-07 document inspector

observations regarding corrective action implementation.

The two most

significant corrective actions were enhanced CRD inspection and testing

practices and an air conditioning upgrade for the normal switchgear

rooms which house the CRD cabinets. The air conditioning upgrade was

completed in May 1996.

This upgrade was an effective long term

10

corrective action to establish adequate environmental conditions for CRD

cabinet circuitry. The inspectors determined that corrective actions to

address the CRD circuit card failures were effectively implemented.

M8.4 (Closed) LER 50-280/95006-00:

emergency service water pumps 1-SW-P-lA

and lC declared inoperable due to low flow and speed indications.

During a performance test on August 22. 1995. the 1-SW-P-lC emergency

service water pump was declared inoperable due to indications of low

flow and low speed.

On August 23. 1995. marine growth was removed from

the suction bell and impeller surfaces by a diver and the pump was

successfully tested.

The 1-SW-P-lA emergency service water pump was

tested on August 23. 1995. and it also was declared inoperable due to

low flow and speed indications.

Marine growth was removed form the

suction bell and impeller.

The pump was returned to service following a

successful test on August 24. 1995.

The licensee had previously experienced fouling of the pump suction

bells and impellers by marine growth.

This had occurred twelve times in

the previous two years. A routine cleaning by divers had been

incorporated into a preventive maintenance item for the SWS pumps.

The

warm weather had accelerated the marine growth and caused the

inoperabilities on this occasion.

The inspectors reviewed the

corrective actions for these occurrences which included more frequent

cleaning during the warm weather months and the coating of the suction

bells and impellers with an anti-marine growth coating.

The inspectors

determined that the licensee was continuing investigations into methods

,)

to prevent further recurrence.

M8.5

(Closed) LER 50-280/96005-00: both trains of Unit 1 and 2 charging pump

service water pumps became air bound.

On May 6. 1996. both trains of

the Unit 1 and 2 charging pump service water pumps became air bound

rendering the charging pumps inoperable. Service water was restored to

one Unit 1 pump within one minute.

The remainder of the pumps were

vented and flow was re-established within one hour.

Underwater diving activities on the Unit 2 circulating and service water

piping was identified as the source of the air in the system.

Air from

the divers entered the service water supply lines when valve 2-SW-MOV-

201B was opened in preparation for a safety injection logic test.

The inspector reviewed the licensee's corrective actions which included

revising procedures used to perform maintenance on the circulating and

service water systems.

The procedures had been revised to note the

possible air binding of the lines due to the use of divers in the

systems and the necessary steps to vent the line to remove the air

exhaled by the divers.

11

III. Engineering

El

Conduct of Engineering

El.1 Safety Evaluation to Support Unit 2 Blender Operations

a.

Inspection Scope (37551)

The inspectors reviewed Safety Evaluation 96-122. Makeup. Boration and

Dilution with the Normal Blender Flowpath Unavailable.

b.

Observations and Findings

The inspectors reviewed the safety evaluation and attended the Station

Nuclear Safety Operating Committee (SNSOC) meeting that approved the

safety evaluation for implementation.

The safety evaluation was

initiated to support a procedure change to procedure 2-0P-CH-007.

Blender Operations. revision 1. to allow an alternate method of boration

and dilution with the Unit 2 blender inoperable.

The alternate

flowpaths bypassed the blender and required manual control of valves

located in the auxiliary building.

The safety evaluation required

continuous communications between the control room and the remote valve

locations. placed limits on the amount of boron that could be added by

makeup and specified the dilution flowrate following boron addition.

The safety evaluation was thorough and adequately justified the

procedure revision.

The SNSOC meeting was conducted in a professional

manner and resulted in an indepth review of the subject safety

evaluation.

c.

Conclusions

Safety Evaluation 96-122 adequately justified the use of alternate

boration and dilution flowpaths and the SNSOC meeting was professional

and resulted in an indepth review of the subject safety evaluation.

E4

Engineering Procedures and Documentation

E4.1

Review of Standing Design Change Packages

a.

Inspection Scope

The inspectors reviewed the licensee's standing design change process as

controlled by Surry Station Engineering Services (SSES) Implementing

Procedure. SSES-2.11. Controlling Procedure For Standing Design Change

Package (DCP) Guidelines. revision 1.

The inspector randomly selected

several standing DCPs to review the work scope additions. safety

evaluations. drawings, and/or applicable specifications .

12

b.

Observations and Findings

Procedure SSES-2.11. revision 15. establishes the guidelines to be

utilized by Engineering personnel when preparing a standing DCP.

The

inspector also reviewed the following procedures which were used to

prepare DCPs:

Nuclear Design Control Program General Nuclear Standard

STD-GN-001. Instruction for DCP Preparation. revision 15. and Station

Administrative Procedure VPAP-0301. Design Change Process. revision 6.

A standing DCP is a design change written for the installation of

equipment or components that has a defined design. but an undefined work

scope.

Examples of standing DCPs are:

flow accelerated corrosion

piping replacement. motor termination inspections. concrete repairs. and

solenoid valve replacement.

The design scope describes the modification

to be performed.

The work scope addition is the supplemental scope of

work that is added to the standing DCP.

A work scope addition may not

change the original design scope of the DCP.

The inspector reviewed several work scope additions on the following

standing DCPs:

DCP 92-074:

Misc. Transmitter Replacement

DCP 95-001: Standing DCP MI Setpoint/Scaling Changes/Surry/Units

1&2

DCP 92-083:

Misc. Limitorque Motor Operator Modification

The inspector noted that work scope addition number twenty on DCP 95-001

involved changing the existing "High" temperature alarm setpoint of

140 °F to a new lower temperature of 115 °F.

The field change lowered

the alarm temperature setpoint to provide additional response time to an

increase in Spent Fuel Pool (SFP) temperature.

The licensee initiated

this change in response to recent concerns over SFP cooling issues.

The

inspectors considered that the licensee's work scope addition number

twenty on DCP 95-001 was performed in accordance with applicable

procedures. and was conservative. All the other scope additions that

were reviewed by the inspector contained appropriate specifications.

drawings. system descriptions. and adequate safety evaluations when

required.

c.

Conclusion

The inspectors concluded that all the standing DCP scope additions

reviewed contained appropriate specifications. drawings. system

descriptions. and safety evaluations.

13

IV. Plant Support

Rl

Radiological Protection and Chemistry (RP&C) Controls

Rl.l Transportation of Radioactive Material

a.

Inspection Scope (86750. TI 2515/133)

The inspectors evaluated the licensee's transportation and radioactive

materials programs. including worker training and facility operation

training.

Implementation of revised Department of Transportation (DOT)

and NRC transportation regulations for shipment of radioactive materials

as required by Title 10 Code of Federal Regulations (CFR) Part 71.5 and

49 CFR Parts 170 through 189 were also inspected.

In addition. the

licensee's May 6. 1996. Revised Response to IE Bulletin and Notice of

Violation Radioactive Waste Packaging and Shipment were reviewed and

evaluated.

b.

Observations and Findings

The inspectors reviewed training associated with the revised Department

of Transportation and NRC transportation regulations and found the

training to be comprehensive.

The inspectors reviewed training for

working in the Surry Radwaste Facility (SRF).

The review included

lesson plans. self study instructional material for system's operation

and design information and technical handout material. prints. exam

questions and exam results. The inspectors toured the SRF and

determined that the shipping containers were appropriately labeled and

properly stored.

At the time of the inspection the licensee had

temporarily halted shipments of evaporator bottoms and were evaluating

the options to determine the direction they were going to pursue when

they resumed shipping.

The inspectors reviewed the original response to IE 79-19. Bulletin

Packaging of Low Level Radioactive Waste for Transport and Burial. dated

September 27. 1979 (Serial No. 670).

NRC Inspection Report 50-280/80-16

and 50-281/80-17 and EA 80-28 identified a violation for not adequately

identifying radiation levels on radioactive waste shipped offsite. The

response dated June 20. 1980 (Serial No.544). indicated that procedures

had been revised for the packaging and shipment of solid radioactive

waste to require a minimum of six documented contact readings and to

conspicuously mark the highest contact reading on the package surface.

A commitment was also made to have a Quality Control (QC) inspector

witness radioactive waste loading and shipment operations. A Health

Physics Position Paper. prepared by the Supervisor. Health Physics

Technical Services. dated July 10. 1996. evaluated the aspects of QC

Inspection and Review of Radwaste Shipping Papers. Since the time of

the commitment. significant organizational changes have occurred and a

long successful record had been established showing no repeat of the

earlier violation.

14

The inspectors reviewed the revised commitments that state that the RP

procedures now require that only the highest contact radiation reading

for each package be recorded. and no longer require that each

radioactive waste package be marked with the highest contact reading.

The licensee's response also stated that verification of proper

radioactive waste loading and shipping would be performed by qualified

personnel and periodic audits of the radioactive waste program would be

performed by the Nuclear Oversight Department.

c.

Conclusions

The licensee effectively implemented comprehensive training programs for

the operation of the SRF and shipping radioactive materials. The

inspectors determined that the revised radwaste shipping approach. in

the May 6. 1996 letter was acceptable.

R2 Status of Radiation Protection Facilities and Equipment

R2.1 Radiation Monitor and Calculation Review

a.

Inspection Scope (84750. 86750)

The inspectors reviewed selected SRF radiation monitors for calibration

and alarm set points.

The inspectors also reviewed the analysis and

calculations associated with the Model Ll4-195 High Integrity Container

(HIC) lifting attachments.

b.

Observations and Findings

C.

The inspectors reviewed selected alarm set points in the SRF and

calibration data and determined that monitors were within their

calibration interval and alarm set points were correctly set.

The inspectors reviewed the acceptability of using the Ll4-195 HICs for

multiple shipments and for the handling required to make the shipments.

The inspectors reviewed the calculations performed on the lifting

attachments to demonstrate their multiple use acceptability.

The

analysis showed that the devices were acceptable for at least ten

handling cycles: however. the licensee has restricted their use to three

handling cycles.

The inspectors verified that HIC lifting attachments

were changed out after three cycles. There have been 20 shipments of

evaporator bottoms using the HIC containers this year.

The last HIC

shipment was made on August 20. 1996. The inspector verified the change-

out of the lifting attachments.

Shipments have been temporarily put on

hold pending an evaluation of shipping large quantities of evaporator

bottoms.

This evaluation has a management due date of November 1. 1996.

Conclusions

No concerns with the licensee's SRF facility radiation monitor or

calibration and alarm. set points. equipment. or HIC lifting attachments

analysis were identified during the inspection.

-*

15

R2.2 Tours of Licensee Radiological Control Areas (RCAs)

a.

Inspection Scope (83750. 60855. 71750)

During tours of the licensee facilities. the inspectors selectively

verified that radiological postings and labels were appropriate for the

radiological hazard.

The licensee's Independent Spent Fuel Storage

Installation Radiation Protection Activities were selectively reviewed.

b.

Observations and Findings

The inspectors observed the control of contaminated and radioactive

material and housekeeping within the licensee's Independent Spent Fuel

Storage Installation (ISFSI). low level radioactive waste warehouse and

scrap storage areas.

The inspectors also verified that recent survey

information for the ISFSI was readily available for briefings for

workers needing access to the ISFSI area.

The inspectors independently

verified selected survey points and took independent smear survey

samples from storage containers.

The neutron dose assessment

calculations were reviewed for the inspector's entry. Additionally. the

records for selected individuals who had entered the area under separate

RWPs were reviewed to insure that neutron dose assessments had been

performed and that proper neutron doses had been recorded and assigned.

Postings at the ISFS I. low level waste storage warehouse and scrap

storage areas inside the SRF were found to be properly located.

Additionally. environmental Thermo Luminescent Dosimeters (TLDs) at the

ISFSI were verified to be at their designated locations.

c.

Conclusions

The ISFSI was properly posted and entrance to the location was

appropriately controlled by RWPs.

Environmental TLDs were verified to

be in place.

Adequate dose assignment as a result of neutron dose

assessment was taking place. Surveys were taken as required and results

were selectively spot checked and found comparable.

Smear surveys were

counted and found clean.

Housekeeping was excellent at the ISFSI and

low level waste storage warehouse.

R7 Quality Assurance in RP&C Activities

a.

Inspection Scope (83750)

The inspectors reviewed the licensee's program for identifying and

correcting deficiencies or weaknesses related to the control of

radiation or radioactive material.

b.

Observations and Findings

The inspectors selectively reviewed the DRs related to the control of

radiation or radioactive material.

During discussions with licensee

representatives and reviews of DRs. the inspectors reviewed the details

of DR No. S-96-1771 involving activities associated with a containment

16

entry made on August 17. 1996. to investigate an oil level alarm on

reactor coolant pump 2-RC-P-lB motor.

A root cause investigation was

conducted by the licensee and involved personnel exceeding Digital

Alarming Dosimeter (DAD) limits. The root cause revealed a failure of

the Health Physicist Shift Supervisor (HPSS) to be fully knowledgeable

of and comply with RWP requirements.

The HPSS. in an attempt to conceal

the procedural violations. allegedly falsified records associated with

RWP Briefing Attendance Roster dose set-points for DADs.

The workers received a dose of 186 and 205 mrem.

These doses did not

exceed any regulatory limits.

The HPSS admitted that he missed the RWP

requirement to use a Special RWP and forgot to change the DAD dose alarm

set-points.

He knew the workers exceeded their alarm set-points. knew

the RWP requirements to exit the containment. but made a decision to

allow them to finish the job. knowing that he was violating the RWP.

The licensee took disciplinary action as a result of their

investigation.

Procedural violations for this event were:

(1) Failure

to exit area when workers exceeded their DAD alarm set-point in dose

mode. (2) Failure to write a Special RWP for expected doses in excess of

100 mrem. and (3)

Failure to* maintain complete and accurate

information.

The licensee was informed that this would be tracked as an Unresolved

Item (URI) pending Regional and Headquarters review: URI 50-280 .

281/96010-01: improper actions associated with a containment entry.

The inspectors reviewed DR S-96-1981. dated September 11. 1996,

involving the issuance of a respirator to a worker who was not qualified

by virtue of having an expired respiratory fit test. The respirator was

issued to the same individual on two separate dates (August 15. 1996 and

August 16. 1996) for containment entries.

The worker's fit test

qualification expired on March 31. 1996.

The licensee discovered the

problem while reviewing personnel qualifications for containment entries

in support of steam generator letdown line maintenance.

The individual

was requalified on September 11, 1996.

As part of the investigation.

the licensee was evaluating the need to perform a Whole Body Count.

The

following procedures were identified by the licensee to be violated by

the individual. VPAP-2101. Radiological Protection. revision 11. dated

August 1. 1996. Section 6.4.9 a and c. VPAP-0106. Subatmospheric

Containment Entry, Revision O-PS2. Section 6.2.2. and HP-1042.150.

Respirator Issue revision 1. dated December 12. 1995. Section 4.2.

At

the conclusion of the inspection. the licensee was aggressively

reviewing the following: the software program Personnel Radiation

Exposure Management System (PREMS) that can be used to determine the

worker's qualifications. the records and data available at the

respirator issue point and the training and procedures associated with

respirator issue.

The licensee identified and corrected violation is

being treated as a Noncited Violation: NCV 50-280. 281/96010-02:

Respirators issued to nonqualified persunnel. consistent with Section

VII.B.l of the NRC Enforcement Policy .

17

c.

Conclusions

The licensee was performing self assessments and taking timely and

comprehensive corrective actions.

One URI and one NCV were identified.

RB Miscellaneous Radiation Protection and Chemistry Issues

R8.l Primary and Secondary Chemistry

a.

InsQection ScoQe (86750. TI 2515/133)

The inspectors reviewed and discussed the results of the licensee's

primary and secondary chemistry program.* The inspectors also reviewed

the Nuclear Chemistry Technician Continuing Training Program - 1996.

b.

Observations and Findings

The inspectors reviewed the chemistry results for the TS data associated

with the Primary and Secondary Water Chemistry parameters for the period

from January 1. 1996 through September 11. 1996. and determined that all

required TS chemistry results were maintained at small percentages of

the limits.

The Nuclear Chemistry Technician Continuing Training Program - 1996

includes the following training elements: classroom training. laboratory

training and in plant training.

The inspectors determined that the

areas covered provided adequate continuing training to maintain the

skills necessary to perform the chemistry program.

The training also

included recent industry event updates.

c.

Conclusions

The licensee was aggressively sampling and monitoring the primary and

secondary water chemistry parameters.

Parameters were maintained at a

few percent of TS limits.

The continuing training program appeared

comprehensive and provided adequate training to improve and maintain

technician knowledge and analytical skills.

R8.2

(Closed) Violation 50-281/95023-01: multiple personnel violations of RWP

requirements.

On December 14. 1995. mechanics violated several aspects

of the radiological work permit (RWP) while performing a weld repair to

the Unit 2 letdown system inside containment.

Immediate corrective

actions were documented in NRC IR 50-280. 281/95-23. Additional actions

to preclude recurrence included event discussion during a station human

performance stand down day. revisions to contractor training emphasizing

individual accountability. enhanced maintenance department supervision

over RWP practices during the Spring 1996 refueling outage. and

increased on the job radiological protection (RP) assessment.

The

inspectors subsequently observed RP practices during the Unit 1 incore

detector D repairs and during the Unit 2 reactor coolant pump oil leak

investigation.* These observations were documented in NRC IR 50-280.

18

281/96-01 and 96-02.

Work activities were well planned with appropriate

considerations to minimize radiation exposure.

Subsequent field

observations indicate that workers have improved their understanding of

RWP requirements and individual responsibilities.

The inspectors

concluded that corrective actions to improve RWP comprehension. RP

coverage within containment. and stay time assessment were effectively

implemented.

Fl

Control of Fire Protection Activities

Fl.l Resolution of Thermo-Lag Fire Barrier Issue (64704)

a.

Inspection Scope

The inspector reviewed the action taken to resolve the degraded Thermo-

Lag fire barriers to determine if this action was consistent with the

NRC requirements.

b.

Observations and Findings

In 1991. the NRC found that Thermo-Lag fire barrier material did not

perform to the manufacturer's specifications. Specifically, the

installed Thermo-Lag barriers would actually provide approximately one

half of the specified rating, i.e .. a 1-hour fire rated barrier would

provide approximately 20 to 30 minutes of protection.

The NRC issued

NRC Bulletin 92-01. Failure or Thermo-Lag 330 Fire Barrier System. and

requested licensees with Thermo-Lag fire barriers to take the

appropriate compensatory measures for the areas where the Thermo-Lag

materials were installed. Virginia Electric and Power Company responded

to this bulletin by letters dated July 29. 1992: April 12. 1993: and

December 15. 1995.

The following actions had been taken on this issue

at Surry:

Containment:

The December 15. 1995. letter submitted to the NRC provided a

justification and requested an exemption for the continued use of

Thermo-Lag as a radiant energy shield in the containment.

This item is

presently under review by the NRC.

Communication System Cables in Unit 1 Cable Vault and Emergency

Switchgear Room:

Plant modification DCN 91-10 installed a new radio communication system

with redundant power supplies in separate fire areas as indicated by

drawing 11448-FE-90KA.

The inspector reviewed this drawing and walked

down the new installation.

The new system met the separation

requirements of 10 CFR 50 Appendix Rand the electrical cables for the

old system are no longer in use.

This issue is resolved.

19

HVAC Ducts in Turbine Building Between Fire Dampers and Control Room and

Emergency Switchgear Rooms:

The licensee performed an engineering evaluation and determined that the

installation of the degraded Thermo-Lag installed on the HVAC ducts in

the Turbine Building between the fire dampers and the control room and

emergency switchgear rooms provided protection equivalent to the

required 3-hour fire rating. This evaluation was included in the Surry

Appendix R Report and was based on the 2-hour fire rating of the HVAC

ducts. approximately 1-hour rating of the Thermo-Lag material on the

duct and on the fire suppression system provided in the Turbine

Building.

The inspector reviewed this evaluation and had no questions.

Charging Pump Service Water Pump Supply Piping:

A Thermo-Lag 3-hour fire barrier was initially installed in Mechanical

Equipment Room 3 to provide a fire barrier for the protection of the

fiberglass service water piping to the charging pumps.

This Thermo-Lag

material had been removed and replaced by a cememtitious fire barrier

material. Pyrocrete 241. which was listed by Underwriters* Laboratories.

Inc .. as having a 3-hour fire resistance rating.

The inspectors

reviewed work request 262077-02 (Tracking No. 93-013-001). performed a

walkdown inspection of the installation and verified that this

replacement fire barrier system had been installed. This issue is

resolved.

c.

Conclusions

Based on this review. the licensee has been proactive in the resolution

of the Thermo-Lag issue.

Fl.2 Storage and Preventive Maintenance of Appendix R Repair Equipment

(64704)

a.

Inspection Scope

b.

The inspector reviewed the storage and maintenance of the spare

equipment designated as repair components required to meet the

requirements of 10 CFR 50 Appendix R.

Observations and Findings

During the Appendix Revaluation of Surry. a number of components-were

identified which may be required to be repaired in the event of an

Appendix R fire. These repair items were identified by Procedure

O-EPM-2303-01. RHR/CC Appendix R Equipment Inspection. revision 2. and

were stored in the site warehouse.

The inspectors toured the warehouse

and reviewed the storage of these items.

The small equipment items.

tools. and miscellaneous parts were stored in four locked gang boxes .

The inspectors did not reinventory these items since they had recently

been inspected by the licensee and the gang boxes were locked.

The

20

warehouse also contained two large motors. two pumps (one Residual Heat

Removal (RHR) and one Component Cooling Water (CC)). four electric motor

driven exhaust fans. four large cable reels and miscellaneous equipment.

This equipment was satisfactorily stored.

The inspector reviewed the preventive maintenance required to be

performed on the two large electric motors [Spare Motors 108 and 109] by

Procedure O-EPM-2302-01. Quarterly Inspection of Stored Motors.

revision 1.

This procedure required the electric motor shafts to be

rotated at least two turns at each quarterly inspection.

The most

recent quarterly inspection was performed on September 3. 1996. but the

shafts to these motors were not rotated.

The motor data sheets attached

to these motors identified each quarterly inspection since September

1991.

These data sheets indicated that the motor shafts had not been

rotated since September 1991.

Attachment 1 to Procedure O-EPM-2302-01

identified the spare motors in storage at Surry.

The September 1996

inspection indicated that several additional motors had also not been

properly rotated. This failure to follow a maintenance inspection

procedure is identified as Violation 50-280. 281/96010-03. Inadequate

Preventive Maintenance Performed on Spare Electric Motors.

After conducting the motor prevention maintenance review. the inspector

requested information from the licensee as to the preventive maintenance

being performed on the spare safety-related RHR and CC pumps.

The

licensee indicated that no preventive maintenance was required or was

being performed on these pumps.

Pending further review of the

licensee's position. this item is identified as Inspection Follow-up

Item 50-280. 281/96010-04. Preventive Maintenance Requirements for Spare

RHR and Component Cooling Water Pumps.

c.

Conclusion

The spare equipment required for repairs following an Appendix R fire

were properly stored.

However. a violation was identified for

inadequate preventive maintenance being performed on the spare safety

related electric motors required for installation following an Appendix

R fire.

In addition. an inspection followup item was identified for

reviewing preventive maintenance practices on safety-related RHR and CC

pumps.

F2

Status of Fire Protection Facilities and Equipment

F2.l Operability of Fire Protection Facilities and Equipment (64704)

a.

Inspection Scope

The inspector reviewed the open maintenance work orders on the fire

protection systems. the system engineer's quarterly report data.

maintenance history and the fire protection systems to determine the

performance trends and the material conditions of the plant's fire

protection systems. equipment and features.

-*

b.

21

Observations and Findings

As of September 20. 1996. there were a total of 22 open work requests

related to the fire protection systems and features.

Most of these were

either routine preventive maintenance items or involved minor corrective

maintenance work.

However. one work item involved the removal and

replacement of a post indication valve which controlled the water supply

to all of the fire protection systems in the SRF.

This valve was

leaking and had been closed.

Replacing this valve was not considered a

major work activity, but the valve had been closed and the fire

suppression systems for the facility had been out of service since

August 12. 1996.

The fire protection systems for the SRF are not

included in the Technical Specifications (TS): therefore. the licensee

had not incorporated any compensatory action due to the lack of fire

protection suppression systems for the facility.

Not implementing

compensatory measures for fire protection features not covered by the TS

was identified as a weakness.

As of the close of this inspection. the

licensee had not established a date for the restoration of this system

to service.

The licensee informed the inspector in the event of a fire.

the closed valve could be manually reopened.

The Surry System Engineering Quarterly Report. Second Quarter 1996 was

reviewed.

The rating of the fire protection systems was satisfactory.

The report also identified problems with the maintenance of the 8-hour

Appendix R emergency lighting units.

The inspector interviewed the fire

protection system engineer and found that the principle problem with

these lighting units was a high battery burn out rate due to the loss of

electrolyte in the batteries which was apparently caused by excessive

heat.

An engineering evaluation was in process.

The resolution of this

problem was scheduled to be completed by late 1997.

The system engineer

informed the inspector of a number of problems being experienced with

the facility's fire alarm system. Although functional. this system is

old. obsolete and no longer manufactured.

Replacement parts have been

difficult to obtain.

The need for the replacement of this system was

identified in QA audit 96-02 of the fire protection program.

The inspector toured the plant and noted that. with the exception of the

out of service fire suppression systems installed in the Radwaste

Facility. all of the systems inspected were operational and well

maintained.

c.

Conclusions

The maintenance records. equipment trending data and inspection of the

fire protection components. indicated that there were no maintenance

backlog on the fire protection systems and. with the exception of the

out-of-service fire suppression systems for the SRF. the maintenance.

operability and performance of these systems were good.

The lack of a

site procedure to establish appropriate compensatory measures for

degraded fire protection systems and features not included in the TS was

identified as a weakness.

22

F2.2 Surveillance of Fire Protection Features and Equipment

a . Inspection Scope

The inspectors reviewed the following completed surveillance and test

procedures:

O-LPR-FP-001. Fire Barriers (18 Months)

O-LPT-FP-005. Inspection of Hose Stations and Fire Extinguishers

(Monthly)

O-LPT-FP-022. Operability Test of Fuel Oil Pump House High

Pressure CO2 System

O-LPT-FP-027. Operability Test of Emergency Service Water Fuel Oil

Tank Room High Pressure CO2 System

1-EMT-0902-02. Fire Protection Low Pressure CO2 System Equipment

Test

O-OPT-FP-006. Flow Tests of Fire Protection System (3 Years)

O-OPT-FP-008. Fire Pump Flow Rate Test (Annual)

b.

Observations and Findings

The completed surveillance tests of the fire protection systems reviewed

by the inspectors were appropriately completed and met the acceptance

criteria. However. the inspectors noted that the fire protection system

engineer had not reviewed all of the completed surveillances and tests.

The licensee informed the inspector that the site policy did not require

system engineering to review all completed test procedures.

Each system

engineer was required to review the results of only approximately 10

percent of the completed surveillance tests.

However. the inspector noted that several completed tests on the

principle fire suppression systems were not reviewed by the system

engineer and trending of the performance of the fire protection systems

to analyze the system's performance characteristics was not being

conducted.

The licensee stated that they planned to evaluate trending

in this area.

The station safety and loss prevention supervisor (fire protection

supervisor) monitored the overall fire protection program and reviewed

the completed tests and surveillances performed by his staff.

He also

reviewed the surveillance findings and test results performed on the

fire protection systems by other groups which were unsatisfactory or did

not meet the acceptance criteria .

-*

C.

23

Conclusions

Appropriate surveillances and tests were being performed on the fire

protection features and systems.

F3

Fire Protection Procedures and Documentation

a.

Inspection Scope (64704)

Procedure VPAP-2401. Fire Protection Program. revision 4. was reviewed

for compliance with the NRC requirements and guidelines.

Plant tours

were performed to determine procedure compliance.

b.

Observations and Findings

Procedure VPAP-2401 establishes the administrative guidance used to

implement the fire protection program at Surry and includes the

requirements for the control of combustibles and ignition sources. and

fire brigade organization and training.

The procedure was satisfactory

and met the NRC requirements and guidelines. except for fire brigade

drills. Fire brigade drills are required by VPAP-2401. Section 6.6.12.

to be conducted quarterly. Drills are performed quarterly for each

operations shift. However. drills are not scheduled to assure that each

brigade member participates in at least two drills per year as

delineated in by 10 CFR 50 Appendix R Item L.3.

This specific portion

of Appendix R is not required at Surry.

The issue is further addressed

in Section F5.

c.

Conclusions

The fire protection program implementing procedure met the commitments

to the NRC.

However. the procedure does not require each fire brigade

member to participate in at least two drills per year.

F5

Fire Protection Staff Training and Qualification

a.

Inspection Scope (64704)

b.

The inspector reviewed the fire brigade organization and training for

compliance with the facility's fire protection program and the NRC

guidelines and requirements.

Observations and Findings

The organization and training requirements for the Surry plant fire

brigade are established by VPAP-2401. Section 6.6.

The fire brigade for

each shift was composed of a fire brigade leader and two brigade members

from operations and two brigade members from security.

The operations

fire brigade leader and members are normally auxiliary (non-licensed)

unit operators.

Each fire brigade member is required to receive

initial. quarterly and annual fire fighting related training and

. ,,

24

satisfactory completion of an annual medical evaluation which provides

certification that the fire brigade member can participate in the fire

brigade.

There were a total of 44 operations personnel and 20 security

personnel on the plant's fire brigade.

Although the normal industry practice is to utilize licensed personnel

as the fire brigade leader. the licensee considered the non-licensed

operators as having sufficient training and knowledge of plant

safety-related systems to understand the effect of fire on safe shutdown

capability to meet the commitments to the NRC.

In addition. licensee

personnel were available for consultation. if required. in the event of

a fire.

The inspector reviewed the training and medical records for five

security and five operations personnel and verified that the training

and medical certification for these employees were up to date.

The drill records for 1995 and the first three quarters of 1996 were

reviewed.

These records indicated that at least one drill per quarter

had been performed for each of the five operational shifts. However.

since security has only four shifts. all four security shifts did not

routinely participate in some of the quarterly fire brigade drills.

In

addition. since normally only approximately five personnel respond to

fire brigade drills. several of the fire brigade members may not

routinely participate in a fire brigade drill.

NRC policy is for each

fire brigade member to participate in at least two drills per year.

This is not required at Surry and is considered a weakness.

The inspector reviewed the list of areas in which fire drills had been

held since 1993 and noted that the drills were performed in a number of

different plant areas to assure that the brigade was familiar with the

fire protection and operational features and fire hazards in these

areas.

c.

Conclusions

The fire brigade organization and training met the commitments to the

NRC.

However. not stipulating a minimum participation of at least two

drills per year for each member of the fire brigade was identified as a

weakness.

F6

Fire Protection Organization and Administration

a.

Inspection Scope

The licensee's management and administration of the facility's fire

protection program was reviewed for compliance with the commitments to

the NRC and to current NRC guidelines.

F7

25

b.

Observations and Findings

The designated onsite manager responsible for the administration and

implementation of the fire protection program was the Station Manager.

This responsibility had been delegated to the Supervisor. Administrative

Service.

The Supervisor. Station Safety and Loss Prevention reports to

the Supervisor. Administrative Services and was responsible for the

station fire protection program and ensuring that the appropriate fire

prevention procedures and surveillance tests of the fire protection

features were implemented.

Completed tests and surveillances performed

by the Safety and Loss Prevention staff were reviewed for accuracy.

Tests and surveillances which did not meet the acceptance requirements

were also reviewed and notification reports were prepared for the

appropriate authorization. Coordination of the station's Appendix R

requirements was provided by a fire protection system engineer in the

Nuclear Engineering group.

Engineering support for the design of the

fire protection features was provided by the offsite Design Engineering

and Support organization.

c.

Conclusions

The coordination and oversight of the facility's fire protection program

met the licensee's commitments to the NRC .

Quality Assurance in Fire Protection Activities

a.

Inspection Scope

The following audits and self assessment report were reviewed:

QA Audit 92-15

Fire Protection and Loss Prevention Audit

(Annual and Triennial)

QA Audit S95-02

Fire Protection and Loss Prevention

QA Audit 96-02

Fire Protection Implementation Program

Self Assessment

Safety and Loss Prevention Fire Protection

Program Self Assessment of July 24. 1996

b.

Observations and Findings

These audits and the self assessments were comprehensive and identified

a number of findings. observations and issues for resolution to enhance

the facility's fire protection program.

The inspectors reviewed the

audit findings from each QA report and verified that the items had been

resolved. except for two items in QA Audit Report 96-02 which were

scheduled to be completed by November 1996 .

  • ~

,, I

26

c.

Conclusions

The audits and assessment of the facility's fire protection program were

thorough and appropriate corrective actions were taken to resolve the

identified issues.

FB

Miscellaneous Fire Protection issues

F8.l Fire Protection Related NRC Information Notices

F8.2

The inspectors reviewed the licensee's evaluation for the following NRC

Information Notices (IN) and concluded that these INs had received an

appropriate evaluation and that the required corrective actions had been

completed:

IN 92-18. Potential Loss of Shutdown Capacity During a Control

Room Fire

IN 92-28. Inadequate Fire Suppression System Testing

IN 94-28. Potential Problems with Fire Barrier Penetration Seals

a

IN 94-31. Potential Failure of WILCO. LEXAN-Type HN-4-L. Fire Hose

Nozzles

IN 94-58. Reactor Coolant Pump Lube Oil Fire

IN 95-36. Emergency Lighting

(Closed) Inspection Follow-up Item 50-280. 281/95023-02: modification of

MER-5 power supply cable fire barrier to eliminate need for fire watch.

This item was first documented by NRC IR 50-280. 281/93-30. Paragraph 6

and involved the installation of a 1-hour fire rated barrier for the

power cables located in the Unit 2 emergency switchgear room.

This room

provides the power for the control room and emergency switchgear room

chillers. MER-5.

To meet the requirements of 10 CRF 50 Appendix R.

these power cables in the Unit 2 switchgear room were required to be

installed within a 3-hour fire rated barrier. since an automatic fire

suppression system was not installed in this room.

To resolve this

issue. the licensee will retain the 1-hour fire barrier for these power

cables in the switchgear room and will provide an alternate power supply

to the MER-5 chillers from the non-safety related emergency diesel

generator which was recently i nsta 11 ed to meet the "station blackout"

requirements.

Installation of this alternate power supply will be

accomplished by a plant modification which was scheduled to be competed

in late 1997.

Until this modification is completed. the licensee will

maintain the hourly fire watch currently provided for this area.

The inspector reviewed the fire watch patrol records for the Unit 2

emergency switchgear room and ve:ified that an hourly fire watch patrol

was being performed for this area.

i.'

J I

27

V. Management Meetings

Xl

Exit Meeting Summary

The inspectors presented the inspection results to members of licensee

management at the conclusion of the inspection on October 3. 1996.

The

licensee acknowledged the findings presented.

The inspectors asked the licensee whether any materials examined during the

inspection should be considered proprietary.

No proprietary information was

identified .

-'

a I

28

PARTIAL LIST OF PERSONS CONTACTED

Licensee

R. Blount. Maintenance Superintendent

D. Christian. Station Manager

M. Crist. Operations Superintendent

J. McCarthy. Assistant Station Manager. Operations & Maintenance

R. Saunders. Vice President. Nuclear Operations

B. Shriver. Assistant Station Manager. Licensing and Compliance

T. Sowers. Engineering Superintendent

B. Stanley, Director Nuclear Oversight

J. Swientoniewski. Supervisor Station Nuclear Safety

W. Thorton. Superintendent. Radiological Protection

IP 37551:

IP 40500:

IP 60855:

IP 61726:

IP 62703:

IP 64704:

IP 71707:

29

INSPECTION PROCEDURES USED

Onsite Engineering

Effectiveness of Licensee Controls in Identifying, Resolving, and

Preventing Problems

Operation of an ISFSI

Surveillance Observation

Maintenance Observation

Fire Protection Program

Plant Operations

IP 71750:

Plant Supprot Activities

IP 84750:

Radioactive Waste Treatment. And Effluent And Environmental

Monitoring

IP 86750:

Solid Radioactive Waste Management And Transportation Of

Radioactive Materials

IP 92700:

Onsite Followup of Written Reports of Nonroutine Events at Power

Reactor Facilities

IP 92901:

Followup - Operations

IP 92902:

Fo 11 owup - Maintenance

TI 2515/133:Implementation of Revised 49 CFR Parts 100-179 AND 10 CFR Part 71

Opened

50-280. 281/96010-01

50-280. 281/96010-02

50-280. 281/96010-03

50-280. 281/96010-04

Closed

50-280, 281/94009-01

50-281/96001-00

50-280. 281/96002-02

ITEMS OPENED, CLOSED, AND DISCUSSED

URI

Improper actions associated with a containment

entry. This item is under review by regional

management (Section R7).

NCV

Respirators issued to nonqualified personnel

(Section R7).

VIO

Inadequate preventive maintenance performed on

spare electric motors (Section Fl.2).

IFI

Preventive maintenance requirements for spare

RHR and component cooling water pumps (Section

Fl .2)

IFI

SWSOPI corrective actions (Section 08.1).

LER

Through wall leak in RHR piping (Section 08.2).

VIO

Failure to follow procedures for Deficiency Card

initiation (Section 08.2).

30

50-280. 281/95022-01

VIO

Missed technical specification surveillance

(Section M8.1).

50-281/95004-00

LER

Installation of damaged circuit card resulted in

Unit 2 manual reactor trip (Section M8.2).

50-281/95005-00

LER

Manual trip due to control rods dropping into

reactor core (Section M8.3).

50-280/95006-00

LER

Loss of SWS pumps due to marine growth (Section

M8.4)

50-280/96005-00

LER

Air binding of SWS pumps (Section M8.5).

50-281/95023-01

vro

Multiple personnel violations of RWP

requirements (Section R8.2).

50-280. 281/95023-02

IFI

Modification of MER-5 power supply cable fire

barrier to eliminate need for fire watch

(Section F8. 2).

50-280.281/96010-02

NCV

Respirators issued to nonqualified personnel

Discussed

None

(Section R7) .