ML18151A646

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Notice of Violation from Insp on 950914-1004.Violation Noted:On 950913,activities Affecting Quality Have Not Been Accomplished IAW Documented Procedures as Evidenced by Listed Examples
ML18151A646
Person / Time
Site: Surry Dominion icon.png
Issue date: 11/22/1995
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18151A648 List:
References
50-280-95-20, EA-95-223, NUDOCS 9512110474
Download: ML18151A646 (37)


See also: IR 05000914/2010004

Text

NOTICE OF VIOLATION

Virginia Electric and Power Company

Surry Power Station

Docket No. 50-280

License No. DPR-32

EA 95-223

Unit 1

During an NRC inspection conducted on September 14 through October 4, 1995,

violations of NRC requirements were identified.

In accordance with the

"General Statement of Policy and Procedure for NRC Enforcement Actions,"

NUREG-1600, the violations are listed below:

A.

-

.---

10 CFR 50, Appendix B, Criterion V, as implemented by the Surry

Operational Quality Assurance Program Topical Report (VEP-l-5A),

Section 17.2.5, Instructions, Procedures, and Drawings, requires, in

part, that activities affecting quality be prescribed by and

accomplished in accordance with documented procedures of a type

appropriate to the circumstances.

For operational activities affecting quality these requirements are

implemented, in part, by Virginia Power Administrative Procedure

(VPAP)-1401, Conduct of Operations, Revision (Rev.) l; Operations

Department Administrative Procedure (OPAP)-0005, Shift Relief and

Turnover, Rev. 4; and OPAP-0002, Operations Department Procedures,

Rev. 3.

VPAP 1401, Section 6.1.12.b.l, requires that the Shift Supervisor and

the Unit Senior Reactor Operator maintain, as a matter of highest

priority, the broadest perspective of operational conditions affecting

the facility.

VPAP 1401, Section 6.1.12.c.2, requires that all shift team members be

aware of station status at all times and that supervisory personnel

monitor the performance of shift personnel who could affect station

safety.

OPAP-0005, Section 6.1.4, requires that the departing shift make checks

and remarks on the required *shift relief checklist in a way that informs

the relieving shift of information including significant or important

inoperable equipment including instrumentation.

Section 6.1.5 also

requires that the departing and relieving personnel discuss important

items affecting plant operations.

OPAP-0002, Section 5.3.5, states that the Shift Supervisor and Unit

Senior Reactor Operator are responsible for enforcing compliance with

procedures as written.

Enclosure 1

9512110474 951122

PDR

ADOCK 05000280

G

POO

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I~

Notice of Violation

2

Contrary to the above, on September 13, 1995, activities affecting

quality were not accomplished in accordance with documented procedures

as evidenced by the following examples:

1.

The Shift Supervisor and the Unit Senior Reactor Operator failed

to maintain a broad perspective of operational conditions

affecting the facility, in that, reactor coolant system inventory

was reduced by approximately 4,500 gallons over an approximate

five hour period without knowledge of the activity and its effect

on unit safety.

2.

Not all shift team members were aware of station status, in that,

a unit control room operator unknowingly lowered reactor vessel

water level when he conducted letdown operations to maintain

3.

  • standpipe level indication. Additionally, shift supervision did

not properly monitor the operator performing this evolution which

could.have affected station safety.

The departing day shift failed to make remarks on the required

shift relief checklist to inform the oncoming shift of important

inoperable equipment.

Specifically, the isolation of the reactor

coolant head vent which rendered the only means of reactor vessel

level indication inoperable was not recorded on the shift relief

checklist. Additionally, members of the departing and relieving

shifts failed to discuss this important issue affecting plant

operations.

4.

The Shift Supervisor and Unit Senior Reactor Operator failed to

enforce compliance with procedure l-OP-RC-011, Pressurizer Relief

Tank Operations, Rev. 1, for venting the Pressµrizer Relief Tank

as described in Violation C below.

(01013)

B.

Technical Specification 6.4 requires, in part, that detailed written

procedures be provided for corrective maintenance activities which would

have an effect on nuclear safety and that they be followed.

VPAP-2002, Work Request and Work Order Task, Rev. 5, partially

implements these requirements for maintenance activities.

VPAP-2002, Section 5.7.1, requires that the Shift Supervisor review and

approve work orders on permanent plant structures, equipment, and

components.

VPAP-2002, Section 5.7.2, requires that the Shift Supervisor align plant

systems, as jequired, to support work order task activities.

VPAP-2002, Section 5.7.4, requires that equipment be prepared for

maintenance prior to approval of a work order .

Contrary to the above, on September 13, 1995, the Shift Supervisor who

approved Work Order 00316472, Retract/Install Flux Thimbles, failed to

-*

Notice of Violation

3

ensure that the appropriate plant system was aligned to support the work

order task requirements and failed to ensure that the appropriate

equipment was prepared for maintenance prior to approval of the work

order. Specifically, the Shift Supervisor failed to ensure that the

reactor coolant system was depressurized.

(01023)

C.

Technical Specification 6.4 requires, in part, that detailed written

procedures be provided for activities which would have an effect on

nuclear safety and that they be followed.

Procedure l-OP-RC-011, Pressurizer Relief Tank Operations, Rev. 1,

Section 5.5, establishes the method for venting the pressurizer relief

tank to the Vent Vent System.

Steps 5.5.4, 5.5.5, and 5.5.6.a require

that a Gaseous Group Release Permit be obtained for venting the

pressurizer relief tank to the Vent Vent System; a poly hose be

connected from valve 1-RC-ICV-5025 to the nearest containment purge

exhaust; and, valve 1-RC-HCV-1549, PRT Vent, be closed, respectively.

Contrary to the above, on September 13, 1995, approved detailed written

procedures were not followed to perform venting of the Unit 1

pressurizer relief tank as evidenced by the following:

1.

2.

3.

No Gaseous Group Release Permit was obtained for venting the

pressurizer relief tank to the Vent Vent System.

A poly hose was not connected from valve 1-RC-ICV-5025 to the

nearest containment purge exhaust.

1-RC-HCV-1549, PRT Vent, was not closed.

(01033)

These violations represent a Severity Level III problem (Supplement I). This

violation is applicable to Unit 1 only.

Pursuant to the provisions of 10 CFR 2.201, Virginia Electric and Power

Company is hereby required to submit a written statement or explanation to the

U.S. Nuclear Regulatory Commission, ATTN:. Document Control Desk, Washington,

D.C. 20555 with a copy to the Regional Administrator, Region II, and a copy to

the NRC Resident Inspector at the facility that is the subject of this Notice

of Violation (Notice), within 30 days of the date of the letter transmitting

this Notice.

This reply should be clearly marked as a "Reply to a Notice of

Violation" and should include for each violation:

(1) the reason for the

violation, or, if contested, the basis for disputing the violation, (2) the

corrective steps that have been taken a~d the results achieved, (3) the

corrective steps that will be taken to avoid further violations, and (4) the

date when full compliance will be achieved.

Your response may reference or

include previous docketed correspondence, if the correspondence adequately

addresses the required response.

If an adequate reply is not received within

the time specified in this Notice, an order or a Demand for Information may be

issued as to why the license should not be modified, suspended, or revoked, or

why such other action as may be proper should not be taken.

Where good cause

is shown, consideration will be given to extending the response time.

Notice of Violation

4

Under the authority of Section 182 of the Act, 42 U.S.C. 2232, this response

shall be submitted under oath or affirmation.

Because your response will be placed in the NRC Public Document Room (PDR), to

the extent possible, it should not include any personal privacy, proprietary,

or safeguards information so that it can be placed in the PDR without

redaction.

However, if you find it necessary to include such information, you

should clearly indicate the specific information that you desire not to be

placed in the PDR, and provide the legal basis to support your request for

withholding the information from the public.

Dated ~~tlanta, Georgia

thi~.:.;J-l<IY of November 1995

LIST OF ATTENDEES

NRC Personnel

J. R. Johnson, Acting Deputy Regional Administrator

E.W. Merschoff, Director, Division of Reactor Projects (DRP}

A. F. Gibson, Director, Division of Reactor Safety (DRS}

C. F. Evans, Regional Counsel

B. Uryc, Director, Enforcement and Investigations Coordination Staff (EICS}

W. J; McNulty, Director, Office of Investigations Field Office

J. N. Hannon, Acting Deputy Director, DRP

B. C. Buckley, Senior Licensing Project Manager, Project Directorate II-2,.

Office of Nuclear Reactor Regulation

G. A. Belisle, Chief, Reactor Projects Branch 5 (RPB 5}, DRP

M. W. Branch, Surry Senior Resident Inspector, RPB 5, DRP

L. W. Garner, Project Engineer, RPB 5, DRP

L. J. Watson, Enforcement Specialist, EICS

D. C. Payne, Operator Licensing Examiner, DRS

M. E. Ernstes, Operator Licensing Examiner, DRS

J. E. Beall, Enforcement Specialist, Office of Enforcement (By Telephone}

Virginia Electric and Power Company

R. F. Saunders, Vice President, Nuclear Operations

M. L. Bowling, Manager, Nuclear Licensing and Operations Support

D. A. Christian, Station Manager, Surry Power Station

J. H. McCarthy, Assistant Station Manager, Operations and Maintenance

B. L. Shriver, Assistant Station Manager, Nuclear Safety and Licensing

R.H. Moore, Shift Supervisor

R. D. Scherer, Reactor Operator

Enclosure 2

.

PREDECISIONAL ENFORCEMENT CONFERENCE AGENDA

SURRY

NOVEMBER 6, 1995, AT 1 :00 P.M.

NRC REGION II OFFICE, ATLANTA, GEORGIA

I.

OPENING REMARKS AND INTRODUCTIONS

J. Johnson, Acting Deputy Regional Administrator

II.

NRC ENFORCEMENT POLICY

8. Uryc, Director

Enforcement and Investigation Coordination Staff

Ill.

SUMMARY OF THE ISSUES

IV.

V.

J. Johnson, Acting Deputy Regional Administrator

STATEMENT OF CONCERNS/ APPARENT VIOLATIONS

E. Merschoff, Director

Division of Reactor Projects

LICENSEE PRESENTATION

R. Saunders, Vice President - Nuclear Operations

VI.

BREAK / NRC CAUCUS

VII.

NRC FOLLOWUP QUESTIONS

VIII.

CLOSING REMARKS

J. Johnson, Acting Deputy Regional Administrator

Enclosure 3

_***

A.

ISSUES TO BE DISCUSSED

10 CFR Part 50, Appendix B, Criterion V, Instruction, Procedures and

Drawings; VPAP-1401, Conduct of Operations; and OPAP-0002,

Operations Department Procedures require that operational activities

affecting quality be accomplished in accordance with prescribed

procedures. On September 13 operational activities were not

accomplished in accordance with procedures as evidenced by the

following examples:

1 .

The SS and the Unit SRO failed to maintain a broad perspective

of operational conditions affecting the facility. As a result, RCS

coolant inventory was inadvertently reduced by approximately

4500 gallons over an approximate three and one half hour period.

2.

3.

4.

A Unit Control Room Operator was not aware that reactor vessel

water level was being lowered when he initiated letdown

operations to maintain RVWL standpipe indication. Additionally,

shift supervision did not properly monitor the operator performing

this evol_ution which could affect station safety.

The departing day shift failed to make remarks on the required

shift relief checklist to inform the oncoming shift of important

inoperable equipment. The reactor coolant head vent was

isolated rendering the only means of reactor vessel water level

indication inoperable. Members of the departing and relieving

shifts did not discuss this important item affecting plant

operations.

The SS and Unit SRO failed to enforce compliance with procedure

1-0P-RC-011 for venting the PRT.

,

NOTE:

The apparent violations discussed in this predecisional

enforcement conference are subject to further review and are

subject to change prior to any resulting enforcement decision .

8.

ISSUES TO BE DISCUSSED

Technical Specification 6.4 requires that written procedures be

provided and followed for corrective maintenance activities.

Procedures for maintenance activities were not followed for WO 00316472, Retract/Install Flux Thimbles, which was approved by the

SS on September 13, 1995. Specifically, the plant system was not

aligned and the equipment was not prepared for maintenance to

support the work activity, in that, the RCS was not depressurized.

NOTE:

The apparent violations discussed in this predecisional

enforcement conference are subject to further review and are

subject to change prior to any resulting enforcement decision.

C.

Technical Specification 6.4 require that written procedures be provided

and followed for operation of all systems involving nuclear safety .

On September 13, 1995, approved detailed written procedures were

not used to perform venting of the Unit 1 PRT as evidenced by the

following:

1.

No Gaseous Group Release Permit was obtained for venting the

PRT to the Vent Vent System as required by procedure

1-0P-RC-011, step 5.5.4.

2.

A poly hose was not connected from valve 1-RC-ICV-5025 to the

nearest containment purge exhaust as required by procedure

1-0P-RC-011, step 5.5.5.

3.

1-RC-HCV-1549, PRT Vent was not closed as required by

procedure 1-0P-RC-011, step 5.5.6.a.

NOTE:

The apparent violations discussed in this predecisional

enforcement conference are subject to further review and are

subject to change prior to any resulting enforcement decision.

.}.-

. * ...

i

.

VIRGINIA POWER

\\

SURRY POWER STATION

PREDECISIONAL ENFORCEMENT CONFERENCE

NOVEMBER 6, 1995

Enclosure 4

..' .. * .

VIRGINIA POWER

INTRODUCTION

R. F. Saunders

Vice President - Nuclear Operations

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AGENDA

  • Introduction
  • Management Perspective
  • Summary of Events

and Lessons Learned

  • Corrective Actions
  • Safety Significar,ce

and Program Effectiveness

  • Conclusions

-

3 -

  • . '

R. F. Saunders

D. A. Christian

W. H. Moore

R. D. Scherer

J.H.McCarthy

B. L. Shriver

B. L. Shriver

VIRGINIA POWER

MANAGEMENT PERSPECTIVE

D. A. Chrisnan

Stati,on Manager

- 4 -

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MANAGEMENT

PERSPECTIVE

  • .

-..

Events of September 13 - 14, 1995 Revealed Weaknesses in the

Control of Some Plant Evolutions

-

An Undetected Loss of Reactor Vessel Inventory Resulting

from Inadequate Configuration ~ontrol Due to a Weakness in

Operations Crew Knowledge

-

Release of Work on the Seal Table Due to a Failure of Team

Members to Verify Changes in Reactor Coolant System

Conditions

-

Venting of the Pressurizer Relief Tank without Meeting

Procedural Requirements by Operations Management

The Overall Outage Schedule and Safety Assessment Assured

that these Weaknesses did Not Challenge Safety

- s -

.*.

.

.* *

..*

,:

MANAGEMENT

PERSPECTIVE

Outage Schedule Development

-

Philosophy of Incremental Change Based on Surry Experience

-

Developed by Interdepartmental Outage Integration Team

-

Outage Schedule and Duration Approved by Station Management

,

Outage Safety Assessments Assure "Defense in Depth"

-

Safety Assessment is an Integral Part of Initial Outage Schedule

Development and is Approved by the Station Nuclear Safety and

Operating Committee

-

Changes in Outage Sequence are Evaluated and the Safety

Assessment is Revised

-

Station Management Review Actual Plant Status Using the Critical

Safety Parameters

- 6 -

MANAGEMENT

PERSPECTIVE

Pre-Outage Preparations Included:

  • .. '*

.

'

-

Simulator Training on New Plant Cooldown/Depressurization .

Process

-

Refueling Crew Training

-

ALARA Awareness Training for 552 Personnel

-

Readiness Reviews

-

Outage Work Schedules

-

7 -

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MANAGEMENT

PERSPECTIVE

Immediate Management Actions were Taken to Address each

Issue and Assure Improved Crew Performance

-

Work Activities Potentially Affecting Reactor Coolant System

Inventory were Halted and the Status of Other Safety

Equipment was Verified

-

Station

Management Provided

Coaching to Reinforce

Operations Standards for Command and Control

-

Training was Provided to Address Operator and Shift

Technical Advisor Knowledge Weaknesses

Procedural Controls were Strength.ened

-

Management Oversight was Strengthened

Category I Root Cause Evaluation was Initiated

- 8 -

MANAGEMENT

PERSPECTIVE

Category I Root Cause Evaluation (RCE) was Initiated on

September 14, 1995

-

Interdepartmental Team Including Members from Corporate Nuclear Safety,

Station Nuclear Safety, Training, and North Anna Power Station Operations

-

Independent Management Oversight

Root Cause of Undetected Loss _of Reactor Vessel Inventory

was Determined

-

Inadequate Configuration Control Due to a Weakness in Operations Crew

Knowledge

RCE Identified Other Issues

-

Release of Work on the Seal Table

  • Caused by Failure of Team Members to Verify and Communicate Changes

in Reactor Coolant System Conditions

-

Venting of the Pressurizer Relief Tank without Meeting Procedural

Requirements

  • Caused by Inappropriate Personnel Performance

- 9 -

MANAGEMENT

PERSPECTIVE

Initial Actions were Effective

-

No Problems were Experienced with Subsequent Draindowns

-

Operations Command and Control was Maintained

-

Knowledge and Understanding were Enhanced

-

Management and

Licensed

Operator Sensitivity were

. Enhanced

Longer Term Actions Include:

-

Continued Coaching and Monitoring of Operations Personnel

to Ensure Standards are Being Met

-

Training and Procedural Enhancements to Ensure Shift

  • Teams are Better Prepared to Implement the Outage

Schedule

- 10 -

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VIRGINIA POWER

SUA(MARY OF EVENTS

AND LESSONS LEARNED

R. D. Scherer

Reactor Operator

-:-- 11 -

w .. H .. Moore

Senior Reactor Operator

  • .. ',

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REACTOR VESSEL HEAD VENT

AND STANDPIPE DIA'GRAM

Cloop

Cloop

TC

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1-RC-184

D

j5% 29.0'

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-ll'll, 27.5'

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+--Tygon

1-RC-135

POR\\f

24.0' Tap of_.,.

18.7' R-fllrve

PRT

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REACTOR VESSEL

INVENTORY

e: . ,

Pressurizer Relief Tank (PRT) Pressure was Maintained while

the Reactor Coolant System was Drained from 11% Pressurizer

Level to 18 Feet

Preparation of Reactor Vessel Head Vent Tagout

-

Separate Technical Briefings

  • Reactor Operators
  • Senior Reactor Operator

I * *

  • Auxiliary Operator

Reactor Vessel Head Vent was Isolated for Spoolpiece Removal

The Reactor Vessel Level Standpipe became Inoperable, but

was Not Recognized as Such Due to Knowledge Deficiency

- 13 -

I

  • ..

REACTOR VESSEL

INVENTORY.

Control of Reactor Coolant System (RCS) Inventory

-

Minor Level Changes were Induced to Verify Reactor Vessel Level

Standpipe Response

-

Maintained Reactor Vessel Standpipe Indicated Level at 18 Feet

  • Maximized Letdown Flow
  • Adjusted Charging Flow

Reactor Vessel Standpipe Indicated Level Decreased from 18

Feet to 13.3 Feet when the Reactor Vessel Head Studs were

Detensioned

Actuons were Immediately Initiated to Restore RCS Level to 18

Feet

Reactor Vessel Head Vent was Returned to Service

- 14 -

  • -

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.:

INCOREFLUX

THIMBLE SEAL

......

Senior Reactor Operator Preparation/Perception

-

Believed Reactor Coolant System (RCS) was at Atmospheric

Pressure

  • !Board Walkdown Prior to Shift Turnover
  • Interface with Chemistry Department Regarding Pressurizer

Sampling

Determination that the RCS was Pressurized During the

Disassembly of an lncore Flux Thimble High Pressure Seal

-

Suspended Work on Flux Thimbles

-

Stopped the Release of Pressurizer Safety Valve Work

-

15 -

SHIFT PERSPECTIVE

Typical Operations Performance Ensures:

-

Supervisory Oversight is Provided

-

Evolutions are Well Unders*.:ood

-

Plant Conditions are Known

-

Procedures are Used

      • *

These

Events

were

Not

Characteristic

of

Operations

Performance

Shift Assessment and Lessons Learned

-

Questioning Attitude

-

Supervisory Oversight

-

Shift Turnover

-

Communications

-

Broad Perspective

- 16 -

VIRGINIA POWER

CORRECTIVE ACTIONS

J. H. McCarthy

Assistant Station Manager

Operations and Maintenance

- 17 -

  • *

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IMMEDIATE

CORRECTIVE ACTIONS

Reactor Coolant System (RCS) Level was Restored

Measures were Implemented to Ensure Configuration Control

Reactor Vessel Head Vents were Tagged Open

-

Configuration of Important Safety Systems was Confirmed

Work Activities Potentially Affecting RCS Inventory were Halted

Management Initiated a Category I Root Cause Evaluation

- 18 -

.. ,*i ..

CORRECTIVE ACTIONS

CONTINUED DURING THE OUTAGE

Management Oversight was Strengthened

.

'

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'

Management Expectations for Operations Personnel and Shift

Technical Advisors .(STA) were Clarified and Reinforced

-

Nuclear Safety Policy

-

Command and Control

-

Critical Monitoring of Plant Parameters

-

Shift Turnover

-

Configuration Control

Station Manager Approval Required for Fuel On-Load

-

Core On-Load Assessment

- 19 -

-- --*--------

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CORRECTIVE ACTIONS

CONTINUED*DURING THE OUTAGE

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Training was Conducted for Operations Personnel and Shift

Technical Advisors *

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Operations Standards

-

Management Expectations

-

Reactor Coolant System (RCS) Inventory Control

-

Reactor Vessel Head Vent and Level Standpipe Interrelationship

-

RCS Inventory Balance

Unit 1 Procedures were Revised to Provide Better Guidance to:

Ensure Reactor Vessel Level Standpipe Operability

-

Perform an RCS Inventory Balance

Outage Schedule was Revis,d to:

-

Reduce Multiple Reactor Coolant System Inventory Activities

-

!Unasolate the RCS Loops Only when tlhe RCS Level was > 5% in the

Pressurizer

- 20 -

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LONGER TERM

CORRECTIVE ACTIONS

Verify that Operations Standards Clearly -Define Management

Expectations

Communicate Operations Standards and Monitor Operations

Personnel Performance to Ensure Standards are Being Met

Develop and Provide Refueling Outage Preparatory Training to

Ensure that Shift Teams are Better Prepared to Implement the

Outage Schedule

Actions Resulting from the Category I Root Cause Evaluation:

-

Developed a Specific Operations Procedure that Controls the

Manipulation of the Reactor Vessel Head Vent Valves

Revised Unit 2 Procedures to Provide Better Guidance to:

  • Ensure Reactor Vessel Level Standpipe Operability

- * Perform a Reactor Coolant System Inventory Balance

- 21 -

*
      • , ..

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.

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LONGER TERM

CORRECTIVE ACTIONS

Actions Resulting from the Category I RCE (Continued):

-

Revise Continuing Training for Operations Personnel and Shift

Technical Advisors (STA)

  • Enhance Discussion of the Reactor Vessel Head Vent and Level

Standpipe Interrelationship

  • Emphasize STA Responsibilities During Outages

-

Provide Continuing Training to Operations Personnel and Shift

Technical Advisors

  • Need to Maintain Questioning Attitude

Changes

  • Need to Maintain a Broad Perspective of Unit Activities

- 22 -

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VIRGINIA POWER

SAFETY SIGNIFICANCE AND

PROGRAM EFFECTIVENESS

B. L. * Shriver

Assistant Station Manager

Nuclear Sa/ ety and Licensing

- 23 -

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SAFETY SIGNIFICANCE

AND PROGRAM EFFECTIVENESS

Individually and Collectively the Issues were Not Safety

Significant

-

Residual

Heat

Removal

System

Operation

was

Not

Challenged

  • System Performance was Not Affected
  • Inaccurate Reactor Vessel Level Standpipe Indication was

Self-Correcting

-

Equipment and Procedures Provided Alternate Methods of

Core Cooling

-

No Identifiable Radiological Exposures

-

Radiological Releases were Within Administrative Limits

- 24 -

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SAFETY SIGNIFICANCE

AND PROGRAM EFFECTIVENESS

Weaknesses in Activities During the* Preparations for Reactor

Head Removal were Not Due to a Breakdown in Control of

Licensee Activities and were Not Due to a Lack of Attention to

Licensed Responsibilities

-

Management Programs and Procedures Ensured that an

Adequate Margin of Safety was Maintained

-

Event Causes were Different and Not Indicative of a

Programmatic Breakdown of Control or Inattention

-

Other Critical Outage Activities were Properly Controlled

-

Station Response Demonstrates an Overall Commitment to

Safety

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25 -

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SAFETY SIGNIFICANCE

AND PROGRAM EFFECTIVENESS

A Comprehensive Corrective Action Plan was Implemented

Immediate Actions were Taken to Assure Reactor Coolant

System Inventory was Maintained and Outage Activities were

Controlled

-

Corrective Actions Continued During the Outage to Improve

Crew

Knowledge

and

Strengthen

Implementation

of

Operations Standards

-

Longer Term Corrective Actions have been Initiated to

Provide Additional Assurance that Operating Crews Fully

Meet High Standards

- 26 -

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CONCLUSIONS

Not Indicative of Programmatic Deficiencies

Not Representative of a Breakdown in Control of Licensee

Activities

Not Representative of a Lack of Attention Toward Licensed

Responsibilities

No Nuclear Safety or Radiological Significance

Prompt Corrective Actions and Management Follow-Up

Effectiveness of

Programs Assured through Critical and

Comprehensive Self-Assessment

- 27 -

MlN REQ'D EQUIP FOR

PRIMARY /BACKUP

COOLING METHODS

AVAILABLE

(AS PER J-OSP-ZZ-004)

NO

RCS

INTACT

N/A [3

Fully Operable

Acceptable

Condition Green

REFUELING

~REMENTS MET

l!:.J YES

NO

Component(s) Degraded or 1 Power Supply Unavailable

Acceptable but degraded

Condition Yellow

Component Inoperable

Function or System Inoperable

Condition Orange - Contingency actions may be required

Function or System Requirement Unacceptable

Unacceptable condition

Condition Red

Enclosure 5

r

MIN REQ'D EQUIP FOR

PRJMAR Y/BACKUP

COOLING METHODS

REFUELING

REQUIREMENTS MET

G

YES

NO

Component(s) Degraded or 1 Power Supply Unavailable

Acceptable but degraded

Condition Yellow

Component Inoperable

Function or System Inoperable

Condition Orange - Contingency actions may be required

Function or System Requirement Unacceptable

Unacceptable condition

Condition Red

Enclosure 6

  • -1