ML18151A427
| ML18151A427 | |
| Person / Time | |
|---|---|
| Site: | Surry |
| Issue date: | 05/17/1990 |
| From: | Blake J, Kleinsorge W NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| To: | |
| Shared Package | |
| ML18151A428 | List: |
| References | |
| 50-280-90-07, 50-280-90-7, 50-281-90-07, 50-281-90-7, GL-88-14, IEIN-88-067, IEIN-88-67, NUDOCS 9006070280 | |
| Download: ML18151A427 (80) | |
See also: IR 05000280/1990007
Text
Report Nos. :
UNITED STATES
NUCLEAR REGULATORY COMMISSION
REGION II
101 MARIETTA STREET, N.W.
ATLANTA,GEORGIA30323.
50-280/90-07 and 50-281/90-07
Licensee:
Virginia Electric and Power Company
Glen Allen, VA 23060
Docket Nos.:
50-280 and 50-281
License Nos.:
Facility Name:
Inspectors:
- March 2; March 12-16 and 26;1~~
Team Members:
Scope:
asman
Mi 11 er
Naidu
ultz
g
J J. Blake, Chief
at rials and Processes Section
Engineering Branch
Division of Reactor Safety
SUMMARY
Date Signed
Date Signed
This special, announced inspection consisted of an in-depth team inspection of
the maintenance program and its implementation.
NRC Temporary Instruction
2515/97 issued September 22, 1989, was used as guidance for this inspection.
Results:
Overall, the maintenance program and its implementation were judged to* be
marginally SATISFACTORY with* a strong potential for improvement.
The more
significant areas of strength and weakness are highlighted in the Executive
Summary, with details provided in the report. one violation was identified:
"Failure to Follow Procedures for Maintenance" - paragraph numbers 2.e., 2.h.,
3.b., 3.i., and 3.k.
One unresolved item was identified:
"EOG Day Tank Fuel
Transfer Line Analysis
11 paragraph 2.f.
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EXECUTIVE SUMMARY
This NRC maintenance team inspection rated the Surry maintenance program
and its implementation marginally satisfactory with a strong potential for
improvement.
The satisfactory rating indicates adequate development and
implementation of the important elements of a maintenance program, with the
areas of weakness being approximately offset by strengths in other areas.
The inspection was conducted by an eight-man team using inspection guidance
provided in NRC Temporary Instruction 2515/97.
A principal feature of this
instruction is a maintenance inspection logic tree used to collate and present
the maintenance inspection findings.
The tree prepared by the NRC from inspection of Surry maintenance is presented
as Appendix 3 to this report. It depicts the ratings determined for individual
maintenance elements and the overall satisfactory rating.
The ratings are
discussed in report Section 4.
The team identified the following significant strengths and weaknesses:
Significant Strengths
System engineers support to craft activities
- The MOVATS testing program
The procedure upgrade program and the positive effect the program
has on procedures
The training program and facilities
Significant Weaknesses
Poor material condition of the Containment Air System
Poor material condition of the Heating, Ventilating and Air
Conditioning System
Poor allocation of resources
No effective prioritization program
The current Post Maintenance Test Program is inadequately defined
Control of maintenance backlog is ineffective
One violation was identified during the maintenance inspection.
It involved
several examples of failure to follow procedures for maintenance.
One unresolved item was identified relating to the analysis of the day tank
transfer line for the Emergency Diesel Generator.
~/
1-2
1.
INTRODUCTION
This inspection was conducted to assess the effectiveness of maintenance at
Surry Nuclear Plant utilizing guidance given in NRC Temporary Instruction
2515/97.
It was performed by;a eight-man team during February and March 1990.
Jhe inspection findings and conclusions are described in report Sections 2
through 4. Section 2, Inspection Details, describes the conduct of the
inspection and the findings obtained. Section 3, Issues, describes the more
outstanding issues identified during the inspection. Section 4, Evaluation of
Plant Maintenance, summarizes all of the findings and logic which culminates
in the overall rating of maintenance effectiveness at Surry. A special
maintenance inspection logic tree developed for the NRC was utilized to collate
findings for the rating process. It is discussed in Section 4 and presented in
Appendix 3.
',~
The last section of the report, Sections 5 describes the exit inte~view held
with the licensee following the inspection.
- '
2
2.
INSPECTION DETAILS
This'inspection was performance based and included:
General equipment condition and housekeeping in the various equipment
spaces were examined and evaluated.
Pumps, valves (including operators),
piping, supports and foundations were inspected for general condition and
cleanliness, leaks (water, oil,. and grease), rust/preservation, lubrica-
tion, dirt/trash, etc. Switchgear, relays, printed circuit control
boards,circuit breakers~ switches,lights, batteries and chargers,
invertefs, motor starters, wiring, connections and cables were inspected
for general condition and cleanliness, terminations, corrosion, lifted
leads, spare wires, boric acid, and missing parts.
In-process maintenance work activities.
Work performance, procedure
compliance, proper documentation, ~leanliness and housekeeping, material
control, system control (tag-out, LCO, etc.), tool control, Post.
Maintenance Testing (PMT) requirements, and persohnel qualification,
as applicable to the specific work, were evaluated.
Maintenance work histories for selected systems were examined by reviewing
- a brief description of the 100 newest completed WOs.
Selected open and
completed WOs for each system were examined in detail for technical
adequacy to include nature of trouble, work description, PMT, complete-
ness, readability, and legibility.
Health physics in its relation to maintenance
The inspection findings for systems, health physics and for miscellaneous
maintenance work observed are described below. All findings of importance to
the evaluation are included in Section 4.
2.a. SAFETY INJECTION (SI) SYSTEM
Background
The function of the SI system is to provide adequate emergency cooling to the
reactor core in the event of a LOCA or high energy line break.
Depending on
the accident scenario this is accomplished with the passive accumulators, the
low head SI pumps, the high head (charging) pumps, and associated piping and
valves.
Inspection
The inspection included walkdown of the majority of both unit 1 and 2 SI*
systems outside the containments, and examination of 17 completed WOs related
to the SI system.
'*, ................
3
In addition, the team observed the following maintenance work activities
related to the SI system:
Maintenance
.Work Document ID
Description of Activity Observed
Repair of oil leaks on Charging Pump 01-CH-P-lB
Repair of oil leaks on Charging Pump 01-CH-P-lB
PM (Vibrational Analysis) on Low Head SI Pump
1-SI-P-lB
The team evaluated th~ following general maintenance areas while inspectjng
the SI system: Post Maintenance Testing (PMT); QA/QC Involvement in the
Maintenance process; Predictive Maintenance (including a sample of vibrational
and oil analysis data for Low Head SI Pumps IA and 2A); and Control of Vendor
Manuals.
Findinas
The inspections, observations,and record reviews revealed the following:
In general, material condition and housekeeping were good with the exception
of some poor conditions, as detailed below. Although these conditions
indicated a need for improvement in some areas, they were minor compared with
the generally good condition of other areas observed.
There were five areas where the unit 2 SI piping configuration does not agree
with flow diagram 11548-FM-089A, Sheet 2.
In addition, there was a temporary
support installed for valve 2-SI-MOV-2885C. These problems had been identified
by the licensee during a wa*lkdown inspection in November-December, 1989, but
no corrective action had been initiated as of the close of this inspection.
The failure to initiate corrective action for this known condition and the
licensee identified drawing errors indicate a weakness in taking timely
corrective action discussed further in section 3.e.
In addition to the above discrepancies the team found that Sheet 3 of drawing
11548-FM-089A, shows a union in line 3"-SI-347-1503 which does not exist
(Drawing Change Request 90-1364 issued after identification by the NRC).
Also,
sheet 1 of the drawing indicates that valve 1-SI-69 and 2-SI-69 are locked
closed (It appears this is another drawing error since procedures do not
require that these valves be locked).
Dr~wing Change Requests 90~1259
and 90-1363 were issued after identification of this problem by the NRC.
Although the above drawing discrepancies including the five discrepancies
identified by the licensee, do not affect plant or system operability, they
are an indication of configuration control problems discussed further in
section 3.b .
4
Several instances of mi~sing fasteners or screws were identified.
Examples:
handwheel nut on valve 2-SI-51, pump 2-SI-P-lA electrical junction box cover
screws, bolt on motor inspection plate for valve 2-SI-MOV-2890A, upper limit
switch junction box cover screws for valve 2-SI-TV-202B, motor cover plate
. screws for valve l-SI-MOV-1869B, junction box cover screws for valve
1-TV-RM-lOOA, and junction box cover screws for valve 1-TV-CC-105C.
Pressure gauge 1-SI-PI-1942 was overdue for calibration - sticker indicated a
due date of 10/27/89.
Investigation revealed that this gauge is not in the
calibration program since it is used only on rare occasion for testing
Accumulator Discharge Check Valves (see Operating Procedure 1-0P-7.1.1) and is
calibrated on an as needed basis~ However, there is nothing in the operations
procedure to ensure that the gauge is calibrated when used.
For valve l-SI-MOV-1090C, body to bonnet fastener washers were corroded
(excessive rust) and the fasteners and bonnet flange were coated with what
appeared to be floor wax.
The system engineer indicated that the fasteners
(including washers) had been evaluated by engineering (EWR 89-198) and were
considered to be acceptable.
A number of valves/components appeared to be leaking and no deficiency tags
were found.
Examples:
valves 1-SI-RV-1845B (WR 542552 issued and probably
will be scheduled to work next outage), 1-SI-193 (per system Engineer, minor
leak identified on 1/13/89, no repair required), l-SI-233, and l-SI-150
(existing WR 637554); pressure gauge 1-SI-PI-100; and flow element
l-SI-FE-1940.
This indicates a weakness in the deficiency identification
and tagging program and is discussed further in section 3.d.
Many SI valves and components were bagged or wrapped in poly, but were not
tagged.
It was not clear whether these components had leaks.
Further
discussions with the licensee health physics (HP) personnel revealed that the
bags were a result of the licensee's leak reduction and contamination control
programs.
Some might be to control small leaks~ while others were to prevent
spread of contamination from items such as motor operated valve (MOV) valve
stems.
At the time of the inspection, HP was tracking 688 primary sources of
contamination.
Forty-three new sources were identified in February, 1990 and
only one was repaired in February.
No significant improvement has been made
since June, 1989, when the number was 679.
This indicates a weakness in
taking timely corrective action and is discussed further in section 3.e.
A number of instances of loose flex conduit connectors or broken flex conduit
were identified.
Examples - valve 1-TV-RM-lOOA, valve 2-SI-TV-202B, valve
1-SI-MOV-1869B, valve 1-TV-CC-105C, valve 1-TV-VG-109B and valve
2-SI-S0V-202A1.
.
A few instances of loose spare parts were identified. Examples - 1
11 pipe cap
on valve l-SI-102A, 3
11 pipe tee in contaminated area at pump l~SI-P-lC, 1
11
pipe cap and 2 small nuts in unistrut at pump 2-SI-P-lB and 1
11 pipe cap on
valve 1-SI-MOV-18908..
5
Flow orifice 1-SI-FE-1941 was installed backwards.
This had been identified
. by the licensee and justified as being acceptable until the next outage.
The base and fasteners of a Containment Spray (CS) pipe support (upstream of
valves 1-CS-lOlC and 101D) was excessively rusty.
Many areas were identified where care had not been exercised in protecting
piping and components during painting, resulting in a generally sloppy
appearance and many areas of paint on stainless steel pipe. Examples~ large
contaminated areas in units 1 and 2 auxiliary building basements and contami-
nated areas in the 1-SI-P-lA pump cobicle.
One small diameter pipe clamp (near valve 2-SI~36) was not attached to the
pipe (licensee identified - WR 675422 written, not yet submitted) and another
was missing (near valve 1-SI-MOV~l869B).
A very thick deposit of some unknown substance covered the packing leak-off,
drain piping at valves 1-SI-MOV-1867C and D.
PG (Primary Grade Water) pipe at pump 1-Sl-P-lA was not capped.
Oil ~as standing on the flange of pumps 1-SI-P-lA and 2-SI-P-lA *. Also Pump
2-SI-P-lA had an upper seal leak with heavy boron buildup (identified by
licensee - WR 675427 written but not issued) and excessive grease at lower
motor bearing.
The handwheel for valve 2-SI-425 was laying on the floor (work order 085615
issued to replace valve for other reasons).
Two pressure gauges (
11A
11C
located above valve 2-SI-MOV-2869B were missing glasses.
Areas of insulation were ~issing near valves 2-CC-210A and 2-TV-BD-200B.
Although housekeeping was generally good, poor conditions were noted in
contaminated areas in the charging pump cubicles and the auxiliary building
basements of both units.
Example - 2C Charging Pump platform was very oily,
loose rags, pen, tape, spare parts, and insulation on lube oil piping was
badly deteriorated.
The licensee pointed out that they were aware of the
areas in the auxiliary building and had plans to further decrease the
conta~inated areas and improve housekeeping.
As a result of the above inspections, the following new WRs were issued:
641171, 641175, 641174, 641173, 641179, 641178, 641170, and 641167.
During
the inspection, the team found that a number of work requests had been written,
but not submitted, by the SI System Engineer during the late 1989 system
walkdown. This and the above noted deficiency tagging problems are discussed
further in paragraph 3.d.
6
Review of completed Work Orders revealed that in general, instructions for
performing work lack detail and are not always followed ( examples - WO 083101
limit switch replaced, WO did not specify to replace; MOVATS testing performed
on many MDV WOs without WO specifying to run test). In addition the
11Descrip-
tion of Work Performed" block is often sketchy and lacks detail.
In some cases
this block contains instructions by the foreman rather than description of the
work performed. These Work Order weaknesses appear to be a partial result of
the Work Order procedure, which lacks details relative to responsibilities
and a block-by-block description of Work Order generation and performance.
Weaknesses in completed Work Orders are discussed further in paragraph Nos 3.g
and 3.s.
-~
Weaknesses were identified in the Post Maintenance Test program and are
discussed in section 3.h
..
In general, QA/QC was adequately integrated into the maintenance process.
The two most recent audits, S89-25 and S89-06 were reviewed; although rather
limited in scope, the audits identified good findings. It was noted that while
the program requires only biennial audits in the maintenance area the time
between audits appears to be offset by the work of the QA performance group
(who are presently performing monthly evaluations of maintenance), and the
surveillances being performed by QC.
QA Performance Evaluation Reports
90-01-01.00 and 90-02-03.00 were reviewed. It appears these evaluations are
well planned and executed and are producing excellent *results.
The team noted a problem with timeliness of corrective action relative to
QA audit finding S87-22-03.
This is discussed further in section 3.e.
In general,the predictive maintenance program, consisting of "state of the artll
vibrational and oil analysis, was considered a strength in the licensee's
program.
However, the following weaknesses were identified in the current
program. 1) The predictive maintenance procedure, section 5.1 of the Mainte-
nance Policies and Procedures Manual, is outdated and does not reflect the
current site practice of integrating the ASME Section XI vibration testing of
Section XI pumps into the predictive analysis program.
In addition, the
procedure does not cover the equipment that is currently being used.
2)
Although the program does not yet include Thermography, the licensee plans to
add Thermography to the program.
In addition, a draft of a new program,
procedure MDAP-0009, has been written and is being reviewed.
The new program
should further improve the program and correct the weaknesses identified above.
Based on interviews with maintenance personnel and observation of *work, techni-
cians, mechanics, and foreman appeared to be well qualified and performed their
tasks in a professional manner.
There appeared to be a good philosophy of
working and adhering to work documents and procedures. During plant tours and
observations of work, the team noted an attitude of following all requirements
such as safety and HP requirements.
The program for vendor manual control was well documented and a spot check of
vendor manuals showed good control.
7
In general, the system engineering organization appeared to be well qualified,
intimately involved in the maintenance process, and familiar with their systems
- a definite strength for the maintenance program.
2.b AUXILIARY FEEDWATER (AFW) SYSTEM
Background
The AFW is designed to provide feedwater to the steam generators when main
feedwater is not available.
The AFW system consists of two electric motor-driven and one turbine-driven
pumps, per unit, taking suction from a condensate storage tank.
The AFW system
is provided with complete sensor and control instrumentation to enable the
system to automat,cally respond to a loss of steam generator inventory.
Inspection
To evaluate maintenance of the AFW system in Units 1 and 2, the team conducted
walkdown inspections, examined selected documents, witnessed three periodic
tests performed on the Terry turbines in Units 1 & 2, and conducted interviews
with cognizant licensee personnel.* The walkdown inspections focussed on
general equipment condition, housekeeping, and proper identification of the
equipment.
Documents which were reviewed included PM procedures and vendor
manuals for equipment in the AFW system, completed periodic tests (PTs), Work
Orders (WOs) and licensee*s evaluation of NRC Information Notice (IN) 88-67.
Findings
The housekeeping in the general area was good.
Maintenance and periodic tests
were routinely performed on the equipment. The team identified a problem
related to verifying the operability of the Terry turbine automatic overspeed
trip mechanism. This matter is discussed further in paragraph 31.
The inspection team determined that three industry/NRG initiatives related to
MOVs, check valves larger than 2
11
, and check valves in air systems affected
the AFW System.
There are two MOVs in the FWS of each unit. During the review of the adequacy
of the MOVs, the calculated values of the maximum target thrust was determined
to be less than the minimum values for the motor operators for all four valves.
Adequate justification was provided for continued operation.
The valve
operators are scheduled to be replaced wi-th Limitorque type motor operators
with larger target thrust values during the next refueling outage for each
unit *
- ,
8
A check valve is installed in each of the three inlet *pipes supplying steam to
the Terry turbine auxiliary feedwater pump through a common header. These check
valves have not been previously included in the IST program; these valves can
only be inspected on disassembly and cannot be tested. The licensee's current
check valve program requires the disassembly and inspection at least one check
valve per unit, per refueling outage.
Also, each unit has check valves installed in the instrument air system to
supply air to the ASCO type SOVs to open the Terry turbine steam inlet valves.
Depending on their location, the check valves either protect the integrity of
the Instrument Air System or the Nitrogen backup system. These check valves
are scheduled to be leak tested during the next refueling outage.
The team
observed a pressure gage on the Nitrogen backup air cylinder to indicate that
the Nitrogen pressure was less than instrument air pressure as is required to
prevent the Nitrogen from entering the instrument air system.
However, there
was no requirement to calibrate this pressure gage to ensure an accurate
Nitrogen pressure indication.
2.c
COMPRESSED AIR (CA) SYSTEM
Background
The compressed air system (CAS) is divided into three subsystems: the
instrument air (IA), the service air (SA), and containment instrument air
systems.
The IA and containment IA systems are designed to provide reliable,
dry, oil-free air for pneumatic controls and valves outside and inside
containment, respectively. Major components in the CAS include rotary screw,
positive displacement, and liquid seal ring compressors, air driers, backup
accumulators, and check valves required to maintain integrity of backup
All piping in the CAS is stainless steel and/or copper.
Inspection
Most major components and many end-use devices outside containment were
included in* the walkdown inspection of the CAS.
In general, material condition
was adequate, with some exceptions. The licensee's response to
NRC Generic
Letter (GL) 88-14 "Instrument Air System Supply System Problems Affecting
Safety-Related Equipment"
was also reviewed.
Pursuant to this review, the
team examined records of licensee air quality checks and selected corrective
maintenance records to determine the extent of maintenance work performed as
a result of air quality.
Findings
Overall, IA quality outside containment was very good; the licensee has
recently replaced inefficient refrigeration air driers with twin-tower
dessicant units. Hydrocirbon and dewpoint measurements were well within
specification; however, particulates were typically 5 microns, and the
licensee is aiming for 3 microns, per Instrument Society of America (ISA)
specification ISA-S7 .3. The team found, however, that spare discharge filters
- , * '
'*
9
and dessicant for the new air dryers were not stocked in the warehouse at the
time of the in~pection, but have been ordered. Other spare parts, such as
regulators, fittings, and valves were properly stored, and retrievable.
The team found numerous examples of end~use devices, many of which vibrate
during normal operation, connected to IA root valves by lengths of small-
diameter copper tubing. This was considered significant by the team and is
discussed further in section 3.c.
In contrast with the IA quality outside containment, containment IA quality was
poor and is discussed further in Section 3.c.
The team found that the licensee has not tested the check valves which ensure
availability of backup accumulators required for safe shutdown and accident
mitigation. These check valves were recently added to the licensee's inservice
test (IST) program and will be tested at the next refueling outage. This issue
is also discussed in paragraph 3.c.
2.d 480 AND 4160 VOLT AC DISTRIBUTION SYSTEMS
Background .
The pufpose of the 4160 VAC distribution system is to provide station and
emergency (safety-related only) power to large motors (300 horse power (hp)
or greater) and to the 480 VAC distribution system using 4160/480 V trans-
formers.
This power is provided to non-safety related (NSR) power generation
loads and to safety-related (SR) equipment.
The emergency power is provided
by three 4160 VAC SR diesel generators.
The 480 VAC distribution systems provides power to SR and NSR loads such as
battery chargers, motors less than 300 hp, motor control centers (MCCs) and to
the 240 V and 120 VAC distribution systems using 480/240 V and 480/120 V
transformers.
Inspection
The walkdown inspections were performed for both the power generation and
safety-related 480 V and 4160 V AC distribution systems in both Units 1
and 2.
The majority of the power generation panels, MCCs, and switchgear was
inspected; all the cubicles in the safety-related 480 VAC MCC were inspected;
and the majority of the 4160 VAC safety-related switchgear panels were
examined, including all the emergency diesel generator electrical panels.
- ..
10
The team observed portions of the various types of preventive maintenance (PM)
and corrective maintenance (CM) electrical work activities described below:
Comeonent ID
Work Activit~
02-CW-PMP-2A
Assembly of rebuilt motor
02-CP-PM0-15C
Motor bearing replacement & test
01-CR-CRN-8
Inspection & test of trolley
hoist
01-AS-PMD-lA
Pump motor leads reconnect
Ol-EE-P-100
Calibration of level switch
Ol-EE-P-101
Calibration of level switch
.Ql-81-RCDR-SDE
Troubleshooting recorder inputs
02-W-PM0-18
Inspection, lubrication, and
service of pump motor
Ol-HS-PM0-3B
Inspection, lubrication, and
service of pump motor
01-BB-REL-PRRXB
Replacement of relay
02-EPL-BKR-181
Troubleshoot and return breaker
to service
The team examined, in detail, 36 completed work orders, and in addition,
reviewed post maintenance testi~g on a~other 23 work orders for switchgear
sent to an outside vendor for refurbishment.
The team reviewed 32 electrical CM and PM procedures.
Eleven procedures were
for the emergency diesel generators. Eleven (9 PMs & 2 CMs) were for MCCs,
circuit breakers, and switchgear. Three of these procedures were proposed,
bu.t not approved.
The other procedures were for various types of CM and PM
tasks for motors, time relays, batteries, battery chargers, cable
terminations, and electrical .calibrations.
findings
The walkdown inspections, observations, discussions with licensee personnel,
and document (work orders and procedures) reviews revealed the following:
In general, the material condition and housekeeping for the SR 480V and 4160V
and the NSR 4160V AC MCCs and switchgear panels were in good condition with
the following exceptions:
0
0
Iri the majority of the SR 4160 V panels, spare wires were not properly
identified and capped (taped back).
In several instances the tape was
loose or there was exposed bare copper. In four panels, Unit 1 - 15Jl0
and 15Jll and Unit 2 - 25J3 and 25Jll, the wrong type of tape was used.
This orange and purple plastic tape was extremely loose.
The licensee
took corrective action to fix these problems.
In the NSR 480 V MCCs, the cubicles were dirty. In NSR MCCs 2C2-l-53 and
lGl-1-lC numerous lifted leads were not identified or capped.
0
11
In the circulating water {CW) building, both batteries had loose power
connections at the positive and negative terminals. These batteries
provide the 125 VDC control power for the CW 4160 VAC pump motors switch-
gear.
The licensee had identified these conditions but did not take
corrective action until the team questioned the safety of the loose
terminals.
After the completion of the 480 VAC walkdown inspection, the team reviewed
the PM program for motor starters in the SR 480V MCCs.
The PM requirements
for inspection and testing of MCC thermal overload devices, motor starters .
(contactors) and molded case circuit breakers (MCCBs) specified in procedure
EPL-MCC-E/Rl were deferred (cancelled) for the last two scheduled periods due
to lack of manpower.
Licensee personnel stated the deferrals were approved
by the Site Nuclear Operations Committee.
The licensee also stated that
EPL-MCC-E/Rl will be replaced with an upgraded procedure, and the associated
components will be placed in the PM program and the required PMS will not be
deferred due to lack of manpower.
During the review of VPAP-0806, Power
Circuit Breaker and Switchgear Program, the team determined that MCCBs were not
included.
The licensee stated that MCCBs will be included for the next outage.
SR MCCBs will be tested on a five year basis and NSR MCCBs on a ten year
schedule.
With the inclusion of the molded case circuit breakers, the team
considered the new Power Circuit Breaker Program would be very good *
During the observation of work activities, the team found the electrical main-
. tenance personnel were knowledgeable and performed their work in a satisfactory
manner.
The foreman verified that electricians are task qualified to perform
the assigned work.
However, the team observed the foreman and electricians
spend considerable time performing planning duties instead of working in the
field. This subject is further discussed as a issue in Sections 3.g and 3.r.
From the review of the electrical maintenance procedures, the team identified
several weaknesses.
The licensee agreed to upgrade the procedures to specify
specific tolerances, test equipment, and disallow marking "N/A" (not required)
in the functional testing procedural step when operators are not available.
In addition, the licensee agreed to include the vendors recommendations for
motor starters (contactors) in PM procedures.
The team found the electrical
maintenance procedures, for safety-related equipment, had sufficient QC hold
points which is considered a strength.
During the review of completed work orders, the team identified the following
problems:
Work instructions are not adequately detailed
PMT is not specified (See Section 3.h)
Functional testing is not adequately specified
The craft do not specify in adequate detail the work performed and
problems identified in their "Work Performed
11 write up
Craft foremen are required to provide additional planning since the work
orders are very brief
..
12
Summary of Electrical Maintenance
Strengths
Personnel are knowledgeable of work and perform their duties in a
satisfactory manner.
Work is task oriented requiring craft to be qualified for each task.
Personnel use initiative to perform work and functional testing even
when not specifically specified in work order [This refers to PMT for
switchgear sent to outside vendor for refurbishment]
Personnel have a good attitude in the performance of their duties and try
to do things correctly
Weaknesses
- Craft and foremen spend too much time in shop
- Foremen have added burden of doing supplemental planning
Electrical maintenance procedures need to be upgraded
The size of the staff is marginal considering additional temporary duty
assignments and training
- The work backlog is excessive and not being reduced
I
PM have been cancelled due to lack of manpower
- Note:
These items are weaknesses for performing electrical maintenance,
but not necessarily the fault of the Maintenance Department.
The small
planning staff and poor coordination with operations together with
lack of adherence to the schedule work plan contribute significantly to
less effective electrical maintenance *
The team inspected the training program and facilities and found it to be
quite satisfactory with one exception.* The licensee has not completed
obtaining and installing all the necessary laboratory equipment to support
classroom training as planned.
Observations
The team observed the close working relationship of the Maintenance Department
with the various system engineers.
The team also had discussions with
operations personnel who considered the system engineers as an asset to the
plant.
The team also observed that the station engineering management has a
policy of walking down a different system with each system engineer on a
weekly basis.
The team considered this type of management involvement and the
system engineer as a strength.
I .
'.
..
13
2.e. 120 VOLT AC BUS AND 125 VOLT DC SYSTEMS
Background
The function of the 120 volt AC and DC systems are to provide reliable, unin-
terruptable vital power to instrumentation and control systems and components
during 911 modes of plant operation.
Each system includes two independent
trains of distribution panels and associated cabling while two independent
station batteries for each Unit provided emergency power to the vital AC busses
through a combination of uninterruptable power supply/battery charger static
devices on loss of normal AC distribution.
Inspection
The walkdown inspection included the majority of the Unit 1 distribution
system and panels and the station batteries were also inspected.
The team observed the following maintenance activities related to the AC and
DC distribution systems, and observed selected work activities of the I&C
technicians.
1-PT-28.8
Cal-630
1-PT-8.1
2-PT-8.5
Search for grounds on 18 DC Bus
C6rrect indication on Emergency Boration Line
Power Range Nuclear Inst. Calibration
Rescaling of Power Range Drawer
Reactor Protection System Logic (Periodic Test)
Consequence Limiting Safeguards Logic (Hi-Hi
Train, Periodic Test)
The team also reviewed numerous work orders for accuracy and completeness as
detailed below.
Findings
System walkdowns:
Each of the station
1s four vital batteries had been recently replaced. Cells
that were in acceptable material condition from the replaced vital batteries
were utilized to make up a new
11black battery
11 for each unit.* Critical loads,
such as the main turbine generator shutdown lube oil system, were removed from
the
11station
11 battery load, and transferred to the black battery load list.
Installation of this modification was perceived as a licensee strength in that
the modification significantly improved the station battery performance due to
load reduction. Deficient conditions were noted as follows:
o
Design Change Package 8532 (U-1) was not installed in accordance with
specifications. Problems such as ungrounded cable conduit, loose
intercell connector bolts, and loose bolts in the cell platform were
noted.
These conditions indicated a weakness in the control of electrical
work practices and is discussed further in Section 3.o.
' '.
'.
14
o
Cell 52, Vital Battery 2A, was noted to have a low electrolyte level
(the top of the meniscus was below the low level line, but above the
cell plates).
o
Cell 51, Vital Battery 28, was noted to have a thermometer left sitting
in cell. The thermometer was held captive in a rubber stopper, but-the
rubber stopper was simply resting in a cell lid cavity, i.e., cell over-
pressure (from gas) would not have been directed through the cell flame
arrester.
o
Cells 4 and 56, Unit 2 black battery, had significant verdigris growth on
the terminals and intercell connectors. Cells 5 and 11 had significant
chemical deposition on the flame arresters.
During the walkdown of the 125 volt DC (vital) and 120 volt AC (vital)
distribution systems, several items of concern to the team were noted.
In general the material condition and housekeeping of low voltage distribution
panels were marginally adequate.
Poor conditions and practices noted during
the walkdown are detailed below.
0
Most distribution panels contained schedules of breaker assignments that
were in error due to informal changes, such as hand-written corrections,
strike-overs, and white-outs.
When components listed on the schedules
.were compared to the applicable drawing (e.g., D.C. distribution panel 1-2
against Loading Table Bus Distribution Panels DC 1-1 and DC 1-2, dwg
- 11448-FE-llAE), it was noted that several errors existed.
o
Not all wires were labeled and/or labeled correctly (e.g., Vital Bus
1-IIIA, breaker #6 feeder cable was labeled 1VBS15-B; the wiring diagram
and loading table.drawing called for the cable to be labeled 1VBS15.
Vital Bus 1-IA, breaker #3 cable feed to Process Rack 3, was not labeled
as cable 1VSB44).
Spares were frequently not labeled and/or not properly
terminated (125 volt DC Panel 1-2).
Not all breakers were labeled (e.g., breaker #13, DC panel 1- 2).
Not all distribution panels were labeled on the outside to permit
ready identification (e.g., main 125 volt DC distribution panel lB).
Breaker amperage capacity installed in the distribution panels was
frequently different than plan/drawin.g requirements. This was
considered a weakness in the licensee's configuration control program
and is discussed further in Section 3.b.
Vital AC and DC distribution panels, and 480 volt and 4160 volt
breaker test panels (fed from vital DC), were very dirty,. and
contained trash, including loose metallic material. Cable termina-
tions at feeder breakers in the vital panels were occasionally
improper, e.g., not all wires captured under breaker clamp device,
insulation cut back too far, wires splayed in individual feed cables,
e
15
and bend radius too ~harp. Material conditions of panels were
deficient, including e.g., missing knockout plugs, improper hold-down
fasteners, and detached hold-downs for panel wireways. *These*
conditions indicated a weakness in the control of electrical work
practices and is discussed further in Section 3.o.
The system engineer accompanying the craft and inspection team took prompt and
substantive corrective action to correct the discrepancies noted, including
the preparation of work requests, station deviation reports, and drawing
change requests. The effective support to the craft, detailed system
knowledge and expertise, and high motivation of the system engineers was
perceived by the team to be a ncensee strength.
Review of Work Orders revealed the following discrepancies.:
Work Order 78160, dated 13 June 1989, required, Clean & Remove Trash"
from the Safety Related (SR) 125 Volt DC Distribution Cabinet IA (Mark
- 01-EPD-BC-lA-1). * The work actually performed included the disconnecting
and removal of eight ventilation fans from the cabinet. The team was of the
opini~n that the scope of work in the work order should have specifically
. addressed the subject of fan removal with a specific work step authorizing the
removal; a specific step should also have verified the operability of the fans
(PMT) after electrical reconnection.
Work Order 86936, dated 20 October 1989, required, "1. Troubleshoot/Repair"
and "2. Verify Operability" of a ground indication on the SR battery bus (125
Volt DC-Distribution Cabinet 28, Mark #02-EPD-B-2B).
Work actually performed
indicated that, "Found under voltage relay J Box half full of water near
lighting PNL 2Tl.
Need to replace relay and wire lugs. 10/28/89." A further
entry stated, "Replaced relay and lugs. Verified operability and returned to
service. There is still no ground on the DC bus at this time. 10/28/89"
The undervoltage relay replaced was not identified in the work order.
Purchase order or requisition documentation for the relay was not
included with the work order.
Since the relay did not appear to correct the ground, replacement of the
relay was clearly outside the scope of the work order. A work order
revision was not issued to change the.scope of work.
The Mark# for the relay was not listed in the work order, thus no
effective material history was generated as a result of this maintenance
activity.
No indication of what was accomplished to "Verify operability" was
included in the work order, thus the adequacy of the "PMT" was
questionable.
~----
16
No root cause evaluation was indicated as performed to determine why a
relay J Box was half filled with water, or if the fundamental problem
(water source) had been corrected to prevent recurrence of the failure.
Work Order 62675, dated 16 March 1988, required the replacement of motor
bearings on #2 Rod Control MG Set, Mark# 02-EPD-M-MG-2.
The work instructions of the work order were very sketchy, but did
reference the procedure EMP-C-EPL-117 regarding corrective maintenance
on the MG set. This procedure was unused during the work activity for
reasons unknown and not listed in the work order. A superseding procedure
EMP-C-EPCR-08, dtd. 4 Dec. 1986, Rod Drive Synchronous Alternators,
accompanied the work order and was the document used for the work
performed without formal revision of the original work order.
The scope of work in the work order was to
11replace motor bearings". The
actual work accomplished included motor and alternator bearing
replacements, with no revision to the work order.
M&TE used during the repair procedure were not properly listed on the
work order or in the procedure.
Although pre-work vibration analysis accomplished under WO #62597
indicated that the motor to generator coupling "had badly damaged teeth
and coupling grease had turned to powder.", WO# 62675 did riot reflect
that the motor coupling had been replaced_ or repaired. Steps at
paragraph 5.17 of procedure EMP-C-EPCR-08 simply installed the shaft
coupling with no indication of what was actually accomplished.
WO #62597 (vibration analysis) indicated the machine as safety related
(SR), while WO #62675 indicated the machine as non safety related (NSR).
The machine was NSR.
Work Order #66468, dated 16 June 1988, was prepared to
111. Troubleshoot and
Repair" and
112. Verify operability." of a grounded condition on both DC battery
busses when containment DC lighting leads were landed.
The leads had been
lifted and tagged when the condition occurred.
The work order Mark# was listed as Ol-EPD-BKR-14.
The actual grounds
were detected in the 1-ERCl Panel, breakers 6 and 8 feeds.
The Mark#
was not changed.
The scope of work increased significantly after troubleshooting, but no
modifications were made to the work order, i.e.,
8 breakers were replaced in (presumably) the 1-ERCl Panel,
2 light fixtures were replaced in the Blighting loop, 3
fixtures in the C loop, and an unknown number in the A loop,
17
lights in the "RCP cubes" were also repaired,
A work order "Repair or Replacement Follower" specifically required,
"Verify any leads lifted to isolate ground are landed with proper polarity
in accordance with applicable design drawings.
Functionally test circuit
after landing."
No evidence was included with the work package that any
of the lifted leads had been properly landed in accordance with the work
iflstruction.
Work Order #74377, dtd 8 December 1988, required "1. Troubleshoot & Rep~ir."
(and
112. Verify ground is cleared.i
1
) of Ckt. #2 in the DC Distribution Panel 1
- 2, Mark# Ol-EPD-BKR-43, the supply to SI "8
11 accumulator solenoid operated
valves {S0Vs) *. The electricians assigned to perform the task prepared their
own work instructions, including the requirement for tagout, notwithstanding
the inadequate work order received from planning.
The "work instructions"
prepared by the electricians comprehensively.addressed all steps expected by
the team; the instructions also referenced the subsequent Work Request#
submitted after the craft identified the problem SOV.
The work order was stamped, "Determined to be minor maintenance per
SUADM-M-16
11 , thus a "procedure" was not required. Contrary to this work
order stamp, work order preparation instructions specifically listed
maintenance requiring equipment tagouts as not qualifying as "minor
maintenance."
Thus this work order should not have been stamped "minor
maintenance."
The drawings listed by planning for performing the work were "FE-lG,
-lOA, and llAE".
The craft had to use drawing "FE3BK" to perform the
work.
The work instructions prepared by the craft that recorded the work
accomplished were perceived by the team as a job well done.
Work Order #86476, dtd 7 October 198Q, required the electrical craft to,
11 1.
Troubleshoot and repair breaker.", Reactor'Trip Breaker "B" Normal, Mark
- 01-RP-BKR-BNORM.
The problem was reported as the breaker not appearing to be
closed while the I&C craft were performing periodic reactor protection system
tests (PT - 8.1).
"PROCEDURE NOT REQUIRED
11 was conspicuously stamped on the work order,
notwithstanding the work scope authdrizing "troubleshoot" and "repair" of
the breaker.
The work accomplished reflected that the breaker was racked out, manually
closed, continuity checked satisfactory on all three phases (no work
performed), and the breaker was racked in~
PT - 8.1 was continued and
presumably performed without further difficulty.
No further evaluation
or deviation reporting was reflected by the work order *
18
The work was performed on 8 October 1989.
The
11Equipment Returned to
Service
11 date was listed as 6 December 1989, after the plant had returned
to full power.
This equipment should have been
11feturned to service
11
before power operations.
Based upon the above types of examples noted by the team in its review of
closed work orders, the team concluded that work order instructions prepared
during the planning phase of maintenance activities lacked adequate detail.
(Also see section 3.g.)
.. '-,
~,~
Review of maintenance in progress - I&C Group
"--
..
The Instrumentation and Control (I&C) group, re-organized into the Maintenance
Department in late 1989, was responsible for the planning, scheduling, calibra-
tion and maintenance of plant installed, primary and secondary, instrumentation
and controls, and the measuring and test equipment (M&TE) program.
Organiza~
tional and assignment of responsibilities procedures such as SUADM-ADM-47, dtd
18 September 1989, Operation of the Instrument Department, had not been revised
to reflect the re-organization. There was no visible evidence of effective
integration of the I&C group with the Maintenance Department since the group
was fundamentally doing business as before, e.g., work order planning was
performed at the craft level.
Staffing of the I&C group was noted to be a
11 numbers
11 problem, i.e., thirty
five technicians were authorized (no break-down between trainees and
technicians), but only twenty were actually staffed. Of a large group of
about fifteen contractors retained in late 1989, only two remained due to
factors related to the permissible overtime they could work.
Only thirteen
of twenty staff were
11technician
11 grade, the balance were
11trainees
11 in the
apprentice program.
As a consequence, I&C supervision expressed concern that
although they were currently maintaining reasonable control over I&C backlog,
any further increase in maintenance activities could not be adequately
supported by staff on-hand.
I&C Supervisors stated that their attempts at hiring had been halting at best;
resumes received through the personnel department were frequently aged to the
point that calls to prospective hirees found them unavailable. Further, from
point of interview to an offer of employment (while background checks and
clearances were obtained) was also a long enough period to result in the same
answer on calling potential hirees. Staffing was noted to be potential problem
in several areas, e.g., not 100% shift coverage, one person operating entire
calibration program, and ineffective work order planning.
Turnover, to the credit of the licensee, was noted to be a relatively low
number of approximately two per year. Supervision was not advised of the
loss mechanism, although it was understood that termination interviews were
conducted.
The team noted that the I&C group had the lowest level of mainte-
nance backlog of approximately 500 work orders of the three major craft *
' ..
19
The team was concerned about the level of planning performed in preparation of
work orders.
As discussed in Section 3.g., planning for the I&C group was
performed at the craft level.
Work Orders, in general, included work instruc-
tions of the form, Investigate and repair". For example, WO #89582, dated
5 March 1990, was written to "Correct Indication" on the emergency boration
line fl ow i ndi ca tor (Mark #Ol-CH-FT-1110). The job steps stated, "Invest/
Correct Indication", although the actual steps required were:
determining
the installed flow converter was faulty; obtaining and bench calibrating a new
converter; removing installed device (rad area) and installing new calibrated
device; and setting zero and span adjustments in place with a calibration
device.
The craft accomplished the preparation of "work instructions" to
support the work order by revising an existing calibration procedure
1-CAL-311, Boric Acid Bypass Flow (Emergency Borate Flow) F-1-110, dated
3 October 1988.
The revision of the existing procedure was accomplished in
accordance with appropriate procedures. This methodology was noted to be the
normal method of preparing I&C work order instructions on several occasions
during the inspection. It was also noted to be extremely cumbersome because
calibration procedures and periodic test procedures rarely fit the maintenance
activities. This methodology also resulted in work orders that had no overall
coordinated sequence of steps. Interviews with the craft indicated that they
thought they could not extract portions of approved procedures or technical
manuals to prepare supplemental-work instructions.
SUADM-ADM-47, dtd 18
September 1989, Operation of the Instrument Department, supported th.is
perception at paragraph 4.3.8.1 concerning preparation of work orders,
"Identify work procedures that are required.
Pay particular attention and
identify if the procedure will need to be deviated and/or pre-approval is
required." Based upon the above observations, it was the team's opinion that
program and implementation improvement was required in the area of preparation
of I&C supplemental instructions for work orders.
Clearance Program and Implementation Improvements Required:
The team reviewed the clearance log for both units to determine if adequate
clearances were being set to maintain equipment control and provide safety to
the maintenance technicians as well as the equipment itself.
The team noted that the 480 volt feeder breaker for the U-1 w*ater Chi 11 er for
the Air Conditioning Unit (switch gear 1B2-12B) was red tagged.with two red
tags (red tag #1246755 was associated with clearance #62476; red tag #1246062
was associated with clearance 2059274).
The "Remarks" block of the red tag was
annotated "OFF/OFF" on tag #1246755, and "OFF/ON" on tag #1246062.
The team
learned that the two positions referred to the proper tagged position listed
first, and the restoration position listed second.
The listing of these posi-
tions on the tags has been implemented by persons responsible for hanging tags,
but was not required nor described by SUADM-0-13 (dtd 1 Feb. 90), Operations
Department - Operation, Maintenance, and Tagging.
Only the Tagging Record
Form (#888.6A/7A) required the tagged and*restoration positions to be listed
in accordance with SUADM-0-13.
It was the team's opinion that the listing
of two different restoration positions for the same equipment was an implemen-
tation weakness in the clearance methodology.
.
'*
20
The team noted that a large number (91) of station deviation reports (DRs) had
been generated during 1989 related to tagged out components, including:
o
34 DRs for improperly tagged components
o
12 DRs for missing (abused) tags
o
15 DRs involved breakers out of position
o
22 DRs involved valves found out of position
o
9 DRs involved wrong components tagged
The team perceived this as a very large number that potentially affected
personnel safety.
Interviews with Operations personnel indicated that a large
portion of the problems were noted during the termination of outages, where
devices had been mis-positioned for reasons unknown.
The team noted that
paragraph 5.11.3, SUADM-0-13 specifically waived performance of the quarterly
tagout audit (field check of tags) during outages, and that only an Administra-
tive Review of the log was performed prior to startup. Manpower was stated as
one of the limiting factors in not performing field audits during outages,
even though there was a high probability for error during the intensely active
maintenance period. It was the team's opinion, based on the large number of
tagout discrepancies, especially associated with outages, that the field
audits should not be waived to provide reasonable assurance that components.
tagged for long periods of time would be periodically checked in their proper
position.
The team reviewed the tagout log to determine if program requirements were
being adhered to.
Many very old tagouts were in an active status, with no
apparent action currently underway to correct the condition.
(See section
3.m.) Unit #1 tagout #59551 was an Operations tagout on the chilled water (CD)
system. It was noted that tag number 863558 was listed as partially cleared on
a Tagout Partial Clearance form Figure 11; the Tagging Record Block 11 (Tag
Removed) for the tag was not properly signed.
Tag number 801005 was listed as
removed on the Tagging Record, Block 11; the tag was not authorized for
partial clearance on the appropriate Tagout Partial Clearance form.
Procedural Weaknesses Identified During Periodic Testing:
The team observed the performance of Periodic Test 1-PT-8.1 (Rev. 1), Reactor
Protection System Logic (For Normal Operations), on U-1.
The test ensured the
continued proper operability of the reactor trip portion of the reactor
protection system. Several strengths of the I&C technicians were noted during
the testing, including a good pre-job briefing that addressed previous
"lessons learned", good procedural adherence, good command and control of the
evolution by the team leader, and good communications between the three, two
man groups of technicians performing the test *
.
' .
21
Several procedural inadequacies were also noted as follows.
The craft
technicians were confused about the extent of completion of an Engineering
Work Request (EWR) affecting Extraction Steam Motor Operated Valves (MOVs),
and therefore convinced the Shift Supervisor (S/S) to unnecessarily
de-energize the breaker to an Extraction Steam valve (MDV ES-lOOA) as a part
of establishing initial conditions. Although the procedure did not address
the subject, the lead I&C technician, based on his understanding of the EWR,
requested the S/S to de-energize the.MDV to prevent an inadvertent actuation
of the valve during the logic testing.
In fact, the EWR had only been
partially completed on U-2, and then was canceled; the EWR had no
applicability to Unit 1 testing. It was the team's opinion that the procedure
should be unit-specific to the extent that a subject affecting only one unit
should be addressed in each unit procedure.
,
Precautions and Limitations paragraph 4.2 stated, "Bypass breakers will ti~ly
be closed long enough to perform required testing on associated trains.
11
The
team perceived this wording as vague when compared to the requirements of.
Technical Specifications (TS), Table 3.7-1, Action Statement 11. which stated,
" ****. one channel may be bypassed for up to 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> for surveillance testing
per Specification 4.1 ****
11
It was the team's opinion that the TS
requirements should be included in the Precautions and Limitations, and that
clock times should be entered at paragraphs 5.15 and 5.68 (time breaker
closed/opened) to assure specific awareness and compliance with TS
requirements.
The technicians demonstrated such awareness.
During performance of the procedure (at Step 5.83), a relay failure occurred
(promptly detected by the technicians by smell).
No provision had been .
provided in the procedure (or any higher tier procedure) for "backing out
11
of the sequence safely, thus a one-time change was executed to back out and
restore the plant to safe conditions. It was during this failure that the use
of a
11 For Reference Only
11 drawing occurred as discussed below. The fail~re
occurred relatively early in performance of the procedure, thus adequate time
was available to permit the time- consuming procedural change, and not violate
the two-hour requirement addressed above. It was the team's opinion that
instrument test procedures could be enhanced by consideration of the situation
of plant restoration if a system failure occurred, especially for time
sensitive procedures such as this.
A "For Reference Only" drawing (as opposed to a controlled drawing), Drawing
113E244, Reactor Protection System, was used by the technicians and their
supervisor for troubleshooting and procedure revision preparation, and
operational considerations by the Shift Supervisor to establish safe plant
conditions, without assuring the drawing was correct by comparison to a
controlled drawing.
The drawing was a logic wiring diagram for the reactor
protection circuitry. The team perceived the use of.uncontrolled drawings in
this manner as an implementation weakness since plant modifications could have
been made that would not have necessarily been recorded on the uncontrolled
drawing.
The use of the "For Reference Only
11 drawing was in violation of the
.
' .
22
licensee's procedure for use of station drawings, SUAD~-ADM-11, dated 29 Nov.
1989, Station Drawing Revision and Distribution, which stated at paragraph
4.7, "Individuals using drawings or aperture cards shall be responsible for
ensuring that the item used is the latest revision." This failure to follow
procedure is an example of violation 50~280,281/90-07-01.
Revision 1-16-90 to 1-PT-8.1 was a permanent change executed on 7 February
1990 (added a cautionary note to the procedure that had been omitted at the
last procedure update).
The team noted that the included 10 CFR 50.59
Screening Checklist on the Procedure Action Request (Form No. 730682) was not
completed correctly; i.e., the form required the listing of Sections of the
UFSAR that had been reviewed in performing the 50.59 evaluation, but none were
listed. The team perceived this failure to follow procedure as an
implementation weakness in executing procedure changes.
2.f EMERGENCY DIESEL GENERATOR (EDG) SYSTEM
Background
The purpose of the emergency diesel generator (EDG) system is to provide a
dependable source of onsite power capable of automatically starting and
supplying electrical power to loads necessary for safe shut down and
maintenance of safe shutdown conditions under all design basis conditions.
Major equipment and auxiliary systems included in the system walkdown were
three 20 cylinder diesel engines, generators, starting air systems, engine
cooling, fuel system, lubricating oil, and governors.
Inspection
The walkdown inspection included the majority of the above systems.
In
addition, the team witnessed monthly performance tests of an EOG, an engine-
driven compressor in the starting air system, the replacement of a starting
air system compressor, and reviewed closed and open work orders.* The team
also reviewed selected PM procedures for EDG components against vendor manual
requirements for EDG system equipment.
Findings
At the time of the inspection, the team found that the licensee did not have
documentation verifying that the EOG fuel oil transfer lines {approximately two
inches OD) were seismically qualified. These lines are installed between the
day tanks and the EDGs.
In addition, the teamfound one of the in-line flex
hoses replaced with a rigid section of pipe.
The licensee could neither
adequately determine the reason the flex hose was replaced nor provide
..
>
'
,
23
documentation which controlled or recorded the work involved. These flex hoses
serve to isolate the day tanks and associated piping from vibration while
the EOG is running.
During the inspection, the licensee performed a seismic
evaluation of the fuel lines and concluded that the existing configuration
was acceptable. However, the licensee plans to add supports, and replace the
rigid section of pipe with braided hose.
Need for further NRC review of the
calculations involved (SEQ-1517) will be identified as unresolved item
50-280/90-07-02 "EOG Day Tank Fuel Transfer Line Analysis."
Material condition of equipment in the EOG spaces was, in general good, with
exceptions noted below.
Several problems associated with a work order are
also listed below.
The team found a significant air leak at an air fitting on the pressure switch
which controls the motor-driven air compressor of the engine and motor-driven
compressor set in the air start system for EOG 3. A WO was written to correct
the problem.
The team observed work activity on WO 93103 for replacement of an air
compressor (one of six being replaced).* The compressors were being replaced*
because of moisture-induced deterioration of valves, and unavailability of
replacement valves. Since there were no air driers or coalescing filters at
the discharge of the air compressors, the new compressors are subject to the
same damage as those which were replaced. Details of this issue are discussed
in paragraphs 3.c and 3.f
In addition, on WO 93103, the team found that the vendor technical manual for
the compressor specified light oil or anti-seize compound for thread lubricant,
with 20 percent reduction in applied torque if anti-seize is used.
The work
package, however, only specified the threads be
11lubricated". The craft
applied anti-seize to the threads without questioning what type of lubricant
to use, and proceeded to torque the fasteners to the values indicated on the
work order. The specified torque values were based on the use of anti-seize,
however, had the craft used light oil and the torque values furnished with the
work order the fasteners would have been undertorqued.
The team noted that a valve which admits air to two air starting motors on one
of two trains in the air start system was not functioning properly.
The
licensee indicated the root cause was due to poor air quality. This issue is
discussed in paragraph 3.c.*
Local indications and remote sensors for vital EOG system conditions, such as
engine temperature, and starting air system pressure were not calibrated. The
remote sensors provide input which triggers the
11Diesel Trouble
11 control room
The result is a 11 sources of EOG system condition may not be
accurate. This issue is discussed in paragraph 3.1 *
..
24
2.g HEATING VENTILATING AND AIR CONDITIONING (HVAC) SYSTEM
The functions of the HVAC system is to provide for contamination control by
ensuring that air is not recirculated in areas of potential contamination, and
provide adequate seasonal ventilation and/or temperature control in occupied
machinery spaces including the control and relay room area. The system
consists of ductwork, fans, filters, dampers and associated controls.
Inspection
The team performed a walkdown inspection of the subject system in such areas
as the auxiliary building, mechanical equipment rooms -1, -2 and -3, control
room, and emergency switch gear room.
A selected sample of (20) completed work orders and the following Engineering
Work Requests (EWRs) were reviewed ..
Title 89-540
90-078 89-687
87-170 89-336
Evaluate VS Pressure Switch Calibration, Units 1 and 2
Evaluate VS MGR.Chiller Existing Capabilities (E4A, B, C)
Surry 1 and 2
Evaluate VS Fan Duct (l-VS-F-2, 12A and -128)
Repair of Containment Recirculation Fan (2-VS-F-lA)
Evaluate VS Repairs for Startup, Units 1 and 2
The team observed maintenance work in progress on three nonsafety-related
chillers listed below:
Component
01-CD-REF-lA
02-CD-REF-1
01-CD-REF-18
Findings
089693
089691
Activity Description
Weld Repair Tube Sheet and Gasket
Seating Surface and Recoax
Overhaul Compressor and Rod-Out Tubes
Overhaul Compreisor and Rod-Out Tubes
The above inspections, observationsl interviews and record/document reviews
revealed the following:
Rather than focussing on permanent repairs on the HVAC system, the licensee is
performing temporary fixes which include making extensive use of Foster's Duct
Sealant and red duct tape to plug holes and leaks in the ductwork throughout
the system.
The team observed an unusually large number of work request
tags on the vast majority of rotating components i.e., fan motors, sheaves,
dampers, actuators, metering devices, fan belts, etc. By-and-large, the
reason for these tags was for components requiring corrective maintenance or
replacement *
.
- ,
' .
>
25
Under the current licensee program, work requests are evaluated, and based
on their merit they are either rejected or accepted. If accepted, they are
assigned a work order number and a priority number.
According to figures
provided by the licensee there are pres~ntly approximately 220 outstanding job
orders for the VS waiting disposition.
In addition, there are 15 others, also
outstanding, waiting on parts non-traceable to equipment manufacturers.
All of the above work orders have been assigned a priority ranging from number
1 through 3 as required by SUADM-M-11, Attachment 2.
By this procedure, any
work order given a priority range of 1 through 3 must have the work begin from
48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> up to a maximum of 4 weeks, for priority 3.
Because of the this observation, the team has determined that this procedural
requirement is not being enforced since the scheduled start date on all of the
above and many other WRs has passed without work initiation. This failure to
comply by established procedural requirements is considered a programmatic
. weakness.
This matter is discussed further in Section 3.m.
2.h
MISCELLANEOUS MAINTENANCE ACTIVITIES
Inspection
The team observed the below indicated maintenance work activities related to
other systems:
Maintenance Work
Work Document ID
Description of Activity Observed
Alignment of Condensate Polishing (CP) Pump
EWR 86448
02-CP-P-15C
Alignment of CP Pump 02-CP-P-430
JN 087715
Preventative Maintenance
WO - Work Order
EWR - Engineering Work Request
JN - Job Number
Findings
The above inspection/observations revealed the following:
During observation of pump 02-0P-P-430 alignment using WO 93028, the team
noted that the only instruction on the WO was "Align Pump" with no reference
to any procedure, vendor manual, or other document.
Maintenance personnel
stated that this was in the "skill of the craft" and no procedures were *
needed.
Further review revealed that a detailed procedure was available for
pump alignment using the dial indicator method.
The procedure had numerous
sign-off steps, acceptance criteria, and the job had been started using the
procedure.
However, after the job started, the decision was made by the craft
to use the optical alignment method.
Since no procedure was available for
this equipment, the vendor manual for the equipment was used.
When q~estioned
.
'*
>
26 *
by the. inspector, the foreman stated that based on training, they knew what
the acceptance criteria were and therefore did not need a procedure.* The team
questioned the Mechanical Maintenance planner and supervisor responsible for
the WO and the response was that the WO probably should have referenced the
vendor manual for the alignment.
However, they further indicated that they
were busy trying to keep up with the more important jobs and did not have
adequate resources to do detailed planning of non-safety-related jobs and had
to depend on the "skill of the craft." This is an example of weaknesses in
planning and adequate resources discussed further in sections 3.f. and 3.g.
In general, maintenance mechanics, technicians, foremen and supervision
appeared to be well qualified, knowledgeable, and work was performed in a
professional manner.
In review of activities related to erosion/corrosion heater drain pipe
failure, the team found that the licensee has a well defined program for
inspection 'of pipe for erosion/corrosion thinning. The program is defined in
Engineering Standard SDT-GN-0033 which was in response to NRC Generic Letter 89-08 and was implemented January 1, 1990.
Prior to that date, procedure
SUADM-M-33 defined the program.
The pipe section that failed (at the
- discharge from flow control throttling valve LCV-122B) was not in the program,
however, the elbow next to the pipe section was in the program.
There had
been no reason to suspect the pipe section prior to the failure. Although the
similar pipe section in Unit 2 had been replaced with CR-MO steel, the
replacement was a convenience replacement while replacing the elbow and not
because of excessive thinning.
The licensee
1s actions and planned actions
after the pipe failure appeared to be conservative and aggressive. Similar
piping at the discharge throttling valves for the other Unit 1 train and both
trains on Unit 1 were inspected for thinning.
The other Unit 1 train had
significant thinning and required pipe replacement.
Piping in both Unit 2
trains was acceptable.
The licensee was compiling a list of all throttling
valve configurations in the systems covered by the program.
This list was to
be examined for other similar piping that should be inspected.
The team also reviewed several completed work orders (WOs) related to work
performed on Motor Operated Valves (MOVs), replacement of electric solenoid
operated valves (SOVs) to extend the longevity of the qualified lives, and
replacement of components in NAMCO type limit switches, also to extend the
longevity of the qualified lives. Problems related to incomplete summary
descriptions on the cover sheet, partially complete information on the
model/serial numbers, and using the wrong illustration were identified. These
findings are discussed further in paragraph 3s.
The team noted an example of failure to follow procedures associated with
initallation of radiation monitor RM-SW-107 which involved failure to complete
sign-off steps in sequence; i.e., precondition step 2.4 was not signed off
even though work had proceeded to installation step 4.18. This constituted a
nonconformance to upper tier procedure STD-GN-0001 which mandates that sign-off
steps be completed in sequence barring specific notes to the contrary. The
licensee initiated DR Sl-90-321 to begin corrective action.
.
- .
,.,
"
27
2.i
HEALTH PHYSICS
The team determined that the HP group was included in the planning and
scheduling of maintenance activities through representation at all daily
planning and briefing meetings. Interviews with maintenance and HP personnel
indicated that good lines of communication existed between the groups.
In addition to the licensee's general employee training for radiological
protection, the licensee had provided most maintenance workers advanced
radiation worker training. The training*provides maintenance workers with
additional instruction and practice in radiological survey and work practices.
The graduates are allowed to perform limited radiological monitoring functions
at their work sites as directed by health physics personnel. The majority of
maintenance workers interviewed believed that the training had helped thew
understand how radiological protection activities could be integrated into the
maintenance activities. The advanced radiation worker training had been
provided to about 60 percent of the maintenance staff and the licensee planned
to provide the training to all maintenance personnel.
Maintenance workers reported that the licensee's on-going decontamination
program was very beneficial to the maintenance process. Workers reported that
ready access to non-contaminated areas, that were contaminated in previous
years, had improved maintenance efficiency. Workers reported that there was
more effort by maintenance personnel to keep systems .and components from
leaking contaminated fluids and that housekeeping during and following
maintenance activities was an important element of their job. The licensee's
area of contaminated floor spaces has steadily declined in recent years *. The
licensee's floor.area contaminated in 1989 declined from 20,500 square feet
(ft2) in January to 14,500 ft2 in December. The licensee's goal for 1990 was
to reduce the area contaminated to 11,500 by December, 1990.
The,licensee's collective personnel exposures were 792 and 420 person~rem
per unit in 1988 and 1989. The licerisee's collective personnel exposure goal
for 1990 was 303 person-rem per unit. In interviews with maintenance workers
the team determined that worker awareness of ALARA goals and objectives were
high. The interviewed maintenance workers could adequately describe methods
for keeping collective radiation exposures ALARA and knew their lifetime,
quarterly, and annual radiological exposures. Workers reported that ALARA
activities were strongly supported by management. The licensee strengthened
its ALARA program during 1989 providing additional resources and management
attention to implement various source term reductions and ALARA program
initiatives. To increase facility staff involv~ment in the ALARA program,
various departments, including maintenance, were required to develop and.
implement department action plans to minimize personnel dose. Worker awareness
of the ALARA program was a program strength *
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28
3.
ISSUES
3.a. SUITABILITY ANALYSIS FOR REPLACEMENTS
American Society For Mechanical Engineers Boiler and Pressure Vessel (ASME
B&PV) Code Section XI, Paragraph IWA 7220 requires the Owner to conduct an
evaluation of the suitability of replacements, prior to authorizing the
installation of those replacements. This requirement is implemented, by the
licensee in Procedure SUADM-M-08, dated February 27,1990,
11ASME Section XI
Repairs and Replacement Programs"
The lic~nsee informed the team that
SUADM-M-08 is applicable to pressure retaining components and their supports
only (items covered by ASME B & PV Code Subsections IWB, IWC, IWD, and IWF).
The licensee's program does not address the IWA 7220 suitability analysis
requirements for non pressure retaining replacement parts, such as bearings,
bushings, springs, stems, disks and shafts (items covered by ASME B & PV Code
Subsections IWP and IWV).
The lic~nsee was unable to provide a single example
where there was objective quality evidence attesting to the fact that a
responsible individual had made a conscious decision that replacements
11 in
kind", of non pressure retaining parts for Section XI components, were
suitable for the intended service.
The team concluded that a weakness exists in the licensee's program related
Code Paragraph IWA 7220 for non pressure retaining components and for the
documentation of suitability analysis for all first time replacements "in
kind.
11
3.b. DOCUMENT CONTROL/CONFIGURATION MANAGEMENT _SYSTEM FOR MAINTENANCE
Drawing Revisions Not Issued Following Plant Modifications
During walkdowns of the 120 volt AC and DC vital and semi-vital distribution
system, the team noted several occasions where breaker amperage capacity listed
on drawings differed from the installed breakers as follows.
o
Drawings 11448-FE-llAE (Rev. 3), Loading Table Bus Dist. Panels DC 1-1 &
DC 1-2, and 11448-FE-lBJ, Wiring Details, Misc CKTS, Sheet 2, reflected
all breakers as being 15 ampere capacity. The installed breakers were 20 *
_ amp.
o
Drawing 11448-FE-llAA (Rev. 7), Loading Table, Vital Bus Distribution,
Panels 1-1, 1-III, reflected feeder breakers 16 and 19 to be 15 amp and 30
amp respectively. The actual breaker sizes installed were 20 and 15 amp
respectively.
o
Drawing 11448-FE-llAC (Rev. 6), Loading Table Semi-Vital Bus Distribution
Panel lSVBl, reflected breakers 32 and 33 as 20 amp and 30 amp respec-
tively. The installed breakers were 50 amp and 20 amp respectively.
..
29
Based on the large number of the above types of errors noted during the
walkdowns, the licensee initiated a check of all 120 volt AC and DC vital and
semi-vital panel breaker installations against all affected drawings, and
noted numerous errors (randomly dispersed within 16 additional drawings) of
similar nature i.e. labeling and fuse sizes in other panels and their drawings.
During the time of the inspection, it could not be determined why the errors
occurred.
The majority of incorrect drawings were considered to have occurred
following plant modifications; e.g., occurred as a result of performing a work
order to correct a tripping breaker.
In any case, drawings were not properly
updated in accordance with plant procedure (as it now exists) SUADM-ADM-11,
dtd. 29 November 1989, Station Drawing Revision and Distribution, which
required drawing revisions be issued when plant modifications were made or
when as- built conditions different than drawings were discovered. The
licensee verified that the proper sized breakers and cables were installed in
accordance with modification requirements. A total of eleven drawings required
~
correction. The licensee advised the inspection team that a program existed
for drawing changes upon completion of field design changes; based on the
examples noted by the team, it was concluded that the program for control of
drawing changes had not been effectively implemented.
This failure to follow
procedure is an example of violation 50-280,281/90-07-0l.
Vendor Supplied Information Not Incorporated in Plant Documents in Accordance
with Procedure
The team was concerned that vendor supplied information that necessitated
changes to plant procedures and documents was not being properly processed and
incorporated into station requirements.
The team reviewed a specific example
of vendor supplied information to determine if the licensee's process for
handling of vendor information was being properly incorporated.
Limitorque Corporation published Maintenance Update 89 - 1 in December 1989.
This important bulletin addressed several maintenance topics applicable to
Limitorque actuators, such as:
0
0
0
actuator pinion gear fit-up, orientation, and location
gear to shaft key material, fit-up, and retention (staking)
set screw spot drilling and retention (lockwiring/staking).
Although this bulletin had been received by both corporate and site personnel
responsible for the Motor Operated Valve (MDV) maintenance program, the team
noted that:
o
MOV maintenance procedures had not been updated to reflect the
requirements of the bulletin,
o
the TSC library, controlled document Vendor File and Vendor Manual
did not contain the bulletin or any reference to its contents, and
o
the licensee's Commitment Tracking System (CTS) did not contain
reference to the contents of the bulletin .
30
The team was able to.determine that a memorandum had been prepared by the
station MDV Coordinator that called the attention of Maintenance Engineering
to the contents of the bulletin, but no further action had been taken.
The
team determined that neither corporate nor site personnel directly associated
with the MOV program were aware of their responsibilities for processing
vendor supplied information such as the Limitorque Bulletin.
Station requirements for processing vendor supplied information were found in
SUADM-ADM-31, Vendor Interface/ Control of Vendor Documents, dated 5 Dec.
1985, at paragraph 8.0, Vendor Supplied Information, which stated,
8.1.1
11All technical correspondence from any vendor *.* shall be reviewed
by the appropriate department.
Each Department Head is responsible for
insuring that any of this correspondence received in his department is
forwarded promptly to the Supervisor Records Management.
8.1.2 If it is determined that corrective actions are necessary the item
shall be placed on the Commitment Tracking System.
8.1.3 If the completed item causes a change to the Vendor Manual or to the
Vendor File, the attached form
11Vendor
1s Manual/File Revision
11 (Attachment 3)
shall be completed by the Licensing Coordinator and forwarded to the TSC
Library for a controlled distribution and filing .***
11
The team noted that
Attachment 3 was the checklist that would cause, among other items, required
revisions to station procedures to be implemented.
Based upon the above example, the team concluded that the program for control
and incorporation of vendor supplied information was not being effectively
implemented in accordance with required station procedures. This failure to
follow procedure is an example of violation 50-280,281/90-07-0l and is
discussed further in section 3.k.
3.c. AIR SYSTEMS
The team found numerous examples of end-use devices which vibrate during
normal operation and are connected to stationary IA root valves by lengths of
small-diameter copper tubing. This was considered significant in light of
much industry experience with trips and transients due to vibration-induced
air line failures, including a trip at Surry
1s sister plant, North Anna
(February, 1989) in which an IA line on a feedwater regulating valve failed
due to vibration; a steam generator tube plug failure and tube rupture were
associated with this large transient.
Compressed air is supplied to containment by four (two per unit) rotary water
seal ring compressors which take a suction on the containment (typically
99 percent relative humidity at 118 degrees F.) then discharge into refrigera-
tion air driers. These air driers are not capable of attaining dew points of
less than 35 degrees, even under optimum conditions. The licensee
1s response
of February, 1989, to NRC GL-88-14 committed to conformance with ISA S7.3 which
states, in part, that at no time shall IA dewpoint exceed 35 degrees.
31
An annual PM procedure, IA-C-M/A2, written in 1985, covers the containment IA
air compressors and discharge air filters, inside the refrigeration air
driers at the discharge of the air compressors.
The team found that the most
recent performance of this PM procedure for the refrigeration air driers was
in mid-1989, by a contract maintenance firm.
At that time, the contractor
indicated that two of the discharge filters were so rotted and corroded they
could not be left in place; discharge air from these air driers to containment
IA loads was not being filtered at the time of the inspection. The remaining
two filters were dirty, however, they were left in place because spare filters
were not on hand.
This was still the case at the time of the inspection, per
cognizant licensee personnel. Further, the team found that the only time
prior to 1989, this procedure was ever performed was January, 1987 during
which time, th~ steps for inspection of the discharg~ filters was checked off
as "Not Applicable". There are no other records, per the licensee, that these
filters were ever changed since installation of the air driers, or about 7
years.
In addition, the team reviewed station deviation reports (DRs)
relating to water found in end-use devices and high dewpoints in the
containment IA system.
These DRs document ~ater squirting from solenoid
operated valves, flow gauges full of water, and dewpoint readings greater than
60 degrees F, among other things.
Interviews with statinn personnel also
indicated that air regulators at end-use devices were typically full of water
when blown down during outage PM work.
The lack of attention and timely
commitment of resources by management towards needed upgrades in the contain-
ment IA system, despite documentation of numerous problems, as well as the
general material condition of the containment IA system was considered a
weakness in the licensee's maintenance program.
The team found that check valves which ensure operability of backup accumula-
tors for air-operated valves required for safe-shutdown were not in the
licensee's inservice test (1ST) program.
These check valves were added to
the program late in 1989, and are scheduled for testing, however, the failure
to recognize the requirement for inclusion of these valves _in the IST program
was considered a weakness by the team.
In the EDG air start system, the licensee experienced chronic problems with
leaking check valves and compressors which have required frequent in-head
valve replacement; these valves are no longer available for this vintage of
compressor. Recently, the licensee replaced all six discharge check valves,
and has been in the process of replacing all six compressors under various
engineering work requests (EWRs).
These problems were primarily due to poor
air quality, per licensee correspondence, and cognizant licensee personnel.
Degradation of the air compressors and the check valves was due to accumulation
of water on top of the check valves, and *passage of the water into the air
compressors. The adequacy of the EDG air start system was also addressed in a
type 2 request for engineering and construction assistance, dated June 30,
1989, in which station engineering personnel identified two concerns which
were: the absence of a program for monitoring or controlling EDG starting air
quality, and the hi9h likelihood _that the air start receivers (18 total, 20
cubic feet per tank) are full of rust and scale from years of wet service.
,.
32
The team then witnessed the routine blowdown of the air start system for
EOG 1, and a significant quantity of water was discharged. Also note, that
the licensee recently removed over 20 pounds of rust from inside the service
air receiver in the turbine building. Air quality in the EOG air start system
can also affect the performance of the solenoid operated valves which admit
air to the air starting motors. Sluggish performance of one of these valves
was documented in August, 1989, for EOG 2 in which the licensee produced
-traces of engine RPM versus time. Cognizant licensee personnel indicated to
the team that the valve's degraded condition was primarily due to poor air
quality.
To alleviate these problems, and improve reliability of the diesel
air start system, station engineering personnel recommended installation
of air driers and filters, the goal being conformance with ISA S7.3.
The
licensee's response to the problems cited above so far has been a lack of
commitment to long term corrective action, with more emphasis on short-term
solutions with respect to the material condition of the EOG air start system.
This was considered a weakness in the licensee's maintenance program.
3.d. DEFICIENCY IDENTIFICATION AND TAGGING
During walkdown inspections and observation of work, the team evaluated the
licensee's program for deficiency identification and tagging.
The following
problems were identified with the program:
During walkdown of the SI system, a number of small leaks and minor deficien-
cies that had not been identified by the licensee were identified (see section
2.a for details).
In addition, many deficiencies identified in the walkdown
had been identified by the licensee during their walkdown in late 1989.
However, deficiency tags written by the system engineer had not been hung nor
had WRs been submitted.
A number of deficiencies were identified that had been previously identified
by the licensee, WRs had been issued, yet the deficiencies had not been tagged
or the tags had been removed.
Health Physics (HP) personnel responsible for
identifying leaks and sources of contamination estimated that 10% of the tags
they hang get torn off or removed for some reason before the corrective work
is accomplished.
During the SI system walkdown by the team (in the first week of the inspection)
deficiencies identified in systems other than the SI system had not been tagged
or WRs initiated by the close of the inspection. The SI system engineer, who
accompanied the team on the walkdown inspection, did not feel obligated to tag
the deficiencies in other systems *
.Inconsistencies i.n tagging known deficiencies detracts from the overall
process of identifying deficiencies and initiating corrective action in that
people are less likely to initiate a tag since they cannot be sure whether a
problem has already been identified and corrective action initiated. The above
problems appear to be the result of a weak procedure for identification and
tagging of deficiencies. The procedure (SUADM-M-11) does not clearly specify
..
33
that anyone identifying a deficiency is responsible for initiating a WR card
(tag).
In addition, the word "should is used throughout the procedure,.
.
detracting from the effectiveness of the procedure. Procedures could be
strengthene~ by requiring that all personnel who are in the plant on a regular
basis routinely take WR cards with them and tag any deficiency noted.
3.e. TIMELINESS OF CORRECTIVE ACTION
During the inspection, a number of cases were identified where actions to
correct known problems were not taken in a timely manner.
These items,
discussed in detail in this section or other sections of the report,are
summarized as follows:
In late 1989, the licensee performed a walkdown of the SI system and identified
a number of areas where the piping configuration was not like the drawing:
Five areas where the Unit 2 SI piping configuration. did not agree with flow
diagram 11548-FM-089A, Sheet 2 were identified. By the end of the inspection,
a drawing change request still had not been issued to correct the drawings.
Although the configuration problems do not affect plant or system operability,
corrective action has been slow. Also, a temporary support was found installed
for valve 2-SI-MOV-2885C in the same late 1989 walkdown.
As of the close
of this inspection, an Engineering Work Request (EWR) had not been issued to
evalu~te the support. The above problems indicates weakness in taking timely
corrective action for known drawing errors and deficient conditions.
During the review, the team found that adequate corrective action had not been
completed for QA audit finding S87-22-03 issued in October, 1987.
The .
finding identified numerous discrepancies i~ completed WOs (the team also
found problems with completed WOs - see section 3.s). This audit finding
relative to adequate corrective action by maintenance to improve the quality
of WOs has been escalated by QA to step 2 (August 15, 1989) of a 3 step
escalation process. This is another example of problems with timeliness of
corrective action.
HP was tracking 688 primary sources of contamination. Forty-three new sources
were identified in February, 1990, and only one was fixed indicating lack of
attention to the problem.
Necessary modifications to the radiation monitoring system, such as elimination
of high background readings in monitor locations, has existed for years - see
section 3.f.
The need to replace containment instrument air.filters was identified in
mid-1989.
The filters still have not been replaced (see section 3.c).
Necessary modifications to the HVAC system have existed for years - see
section 3.f *
.
'
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34
3~f ALLOCATION OF RESOURCES
In an effort to determine the root-cause for delays in corrective maintenance,
the team interviewed cognizant engineers, foremen and craft.
From these
interviews, the team has ascertained that there are several contributing
factors responsible for this lack of maintenance and the resulting HVAC system
degradation~ These are as follows:
1.
The licensee's resources are committed on a priority basis, first on
those systems which are important to nuclear safety, second, on systems
necessary for power generation and third, on balance of plant systems/
noncritical to safety. Because most of the HVAC system is nonsafety-
related, manpower -dedicated for system maintenance is limited to a crew -
of four, with no allowance for overtime. System maintenance is for the
most part, limited to the safety-related section of the system and its
associated components.
Management's support for maintenance on the
balance of the system is very limited and, not program driven i.e., a
component operates until it breaks down.
When it (component) no longer
functions, it is tagged out and repaired or replaced depending on avail-
ability of funds, parts and/or manpower.
2.
The team ascertained that the licensee maintains little or no inventory
of replacement parts i.e., fan belts, sheaves, motors for quick
maintenance/repairs are not on hand. Therefore, simple off the shelf
replacement,parts are purchased through a cumbersome procurement system
which treats all replacements as though they are safety-related causing
long delays and extended down time.
Other examples of system degradation and the licensee's failure to respond in
a positive manner are as follows:
On July 31, 1989, the station experienced an ESF actuation at a time when
the ventilation system VS was being aligned, i.e., repositioning of the
HVAC dampers, for testing purposes. -An engineering work request EWR 89-540, was issued to investigate the root cause of the problem and report
the findings to management.
A review of the subject reports entitled,
Systems Engineers Review of Ventilation ESF Actuation Surry Power Station,_
-dated August 23, 1989, identified the root-cause as VS leakage and
actuator blow-by combined with reduced Instrument Air Header pressure.
_ The reports stated that actions in progress taken to correct the problem
included: Service all actuators to eliminate blow-by, walkdown system to
identify and repair all air leaks, verify pressure switch settings for
compliance with design requirements.-
The team determined that as of March
29, 1990, no substantive corrective action(s) had been taken on subject
actuators and sixteen related dampers. This was attributed in part, to a
lack of replacement parts for reasons discussed earlier. A detailed
walkdown of the system to identify and repair all leaks has not been
performed, hence the system continues to leak a-ta rate of approximately
47 cubic feet per minute and lastly, pressure switch verification setting
is only partially completed.
~ ---
--
-
,.
35
Also, by document review,.i.e. EWR 87-170, 3/12/87, 87-170A, 5/8/87 and 89-336 with Field Changes A-Y dated 5/19/89 through 2/14/90, and through
discussions held with cognizant personnel, the team has determined that
the containment air cooling recirculation and air cooling control rod
drive mechanism (CROM), systems in both units are worn-out and unable to
function as originally designed. These documents show that as of May 1987
fans, dampers, louvers, actuators and linkages in the containments
recirculation system were no longer able to function as designed and
required extensive structural/welding repairs or replacement.
Bids for
replacement were solicited in December 1987 but the licensee rejected the
two responses submitted for consideration.
More recently the licensee
issued station commitments CTS 89-7836~001, 89~7460-001 to replace the
containment recirculation fans and dampers by June 4, 1992.
In reference to EWR 89-336, the team ascertained that the air cooling
CROM, system is in a similar degraded condition in that doors, dampers,
linkage brackets, louvers, fans and even some of the ductwork no longer
function as designed in that it required 22 field changed to the subject
EWR to help remedy existing field conditions.
For example, certain
dampers had to be either blocked or wired open for continued operation,
ductwork from fan 1-VS~F-4B to the main duct trunk line required extensive
structural/welding repairs, control rod vent shroud cooler access cover
seats required extensive repairs, damper linkage brackets on control rod
shroud cooling fans 2-VS-F-60A, -60C and -60D were found broken and were
wired open for continued operation. Similar temporary fixes were imposed
for the dampers on recirculating fan 1-VS-F-lB. These conditions help to
demonstrate further the systems degradation, resulting from inadequate
maintenance and a lack of the necessary resources to keep the system
functioning as designed.
During review of annual calibration data for various detectors in the radiation
monitoring system (RMS), the team noted that Procedure No. CAL-001, dated
17 Aug. 1989, Log Ratemeter Scintillation Detector Source Calibration, Initial
Conditions paragraph 3.3 required, "Background/process count rate must be at
least one decade below the calculated calibration source count rate." A review
of the latest calibration data performed for RM-CC-105 and 106 (Component
Cooling Water [effluent] A & B respectively) in January and February 1990
respectively showed the background counts to be approximately 1.1 E+5 cpm,
and the calibration source strength to be about 7.0 E+4 cpm.
That is, the
background was higher than the source strength, opposite that of the initial
conditions requirements.
Based on interviews with the craft, the team learned
that this condition had existed for several years, and that on each occasion
of performing th~ procedure, a procedure deviation was prepared to permit
omitting the paragraph 3.3 initial condition requirement.
The problem was
described as being caused by contaminated sediment on the walls of the CC
piping; thus the monitors were not observing actual fluid activity levels.
The team noted that a Technical Report (No. NE-697, Rev. 0), entitled "Changing
RM-CC-105/106 to Off-line Monitors, Type 1 Final Report, Surry Power Station"
was issued in March 1989, and recommended the off-line monitoring system as the
most practical and only solution expected to work.
A Request for Engineering
'.
36
and Construction Assistance (Type 3) was initiated by the station on 14 July
1989, with a required start date of 1 September 1989 and required completion
date of 1 June 1990. Capital Project Type 3 IR-6369 was issued on 1 August
for "Replacement of CC Radiation Monitors".
Since much of the RMS was not operating in accordance with UFSAR commitments,
a special SNSOC Radiation Monitor Subcommittee had been reviewing the overall
status of the Surry RMS for the past several months.
In their report of 9
March 1990, endorsed by SNSOC on 15 March 1990, a "Long Term Action Item" (#3)
was listed as:
113. A Type 3 study will be initiated for replacement of RM-CC-105, 106 if
necessary.
a. Track progress of CC task team.
If fixed background is found to be
significant, proceed with Type 3 IR 6369 (on hold) to replace monitors.
-ENG/NSS
11
No information was provided about the "on-hold" status of the
plant modification.
The team perceived the above lack of substantive action as an inappropriate,
continued delay in performing required plant modifications.
An appropriate
engineering study had been completed, and there was no evidence that any
conditions had signtficantly changed during the past year. Therefore, it
appeared to the team that it was time to get o~ with correcting the problem,
rather than continuing to study the problem ad infinitum.
In addition to the
monitoring problems caused by the high background, the team was concerned
about the mentality that continued deviations of procedures tended to foster
in the craft - i.e., simply revise the procedure if it is not possible to
perform in accordance with the procedure. It was the team's opinion that
adequate resource commitment should be made by management to avoid forcing
craft personnel into deviating procedures because equipment was not
functioning according to design.
Other long-standing problems with permanent solutions proposed but not yet
implemented due to lack of resource allocations are associated with the EOG
air start system and containment IA system.
Six compressors were being replaced on the EOG air start system. These
compressors required constant maintenance and eventual replacement due to
moisture backflow (past in-line check valves) during compressor idle stage and
resultant rusting valves. The proposed permanent solution to the problem
(addition of air dryers and filters at the compressors* discharge) was deleted
from the 1990 station budget.
Containment IA was known to be below industry standards by the licensee for
many months.
Problems include lack of filters, high-dewpoints and water in
end-use devices. Solutions and needed repairs have been proposed.
However,
no improvements or repairs had been completed at the end of this inspection *
The above problems indicate a significant weakness in the allocation of
resources and in addition in the timeliness of corrective action for known
problems.
..
. ...
37
3.g JOB PLANNING
Supplemental Work Instructions Accompanying Work Orders Were Frequently
Inadequate
The team reviewed two types of procedures in use by the licensee: formal
procedures that were used on a repetitive basis to perform recurring
maintenance activities, and supplemental work instructions" that were
prepared as a part of the planning process for unique maintenance activities.
"Procedures are di~cussed in Section 3.n of this report.
The latter
"instructions", considered by the team to have the force of procedures in
implementation, were reviewed as a part of the planning process, since they
should typically be prepared during the planning phase of Work Order
preparation.
The team noted that approximately two-thirds of all work orders reviewed
utilized work instructions that had the intent and complexity of "investigate
and repair".
Review of these types of work orders led the team to the
conclusion that many functions such as utilization of proper procedures,
technical manuals, and performance of appropriate post maintenance testing
(PMT), may not have been accomplished.
For maintenance activities observed by
the team, it was noted that "planning" typically occurred at the craft level,
when the assigned craft was ready to go into the field to accomplish the work.
Investigate and repair" activities accomplished just that, i.e., no revision
to the details or scope of work in the work order was accomplished after
"investigat1ng", prior to proceeding with the "repair. In an effort to
determine the reasons for observed implementation problems, the team focused
on the planning and work order preparation program.
SUADM-M-12, dtd 20 April 1989, Work Order Planning, was the governing document
for the preparation of Work Orders by the planning department. This procedure
was noted to be weak because details of an acceptable program were absent from
the procedure.
The procedure did not contain a reference list, thus such references as
ANSI N18.7 - 1976, Administrative Controls and Quality Assurance for the
Operational Phase of Nuclear Power Plants, and INPO 85-038, Guidelines
for Conduct of Maintenance at Nuclear Power Stations (Nov. '85) were not
included. Station procedures necessary for the implementation of work
orders, such as clearances, housekeeping, system cleanness, rigging, and
calibration, were also not included.
Section 2.0, Work Order Planning addressed the subject of providing
details to accomplish work with the following:
"2.3 The planner will check the work order for completeness, clarity and
accuracy and add any* additional required information." Since this
instruction appeared to apply to the original Work Request, the team
observed that details listed in the Work Order were usually no more than
what had appeared in the Work Request.
' .
'*
!I'
38
112.4 The_ planner will plan the job and estimate resources required.
2.4.6 Work procedures required will be identified and obtained.
11
For most Work Orders reviewed by the team, it was noted that the
11originator
11
of the Work Request performed the
11job planning/procedure writing" in his
preparation of the document that identified the problem, i.e., the work
request.
For maintenance activities that were observed and reviewed by the
team during the inspection, the work request would state,
11 Item Xis failed.
Troubleshoot and repair.
11
This was translated to the Work Order, and in most
cases became the
11procedure
11 for repair of the component.
In general, no
amplifying "procedural steps" or supplemental work instructions were prepared
except for complex repair activities.
11Planning
11 was performed at the craft
level, at the time the repqir activity was started.
Many maintenance.activities were not addressed by a pre-prepared procedure,
thus it was frequently necessary and appropriate to provide supplemental work
instructions in the Work Order. If procedures were available, work
instructions should be prepared to sequence the work, or direct the use of
~ections of pre- approved maintenance procedures or technical manuals.
In
cases where pre-approved procedures were available and accompanied the Work
Order, the team observed the use of one or two pages of the procedure that was
forty or fifty pages in length - the unused pages were marked
11 N/A 111 as not
appropriate to the Work Order being performed ..
o
No approval process for the content of the Work Order or the adequacy of
the planning process was included in the SUADM-M-12 procedure. Craft
concurrence was not included in the process. Quality review of the
work orders was not specified.
No check lists of necessary work order
attributes were available to assist the planners in preparing comprehen-
sive work orders.
o
Paragraph 2.4.1 stated, "Required plant status and initial equipment
conditions will be identified~"
No further details were provided in
the SUADM-M-12 procedure about preparatory steps for the setting of
clearances, establishing necessary plant conditions, or other meaning
the paragraph may have had.
Guidance on special considerations was not included in the procedure.
As examples, safety considerations such as confined space or fire
protection work permits were omitted from the planning procedure.
11Interfaces with other crafts or departments will be identified and
necessary work requests submitted.
11 was the extent of consideration
given to items such as RWPs, scaffolding, and special chemical
requirements. No guidance on the extent or level of detail of work
instructions was provided, i.e., word by word instructions for some
types of activity, but limited guidance,
11skill-of-the-craft
11 for
other activities. Guidance concerning pre-planning walkdowns of the
expected maintenance activity was not included.
' *.
' .
- *::.
39
Based upon the above types of inadequacies in the work order planning and
preparation instructions, the team concluded that the work order planning
program needs significant improvements.
During interviews with the craft and planning department personnel, the team
learr~ed that
11 planners
11 did not function as a centralized group responsible
for preparation of detailed work instructions. Planners were forced to
function as schedulers and material procurement personnel.
By craft, the
following was determined to be the planner staffing strength:
Staff
Contractor
On loan from
craft resources
Electrical
1
2
2
2
Mechanical
9
4
1
The planning department staffing did not permit the detailed work instruction
preparation that was typical 9f the industry, and the burden of this segment
of the planning effort defaulted to the craft. Since the craft felt they knew
what they were going to do, pre-job details. were frequently not added to the
work orders for the electrical and ~echinical crafts.
I&C technicians
generally attempted to revise existing procedures to
11make them fit
11 the
intended maintenance activity.
Based on the extent of the observed problems with the procedure governing the
maintenance planning effort, the inadequacy of work control documents, and the
sparse planning staff, the team concluded that the program for preparation of
maintenance authorization documents was a significant weakness.
3.h. POST MAINTENANCE TESTING (PMT) PROGRAM WEAKNESSES
The PMT program is governed by the following two procedures:
SUADM-M-27, Revision 1, Requirements for A Post Maintenance Testing
Follower
SUADM-M-47, Revision O, Post-Maintenance Test/Verification program
The following problems were identified with the program:
The current PMT program, procedure M-27, is very limited for equipment other
than ASME Section XI equipment.
The procedure was written -to cover Section XI
testing and has been revised to cover other safety-related equipment and, on a
very limited basis, non-safety-related equipment.
However, the procedure is
.primarily a Section XI procedure and provides very little detail for other
. '
.
'-.,,
40
equipment, e.g., electrical. Although, the PMT Follower is used for all
safety-related WRs, the lack of procedural detail results in inconsistences in
specifying PMT for equipment other than Section XI.
Personnel responsible for specifying PMT on the Follower have experience
primarily in Section XI testing and are not qualified to specify testing in
other areas such as electrical. Again, this results in inconsistences in
specifying test requirements.
On some WRs reviewed, the PMT follower
indicated that engineering was contacted for the required PMT.
However,
without procedural guidance, desired results cannot be assured.
In the electrical and I&C areas, the PMT Follower is attached to the work
order. The electrical and I&C sections stated that they are only required to
perform the PMT specified on the Follower. The planners stated they are not
responsible for PMT.
Fortunately, most of the electrical and I&C procedures
have sufficient testing and calibration requirements that are equivalent to
PMT.
However, two weaknesses were identified. One item is that when switch-
gear is sent to an outside vendor for refurbishment, PMT was not adequately
specified. Another item is that the maintenance procedural step for functional
testing can be marked
11 NA
11 (not required) if Operations is not available to
perform the step. The licensee stated that the procedures will be revised
disallowing NA
1d steps for functional testing by Operations.
The licensee
stated that temporary corrective action will be immediately implemented by
requiring that qualified electrical system engineers will specify all PMT on
the Followers until the new program is in place. The team considered these
responses by the licensee as acceptable.
Based on previous assessments (INPO and Licensee), the weaknesses in the PMT
program had been recognized and corrective actions initiated.
In October,
1989, a task team was assigned to develop a new PMT program.
At the time of
the inspection, a new comprehensive PMT was under development.
The program is
detailed in procedure M-47 and consists of a series of matrices for each
component under the program.
At the time of the inspection, the only matrix
that had been issued was for the Auxiliary Feedwater Pumps.
The scope of
equipment to be included in the program was still being developed.
By the
close of the inspection, the scope had been defined and was to include all
equipment on the mechanical and electrical
11Q
11 list {approximately 15,000
items). Licensee personnel indicated that tentative plans are to have
matrices completed for ISI/TS (Inservice Inspection/Tech Spec) items in 1990,
safety-related items in 1991, and BOP (balance of plant) items in 1992.
To
date, matrices have been developed for a significant portion of all ISi/TS
check valves, motor operated valves (MOVs), and safety-related 4160v and 480v
breakers. However, none of these matrices have been through the review
process and added to the procedure.
3.i. TESTING OF AUXILIARY FEEDWATER TURBINE
The auxiliary steam turbine-driven pump unit consists of a Terry turbine
coupled to an Ingersol (Ingersol/Dresser) pump equipped with a Woodward
governor and a trip throttle valve manufactured by Gimpel Machine Works
Incorporated (Gimpel), Philadelphia, Pennsylvania. Industry wide problems
,.
41
including overspeed trip failures were encountered with the Terry turbine
and IN 88-67 described two instances where the Terry turbines failed to trip
on overspeed.
INPO issued at least three SOERs on this subject. Major.
maintenance was performed on the Terry turbines installed at Surry Units 1
and 2 during 1988 (WO 58211) and 1986 (WO 41408), respectively. Attachment 8
to WO 58211 indicates that the Terry turbine overspeed trip was set at 6280 rpm
and verified to trip at the set point.
WO 41408 records did not indicate that
the overspeed trip mechanism operated. The Terry Corporation, the manufacturer
of the Terry turbine, in Instruction Section 7 of the Instruction Manual states
in part,
11It is most important that every overspeed device and trip mechanism
be tested regularly, preferably once monthly. This will insure that the
tripping mechanism is operating freely.* The test can be made manually or by
overspeeding the Unit. The mechanism, when tripped, should respond instantly
and reduce the speed of the Unit, or hold it from overspeeding with the
throttle valve wide open.
Record trip set point and date of initiation.
Verification of proper functioning and setting of the overspeed trip device
during initial startup is mandatory. This should be accomplished with the
turbine disconnected from the driven equipment.
11
The licensee did not
translate the vendor recommendations into a procedure to conduct an overspeed
trip testing of the turbine.
The team reviewed the action taken by licensee relative to IN 88-67 entitled,
11PWR Auxiliary Feedwater Pump Turbine Overspeed Trip Failure.
11
Station
Commitment Assignment/Response Form (SCARF) 88-6067-003, which was initiated
to track the actions relative to IN 88-67 stated that the Woodward governors*
would be replaced for Units 1 and 2 during the next refueling outages. It
also stated that the Terry turbine for Units 1 and 2 were overhau.led in 1988
and 1986, respectively, during which the tappet balls were replaced and
overspeed tests were performed.
In view of the recent overhaul and subsequent
overspeed trip test, the SCARF requested an extension of time to develop a
procedure to conduct an overspeed trip test with the new governor.
The
licensee was unable to produce any records to substantiate the statement in
the SCARF that the overspeed trip test was conducted on the Unit 2 Terry
turbine.
The Industry Operating Experience Review (lOER) Committee reviewed the "Testing
of Steam Turbine/Pump Overspeed Trip Devices" and provided a recommended action
plan. The document referenced:
'
Current Loss of High Pressure Core Cooling Systems.
Reliability of PWR Auxiliary Feedwater Systems.
(INPO) SEN 55:
Failure of Woodward Governors results *in Auxiliary
Feedwater Pump Turbine Overspeed Trip Failure.
NRC IN 88-67:
PWR Auxiliary Feedwater Pump Turbine Overspeed Trip
Failure.
NRC Case Study Report AEOD/C602:
Operational Experience Involving
Turbine Overspeed Trip, dated August 1986.
' ...
..
42 .
The action plan for Surry stated three concerns and outlined the actions to be
taken for each concern. However, the team determined that attributes such as
the following were not considered:
Recommendations of the manufacturer of the Terry turbine
Research of the overhaul and maintenance records to determine if
overspeed trip tests were indeed performed.*
Engineering evaluation to determine the consequences of operating the
Terry turbines without knowing if overspeed trip device fails to operate
and overpressurizes the piping downstream of the turbine.
The frequency at which the overspeed test should be performed considering
attributes such as, the vendors recommendation to test the overspeed trip
mechanism monthly, the complexity of uncoupling the pump before the test,
the fact that the Terry turbine is operated infrequently, and that there
are no pressure relieving devices downstream of the AFW turbine.
IN 88-67 dated August 27, 1988, described a failure of the AFW pump turbine
overspeed mechanism in July 1988 at the San Onofre Station. A failure of the
overspeed trip mechanism occurred at the Ranch Seco Station during January
1989 during which the AFW System was pressurized. The team determined that
contrary to paragraph 6.2.1 of Procedure VPAP-0504, research and evaluation of
the Vendor Technical Manuals was not performed and the recommendations of the
vendor to test the overtrip mechanism was not incorporated in a suitable
procedure.
Station requirements for processing vendor supplied information were found in
SUADM-ADM-31, Vendor Interface/ Control of Vendor Documents, dated 5 Dec.
1985, at paragraph Nos. 8;o, 8.1.1, 8.1.2,and 8.1.3 (see section 3.b)
Based upon the above example, the team concluded that the program for control
and incorporation of vendor supplied information was not being effectively
implemented in accordance with required station procedures. This failure to
. follow procedure is an example of violation 50-280,281/90-07-0l *
3.j. PERSONNEL SECURITY TRAINING
Training in security access control was noted to be lax in at least one case
by the inspection team.
One maintenance technician was observed to
11 another technician into the Emergency Switchgear and Relay Room.
Confusion between the concept of
11accountability
11 and
11controlled
accessibility
11 appeared to be the cause of the problem.
The licensee agreed
to take appropriate action in the matter .
.
...
.,
43
3.k. CONTROL AND CALIBRATlON OF MEASURING AND TEST EQUIPMENT (M&TE)
Procedure SUADM-M-39 (dtd 13 Dec. 1988), Control of Measuring and Test
Equipment, established the facility M&TE program.
The procedure detailed the
issue, recall, storage, and segregation of special, limited-use, or expired
M&TE.
The procedure also provided instructions for placing damaged equipment
out-of- service, and for resolution of out-of-tolerance equipment used in the
field. Although the calibration laboratory was small, it was found to be
clean and organized, and adequate in its function.
Each piece of equipment was assigned a unique
11SQC
11 number by which the
equipment
1s calibration and use history was tracked. All tracking and recall
was performed manually on cards associated with the equipment by the SQC
.
number.
No formal
11 system was employed by the licensee for pieces
of M&TE under control of the I&C and Operations group; two way traceability on
equipment used in quality work was maintained by, 1) recording the equipment
and its SQC number on the work order itself, and 2} recording the date and
procedure that the M&TE was used on a Test Equipment Record card (Form#
MTM06) attached to the equipment itself (instructions for use of the MTM06
form were not included in the SUADM-M-39 procedure, but appeared to be
properly implemented).
Electrical and mechanical craft similarly maintained
storage of limited M&TE under their control, but most electrical and mechanical
items were checked _in and out of tool issue points. Recall of M&TE approaching
the calibration due date was controlled by manual review of history cards
segregated into month-due categories. The M&TE.technician generated a
Certification Due Notice, and forwarded it to the cognizant supervisor having
possession of the instrument.
Although the program appeared fundamentally adequate, several areas of concern
were noted by the team. A high level of responsibility was placed on the
various disciplines for proper control and handling of M&TE due to the
decentralized control of the equipment.
All disciplines except Operations
readily complied with requirements of SUADM-M-39 related to use, storage, and
recall. The team concluded that many of the following types of problems were
the result of no single point of contact in the Operations department taking
responsibility for the program.
Several areas of procedural non-compliance in M&TE control were noted in the
Operations department.
For ~xample, Section 8.0 of SUADM-M-39 addressed the
subject of storage of M&TE, including segregation;environment, and handling.
M&TE under the control of Operations was stored in two lockers behind the
control room adjacent to an air-conditioning unit. The lockers included all
kinds of paraphernalia, including some very heavy test gear such as connecting
piping, discarded radios and their associated chargers, etc. The lockers were
in total disarray, thus storage conditions could have (and had) damaged or
disrupted calibration of the instruments. As an example, an Eagle Eye Flow
Meter (3 - 9,000 GPM range) had a calibration sticker reflecting calibration
of 08/22/89, and due date of 8/90 (SQC #3708).
The meter face had been broken
out of the meter for a long period of time, but reflected a last used date of
2/18/90 on the Test Equipment Record Card (i.e., the equipment had not been
.
....
.>
r
44
removed from the system). The test for which the equipment was used was
illegible, and the card was not annotated with the SQC # of its associated
equipment (Card loose in the meter container).
Two 1,500 - 4,500 GPM flow
meters were also stored in the locker, one with a broken meter face.
Neither
meter was calibrated because the calibration facility did* not possess equipment
accurate enough for the 2
11 H20 range of the meter.
Two pressure gages were also found in the locker.
One O - 5000 PSIG pressure
gage was
11tested
11 12/17/87 (not in M&TE system), and one O - 1000 gage was
"calibrated" 1/29/90, and
11due
11 2/29/90 (i.e., past due - # SQC.3655).
Two dual stage (0 - 4,000, 0 - 400 PSIG), pressure regulators were also found
in the locker that were used to perform containment penetration leakage tests.
These regulators were un- tested and un-calibrated. Paragraph 6.2 of
SUADM-M-39 specifically required all M&TE to be calibrated prior to use on
safety-related systems, but specifically excepted devices that were contin~
uously monitored during use with other certified equipment (in this case, the
regulators were used with high accuracy, Heise gages).
In that instance,
paragraph 6.2 required application of a "No Calibration Required" sticker to
certify the acceptable use of the device with other calibrated devices.
Similar situations were noted with several power supplies in use by I&C
technicians.
In all cases (regulators, power supplies) observed by the team,
"No Calibration Required" stickers were not affixed to the devices which was
contrary to procedural requirements.
Improper storage conditions were also noted by the team for laboratory type,
six foot high, roll around instrument racks that were under the cognizance of
the I&C group, not Operations. * To meet seismic restraint requirements, the
licensee had "temporarily" (Summer of 1989) wrapped a large chain around the
upper cabinets in the rack.
The upper cabinets included power supplies,
counters, digital voltmeters, etc. The chain was then wrapped around an
adjacent stanchion to keep the entire assembly from damaging adjacent reactor
protection instrument racks. Th.is storage method was perceived by the team as
a poor practice since a bump into the rack resulted in the chain wrenching on
the instrument cabinets.
The licensee should correct this condition of
improper storage storage of M&TE.
The team reviewed instrument history sheets and recall lists, and noted that
several instruments under the control of Operations were overdue for calibra-
tion for several years (e.g., SQC # 3653 - 3/87, 3589 - 10/88, 3566 - 10/88,
3562 - 7/85, 3544 - 6/86). Several Notice(s) of Instrument Restriction had
been generated because the device(s) had gone beyond their certification
due date; there was no evidence that compliance with paragraph 7.5 of
SUADM-M-39 had occurred regarding application ~f Certification Overdue
stickers, and return of restriction notice copies to the calibration facility.
The team was especially concerned that the inventory of required test equipment
to support the plant was being "lost" due to such events as breakage and
contamination, but not being recognized due to lack of control of calibration
status. The team perceived this lack of control as a significant implementa-
tion weakness.
'*
.
....
_.,
45
The above examples in addition to those discussed in sections 2.e, 3.b and 3.i
indicate, that the licensee failed to follow procedures for maintenance. This
will be identified as violation 50-280,281/90-07-0l :"Failure To Follow
Maintenance Procedures
11
In exploring potential
11 loss
11 mechanisms of test equipment, the team learned
that the licensee has no facility for calibration or comparison checking of
contaminated equipment. If an M&TE device becomes contaminated (Heise gages
were a good example), the device was simply stored, and used in contaminated
applications only, until the expiration of its normal calibration period. At
this time, the device was permanently retired, with no check of accuracy
before retirement.
Thus compliance with paragraph 7.6 of SUADM-M-39 regarding.
evaluation of out-of- calibration conditions when a device was presented for
calibration was not possible. The licensee advised the team that the
,.
situation of contaminating an instrument had not occurred for a long period of
time.
The team noted areas of strengths and concerns for devices requiring off-site
calibration due to cal lab limitations.
For example, the qualified vendors
list was up-to-date, and a sample .check of devices recently sent
11out
11 for
calibration showed the items to have been sent to a qualified vendor.
The team
noted an effort on the part of the instrument technician to anticipate the
lead time required to obtain authorization to send devices off-site but also
noted a few cases where the ~evice was over-looked until due/past due.
However, on occasion, the attempts to anticipate calibration requirements were
thwarted by extremely variable processing time (months) on purchase orders to
requisition the calibration service. The net result was several items of M&TE
were out of calibration before required vendor support could be authorized and
obtained. Multiple pieces of the same equipment prevented this from becoming
a significant problem.
Related to sending equipment off-site, the team noted that infrequently,
quality control personnel performing receipt inspection of returned M&TE would
erroneously retain and/or separate an instrument
1s pedigree papers from its
associated device. Again, this was not a significant problem because
ultimately, the papers could be traced and recovered.
However, the situation
was of concern to the team because the licensee currently utilized only one
technician to manage the calibration program, and manage and operate the
calibration laboratory.
No persons-in-training were assigned to the
laboratory. It was the team's opinion that a program improvement in this
area should be considered by the licensee.
Another team concern was related to availability of M&TE device accuracy to
the technicians performing maintenance activities. This was of concern to the
team because procedures in use by technicians were noted to cover the entire
spectrum of required accuracies and required instruments to suppo~t the
procedure *
'*
46
For example:
(1)
Procedure l-PT-2.lA, dated 17 July 1987, Reactor Coolant Wide Range
Temperature (T-1-410), stated at Initial Conditions paragraph 3.4, "Insure
that the test equipment to be used has adequate precision and range to
measure the desired parameter and has been calibrated against standards
traceable *** ".
(2)
Procedure Cal-001, dated 17 August 1989, Log Ratemeter Scintillation
Detector Source Calibration, stated at Initial Conditions paragraph 3.6,
"The following test equipment or equivalent is available, calibrated and
meets accuracy requirements as specified.
3.6.1 Frequency counter or Scaler Timer.
3.6.2 Digital multimeter."
No accuracy requirements were specified.
(3)
Procedure Cal-044, dated January 12, 1990, stated at Initial Conditions
paragraph 3.2, "The following test equipment or equivalent is available
and calibrated. *
3.2.1 Function generator, HP 3310A.
3.2.2 Pulse generator, Rutherford 816.
3.2.3 Digit~l multimeter, Fluke 8110A.
II
The team observed that the first two examples relied on the technicians to
perform instrument acceptability determinations, and did not provide accuracy
values for the instruments that could be used in the performance of the
procedure.
The team concluded that preparation of
11upgraded procedures"
was tending towards overcoming inadequacies in accuracy requirements versus
accuracy of instruments available. It was the team
1s opinion that as an
interim methodology, the licensee should consider making readily available *to
the craft all M&TE instrument accuracies such that if accuracy criterion are
specified by a procedure, the craft will be able to readily determine
acceptability of instruments in use.
3.1. DEFINITION OF MAINTENANCE REQUIREMENTS
The team reviewed instruments and control devices to determine if adequate
calibration activities were being accomplished on control room indications
that operators would use to implement normal, off-normal, and emergency
operating procedures.
The team examined three categories of devices: 1) those
that fulfilled Technical Specification requirements, 2) those that fulfilled
regulatory guidance or operating procedure requirements, and 3) those that
provided personnel and/or equipment safety functions.
The team learned.that
instruments in the first category (some safety-related) were subjected to
formal, proceduralized Periodic Tests (PTs) that accomplished instrument
47
calibrations and checks consistent with Technicai Specification (TS) require-
ments. A sample check of the PT index, that listed the applicable PT procedure
number, the related TS table requirement, and the frequency, showed that all
instruments were properly addressed.
An informal checklist was in use by the
licensee that distributed the many calibrations (by month) over an 18-month
cycle. The team concluded that, based on the sampling conducted, an adequate
periodic calibration program for TS required instruments had been implemented.
It was noted, however, that periodic calibrations were in the beginning stages
of integration with the station preventive maintenance program.
In the second category of instruments, the team selected as a sample base,
Reg. Guide 1.97 instruments and learned that these instruments were equally
well addressed in periodic calibrations as the Technical Specification
required instruments.
However, of concern to the team was the fact that a
Reg. Guide 1.97 instrument did not have a formally approved procedure for
accomplishing appropriate calibrations.
For example, Unit 1 pressurizer
relief tank (PRT) temperature (T-1-471} was calibrated using a (apparently
startup) procedure that was not dated and not approved.
The last calibration
performed using the informal procedure was September 1989.
The team noted,
however, that Procedure Number 2-Cal-333 had been approved for the Unit 2 PRT
temperature device on 11 March 1986. Several other U-1 devices had no
currently approved calibration procedure, such as:
o
Containment Vacuum Pump Discharge Flow (F-CV-150)
o
Throttle Pressure (P-MS-102}
o
SW Flow to Control Room Chillers (PDI-SW-130A, B, C)
o
SW Flow to Component Cooling Heat Exchangers (PDI-SW-132A,
B, C, D)
These instruments were non-safety, but used by control room operators to
implement operational procedures.
The last category or group of instruments the team was particularly concerned
about were instruments that provided control room operators direct indication
of the integrity of operating safety-related equipment, e.g., the EDGs.
Several local alarm windows at the EOG local control panel were actuated by
pressure and temperature switches, such as:
Oil Pressure (low)
Crankcase Pressure
(high}
Cooling Water Press.
(low)
Starting Air Press.
(low)
Engine Temperature
(high}
20 psig (engine speed 125 - 870 rpm)
44 psig (engine speed above 870 rpm)
1 - 1.7" H20
20 psig
165 psig
190 deg. F.
.. .
48
Fuel and lube oil parameters were also monitored. These devices, in addition
to local alarms, provided contacts in a supervisory alarm circuit for the main
control room annunciator 1J-H7, "EOG #1 Trouble (similar for all diesels).
Control room personnel initiated off-normal response procedures on receipt of
the alarm(s).
None of the pressure or temperature devices that initiated
alarms were included in a periodic test/calibration program.
In addition, the
team noted that local reading instruments, e.g., the many pressure gages on
the air start receivers, were similarly not included in any periodic test or
calibration program.
Thus an auxiliary operator, when dispatched to the EOG
local panel on receipt of a control room alarm, could not be assured of valid
indication for engine parameters.
The lack of periodic calibration of
critical engine instrumentation was perceived by the team as a program and
implementation weakness.
The team noted, however, that another important
system, instrument air, did have many of its pressure control switches (e.g.,
those associated with the compressor operation) in a periodic test/calibration
program.
Coverage was found to be system dependent.
The licensee did not
have an instrument list, thus covered instruments were not able to be readily
determined.
The licensee advised the team that the "PM Upgrade Program** would
address this problem on a system by system basis as the program analysis is
completed during the next several years. It was the team's opinion that the
I&C group should provide Operations with a list of those instruments providing
direct or indirect indication (alarms) to the control room of system
integrity. Operations should evaluate those instruments that are not
calibrated for potential safety of equipment impact such that a decision on
the necessity for the instruments to be calibrated can be made in a more
timely manner.
The team concluded that the PM Upgrade Program when
implemented as described should tend to correct currently observed problems.
3.m. PRIORITIZATION AND BACKLOG CONTROLS
The team reviewed the licensee's records, schedules, interviewed maintenance
department personnel, and attended planning and scheduling meetings to
determine the effectiveness of the licensee's prioritization scheme, and the
extent and control of the maintenance backlog. Specific areas examined
included prioritization, deferred preventive and corrective maintenance,
and
measurements of past and current backlog *
During their review of work orders, the team observed numerous high priority
work orders that were very old:
WO#
Priority
WO Approval Date
076790
1
89/01/12
077997
1
89/02/03
086587
1
89/10/10
088023
1
89/11/17
The team reviewed the program for work order prioritization to determine the
adequacy of the program, and whether it was being properly implemented.
Procedure SUADM-M-11, dtd. 14 April 1989, Work Request System, was the
49
governing procedure for assignment of corrective maintenance (CM) priorities.
(Preventive maintenance activities were always assigned Priority l; this issue
is discussed below.)
Paragraph 3.2.1 stated, "The OMC completes Blocks 10 -
12, Blocks 14 - 20, reviews the WRC for accuracy and completeness." The
Operations Maintenance Coordinator (OMC) was the SRO-qualified person making
the prioritization decision for entry in Block 11 of the Work Request Card
{WRCJ.
Attachment 2, Work Request Card Completion, provided the guidance for
priorities as follows:
Priority 1
Priority 2
Priority 3
Priority 4
Priority 5
Priority 6
Priority 7
Urgent work, scheduled to start in 24 - 48 hrs.
Priority work, scheduled to start one week after approval
Used to build a backlog of work, ordinarily scheduled to
start 4 weeks after approval
Work to be done at time specified by originator, such as
outage
Priority work done during a trip
Work on equipment without a redundant system - treated as
priority as it could cause a shutdown
Work on equipment that could cause a shutdown if the redundant
system failed.
The team noted in practice that only priorities 1 - 4 were used in work
- orders.
The team also noted what was considered a significant program
weakness in the above prioritization scheme:
o
The scheme did not consider Technical Specification (TS) LCO limitations
o
The scheme did not consider safety of personnel
o
The scheme did not consider safety of equipment
o
The scheme did not consider impact on unit generation capacity, etc.
The team discussed the above considerations, both the written program and
team's opinion of an adequate scheme, with the station personnel responsible
for prioritization assignment and learned the following.
Priorities 1 - 3
were assigned based on consideration of Technical Specifications, safety of
equipment and personnel, and unit generation capacity. Equipment redundancy,
extent of degradation, and assessment of risk of challenge to safety systems
were considered in the priority assignment.
As discussed below, the team also
learned that high priorities were conservatively assigned in an attempt to
overcome production sluggishness caused by other factors. Priority 4 appeared
to be the only priority that was assigned in accordance with the program
requirements - i.e., a Priority 4 Work Order was planned for a normal outage.
It was the team's opinion that the current program for priority assignment
constituted a weakness, however, the manner in which. the ineffective program
was being circumvented and implemented was adequate.
The team learned that once a priority had been assigned to a work order,
limitations on WPTS access and system difficulties made the change of the
priority very difficult. This was considered a program weakness because
several aged, Priority 1 work orders were being carried in the system that
were not actually high priority any longer. For e~ample, WO# 088023 required
the fabrication and installation of missing generator shroud bolts on #3 EOG.
>
50
It was a Priority 1 work order when written because the shroud was rubbing
on the engine to generator shaft; now that the shroud was temporarily,
correctly positioned by temporary bolts, it was appropriate to change the work
order to a lesser priority. The priority revision had not been made because
the change was too difficult. It was the team's opinion that a program change
should be made so that assigned priorities have meaning.
In the area of preventive maintenance deferrals, the team noted that the
corporate reported performance indicators for 1989 averaged approximately
1.1%, closely approximating the licensee's goal.
"Deferral" was defined as
the percentage of PM during the monthly period not completed within _the
assigned grace period (lX periodicity for EQ, 1.25X periodicity for non-EQ).
During the team's review of individual deferral approval sheets, the team
noted that the actual deferral rate was much higher during 1989, somewhere
approximating 15 - 20% average for the year (as high as 43% in June 1989).
The discrepancy between "reported" and actual deferrals related to the method
of record keeping - only if a PM activity were scheduled, then not completed,
did the PM become a reported "deferral
11
The team concluded that this m~thod
of record keeping constituted a poor practice in that it did not give a clear
picture of the amount of deferred preventive maintenance that contributed to a
high backlog.
Changes in record keeping and aggressive attention to completion
of PMs have recently been initiated that should cause reported "deferrals" to
track actual deferred preventive maintenance. Actual deferred PMs for February
1990 were approximately 1%.
A review of recently deferred PMs showed that some very important PMs were
being deferred for illogical reasons.
For example, PM EE-EDG-M/Al, Emergency
Diesel 1 Year Service and Inspection, stated the "Reason for Deferral" as,
"Parts" although the PM was not new.
Engineering review of the deferral had
rejected "parts
11 as not being technically justifiable.
PM EE-C-M/Ml, a
Monthly Compressor Check of the EDG air start compressor (Mark# 01-EGl-
C-QXl), stated the reason for deferral as,
11PM missed due to parts - new PM
11
Again, engineering review of the deferral had rejected "parts** as not being a
technically justifiable reason, and noted that the PM was the same as the
quarterly scheduled PM since 1987.
Manpower was also frequently listed as a
reason for deferral. It was the team's opinion that parts unavailability and
lack of manpower for long-standing PMs constituted poor planning.
The PM
Deferral Review Sheet did not provide for listing the last time the PM activity
was accomplished, i.e., how far beyond end-of-grace, although that information
was available in the WPTS by performing a special report run-off. If a PM
activity was indefinitely deferred, it was simply noted as "missed
11 at its
next due date in the WPTS to permit clearing the previously generated work
order number from the system.
The team also noted that all PMs were assigned
a priority of 1. This tended to defeat the purpose of a prioritization scheme,
and prevented effective management of backlogged work.
It was the team's
opinion that a significant program improvement would accrue from a two-fold
scheme that related PM priority to importance of operation to the plant and
importance of operation to the component itself *
.
f
51
For each deferred PM, the discipline supervisor was required to review the
deferral, then engineering reviewed and approved/ rejected the deferral. The
responsible superintendent (e.g., maintenance) reviewed and approved all
deferrals; SNSOC approval was required for all EQ PM deferrals. It was the
team's opinion that a program improvement would accrue from an increasing
level of management review of deferred PMs for increasing amounts of time
beyond end-of-grace period.
The licensee's program for backlog control was largely not proceduralized.
Passing mention of backlog control was made in procedure SUADM-M-14, Work
Order Scheduling, dtd 19 Dec. 1989, para. 2.3, that stated,
11A preliminary POD
will be established to reflect carry-over work, new work scheduled from the
backlog schedule, and new work scheduled as a result of station needs.
11
Backlog control was observed to be a de-centralized function of the craft~
schedulers reminding the craft foreman of outstanding work orders, and the
need to continue to work off backlog as
11filler
11 items when manpower
permitted. The centralized planning and scheduling function dealt primarily
with the high priority work items on a day-to-day basis. The above type of
backlog control was largely a function of planning, i.e., craft-level planning
for the I&C shop, shared craft-level and centralized planning for the
electrical craft, and mostly centralized planning for the mechanical craft.
In addition to craft "lists
11 of backlog items, the Operations_ Department had
recently begun preparing prioritized lists (watch station basis weekly) of
plant equipment that requi,red increased operator action because of equipment
faulty operation.
For example, numerous work orders were outstanding on
service water temperature control valves (Mark #s SW-TCV-108/208); since their
operation was unreliable, operator action was routinely required to monitor
and adjust. These lists of approximately 200 items affecting all crafts were
used to help set craft work priorities.
Even though the control of backlog-was not proceduralized, management tracked
and was acutely aware of backlog through performance indicators. A review of
the performance indicators showed an overall increasing trend of outage and
non-outage backlog from June 1989 (when data was first available) to the
present.
As of 28 March 1990, the total outstanding work items numbered 4727,
which included corrective maintenance {CM) work orders, PMs, and EWRs.
By the
end of 1989, the average age of non-outage CM had increased from approximately
200 to 300 days, but then dropped back to about 200 days in January 1990. The
total non-outage CM at the end of March 1990 was 2027 items broken down as
follows by craft and readiness to work:
Mech
Elect
Labor
Const. Other
In planning 447
374
183
59
7
16
698
Working
71
65
62
3
12
29
1
..
>
52
In addition to the above, approximately 500 PM activities were performed each
month for the three major crafts as follows:
Mech
Elect
240
200
60
Approximately 50 of the 2,000 CM items were recorded as Priority 1 work items.
Each of these work items was reviewed by the team with the licensee for its
safety impact on the operational status of the plant.
As discussed above
concerning work order prioritization, Priority 1 was applied to work orders in
a very conservative manner.
That is, only approximately five of the fifty
work orders. were actually high priority. The ba 1 ance of the work orders were
being treated as high priority because of their long term, potential impact on
equipment or on generating capability if further, significant degradation
occurred.
The five work orders were receiving detailed attention consistent
with their impact on plant operation. The team's review of other lesser
priority, outstanding work orders showed many of them to be 100 1s of days
old.
In a related issue, the team reviewed the open clearance (equipment
tag-out) records and noted the following figures:
Number of *
Days Active
Tagging Reports
Ave
Maximum
Unit 1
146
215
1,598
Unit 2
72
148
1,013
The team noted that there was a direct correlation between very aged equipment
clearances and work orders, i.e., most of the old clearances continued to
exist due to incomplete very old work orders.
The licensee advised the team that recent efforts at increasing the coordina-
tion between the craft and the support interfaces were having a positive
effect in stopping the increasing trend.
As noted in Section 3.r of this
report, it was the team's opinion that substantive action should be taken
by the licensee to improve the effectiveness of coordination and improve the
support interfaces to positively reverse the adverse trend of backlog.
3.n. PROVIDE MAINTENANCE PROCEDURES
The team reviewed procedures as a part of work observed in progress, and as a
part of work packages already accomplished. Comments on procedures generated
as a result of observation of the work in progress are discussed in Section
2.h.
Comments derived from review of work packages are included below.
Procedure ECM-1503-1, Rev. l,*MOV Motor Repair and Replacement, ,provided
instructions for replacement and repair of MOV motors. This procedure was
approved for use on 15 June 1989, and represented the
11upgraded
11 format.
This
procedure was also one of those in the licensee's special MOV program and
therefore received special scrutiny during its preparation phase.
...
..
53
The team carefully reviewed this procedure to determine the adequacy of the
licensee's maintenance procedure upgrade program. Split responsibility
between the electrical and mechanical craft existed in the MOV actuators - the
electrical craft were responsible for the actuator motor, and limit and torque
switches.
The mechanical craft had responsibility for the balance of the
actuator. Notwithstanding the special attention that the procedure had
received, the team noted the following areas for improvement.
Although portions of this procedure addressed many electrical operations that
had to be performed with the valve energized, paragraph 4.0 Precautions and
Limitations only listed "None". Paragraph 6.2.8 included a Caution that
stated, "Possible equipment damage.
Incorrect pinion gear installation may
not be detected in testing.", and then required, "Install pinion gear IAW
Attachment 1." Attachment 1 was found to be an elementary drawing of the
pinion gear configuration (gear shoulder related to the motor), with no
detailed information concerning the gear key (when applicable), set screw, nor
lockwire. A review of the Limitorque Instruction and Maintenance Manual
(SMBI-180D), SMB-0 to SMB-4 & SMB-4T, Reassembly, determined that Step 5.
required, "When reinstalling the motor pinion, pc #40, insure it is a tight
fit on the motor shaft (preferably a light press fit). Note that the SMB-0
motor pinion is installed with the set screw lockwire between the gear teeth
and the motor flange.
On the SMB-1 through 4, the gear teeth are between the
set screw/lockwire and the flange.
11
Limitorque drawing 08-408-0001-4 showed
the gear configuration and the lockwire installation, but was not included in
the subject procedure.
It was the team's opinion that inadequate detail was included in the upgraded
procedure in that the procedure did not include the fundamental repair
information of the Limitorque maintenance manual. Since the repair manuals or
portions thereof were not noted to accompany work orders, and the above
information could not necessarily be relied on to be skill of the craft, it
was also the team's opinion that such information should be included int.he
appropriate procedure.
Similar increased attention to detail was requi_red in mechanical MOV
procedures.
As an example, procedure MMP-C-MOV-178, dtd 20 September 1988,
Removal and Overhaul of Limitorque Model SMB-000 through SMB-00 and SB-00, was
used to overhaul an SMB-00 type operator (WO 565294, Charging Pump to Regen Hx
Stop Valve, MK #02-CH-2289A).
Page 36 of the procedure included in the work
order contained an illustration of the disassembly of a SMB-000 shaft (vs
. SMB-00), and the part numbers identified in the illustration were specific
only to the SMB-000 operator. Additionally, the part nomenclature and
assembly sequence was different from the SMB-00 operator. Although the
procedure was revised on 21 October 1988 (during the performance of the
maintenance), the illustration of the SMB-000 actuator remained unchanged on
page 37.
Both revisions of the procedure were used in WO 565294 to perform
the actuator overhaul, including replacement of the hypoid gear which was most
affected by the procedure error.
The above procedural problems were perceived by the team to be examples of
weaknesses in the procedure preparation program.
..
..
54
3.o
CONTROL OF ELECTRICAL WORK PRACTICES
Electrical work practices:*
Design Change Packages 8532 and 8534 (U-1 and U-2 respectively) installed new
station batteries (vital 120 volt DC power distribution system).
The team
noted during system walkdown inspections that several conditions fn the
batteries were not consistent with installation specifications. For example,
vital batteries lA and lB each required two conduit installations for
intercell cabling between battery halves. Neither cable conduit was grounded
in either battery.
The team reviewed NUS-2030, Specification for Electrical
Installation for Surry Units 1 & 2, Category Safety Related, and noted that at
paragraph 6.9, '.'Metal conduit systems shall be grounded by copper cable
connections to the ground grid, grounded cable tray system, or to building
steel using tinned copper lugs."
Vital battery lA, cell 30 to 31 intercell connector, exhibited two 1/4"
terminal bolts that did not not appear to have been properly tightened. The
lockwasher under the nut was not compressed (1/32" gap) against the Belleville
washer.
The support platform (battery rack) for vital battery lA was noted to have two
loose bolts (lockwasher not compressed and locking) on the end piece at cell
18.
The same condition was observed at cell 43.
Based upon the above observations, the team concluded that electrical work
practices and control, and the attendant quality control inspections, were an.
implementation weakness and required strengthening.
In each of the above
cases, the licensee immediately initiated the appropriate station deviation
report and work request to correct the adverse condition.
Material conditions of panels:
During system walkdown inspections of 120 volt AC and DC vital panels, the
inspection team noted occasions of dirty panels and poor material conditions
as follows *
While observing troubleshooting for ground faults in the vital 125 volt DC
distribution system, the team noted that the U-1 480 volt and 4160 volt
Breaker Test Panels (fed from 120 volt vital DC via cable 1B63) contained
significant amounts of trash and dirt. Numerous parts bags, several screws,
cut tie wraps, and cut wire ends were found in.the 480 volt test panel.
The
insulation on one wire run was badly frayed, not tie-wrapped, and not properly
stood off the panel frame to prevent chaffing on the door edge (after
repositioning the wire run, the ground improved significantly). One of two
hinge pins in the panel door was missing.
An un-numbered "Rod Control Signal Circuit" connection box, immediately
adjacent to the U-1 480 volt Breaker Test Panel, was missing one of four cover
screws in the gasketed cover plate, thus the box was not properly sealed
against moisture intrusion (immediately corrected).
55
U-1 125 volt DC distribution '.panel lB was extremely dirty and contained cut
tie wraps, discarded danger ~ag pieces, and numerous pieces of conduit Sealant.
Several improper nuts were used (acorn type nuts apparently lost) to hold the
cover panel captive. Panel 1-2 (125 volt DC.fed from lB) was also dirty,
containing screws, cut cable ties, tape, cut wires, and a case (panel) nipple
on top of the panel.
Similar conditions were observed in the 120 volt AC vital panels. Vital Bus
Distribution Panels 1-IA and 1-IIIA were found dusty (from concrete), dirty
with metal shavings from drilling, and contained cut tie wraps and wire ends.
In addition to dirt, Vital Bus 1-1 contained numerous pieces of excess
expandable foam (fire barrier material) in the panel bottom.
Panel 1-1 was
also missing two knockout plugs (one top, one side); Semi-Vital Bus Dist Panel
lSVBl was missing a knockout plug from the panel top.
Based upon the above observed material conditions, the team concluded that
the licensee's program and implementation for control of housekeeping during
electrical maintenance in 120 volt AC and DC panels constituted a program
weakness.
Improper terminations:
In addition to the adverse material conditions observed, the team noted several
instances of improper terminations as follows.
The U-1 480 volt Breaker Test
Panel (fed from vital 120 volt DC) had two wires in one wire run with lugs
bent over more than 90 degrees of crimp angle.
U-1 125 volt DC distribution
panel 1-2 had several unlabeled spares that were not correctly terminated
(bent over, loose wrap of electrician's tape). Several examples were noted of
excessive insulation cut back at the breaker feed cable (1/4
11 vice required
1/32
11
) and not all wire strands captured under breaker terminating clamp
(e.g., 125 volt vital DC panel 1-2, breakers 11 & 15, and 120 volt vital AC
panel 1-IIIA, breakers 3 & 5). Excessive insulation cut-back in 125 volt
vital DC panel lB had permitted the wire strands on one feed cable to splay
apart, potentially permitting strand breakage. Although the team recognized
that some of the above conditions may have existed since the plant was
constructed, there were also occasions of modifications that could have
permitted correction of the deficient conditions. Current practices were
clearly defined by the requirements of NUS-2030, Specification for Electrical
Installation for Surry Units 1 & 2, Category Safety Related in Secti,on 5, that
addressed termination requirements.
Based upon the above adverse conditions,
the team concluded that the licensee's ~rogram and implementation for control
of standard practices during electrical maintenance in 120 volt AC and DC
panels constituted a program weakness.
3.p. PERFORMANCE OF MAINTENANCE TRENDING
The team noted that the primary vehicle for reporting conditions adverse to
quality was the Station Deviation Report. Procedure SUADM-LR-13, dtd 29 Dec.
1989, Station Deviation Reports, provided detailed instructions for initiating
and processing Deviation Reports.
The team noted that the system was applic-
able to both safety related (SR) and non-safety related (NSR) components,
-*
56
systems, materials and services. The team's review of program criteria and
actual deviation reports (DRs) indicated that the threshold upon which station
personnel based their decision to prepare deviation reports was low.
During
1989, approximately 4,000 reports were initiated and evaluated.
Root Cause
Evaluations (RCE) were initiated based upon the significance of the deviation
report.
The licensee had recently implemented the Component Failure Evaluation (CFE)
Program (SUADM-M-48, dated 29 December 1989) as a direct adjunct to the
station deviation reporting system. A station deviation would normally set
the CFE program into motion for all SR component failures (except MOVs which
were handled separately under the MOV program).
NSR component failures were
evaluated under the CFE program when directed by management.
The CFE program
was designed to perform evaluations that did not require the extensive degree
of investigation necessary in the RCE program.
Since the CFE program had just been initiated, approximately twenty
evaluations had been completed.
The evaluati~ns were comprehensive, and
appeared to provide an adequate basis upon which a meaningful trending program
of component failures could be based.
Trending of station deviations has become more effective during the latter
half of 1989 with increased attention and staffing by the responsible station
group.
Monthly trend reports on station deviations have been issued that
depict major categories, such as procedure errors, personnel errors, EDGs,
pumps, and valves.
The level of detail in the trend graphs required
interested parties to review specific categories of deviations to formulate
plans of action.
Each monthly report also focused on the details of a
particular category; e.g., the December 1989 report, published in February
1990, focused on types of personnel errors for the whole 1989.
In the
maintenance area, 187 deviations were written, of which:
54 DRs involved valve maintenance
37 DRs involved pump maintenance
57 DRs involved procedures not processed correctly
82 DRs involved inadequate maintenance (e.g., wrong part, wiring not per
specification, not correctly installed)
Insufficient data history had been collected to permit trending of the above
types of data, although the licensee was moving in that direction. * Programs
had been implemented on a case basis in response to the initial DR(s) to
_correct the above types of problems - trending of the data could be used as a
tool to determine program effectiveness.
Based upon the above observations, the team concluded that the licensee had
implemented an adequate program for trending of maintenance problems.
Continued data collection and evaluation was required to determine the
program's effectiveness.
57
3.q. TOOL AND EQUIPMENT CONTROL
The team found three tool issue points in use; the primary tool issue point was
in the upper level of the condensate polishing building, and the contaminated
tool issue point (Auxiliary Tool Room) was located on the 45' level of the
Auxiliary Building. A third issue point was located outside the power block,
and was used as a construction issue point.
Tool inventory control was adequately coordinated between the issue points.
Cognizant division supervisors were responsible for notifying the tool room of
tool requirements.
The team observed evidence of supervisors properly fore-
casting tool requirements for forthcoming maintenance activities. Positive
inventory control resulted in approximately one or two demands per day for
devices that were not available at the issue point. A strength worthy of,.note
was the issue room's control of special tools and devices.
On each occasion
of acquiring, through manufacture or purchase, an unusual device or tool for a
special application, a photograph has been taken of the device, and its special
storage location annotated on the photograph.
Positive control of these
devices has been maintained, and workers seeking special tools simply have to
"thumb through
11 the book of photos until the desired device was located.
Rotating tools such as air grinders and electric drills were on a comprehensive
preventive maintenance program that included items such as lubrication checks
and ground fault checks.
Evidence of the checks having been done was attached
to the tool. The team noted that slings, cables, chain falls, etc. were also
subjected to periodic testing; distinctive colored tape was used to mark the
device when next due for test. A unique serial number for each device was also
attached by tag that permitted test tracking.
One nylon sling was noted by the
team to be in a ready-to-issue bin with no evidence of having been properly
tested.
Electrical and mechanical M&TE devices were found stored in a segregated area.
Positive control of issue and return was maintained, and included tracking of
the work order on which the M&TE device was used.
No effort was made by the
licensee to assure proper calibration of any returned device unless problems
were reported by the user. A complete engineering evaluation was performed
for the situation of a device failing calibration when tested at its normal
cycle. The team noted several micrometer adjustment type torque wrenches that
were stored in ready to issue bins at high torque values. The licensee advised
the team that manufacturer recommendations required setting the wrenches at 20%
of full scale, but these requirements had not been incorporated in procedures
governing operation of the tool room, in torque wrench calibration procedures,
nor posted in conspicuous locations where wrenches were stored. Manufacturer's
recommendations concerning exercising torque wrenches prior to calibration were
also not included in procedures.
Based on the above observations, the team
concluded that although the overall program for tool issue and control was
adequate, several program and implementation improvements should be considered *
'.
58
3.r. SUPPORT INTERFACES
One of the most detrimental conditions concerning the performance of mainte-
nance is the lack of coordination between the support interfaces. Maintenance
support interface problems are predominately with the following departments:
Planning, Scheduling, and Operations.
In addition, the material control for
parts is an area that significantly contributes to the Maintenance Department's
backlog.
In these areas, the team did not find fault with any individuals or
. managers.
The personnel were cooperative with each other and recognized the
limitations of the programs within the plant.
Planning
The team concluded that the Planning Department was not capable of performing
all planning functions independently because it was not adequately staffed.
Consequently maihtenance personnel, foreman and craft, have the added burden
of supporting planning.
For example, there is one permanent electrical
planner, one or two contractors, and two borrowed electricians to perform all
electrical planning.
The permanent _electrical planner spends considerable
time coordinating with scheduling and at the plan of the day (POD) meetings.
Since maintenance personnel support detail planning, this contributes to the
problems of maintenance. Maintenance personnel are required to interface more*
and are not performing their primary function of doing corrective and
preventive maintenance.
In addition, the team does not consider the
Maintenance Department adequately staffed to perform their main function,
reduce the backlog, do detail planning,*and provide craft to the Planning
Department.
Other planning issues are discussed in Section 3.g. and 3.m.
Schedulina
The team did not identify any specific problems with the Scheduling Department
or the schedule.
However, it was recognized that the "plant wide single train
method" is not used for scheduling.
The plant wide single train method is:
only work on equipment in a specific single train is scheduled for a specific
time period (day, etc.).
No other work in the other train(s) is allowed.
Since the licensee does not use the single train method, Operations has more
of a burden in controlling and approving work.
The main problem is schedule adherence.
The Scheduling Department provides
30, seven, four, and one day schedules.
Every day there is a POD meeting for
the next day's scheduled work.
During the periods when the team was onsite,
approxi'mately 40 percent of the POD scheduled work was actually started or
performed. * The licensee's statistics for POD effectiveness is as follows:
Month *
Department
Percent Effectiveness
--
Dec.
14%
Dec.
Electrical
64%
Jan.
22%
Jan.
Electrical
68%
,.
Month
Jan.
Feb.
Feb.
Feb.
Department
Mechanical
Electrical
Mechanical
59
Percent Effectiveness
61%
55%
74%
41%
Maintenance personnel stated that they were frustrated with the large number
of last minute cancellations of work already scheduled and approved at the POD.
During the inspection period, the team did not find any evidence that this
situation would be corrected.
Operations
The Operations Department is responsible for approving maintenance activities.
Through observation and discussions with maintenance personnel, the team
identified the method used to implement this approval as the major "bottleneck'
1
in the coordination of planning and scheduling maintenance. A shift supervisor
located in the control room annex reviews and approves work activities that
have already been scheduled during the POD.
Included in these duties are
reviewing and approving revisions to work orders and procedures. These* duties
of the shift supervisor are necessary for safe plant operation. However, the
method and time of implementation was found to be inefficient. The plant
work schedule for maintenance craft is from 7:00 a.m. to 3:30 p.m. daily
except for a skeleton staff on back shifts. Operations, including the shift
supervisor, isolate themselves during the period of 7:00-8:30 a.m. and
11:00 a.m to .1:00 p.m. daily. During this "quiet time" (3-1/2 hours) daily,
all maintenance activities requiring support and/or approval from Operation
before proceeding is placed on hold.
During the 7:00-8:30 a.m. "quiet time,"
POD scheduled items may be "deferred" and maintenance is not made aware of this
until after 8:30 a.m.
The same holds true for the 11:00 a.m.- 1:00 p.m. "quiet
time" period. Operations has assigned a SRO representative to coordinate with
planning and scheduling (POD).
This SRO interface does not appear to function
very well since the shift supervisor at the control room annex can override the
POD.
Discussions were held with Operations concerning the coordination problems
already discussed. Operations is aware of these problems, wants to correct
them, and plans to assign more li~ensed operators to each shift as soon as
they become available (late 1990).
Conclusion
The team concluded that coordination problems between the departments must be
resolved for the licensee to implement an effective maintenance program and
reduce the large backlog. Material control problems have been previously
identified by the NRC and INPO in other reports.
The team was told that lack
of spare parts continues to be a significant problem area *
..
..
60
3.s. LICENSEE REVIEW OF COMPLETED WORK RECORDS
To-evaluate the licensee's review of completed work documents the team
examined four completed WOs, evaluated the QA review process and reviewed the
the procedure for the QA review.
The team reviewed four completed WOs (79205-01-CH-MOV-12750,
535128-02-CH-MOV-2275A, 83923-02-SI-MOV-2867C, 65954-01-RS-MOV-1558 and
72503-02-CH-MOV-2289A) related to the work performed on Motor Operators.
WO 72503 documents the work activities performed on 92-CH-M0-2289 (charging
pump to regenerative heat exchanger stop valve).
Work performed was documented
on Procedures MMP-C-MOV-178 dated September 20, 1988 and October 21, 1988.
One
of items replaced was the
11Hypoid Gear.
11
The Hypoid Gear is listed as part
number 12 in the Limitorque vendor manual for SMBOO.
However, the above
procedures, on page 36, illustrated the assembly of SMPOOO of drive shaft and,
therefore, the replacement of the Hypoid Gear was not adequately captured i.n
the records.
The cognizant maintenance support engineer gave sufficient expla-
nation to the inspection team and produced evidence to support that the Hypoid
Gear was in fact replaced and the completed WO inadequately documents the
replacement.
QA reviewed this WO and determined it complete and acceptable.
The team reviewed the completed WOs related to the replacements of solenoid
operated valves (SOVs) to extend the longevity of the qualified lives of the
equipment.
The useful life of the SOVs were calculated to be 42 years taking
into consideration the environment (temperature and radiation) in which it *
(the SOV) is located. The following packages were reviewed: WO 71612;
WO 71613; WO 71564; and WO 71567.
WO 71612:
Replaced the 02-MS-S0V202A - In Attachment 7, the WO# was left
blank.
The serial number of the replaced valve is documented as 77826T-2.
The
same number is documented on Page 12. This may be erroneous, because the team
observed that this was the serial number of the SOV installed on 02-MS-SOV-202B
during the performance of periodic testing of the Auxiliary feedwater turbine
on March 16, 1990.
Copies of Attachment 7 are circulated to corporate and
other management officials to denote the completion of EQ related work *
W0-71613:
Replaced the 02-MS-SOV-202B.
On Page 12 of the WO and in
Attachment 7, the serial number of the SOV is indicated as 778262t-l. The
team observed that the serial number on the SOV was 778262t-2 during the
observation of the periodic test of the Auxiliary Feedwater Turbine on
March 14, 1990.
WO 71564:
Replaced the 02-CC-SOV-205A.
On Attachment 7 of model number of
the SOV was not documented.
61
WO 71567:
Replaced the 02-CC-S0V-205C.
On Attachment 7 of the Model number
of the SOV was not documented._ A comment on the cover sheet stated that the
actua 1 stroke of the va 1 ve is l/8
11 1 anger than the design.
EWR wi 11 be
written. However, a EWR number was not identified.
The team reviewed three completed WOs documenting the work performed on NAMCO
type limit switches to extend the longevity of the qualified lives.
02-MS-2S2-201A, -201B, -ZS1-201C documented the work performed on the limit
switches on the mainsteam trip containment isolation valves.
No adverse
findings were identified in this area other than the observations in the
following paragraphs.
Evaluation of the QA Review of WOs
QA reviews 20% of the completed WOs utilizing procedure QADI 35C, Revision 4,
dated February 1, 1990.
The rest are stamped
11Noted
11 and filed. This review
is in addition to QC in-process verifications. Review of this procedure
including Attachment 6.1 indicates that QA is not required to scrutinize a
completed WO to ascertain if it is technically complete in all respects.
The
team discussed with the QA Manager and his staff the above findings. The QA
Manager was responsive to the team concerns that technically incomplete and
incorrect WOs may be erroneously accepted as acceptable documents.
The QA
Manager assured the inspection team that he will consider implementing the
following measures:
Develop an adequate checklist which will reflect the salient steps
verified.
Provide sufficient input to the
11Procedure
11 writing group to retain only
the relevant information in a given procedure which is applicable to the
specific work being performed
Train QA reviewers to review the first few completed WOs prior to
resorting to sample reviews.
Examination of QA Procedure for the QA Review.
The team reviewed several completed WOs including those identified in above
paragraph in this section and observed the following weaknesses:
The procedures contained more general
11nice to have" than specific "need
to have
11 information, thus making the WO n10re voluminous.
The description of the work performed (on the cover sheet) did not
adequately describe the accomplishment *
62
If cable splicing was required, the WO should document that the cables
were crimped, bolted or terminated.
The engineers should determi.ne the
size of the conductors and specify the connection method.
If* replacing a SOV, the WO should state if the existing CONAX connector
was retained, or a new CONAX connector was used.
Attachment 7 for SOV WOs are used by licensee management to demonstrate
that EQ is current.
As such, the information on Attachment 7 should be
complete and accurate.
Procedures MMP-C-MOV-178, dated September 8, 1988 and October 21, 1988,
used to reflect work performed on SMPOO type Limitorque operators should
have a note on pages 3b and 37, respectively, to indicate-that the
illustration (SMPOOO) provided on those pages were incorrect.
The summary in WOs for limit switch (LS) related activities should
precisely state if the LS was replaced or if only the gasket covers were
replaced.
The exact torque valve to which the bolts (screws) were
torqued to should be stated.
4.
Evaluation of Maintenance
Summary Rating of Maintenance Process
Program:
SATISFACTORY
Implementation:
SATISFACTORY
The evaluation completed by the NRC team rated both the Surry maintenance
program and its implementation SATISFACTORY
The Surry maintenance rating was obtained by collating and assessing the
maintenance team inspection findings iri a special maintenance inspection logic
tree. The tree completed for Surry maintenance inspection is depicted in
Appendix 3.
The tree divides maintenance evaluation into three "parts" (I,
II, and III). The parts are divided into eight "areas" (1.0 through 8.0) and
the areas into individual maintenance topics or "elements" (1.1, 1.2, 2.1,
etc.). Based on their inspection findings (negative and positive), the team
established ratings for most of the elements. Subsequently, area ratings were
determined based on associated element ratings; part ratings based on the
associated area ratings; and, finally, a total_maintenance rating was
determined from the ratings for the parts. The team did not weight all
findings or ratings equally. *
.
)
63
Four rating categories were used and a color was assigned to each to aide in
displaying the ratings on the maintenance inspectiori tree. The rating
categories were as follows:
11Good
11 Performance (Green)
11Satisfactory
11 or
11Adequate
11
Performance (Yellow)
11Poor
11 Performance (Red)
(Blue)
Overall, better than
adequate, shows more than
minimal effort; can have a
few minor areas that need
improvement
Adequate, weaknesses approximately
offset by strengths
Inadequate or missing
Not evaluated or Insufficient
Information to Evaluate
Each part, area and element, as well as overall maintenance, is represented by
a block on the tree. Most of the blocks are split into two parts with the
upper portion representing program or process and the lower half representing
implementation.
The exception is for the part I blocks which are not
considered to have separate programs or implementation.
The parts and areas of the maintenance inspection tree are described below.
The inspection findings that contributed to the ratings are also given.
Individual element ratings are not described but are shown in Appendix 3.
4.a. Overall Plant Performance Related to Maintenance (Tree Part I)
Rating:
Satisfactory
This part of the tree is an overall assess~ent and rating of maintenance
through direct measures:
Its rating was based on the SATISFACTORY rating
determined for
11direct
11 measures below *
.. 4.a(l)
_Direct Measures (Tree Area 1.0)
Rating:
SATISFACTORY
The direct measures used to assess this area are the plant historic data
(tree element 1.1) on the performance of the operating units and observations
of housekeeping and material conditions observed in walkdown inspections
(element 1.2).
Historical Data Related to Maintenance
64
The team examined historical data for licensee's maintenance and maintenance-
related activities. The data covered the period from the beginning of 1989 to
present, plus some 5 year trends. The data reviewed was included in the
. Virginia Power Nuclear Performance documents issued on a monthly basis. The
data reviewed does not provide a totally accurate picture of the plants today
since both units returned to service from extended outages in the period
(Unit 1 - 7/89 and Unit 2 - 11/89). The results are mixed (some good and some
poor). The equivalent availability was poor at the beginning of 1989 and good
at the end of 1989 and to date in 1990 with a declining 5 year trend. The
forced outage rate was poor for 1989 and good to date for 1990 with an upward 5
year trend. The number of unplanned reactor trips was good to date for 1990
with a mixed (declining for Unit 1 and upward for Unit 2) 5 year trend. The
number of ESF actuations was mixed (good .for Unit 2 and poor for Unit 1) for
1989 and good for both units to date for 1990.
Radiation exposure was poor for
1989 and good for the beginning of 1990 with an improving 5 year trend. The
corrective maintenance backlog was excessively high for 1989 and appeared
to continue trending upward for the beginning of 1990.
In review of licensee
reports, i.e., LERs and r~ctor trip reports, for indicators such a unplanned
trips and ESF actuations, there was no conclusive evidence indicating
maintenance problems contributing to the events.
The findings of the team's evaluation of the historical data and the walkdown
inspections consisted of numerous minor discrepancies.
Examples are noted in
Section 2.a,b,c,etc. above.
On the basis of the number and significance of
the discrepancies observed the team rated the area SATISFACTORY
4.b Management Support of Maintenance (Tree Part II)
Rating:
Program:
SATISFACTORY
Implementation:
SATISFACTORY
This part of the tree is an assessment and rating of areas of the tree which
represent management's support of maintenance through their commitment and
involvement, organization and administration, and provision of technical
support for the maintenance process.
4.b(l)
Management Commitment and Involvement (Tree
Area 2.0)
Rating:
Program:
SATISFACTORY
Implementation:
SATISFACTORY
65
This area consists of upper management's direct encouragement and promotion of
improvements in maintenance.
The rating of the program and implementation was
based on the following findings of strengths and weaknesses:
The STRENGTHS noted in this area included:
Management commitment to industry initiatives is good
MOV program is good,
System engineer program very strong (2.e)
Manager of engineering performed weekly walkdowns with a system engineer
(2.d)
The WEAKNESSES noted in this area included:
Problems identified in NRG Information Notices and industry communications
not available to working level people
Goal achievement not good (performance indicators)
Recognition and response to adverse performance indicators slow
Response to QA findings not always timely (2.c & 3.e)
Observations in this area included:
Reliability centered maintenance program not embraced
Self assessment performed late
189
Plant participating in EPRI plant aging program
Plant PM upgrade program
Procedure Upgrade Program
MOV program upgrades
Training Program is INPO accredited
4.b(2)
Management Organization and Administration
(Tree Area 3.0)
Rating:
Program:
SATISFACTORY
Implementation:
SATISFACTORY
This area consists of management's support of and involvement in the control
of maintenance through developing and implementing a maintenance plan setting
goals and policies; allocating resources, defining maintenance requirements,
monitoring performance, providing document control and determining the need
for improvements to plant material condition. Its rating was based on the
following strengths and weaknesses:
The STRENGTHS noted in this area included:
Instructors from NTD required in plant
Supervisory span of control is good (2.a & 2.h)
NO sacrifices of safety are made to meet production goals
- '
,.,
..
66
Predictive maintenance, oil and vibration analysis is good (2.a)
Post maintenance debriefs addressed possible additional requirements
Post maintenance debriefs for I&C group effective in identifying problems
and carrying forward to subsequent maintenance.(2.e)
Verbatim compliance by I&C technicians absolute - many changes had to be
initiated to make procedures fit the tasks. (2.e)
Corporate driving force in replacing SOVs to maintain EQ currency, and
causing existing MOV re-inspection
The WEAKNESSES noted in this area included:
Some systems such as IA and HVAC are not goal oriented for required
system improv_ements - evidenced by lack of commitment (3. f)
No visfble evidence of special maintenance department goals and
objectives.
Elect/Mech planning does not have adequate staffing, planning a function
of the craft (2.e, 3.g, 3.r)
Maintenance manpower inadequate (especial HVAC) (3.f)
Periods of no shift coverage by I&C - call in (2.e)
Maintenance often delayed due to non-availability of material (3.r)
Corrective maintenance backlog trend is upward (3.m)
Mairitenance often delayed, not supported, due to "quiet time" in control
room (3.r)
I&C manning not able to support full implementation of PM program
Current PMT program very limited for equipment other than ASME Section XI
(3.h)
Procedure for Predictive Maintenance is outdated (2.a)
Some electrical PMs deferred due to lack of manpower (2.d)
Appropriate Vendor PMT not accomplished (3.i)
Vendor tech manual requirements not implemented (AFW, motor starters PMs,
containment instrument air dryer filter) (2.d & 3.c)
PM program for HVAC limited (2.g & 3.f)
PM program for instruments other than Tech Spec required items was not
prepared or performed (e.g., EOG safety functions for alarm in CR,
pressure gage on N2 back-up to IA for AFW MS inlet FCV (3.1)
Persons specifying electrical PMT are not qualified (3.h)
Persons specifying electrical PMT inconsistently require varying PMT (or
none at all) for the same equipment. (3.h)
ASME requirements related to check valve performance have not been
incorporated in IST program (MS to AFW & IA)
PM deferral rate for
189 was not correctly counted to. provide
representative information. (3.m)
Drawings not updated following plant modifications (3.b)
Drawings not equal to plant as-built (2.a & 3.b)
"For ref only" drawings used in Trouble Shooting, preparation of procedure
revisions, and plant operations decisions (Rx protection system relay
fa i 1 ure) * ( 2. e)
2 occasions of Procedure Action Request (procedure change) not completed
accurately (1 time full,y signed off/1 time error detected by Shift Sup
prior to implementation). (3.b)
..
~---
-
67
Mods to plant procedures and equipment are not considered in a timely
manner (3.f &3.1)
Procedure for preparation and completion of Work Orders*does not contain
adequate detail.(3.g)
Resistance to dedicating adequate funds to replace/adequately repair
system *components (use band-aid repairs too frequently) (3.f)
OPs (operations) control of maintenance shifts work priorities too easily
Observations in this area included:
Maintenance plan has been prepared and in effect
The utility has been forced to utilize contractor support for maintenance
dept and system eng support because of inability to maintain permanent
staff
Thermography predictive analysis program not initiated
PM program undergoing Task Force review
Source documents that could change maintenance requirements are
problematically covered .
. Trend INPO performance indicators
Evaluating each SR work order for root cause problems (Component Failure
Evaluation Program - CFE), initiated Jan 90. Should be an effective
program.
Bi-annual review of maintenance procedures was accomplished (occasionally
not effective, inst. cal proc)
Computer based (WPTS) document control system is used for work orders.
1,7,30 day look ahead attempting to coordinate dept activities.
4.b(3)
Technical Support (Tree Area 4.0)
Rating:
Program:
SATISFACTORY
Implementation:
SATISFACTORY.
This area encompasses the various elements of technical support that are
needed for maintenance to function effectively (e.g., engineering support,
health physics, QC, risk assessment, etc.). Its rating was based on the
following strengths and weaknesses:
The STRENGTHS noted in this area included:
Close liaison existed between system eng and craft.(2.d & 2.e)
Internal/corp. communication channel provided timely exchange of info
Strong involvement from system engineers in their respective
systems (2.a & 2.e)
68
EQ program well supported by corporate and engineering
MOV/Check valves/PM programs good eng support
Procurement and maintenance engineering must approve each part
procurement action.
Elect procedures include many hold points for QC sign-off (2.d)
Performance inspections by QA people (Quality Performance Group)
effectively augmented the maintenance process
Worker awareness of ALARA concerns was high
Advanced Rad Worker quals for QMT workers provided the ability to
perform work that otherwise would have required continuous HP coverage
Recovery of contaminated areas strong program
HP aggressive in identification of sources of contamination
Craft exhibited strong safety consciousness.
Overall HP program continues to improve
Licensing group was strong
Commitment tracking system was good
The WEAKNESSES noted in this area included:
Communications between craft (maint. dept.) and operations were not
optimum for completion of scheduled maintenance activities. (3.m)
Risk assessment was not considered in prioritization of work orders,
however at the implementation level, consideration was given
to safety risk for not accomplishing work. (3.m)
QC procedure for review of completed work order packages is inadequate
Generic letter commitment on Instrument Air poorly handled
Observations in this area included:
Current PMT program is written exclusive of most tests for non-ASME
Section XI equipment.(3.h)
PMT not well defined (3.h)
Persons specifying electrical PMT are not qualified (3.h)
Engineering has not caused all PM requirements to be identified
(e.g., I&C) (3.1)
Many contractors to support engineering
System engineers located outside PA
Engineering analysis via Component Failure Analysis initiated Jan '90.
QMT members provided a high degree of quality control awareness, buf
quality control was frequently exercised by peers.
QC notified at start of all SR work orders
Guidance available for when QC inspection required.
Audit of maintenance dept on bi-annual basis
A
69
4.c. Maintenance Implementation (Tree Part III)
Rating:
Program:
SATISFACTORY
Implementation:
SATISFACTORY
This part of the tree is an assessment and rating of the work, organizational,
hardware and personnel controls necessary to proper implementation of
maintenance.
4.c(l)
Work Control (Tree Area 5.0)
Rating:
Program:
SATISFACTORY
Implementation:
SATISFACTORY
This area encompasses assessment of important elements of work control through
evaluation of maintenance in progress, work order control, planning,
scheduling, prioritizing, etc. Its rating was based on the following
strengths and weaknesses:
The STRENGTHS noted in this area included:
Good technician skills, knowledge, and abilities (2.e)
Good command and control of Periodic Te~t evolutions (2.d & 2.e)
Craft complied with procedures, and were attentive to necessity for
Procedural PARs
All craft assured task qualification proper prior to job start (2d)
Equipment history was readily available/accessible in the WPTS system
for post
184 events
Upgrade program for procedures was generally effective in improving
procedures when compared to pre-upgrade
PMT on periodic tests conducted by the Ops group were good.
The WEAKNESSES noted in this area included:
Clearance program could be improved in tagged position/restoration
position
Coordination with OPs for work accomplishment was poor (3.r.)
Completed work orders for replacing S0Vs to maintain EQ exhibited errors,
omissions and were cumbersome
Work orders occasionally lacked detail, relied heavily on skill of the
craft. (2.a, 2.d & 2.e)
Definition of special tools, special equipment, special people quals
was a function of procedural adequacy, not the work orders. (3.k., 3.g.,
3.n.
..
..
70
Mech/Elect/I&C planning did not have resources to perform detailed
planning - left up to the craft (2.e & 3.g}
I&C planning not integrated with the maintehance dept. - work order inst
were prepared by revising existing alignment procedures. (2.e)
Work instructions associated with the work package were in general very
limited for E and M craft.disciplines.
Programmatic prioritization scheme was time to complete dependent, not
safety of people, safety of equipment, or Tech Spec related. However,
implementation of priorities appeared to take the above types of
considerations into account.
Notwithstanding, many high priority work
orders were years old. Bottom line - no effective prioritization scheme
in effect.
Provision for modification of work item prioritization difficult once
assigned in WPTS, thus assigned priority may have been in error, but not
corrected (3.m)
Risk assessment was not considered in prioritization. (3.m)
Numerous Priority 1 work items were very old - driven by the
program ( 3 .m.)
Backlog of CM work orders has continued to increase in all categories, and
therefore backlog control must be ineffective (3.m)
Backlog CM average age is very old (3.m.)
Deferred PMs only recently brought under control (2.d)
Many (old) procedures did not specify required test equipment, or
tolerances, or acceptance criteria, or special tools.
Maint procedures (WO instructions) for replacing SOVs and MOV related
work were voluminous and cumbersome - not tailored to the specific
application and contained errors.
AFW turbine driven pump PT referenced the wrong Tech Spec requirements
(wrong para.)
Several fundamental instrument alignment procedures had not been initially
prepared and approved (PRT Temperature).(3.1)
.
Elect. Procedures frequently asked Ops to perform a step - if not
possible, N/A the step, (2.d)
I&C PT procedures did not adequately establish I/Cs, reference Tech Specs,
nor provide for exiting procedure in event of equipment failure (2.e)
Procedure for preparation and completion of Work Orders does not contain
adequate detail. (3.q}
Elect PMT was cancelled due to lack of manpower and the PMT was not
carried forward as overdue (2.d)
Current PMT program very limited for equip other than ASME Section XI
(3.h)
Persoris specifying electrical PMT are not qualified (2.d & 3.h)
Persons specifying electrical PMT inconsistently require varying PMT (or
none at all) for the same equipment.(2.d & 3.h)
QC review of completed work orders were not effective in that the reviews
focused only on detecting missing information, not incorrect information.
In some cases, WOs with incomplete information were not detected.(2.e)
Incomplete and erroneous work orders on EQ SOV replacements
Work accomplished lacked adequate description (2.d)
,,.
71
Observations in this area included:
Foreman on the job presence good
Craft were attentive to resolution of problems encountered, but resolution
took inordinate amounts of time
Lifted lead/jumper program and implementation adequate.
Clear provisions for accomplishing emergency work
WPTS computer system provides adequate equip history for items of less
than 5 years age. *
Licensee had to go to off-site facilities for documents related to ASME
Code vessels (i.e, State of Virginia)
Coordinated scheduling of functionally related equipments is not
effectively performed for all disciplines.
1, 7, and 30 day look aheads attempt to perform Work Order coordination
Procedural upgrade program was improving quality of formal maintenance
procedures.
Numerous, minor administrative documentation errors in Work Orders were
detected that were not of safety significance.
4.c(2)
Plant Maintenance Organization
(Tree Area 6.0)
Rating:
Program:
SATISFACTORY
Implementation:
SATISFACTORY
This area encompasses the processes used by the maintenance organization to
control, support and direct maintenance activities. Its rating was based on
the following strengths and weaknesses:
The STRENGTHS noted in this area incl~ded:
All craft and foreman demonstrated good job skills (2.a, 2.d & 2.e)
Procedural adherence was good (2.e)
Unanticipated work problems promptly resulted in work stoppage, and
resolution initiated. (2.e)
Contractors in I&C area were required to meet same qualification
requirements as Surry people, including JPMs to perform plant work.
Contractors were under direct supervision and control of Surry
supervisors.
Contractors were required to operate under all applicable Surry
procedures.
Work request program was an easy, efficient means for any plant person to
identify and report deficient conditions, and was effectively used by most
plant personnel.
Station Deviation reporting system had a low threshold for reporting of
deviant conditions.
Review process provided for substantive evaluations.
(3.p)
System engineers were a visible support to the craft.(2.e)
,-
..
72
The WEAKNESSES noted in this area included:
120 v AC, 125 v DC vital panels contained trash, exhibited adverse
material conditions, and had improper cable terminations. (2.e & 3.o)
Vital station batteries exhibited some poor electrical work practices
after mods. (2.d, 2.e & 3.o)
PM program for HVAC _limited (2~g)
NSR 480 v panels contained excessive dirt and trash. (3.o)
Electrical foreman required to perform work order planning, thus reducing
- job site supervision and ability to initiate productive effort. (2.d)
Deficiencies such as leaks and missing fasteners not identified by
licensee.
(2.a & 3.d)
Deficiencies identified, but not tagged. (2.a & 3.d)
Tagging procedure is weak because of non-definitive requirements (3.d)
Operations support of work order initiation/commencement was inefficient
for at least three hours per day, including from 1100 - 1300. (3.r)
Coordination with OPs for work accomplishment was poor (3.r)
Operations group did not support all attributes of the M&TE program. (3.k)
Observations in this area included:
Contractors were utilized as system engineers.
Necessary clearances and work qualifications were not effectively
planned
I&C contractors met few job qualification requirements, therefore they
were on site for several months before they became an effective
contribution to the I&C group - matter of fact, they were a burden
(e.g., escort requirements)
Program is in its infancy for most maintenance trending programs (3.p)
CFE program initiated in Jan 1990 (3.p)
4.c(3)
Maintenance Facilities, Equipment and
Material Controls (Tree Area 7.0)
Rating:
Program:
SATISFACTORY
Implementation:
SATISFACTORY
This area encompasses the plant maintenance facilities, equipment and material
controls with regard to the part they play in supporting the maintenance
process. Its rating was based on the following strengths and weaknesses:
The STRENGTHS noted in this area included:
I&C, Mechanical supervision co-located with the craft.
Procedures, technical manuals, and M&TE were co-located with the I&C craft
Individual, lockable work space was provided for each I&C technician.
73
The M&TE lab was located in the I&C spaces - was clean and well
maintained, well organized,,but small. (3.k)
NTD laboratory facilities very effective, but not all planned equipment
installed.
Material storage was observed as a strength
The WEAKNESSES noted in this area included:
Material control program was informally implemented by checklist.
Increased material usage scrutiny (material dedication program) caused
excessive delays in initiating maintenance activities, e.g., HVAC. (2.g &
3. f)
,
.
.
Material procurement system was extremely cumbersome.
Inventory of spare parts in some cases (HVAC) was zero. (3.f)
Licensee unable to perform calibration of contaminated M&TE. (3.k)
Storage and recall program/implementation very weak for Ops. (3.k)
Range and characteristics of M&TE not readily available to technicians
(problem because the procedures do not contain required instruments, and
the techs have to perform the evaluation). (3.n)
Test instrument racks secured by large chains to meet seismic restraint
requirements could damage delicate instrumentation. (3.k)
Observations in this area included:
Welding and ma~hine shop areas were found to be small.
Welding of consequente was farmed out to contract personnel.
Mechanical hot shop not available, temporary tents set up for that kind of
work.
Tracking of M&TE used documented in work orders.
Many items of M&TE had a record accompanying the device showing its use.
Evaluation program in place for M&TE failing calibration *
. M&TE Entire program run manually by one person with no --trainee.
4.c(4)
Personnel Control (Tree Area 8.0)
Rating:
Program: GOOD
Implementation: SATISFACTORY
This area encompasses staffing controls (.personnel policies, turnover
minimization, shift coverage, etc.), training, testing and qualification and
the overall current status of personnel (actual turnover rate, extent of
.,
74
personnel trained and qualified~ drug problems, etc.). Its rating was based
on the following strengths and weaknesses:
The STRENGTHS noted in this area included:
Range and span of control of supervision was good.(2.a & 2.e)
Crews are maintained stable (roll together on watch)
Training program INPO accredited.
Strong apprentice training program.
Strong feedback program on training effectiveness.
Required quarterly hours for instructors in plant was high.
Apprentice motivation was high to complete training steps (increase
in pay, peer approval).
The WEAKNESSES noted in this area included:
I&C tech coverage not available 24hrs/day (2~e)
Staff not at full complement for I&C and electrical (2.e)
Backlog is high for mechanical and electrical (2.d & 3.m)
Many craft members pulled for Temporary Assignment (2.d)
I&C not totally integrated with the Maint Dept (2.e)
Craft not always in compliance with security measures (tailgating). (3.j}
Observations in this area included:
Craft foreman could readily (and did) determine individual qualification
status for craft assignment to particular job tasks. (2.d)
Use of contractors in the I&C area to cover staff shortfall was partially
effectiv1=.
10% of I&C production time was devoted to recurrent training.
Qualification process included oral, written, and performance
examinations.
5.
Exit Interview
The inspection scope and results were summarized on April 12, 1990, with those
persons indicated in Appendix 1.
The team leader described the areas inspected
and discussed in detail the inspection results. Proprietary information is
not contained in this report. Dissenting comments were not received from the
licensee.
(Open) Violation 50-280,281/90-07-0l:
"Failure to Follow Procedures for
Maintenance" paragraphs 2.e., 3.b., 3.i., and 3.k.
(Open) Unresolved item 50-280,281/90-07-02:
11 EDG Day Tank Fuel Transfer Line
Analysis" paragraph 2.f *
y
Licensee Employees
APPENDIX 1
PERSONS CONTACTED
- R. Allen, Operations Maintenance Coordinator
- R. Benthall, Supervisor Licensing
- M. Boling, Asst. Plant Manager North Anna
- D. Christian, Asst. Plant Manager for Operations and Maintenance
- J. Downs, Power Planning
- D. Erickson, RP Superintendent
- A. Friednman, Superintendant of Nuclear Training
- E. Grecheck, Asst Plant Manager for Licensing
- R. Gwaltney, Superintendent of Maintenance
M. Hadduck, Supervisor Electrical Maintenance
- D. Hanson, Supervisor .of Maintanance Support
- E. Harrell, Vice President for Nuclear Operations
- D. Hart, Supervisor QA
- M. Kansler, Station Manager Surry
- A. Keagy, Superintendent Materials
- H. Miller, Director Maintenance Support - Corporate
- F. Mone, Planning
- R. Saunders, Manager Licensing
- R. Scanlan, Licensing Engineer
- E. Smith, Manager QA
D. Snoddy, Supervisor Mechanical Maintenance
- R. Thornsberry, Planning
- G. Tompson, Suprervisor Maintenance Engineering
- J. Winebrenner, Supervisor Procurement Engineering
- F. Walking, Nuclear Operations Support
NRC Personnel
- W. Holland, Senior Resident Inspector
- C. Julian, Chief Engineering Branch
- S. Tingen, Resident Inspector
- Attended Exit Interview on April 12, 1990
.....
ADM
ANSI
B & PV
BKR
cal
CD
CFE
CFR
cpm
CROM
cs
cw
deg
dept
DR
EOG
GL
GPM
hp
hrs
Hx
!AW
IN
!SI
!ST
JN
LCO
LER
APPENDIX 2
ACRONYMS AND INITIALISMS
Administration
Analysis and Evaluation of Operational Data
As low as Reasonably Achievable
American National Standards Institute
American Society of Mechanical Engineers
Boiler and Pressure Vessel
Breaker
Calibration
Compressed Air System
Chilled Water System
Component Failure Evaluation
Code of Federal Regulations
Corrective Maintenance
Condensate Polishing
Counts Per Minute
Control Rod Drive System
Containment Spray System
Commitment Tracking System
Degree
Department
Demonstration Power Reactor
Deviation Report
Electric Power Research Institute
Environmental Qualification
Engineered Safety Feature
Engineering Work Request
Generic Letter
Gallons Per Minute
Health Physics
Horse Power
Hours
Heating Ventilating and Air Conditioning
Heat Exchanger
Instrument Air
In Accordance With
Instrumentation and Control
Information Notice
Institute for Nuclear Power Production
Instrument Society of America
- *
Inservice Inspection
Inservice Testing
Job Number
Limiting Condition for Operation
Licensee Event Report
Loss of Coolant Accident
Appendix 2
NA
OMC
p. E.
PW
QMT
rad
rpm
Rx
SCARF
sov
SR
S/S
TS
VAC
voe
WPTS
WRC
2
Measure and Test Equipment
Motor Control Center
Motor Generator
Motor Operated Valve
Not Applicable
Non Safety Related
Operations Maintenance Coordinator
Professional Engineer
Preventive Maintenance
Post Maintenance Testing
- Pl an of the Day
Pressurizer Relief Tank
Performance Test
Primary Water
Pressurized Water Reactor
Quality Assurance
Quality Control
Quality Maintenance Team
Radiation
Reactor Coolant Pump
Radiation Monitoring System
Revolution per Minute
Reactor
Station Commitment Assignment/Response Form
Safety Injection System
Solenoid Operated Valve
Safety-Related
Senior Reactor Operator
Shift Supervisor
Technical Specification
Volts Alternating Current
Volts Direct Current
Work Order
Work Planning and Tracking System
Work Request
Work Request Card
I
.. -
....
TREE IN1TIA TORS
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s
s
s
s/s
............ -
s
_, ..
s/s
s/s
s/s
s/p
s/s
s/s
PRESENTATION TREE
MAINTENANCE INSPECllON TREE
.. -*
....... -
s/s
/s
p/s
p/s
s/s
p/s
s/s
n/g
s/s
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p
s
,co
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n = not inspected
g ...
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APPENou;- 3-~MONOCH,ROME,,
SURRY
.
.
REPORT. NOS. 50-280,281/90-07
g/s
MD*~ nae, &191.I b .. '11 b01
......
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425768-C