ML18151A092

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Enforcement Conference Repts 50-280/87-26 & 50-281/87-26 on 870826.Violation Noted.Major Areas Discussed:Control of Containment Integrity & Valve Alignment
ML18151A092
Person / Time
Site: Surry  Dominion icon.png
Issue date: 09/15/1987
From: Cantrell F
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18151A090 List:
References
50-280-87-26-EC, 50-281-87-26, NUDOCS 8710060067
Download: ML18151A092 (22)


See also: IR 05000280/1987026

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W.

ATLANTA, GEORGIA 30323

Report Nos.:

-Licensee:

50-280/87-26 and 50-281/87-26

Docket Nos:

Virginia Electric and Power Company

DPR-32 and DPR-37

Facility Name: Surry 1 and 2

  • Approved By:

SUMMARY

Scope:

An enforcement conference was held in the Region II Office on August

26, 1987.

Meesrs. J. N. Grace and L.A. Reyes opened the meeting by expressing

concern over the control of containment integrity and valve alignment as

discussed in NRC Inspection Report 280; 281/87-26 dated August 18, 1987.

Virginia Electric and Power Company then made a presentation covering an

overview, chronology of events, safety implications, corrective actions, and

the overall conclusions of the issues.

Attachment I to this report contains

information from the presentation.

Results:

One violation was identified in this report.

8710060067 870929

PDR

ADDCK 05000280

G

PDR

DETAILS

1.

Attendees

NRC:

2.

J. N. Grace, Regional Administrator, RII

L. A. Reyes, Director, Division of Reactor Projects, (DRP)

B. Uryc, Enforcement Coordinator

F. Jape, Test Performance Section Chief, Division of Reactor Safety (DRS)

W. E. Holland, Senior Resident Inspector, Surry

L. E. Nicholson, Resident Inspector, Surry

R. P. Croteau, Project Engineer, DRP

G. A. Schnebli, Reactor Inspector, DRS

S. E. Sparks, Reactor Inspector, DRS

C. P. Patel, Project Manager, NRR

J. G. Luehman, Office of Enforcement

Licensee:

J. L. Wilson, Manager - Nuclear Operations Support

N. E. Hardwick, Manager - Nuclear Programs and Licensing

D. L. Benson, Station Manager - Surry Power Station

E. S. Grecheck, Assistant Station Manager - Surry Power Station

J. A. Price, Quality Assurance Manager - Surry Power Station

Enforcement Meeting

Messers. J. N. Grace and L. A. Reyes opened the meeting by expressing

concern over the administrative control of containment integrity and valve

manipulations.

The events were discussed in NRC Inspection Report 50-280,

281/87-26 dated August 18, 1987.

Mr. J. L. Wilson, Manager - Nuclear

Operations Support, Virginia Electric and Power Company, gave a brief

introduction of the events.

Mr.

E.

S. Grecheck, Assistant Station

Manager, Surry, then presented an overview, chronology of events, safety

implications, corrective actions, and conclusions.

The first event involved the temporary repair of a defective weld in the

unit 2 letdown line between the inside containment isolation valve and the

cohtainment penetration. This event was discovered as a result of a step

increase in the reactor coolant system (RCS) unidentified leakage rate

noted on July 22, 1987.

The licensee isolated the leak from the the RCS

by utilizing excess letdown and subsequently temporarily repaired the

defect on July 28, 1987.

A system schematic and more detailed sequence of

events is contained in Attachment I.

3.

2

With respect to the safety implications, the hole in the defective weld

provided a direct path from inside the containment to the outside

containment isolation valve.

Subsequent calculations by the licensee

indicate that the total allowable leakage was not exceeded.

The licensee

stated that the operation of a drain valve between the weld defect and the

containment (2-CH-142

shown

on Attachment I) was

performed under

administrative control, and the operability of the outside containment

isolation valve was demonstrated.

The second event involved the discovery of four valves in the containment

leakage monitorirg system locked in an incorrect position.

An instrument

technician noted an apparent valve alignment problem while troubleshooting

a pressure transmitter and notified the control room.

Attachment I

contains a schematic and more deta i 1 ed sequence of events.

The va 1 ves

found open created a cross-connect between al 1 four containment pressure

transmitters providing signals to the consequence limiting system (i.e.

containment isolation, spray, etc.).

The licensee concluded that the safety consequences of the two events were

minimal.

Their analysis of the events did, however indicate programmatic

weaknesses in the documentation, administrative control, and station

safety committee areas.

Mr. Wilson concluded that a comprehensive

evaluation and enhancements in these areas will be achieved .

Conclusions

The licensee failed to recognize, evaluate, and control conditions which

resulted in a degradation of containment integrity.

These conditions

were:

Inadequate recognition, evaluation, and control

of containment

integrity with a weld crack in the unit 2 letdown line and the

outside containment isolation valve open.

Operation of a drain valve (2-CH-142) within the containment

isolation boundary of the system with the outside containment

isolation valve open.

Failure to evaluate the operability of the inside containment

isolation valves with indications that they may be leaking.

Routine opening of containment boundary valves such as 1-LM-40 with

no procedure control or operations involvement .

3

These findings *indicated that the programs for evaluation of containment

integrity and for admi n i strati ve contro 1 of the operation of containment

isolation valves were weak.

Failure to provide adequate procedural

control for activities affecting quality is identified as a violation

(280; 281/87-26-01).

Attachment:

Presentation Handouts

  • ATTACHMENT 1

VIRGINIA ELECTRIC AND POWER COMPANY

AUGUST 26 , 1987

  • Introduction
  • Management Analysis
  • Letdown Line Repair

-

Sequence of Events

-

Conclusions

  • LM Valve Alignment

-

Sequence of Events

-

Conclusions

  • Corrective Actions
  • Overall Conclusions

__ ._- ________ ._._ -

MANAGEMENT ANALYSIS

DOCUMENTATION

ADMINISTRATIVE CONTROL

SNSOC

LETDOWN FLOWPA TH

CONTAINMENT

IN

OUT

I

I

I

I

I

I

. HVC 2200A

I

I

I

I

2-158

LCV

LCV

HVC 2200C

I TV 2204

2-CH-159

2460A

24608

I

REGEN

I

I

I

NON REGEN

HX

HVC 22008

I

HX

L!...J

2-CH-142

07/21/87

SEQUENCE OF EVENTS

Letdown Line * Repair

Average Unidentified RCS Leakage

0.17 gpm

07/22/87 0600

Unidentified Leak Rate 0.57 gpm

Investigations in Progress

1330

Containment Entry

1530 . Leak at HCV-2200C Identified

07/23/87 1130

On Excess Letdown; Preparation for

Lagging Removal

1330

Pipe Crack Identified

  • Assess Containment Integrity and Repair

,.

SEQUENCE OF EVENTS

Letdown Line Repair

07/24/87 0930

Closed TV-2204; Verified Operability.

1200

Containment Entry to Drain Letdown Line

2-CH-142 Cycled

1633

Opened TV-2204 to Prevent

Pressurizing Line

07/26/87 1100

Containment Entry; Cycled 2-CH-142

07/28/87 1330

Entry to Install Temporary Repair,

Following Approval by SNSOC

(EWR 87-288)

2030

Charging and Letdown Back in Service

2128

VT-2 Inspection Satisfactory

.

07/29/87 0700

RCS Unidentified Leak Rate 0.27 gpm

>

SEQUENCE OF EVENTS

Letdown Line Repair

08/05/87 0210

Containment Entry Checks Temporary

Repair

0400

Furmanite Can Leak Reported as

15-20 ml/hr

1130

RCS Leakage .10 Unidentified

2230

Procedure for Re-inject Approved by

SNSOC

08/06/87 0040

Containment Entry; Noted Box Had

Moved 1/16"

Reinjected; Leakage Reduced

08/07/87 1720

Additional Clamp Installed per EWR

87-288A, ,

Leakage Stopped

TEMPORARY REPAIRS

  • Permanent Repair Evaluated

-

Failure Analysis Required

-

Weld Repair per ASME XI

  • Temporary Weld Repair

-

No Weld Procedure in Presence of Water

  • -

Sources of Water

  • Temporary Repair with Furmanite

-

Box* is Pressure Retaining Component

-

Sealant is Treated as Gasket

-

No Credit Taken for Strength of Sealant

  • Analysis

-

Seismic

..

TEMPORARY REPAIRS

Added Weight on Piping System

Assumed Crack Would Fail -

Added Piping Restraint

  • -

Temperature

Compound Rated to 604. Degrees F

-

Applicable Codes

Mechanical Joint with Gasket

Temporary Repairs not Discussed in ASME XI, IX, or

ANSI 831.1

..

LETDOWN LINE REPAIR CONCLUSION

'

  • Per T.S. Continued Operation Permitted with RCS Leak

Rate

  • Initial Consideration of Containment Integrity

-

Qualitative

-

Verified TV-2204 Operable

-

Subsequent Calculation Verified Leakage

within La

  • Drain Valve Opened Under Administrative- Control
  • No Direct Correlation Between RCS Leakage

and Appendix J Requirements

LEAKAGE MONITORING SYSTEM

PT

PT

J 1-LM-40

PT

J 1-LM-40

PT r~ IPT

1

I I

1-LM-28

I

I

1-LM-29

I

1-LM-30

I

1-LM-18

1-LM-31

T

SEQUENCE OF EVENTS

LM Valve Alignment .

. 08/03/87 1450

Instrument Technicians Troubleshooting

  • PT-CV-101A

.

Notify Control Room; Open 1-LM-40 to

Remove Suspected Moisture

Unexpected Transmitter Response;

Suspect Incorrect Lineup

Technicians Notify Control Room

2042 * Valve Position Logged as Closed

. *

SEQUENCE OF EVENTS

LM Valve Alignment

08/05/87 1300

Shift Supervisor and STA Disc9ver

Valves Locked Open

Immediately Closed

Determined 1-hour Reportable

08/13/87

Engineering Confirms Postulated Fai_lure *

is Passive

CLS Function was not Affected

LM VALVE ALIGNMENT CONCLUSIONS

  • Initial Determination of *Reportability Conservative
  • Line Up Consistent with Design Basis
  • Safety Consequences Insignificant

-

No Impact on Protective Functions or Containment

Integrity

  • All Valve. Misalignments Fully Investigated

' . *

COMPLETED CORRECTIVE ACTIONS

  • Reverification of All Locked Valves Outside

Containment

  • Interim Manag.ement Directive to Prohibit Opening the

Containment Boundary Not Specifically Listed in T.S.

3.8 without Prior SNSOC Approval

  • Expand SNSOC Minutes to Include Details of

Discussions as Appropriate

  • Conduct HPES Evaluation
  • Initiated QA Audit of Operations Administrative Controls

---

-

~~ ~-----------

CORRECTIVE ACTIONS

  • QA Audit of Operations Administrative Activities and

Programs

-

Special Audit

-

SRO on Team

-

Beyond Compliance

-

Exit with SNSOC

FUTURE CORRECTIVE ACTIONS

  • Enhance Operator Awareness

-

Revisions to Monthly Verification Program

-

Training Improvements

  • Enhance* SN SOC Review of Station Trends
  • Increase Station Supervision Sensitivity to Human

Performance

-

HPES Summary

  • Permanent Repair of Letdown Line by Next Outage

HUMAN PERFORMANCE EVALUATION SYSTEM

SIGNIFICANT PERFORMANCE OF TASK

Frequency of Event (0/o)

50

40

30

20

10

0

Frequency to

Detect Error

Misinterpretation

=---

= Industry

North Anna

IBSurry

Incorrect

Carryout of

Correct Action

Following

Procedure

Incorrectly

  • ~

OVERALL CONCLUSIONS

  • Safety Consequences of Both Events Minimal
  • Thorough Analysis of *soth Events
  • Comprehensive Actions Including

-

Identification

-

Programmatic Enhancements

.....

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