ML18142A559

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Insp Repts 50-280/85-19 & 50-281/85-19 on 850507-0603. Violation Noted:Failure to Implement Adequate QA Program for Design Change 81-103,which Upgraded Electrical Components in Containment
ML18142A559
Person / Time
Site: Surry  Dominion icon.png
Issue date: 06/18/1985
From: Burke D, Marlone Davis, Elrod S
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18142A557 List:
References
50-280-85-19, 50-281-85-19, NUDOCS 8507110799
Download: ML18142A559 (7)


See also: IR 05000280/1985019

Text

..

Report Nos. :

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W.

ATLANTA, GEORGIA 30323

50-280/85-19 and 50-281/85-19

Licensee:

Virginia Electric and Power Company

Richmond, VA

23261

Docket Nos.:

50-280 and 50-281

License Nos.:

DPR-32 and DPR-37

Facility Name:

Surry 1 and 2

Inspection Conducted:

May 7 - June 3, 1985

Inspectors: ~

0.... .\\?4 tp.

D.~Senior Resident Inspec~

~ ll. P1-M2

~

M~sident Inspector

Approved by: JJ ~- ~

.

fe-.r S. Eld/Section Chief

Division of Reactor Projects

SUMMARY

Date Signed

Scope:

This inspection involved 200 inspector-hours on site in the areas of

plant operations and operating records, environmentally qualified (EQ) equipment

installation, plant maintenance and surveillance, plant security, followup of

events and licensee event reports (LER).

Results:

One violation was identified in the area of EQ equipment installations,

failure to implement an adequate Quality Assurance (QA) program for Design Change 81-103, which upgraded electrical components in containment, paragraph 6 .

. . 8507110799 850625

-~

PDR

ADOCK 05000280

G

PDR

. ,.

.

REPORT DETAILS

1.

Persons Contacted

Licensee Employees

2.

3.

R. F. Saunders; Station Manager

D. L. Benson, Assistant Station Manager

H. L. Miller, Assistant Station Manager

D. A. Christian, Superintendent of Operations

E. S. Grecheck, Superintendent of Technical Services

D. Rickeard, Supervisor, Safety Engineering Staff

S. Sarver, Superintendent of Health Physics (HP)

R. Johnson, Operations Supervisor

R. Driscoll, Site QA Manager

W. R. Runner, Supervisor, Administrative Services

Other licensee employees contacted included control room operations, shift

technical advisors (STA), shift supervisors, chemistry, health physics,

plant

maintenance,

security,

engineering,

administrative,

records,

contractor personnel and supervisors.

Exit Interview

The inspection scope and findings were summarized on a biweekly basis with

certain individuals in paragraph 1.

The licensee did not identify as

proprietary any of the materials provided to or reviewed by the inspectors

during this inspection.

Licensee Action on Previous Enforcement Matters

a.

Closed -

Inspector Followup Item (IFI) 280/83-20-04 concerned the

omission of non-licensed STAs from the licensed Operator Requalifi-

cation program.

STAs currently participate- in the Operator Requali-

fication program and are given a separate examination.

The STA

Training program was previously ins*pected by the NRC Training Assess-

ment Team in Inspection Reports 280, 281/84-31.

b.

Closed -

Violation 280, 281/83-20-05 concerned the lack of valve

exercise testing following minor maintenance such as adjustment of stem

packing.

Administrative procedure ADM-71,

ASME Code Section XI

Repair/Replacement Program,

was

revised to ensure the testing

requirements are met~

4.

Unresolved Items

Unresolved Items were not identified during this inspection.

2

5.

Operations

a.

Units 1 and 2 were.inspected and reviewed during the inspection period.

The inspectors routinely toured the control room and other plant areas

to verify that plant operations, testing and maintenance were being

conducted in accordance with the facility Technical* Specificatio11s (TS)

and procedures. The inspectors verified that monitoring eqµipment was

recording as required, that equipment was properly tagged and that

plant housekeeping efforts were adequate.

The

inspectors also

determined

that appropriate

radiation

cont

1rols were

properly

established; clean areas were being controlled in accordance with

procedures; excess material or equipment was stored properly; and

combustible material and debris were disposed of expeditiously. During

tours, the inspectors looked for the existence of unusual fluid leaks,

piping vibrations, piping hanger and* seismic restraint settings,

various valve and breaker positions, equipment caution and danger tags,

component positions, adequacy of fire fighting equipment and instrument

calibration

dates.

Some

tours were

conducted on

backshifts.

Inspections included areas in the Units 1 and 2 cable vaults, vital

battery rooms, diesel generator rooms, fire pump house, switchgear

rooms, control room, auxiliary building, Unit 2 containment and cable

penetration areas to verify certain breaker and equipment positions for

safety-related components.

The inspector routinely conduct partial

wal kdowns of* emergency core cooling. (ECCS) and engineered safety

features (ESF) systems.

b.

The inspectors reviewed the May 11, 1985, event concerning the minor

fire in the reactor coolant system (RCS) head vent post accident

monitoring (PAM) panel in the Unit 1 control room.

While performing

Periodic Test PT-18.6H, the operators cycled solenoid operated valve

(SOV) SOV-RC-lOlA-1 (pressurizer head vent) and noticed the position

indicating light flickering on the control panel. The rear door to the

PAM panel was opened, and dark smoke billowed out.

A short burst of

carbon dioxide from a control room portable fire extinguisher was

manually discharged into the console/panel, while the electrical

breaker for the valve was opened to de-energize the circuits.

The

electrical leads to the bulb socket assembly were charred (burned).

A

short had apparently developed in the indicating light bulb sotket or

the attached 1900 ohm resistor, causing melting and smoking of the wire

insulation and melting of the lamp socket base. The correct bulb was

installed in the socket and the resistor still measured some 1800 ohms

resistance when tested. The battery voltage normally operates between

130 and 134 volts de (Vdc). The 125 Vdc lamp, socket and resistor were

replaced.

While examining the inside of the PAM panel, the inspector

noted a second blackened area similar to the SOV-RC-lOlA-1 panel area

which was blackened by the fire discussed above.

A similar socket

assembly failure and fire had apparently occurred some years ago during

testing.

Licensee and inspector review of this item continues (IFI

280/85-19-02).

c.

Unit 1 began the reporting period in a Cold Shutdown condition during a

two-week maintenance outage.

The unit returned to power operation on

,.

3

May 15, 1984, and operated at power for the remainder of the reporting

period.

Unit 2 remained shutdown in a refue 1 i ng maintenance outage for the

duration of the reporting period.

The inspectors routinely observed

refueling operations.

6.

Environmentally Qualified (EQ) Instrumentation and Electrical Seal Assembly

Review

Recently, while troubleshooting an EQ pressure transmitter (PT-2456, Pres-

surizer Pressure Protection) in the Unit 2 containment, licensee personnel

found standing water and internal corrosion inside the stainless steel

housing of the Rosemount Model 1153, Series D transmitter.

Additional

inspections identified snubber oil in a similar 1153 D transmitter (FT-2484,

Main Steam Line Flow) in the Unit 2 containment.

A rigorous inspection

program was initiated on both units following the Unit 1 shutdown due to

increasing RCS leakage through a residual heat removal (RHR) valve stem

packing.

The following problems were identified.

a.

The Conax electrical conductor seal assembly threaded body was not

properly positioned on the metal tube of the feedthrough subassembly.

The midlock ferrule (similar to a swagelock seal) which seals the

assembly* was found improperly positioned on several Conax assemblies in

each Unit.

In addition, several entire Conax seal assemblies were

installed backwards by threading the conduit National Pipe Thread (NPT)

end into the transmitter; the installations were corrected.

b.

The Conax threaded seal subassembly was not properly tightened on a few

assemblies.

The installation procedures require the midlock cap to be

torqued to 150-180 foot-pounds to properly crush the midlock ferrule

onto the conductor feedthrough tube; however, one assembly was found

only hand-tight, while others were under and over torqued.

In addition,

this significant torque.apparently resulted in broken transmitter neck

seals on several 1153 D transmitters; the factory sealed threaded neck

between the sensing cell and the cy_lindrical stainless steel electronics

housing was found cracked (loose). M*ost of these failures appeared to

have occurred recently during assembly removal and inspections due to

the failures referred to above.

The licensee designed an adjustable

support brace to secure the assemblies during torquing.

c.

Various materials were used to seal the one-half inch NPT threaded end

of the Conax assembly into the Rosemount transmitter head (e.g., RTV,

tefl on tape, nothing, Neo-1 ube 100).

Con ax recommends no sea 1 ant,

tape or lubrication on the Conax assembly threads, however, Rosemount

requires the use of Grafoil tape (qualified thread sealant) on the 1153

transmitters.

The licensee installed Grafoil tape before rethreading

the Conax assemblies into the Rosemount transmitters.

4

d.

Discrepancies were also observed inside the Rosemount transmitters.

Certain screw heads on the two sma 11 phi 11 i ps head screws which

terminate the signal leads inside the transmitter were found cracked at

the base or missing .. The original equipment screws were hollow (bored)

to accept a standard miniature test plug for testing purposes.

The

vendor supplied solid terminal screws, which were installed iii the

transmitters by licensee personnel, to alleviate screw head cracking

during screw installation and removal.

In summary, all 64 EQ transmitters (including

1their Conax assemblies)

and 27 of the 35 SOV assemblies in the Units 1 and 2 containments were

disassembled, inspected and retested, utilizing upgraded procedures.

The eight Target Rock SOV assemblies on the.Units 1 and 2 reactor head

vent systems (four per unit) were visually inspected with no discrepan-

cies observed; the assemblies were not disassembled because of their

inaccessibility; Eight Target Rock SOV assemblies similar to those on

the head vent were disassembled and no discrepancies were found.

In

addition, 12 of the 48 installed SOV limit switch Conax assemblies were

removed and inspected, and no discrepancies were found; the remaining

28 EQ limit switch assemblies are being installed in Unit 2 during this

outage, in accordance with 10 CFR 50.49.

The current Unit 2 refueling

outage is the second after March 31, 1982, and the scheduled deadline

for finalizing the EQ of. the electric equipment (except for NRR

extensions).

Results:

(1) Out of 64 transmitters and assemblies in Units 1 and 2 contain-

ments, at least six were verified inoperable (unqualified) due to

corrosion, water, etc. inside the transmitter or unseated (hand

tight) or reversed ferrules.

An additional 32 transmitters and

seal assemblies may have been unqualified due to misposition of

the ferrule or reversed assembly installation. The broken necks,

thread sealants and terminal screws could have led to additional

transmitter disqualification or failures.

(2) Out of 70 Conax assemblies to the SOV's, four were inoperable

(unqualified) due to corrosion, recessed ferrule or incorrect seal

assembly (Conax PL type vs. containment qualified ECSA type).

Four

were potentially inoperable due to incorrect positioning of the

midlock ferrule on the feedthrough tube subassembly.

(3) 12 of the 48 installed Conax assemblies to the valve limit

switches were inspected and no discrepancies were found; the

remaining 28 assemblies are being installed during the current

Unit 2 outage.

Based on the above data, where ten environmentally qualified safety-

related electrical components were determined to be unqualified, and at

least 36 of the remaining 200 EQ components inside the containments may

have been unqualified due to inadequate i_nstallation procedures, as

well as failure to follow these procedures and to verify that the

Ii.**'

<'

5

activities had been properly performed, a Violation of Appendix B to

10 CFR 50, Criterion V was issued (280, 281/85-19-01).

7.

Licensee Event Report Review

The inspectors reviewed the LERs listed below* to ascertain that NRC

reporting requirements were being met and to determine the appropriateness

of corrective action taken and planned.

Certain LERs were reviewed in greater detail to verify corrective action and

determined compliance with TS and other regulatory requirements. The review

included examination of logbooks, internal correspondence and records review

of Station Nuclear Safety and Operating Committee meeting minutes, and

discussions with various staff members.

(Closed) LER 280/85-05 concerned the locking out of automatic ihitiatfon of

carbon dioxide for fire zone seven with no fire watch present.

When operations

personnel tagged out fire zones five and seven construction personnel *had

intended that only zone five be tagged out; hence, a fire watch was posted

in zone five only. Operations personnel are to verify that a fire watch has

been posted in the area affected prior to removing any fire protection

system for service.

(Closed) LER 280/85-07 concerned a reactor trip/turbine trip due to the

11A11

main feed pump tripping at 17 percent power.

At the time of the trip~ no

valid trip conditions were indicated for the feed pump.

The actuator arm on

the pump's recirculation valve was found to possibly not properly depress

the limit switch associated with the valve position signal to the pump trip

logic.

When th~ recirculation valve opened at the specified low discharge

flow setpoint, it was determined that a valve open signal was apparently not

sent to the feed pump trip logic, which resulted in the pump trip. The

recirculation valve actuator arm was modified to ensure proper limit switch

actuation.

(Closed) LER 280/85-08 concerned the locking out of automatic initiation of

carbon dioxide for fire zone five with no fire watch present.

An operator

tagging out fire zone eight mistakenly placed the tag on fire zone five.

The

11 Red Tag

11 system is to be used when removing carbon di oxi ode systems

~ from service instead of the

1181 ue Tag 11 system.

This requires independent

verification by operations personnel and verification by the party requesting

the tagout that the proper systems were removed or were returned to service.

Within the areas inspected, no violation~ were identified.

8.

Plant Physical Protection

The inspectors verified the following*by observation:

a.

Gates and doors in Protected and Vital Area barriers were closed and

locked when not attended.

6

b.

Isolation zones described in the physical security plans were not

compromised nor obstructed.

c.

Personnel were properly identified, searched, authorized, badged and

escorted as necessary for plant access control.

d.

The inspector observed the monthly test of the Security emergency

diesel generator in accordance with PT 22.5.

Indication of emergency

power is provided on the Secondary Alarm Station via a

11Generating 11

light when the security diesel is running.

No false alarms were

generated during the switchover to emergency power.

A 11 security

alarms and equipment remained operable while being supplied by the

emergency power system.

No violations or deviations were noted.