ML18094A469

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Insp Repts 50-272/89-07 & 50-311/89-06 on 890417-21.No Violations Noted.Major Areas Inspected:Review of Actions in Response to Expeditious Enhancements Described in Generic Ltr 88-17, Loss of Dhr
ML18094A469
Person / Time
Site: Salem  PSEG icon.png
Issue date: 05/12/1989
From: Eapen P, Lopez A, James Trapp
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML18094A468 List:
References
50-272-89-07, 50-272-89-7, 50-311-89-06, 50-311-89-6, GL-87-12, GL-88-17, NUDOCS 8906020145
Download: ML18094A469 (7)


See also: IR 05000272/1989007

Text

.

U.S. NUCLEAR REGULATORY COMMISSION

REGION I

Report No.

89-07

89-06

Docket No.

50-272

50-311

License No.

DPR-70

DPR-75

Licensee:

Public Service Electric and Gas Company

P. 0. Box 236

Hancocks Bridge, New Jersey 08038

Facility Name:

Salem Units No. 1 & 2

Inspection At:

Hancocks Bridge, NJ

Inspection Conducted:

April 17-21, 1989

Inspectors:

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M. Trapp, Reactor Engineer, DRS, EB

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cA?"E. Lopez, Reactor'~ineer, DRS, EB

Approved by:

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P. K. Eapen, Chi e~

Test Programs

Section, DRS, EB

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'date

Inspection Summary:

Routine Unannounced Inspection* on April 17-21, 1989

(Inspection Report Nos. 50-272/89-07 (Unit 1), 50-311/89-06 (Unit 2)

Areas Inspected:

Review of licensee actions in response to the "expeditious

enhancements" described in Generic Letter No 88-17, "Loss of Decay Heat Removal. 11

The inspection reviewed supporting instrumentation, training, procedures and

staff awareness as related to mid-loop operation.

Results:

The inspectors found that all "expeditious enhancements" described in

Generic Letter 88-17 were implemented at Salem prior to drain down to mid-loop

operation.

The inspectors found the management involvement, training, and

staff awareness to problems related to mid-loop operation to be highly effective.

Procedures, instrumentation, and systems required to support mid-loop operation

were consistent with the licensees response to Generic Letter 88-17.

No

unresolved items or violations were identified during this inspection .

DETAILS

1.0 Persons Contacted

1.1 Public Service Electric and Gas Company

  • R. Dulee, -Quality Assurance Principal Engineer

J. Gueller, Operations Manager

  • C. Lashkari, Senior Staff Engineer

J. Lloyd, Principal Training Supervisor

  • L. Miller, Station Operation Manager

M. Reese, Nuclear Training Coordinator

  • G. Raggio, Station Licensing Engineer

T. Worrell, Quality Assurance Lead Engineer

1.2

U. S. Nuclear Regulatory Commission

  • ~-

K. Eapen, Section Chief, Special Programs Section

K. Gibson, Sr. Resident, Salem

  • A. Lopez, Reactor Engineer
  • J. Trapp, Reactor Engineer
  • Denotes presence at exit meeting held on April 21, 1989.

2.0 Review of Licensee Actions in Response to Generic Letter (GL) No. 88-17,

Loss of Decay Heat Removal (2515/101)

Loss of decay heat removal (OHR) during non-power operation and the

consequences of such a loss have been of increasing concern to the NRC.

Many events of loss of OHR have occurred while the reactor coolant system

has been drained down for mid-loop activities such as steam generator

inspection or repair of reactor coolant pumps.

The possibility exists

that two fission product barriers could be breached while these activities

are in progress, since the reactor coolant system and containment will

both be open.

GL 87-12, "Loss of Residual Heat Removal (RHR) while the Reactor Coolant

System (RCS) is partially filled" was issued to all licensees of operating

PWR 1 s and holders of construction permits on July 9, 1987.

Responses

indicated that the licensees did not understand the identified problems,

and the problem continued as evidenced by events at Waterford on

May 12, 1988 and Sequoyah on May 23, 1988.

The seriousness and continuation of this problem has resulted in the

issuance of GL 88-17.

In addition, the Di rector of NRR has written

1 to

the CEO of each licensee operating a PWR, in which he said,

11We consider

this issue to be of high priority and request that you assure that your

organization *addresses it accordingly. 11

He also wrote to each licensed

operator at all PWR plants on

110perator Diligence while in Shutdown

Conditions, 11 and enclosed a copy of Generic Letter 88-17.

3

GL 88-17 requires the recipients to respond with two plans of actions:

a.

A short-term program entitled

11 Expeditious Actions," and

b.

A long-term program entitled 11 Programmed Enhancements."

This inspection addressed the short-term licensee actions as outlined

under 11 Expeditious Actions, 11 of GL 88-17.

The inspectors reviewed the licensee response dated January 6, 1989

to Generic Letter 88-17.

The licensee response provided a detailed

description of action taken to address the eight recommended expeditious

actions identified in the Generic Letter.

The inspectors verified

that the licensee actions are consistent with the NRC guidance

provided in Generic Letter 88-17.

The NRC reviewed the licensee's mid-loop operations in 1987 as

detailed in the NRC inspection reports 50-272/87-28 and

50-311/87-30.

For the details of the NRC review of the licensee's

preparations and conduct of mid-loop operation during the current

Unit 1 -refueling outage (No. 8) see NRC inspection report

50-272/89-03.

2.1 Temperature Indication

The inspectors verified that for mid-loop conditions, the licensee

has taken adequate administrative and procedural steps to provide at

least two independent, continuous coolant temperature indicators

that are representative of the core exit conditions.

The licensee

monitors the core exit temperature using fifty-eight bottom mounted

thermocouples.

Step 2.11.2 of Procedure II-1.3.6 "Draining of the

Reactor Coolant System," requires as an initial condition that at

least two bottom mounted temperature indicators are providing RCS

temperature indication in the control room or control room racks.

Steps 5.1.l(f)&(g) of Procedure II-1.3.6 requires the thermocouples

be displayed in the control room on the plant process computer, or if

local indication is used constant surveillance and communication with

the control room be established.

The procedure requires that a high

temperature alarm be operational with a set point of 200°F.

This

alarm is initiated by the plant process computer and provides an

audible alarm in the control room, in addition to a print out on the

computer alarm printer.

The inspectors found the temperature indica-

tion system to be consistent with the expeditious actions of Generic

Letter 88-17.

The inspectors had no further questions concerning the

core exit temperature monitoring ?YStem .


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2.2

RCS Water Level Indication

The inspectors verified that the licensee has procedures and

administrative controls to provide at least two independent,

continuous RCS water level indications whenever the RCS is in a

reduced inventory condition. The licensee uses two RCS flow trans-

mitters (F0441A, F0400A), recalibrated to indicate RCS level, to

provide indication of RCS level in the control room.

Each transmitter

provides indication in the control room with an alarm set at 97 1-6

11 *

The alarm is audible and lights an overhead annunciator in the control

room.

In addition to the two level indicators in the control room, a

tygon tube is connected to the No. 13 intermediate leg and provides

local indication in the containment.

The licensee requires level

indications with an operable low level alarm in the control room in

Procedure II-1.3.6 Steps 2.11.3 and 2.11.5. Appendix 1 of Procedure

II-1.3.6 provides detailed guidance on how to install the tygon tub~

so that it will provide an accurate level indication.

The inspectors

verified that the tygon tube level indication was installed in

accordance with this procedure.

The inspectors noticed that the

licensee had provided accurate elevation marks so that the temporary

level indicating scale for the tygon tubing could be properly placed.

The inspectors verified that the scales for the RCS flow indications

and alarm description on the overhead annunciators had been changed.*

Procedures were reviewed to assure that precautions were provided for

possible variations in indicated RCS level.

The level indicating system was found to be consistent with the

expeditious actions described in Generic Letter 88-17.

The

inspectors had no further questions concerning RCS level indication

during mid-loop operation.

2.3

RCS Inventory Control

The inspectors verified that the licensee has procedures and

administrative controls to provide at least two available or operable

means of adding inventory to the RCS, in addition to pumps that are a

part of the normal OHR systems.

One. -source of inventory makeup is

from the charging pumps.

Technical Specification 3/4.1.2 requires

one charging pump to be operable in modes 5 and 6.

The second

independent source of makeup comes from either of the two safety

injection pumps.

Step 2.11.7 of Procedure II-1.3.6 requires one

charging pump be operable and one safety injection pump to be avail-

able.

A hot leg injection path for the safety injection pump is also

required to be available by this step.

The inspectors found this to

be consistent with expeditious action described in Generic Letter and

had no further questions concerning this issue.

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2.4 - RCS Perturbations

The inspectors verified that the licensee has implemented procedures

and administrative controls to avoid operations that could perturb the

RCS.

Step 5.1.l(h) of Procedure 11-1.3.6 requires work activities

which could effect RCS inventory be minimized during mid-loop operation.

During each shift the Containment Coordinator and the Senior/Nuclear

Shift Supervisor meet and discuss work activities* which could perturb

RCS inventory.

The content of these meetings is documented.

In addition, during each shift the Nuclear Shift Supervisor will

review shift work activities for impact on RCS inventory.

The

licensee issued a supervisory letter SL-37 "Salem Primary Systems

Loss of Decay Heat Removal" to all supervisory personnel.

Attached

to this letter were posters which describe

1100

11 and

1100 Not" activi-

ties which should be performed to prevent perturbations during

mid-loop operation.

These were displayed thoughout the plant.

The

inspectors found that the licensee had taken positive actions to

avoid perturbations of the RCS during mid-loop operation.

The pro-

cedures and controls were found to be consistent with the applicable

requirements described in Generic Letter 88-17. *The inspectors had

no.further questions concerning this issue.

2.5 Hot Leg Flow Paths

The inspectors verified that the licensee has implemented procedures

and administrative controls to assure that all hot legs are not

blocked simultaneously by nozzle-dams unless a vent path is provided

to prevent pressurization of the upper plenum of the reactor vessel.

The licensee uses steam generator nozzle dams during mid-loop opera-

tion.

The installation procedures require the cold leg nozzle dams

to be installed prior to the hot leg dams and the hot leg dams to be

removed prior to the cold leg dams.

This method of nozzle dam

installation reduces the effects of upper reactor vessel plenum

pressurization.

Prior to draining the.reactor vessel to mid-loop operation,

Procedure 11-1.3.6 Step 5.1.l(b) requires the removal of all three

pressurizer safety valves.

This provides a vent area of approximately

0.5 square foot.

The licensee has calculated that the back pressure

in the reactor vessel with three safety valves removed, at 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />

after shutdown, would be approximately 3.1 psig.

The licensee stated

that the 3.1 psig back pressure was acceptable as the existing cold

leg openings were sufficiently* high to avoid spilling of the reactor

coolant under this back pressure.

The licensee stated that cold leg

openings for maintenance during mid-loop operation would be considered

on a case by case basis, and the required vent area for each opening

of the told legs would be recalculated.

The reactor vessel back

pressure is important to determine the amount of water which could

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spill out of a cold leg opening.

This would also affect the time to

core uncovery.

The licensee stated at the exit meeting that they

would reassess the back pressure issue as part of the long-term

corrective action plan.

The inspectors determined that this was _

acceptable based on the fact that the licensee is aware of the

importance of the upper plenum back pressure and does considered cold

leg openings on a case by case basis.

The inspectors had no further

questions concerning this issue.

2.6

Loop Stop Valves

Loop stop valves are not part of the Salem Unit No. 1 or 2 system

design.

2.7 Containment Closure

The inspectors verified that the licensee has prepared procedures

and administrative controls to assure containment closure prior to

core uncovery during a loss of OHR event.

Procedure II-1.3.6 Step

2.11.1, requires that the equipment hatch be installed prior to

decreasing reactor vessel level more than three feet below the

reactor vessel flange.

Other penetrations in the containment are

isolated using Abnormal Operating Procedure AOP-CONT~2

11Containment

Closure on Loss of RHR.

11

This procedure is entered when RHR is lost

and the reactor vessel level can not be restored.

In most situations,

the containment could be isolated from the control room using the

manual phase-A initiation.

The inspectors concluded that the contain-

ment building could be isolated prior to core uncovery.

The inspectors

had no further questions concerning containment closure.

2.8 Training

The inspectors verified that training conducted by the licensee, made

the licensee personnel aware of the risks associated with mid-loop

operation.

The inspectors verified the effectiveness of this training

by interviewing operating personnel and reviewing the training material

provided to the trainees.

The operators interviewed were found to

h~ve an indepth knowledge of the issues disc~ssed in Generic Letter 88-17.

All operating personnel were trained just prior to draining

the reactor vessel to mid-loop.

The training material and lesson plans reviewed by the inspectors

did not contain all of the material committed to be part of training

in the licensee response to Generic Letter 88-17.

The inspectors

discussed the topics missi~g from the lesson plans with the licensed

operators. It became apparent to the inspectors that all the topics

committed to be taught in the response to the Generic Letter had in

fact be~n presented during the training sessions.

The inspectors

discussed the weakness in the lesson plan and training material with

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the Plant Operations Manag~r who stated at the exit meeting that the

lesson plans would be improved prior to the next use of this course

material.

The inspectors had no further. questions concerning this

issue.

2.9

QA/QC Involvement

The QA organization was found to have extensive involvement in the

mid-loop operation issue.

The inspectors reviewed licensee surveil-

lance report 88-0633 which was a surveillance conducted during the

last drain down operation at Salem Unit 2.

The surveillance results

were satisfactory.

QA had also performed indepth root cause analysis

of industry events relating to loss of RHR and studied these events

for applicability at Salem.

The inspectors interviewed QA personnel

involved in mid-loop operation concerns and found that they had full

knowledge of industry events, and plant specific details relative to

mid-loop concerns.

2. 10 Summary

The inspectors found the licensee management and staff to be aware

of the types of problems which may occur during mid-loop operation.

The actions taken by the licensee in*installation of instrumentation,

training, staff awareness and management involvement were found to be

highly effective. All the expeditious actions addressed in the

licensee response to Generic Letter 88-17, dated January 6, 1989,

were implemented during mid-loop operation.

The licensee was found

to be pursuing additional improvement, for mid-loop operation, as

part of a long-term corrective action program.

3.0 Exit Meeting

At the conclusion of the site inspection, on April 21, 1989, an exit

interview was conducted with the licensee 1 s senior ~ite representatives

(denoted in Section 1) to discuss the results and conclusions of this

inspection.

At no time during this inspection was written material provided to the

licensee by the inspector.

Based on the NRC Region I review of this

report and discussions held with licensee representatives during this

inspection, it was determined that this report does not contain

information subject to 10 CFR 2.790 restrictions.

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