05000311/LER-1981-011, Forwards LER 81-011/03L-0

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Forwards LER 81-011/03L-0
ML18086A572
Person / Time
Site: Salem PSEG icon.png
Issue date: 05/22/1981
From: Uderitz R
Public Service Enterprise Group
To: Grier B
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML18086A573 List:
References
NUDOCS 8106020258
Download: ML18086A572 (3)


LER-1981-011, Forwards LER 81-011/03L-0
Event date:
Report date:
3111981011R00 - NRC Website

text

e PS~G Public Service Electric and Gas Company 80 Park Plaza Newark, N.J. 07101 Phone 201/430-7000 Mr. Boyce H. Grier Director of USNRC May 22, 1981 Off ice of Inspection and Enforcement Region 1 631 Park Avenue King of Prussia, Pennsylvania 19406

Dear Mr. Grier:

LICENSE NO. DPR-75 DOCKET NO. 50-311 REPORTABLE OCCURRENCE 81-ll/03L Pursuant to the requirements of Salem Generating Station Unit No. 2 Technical Specifications, Section 6.9.1, we are submitting Licensee Event Report for Reportable Occurrence 81-ll/03L.

This report is required within thirty (30) days of the occurrence.

Sincerely yours,

    1. t/~~1 r-R. A. Uderitz General Manager -

Nuclear Production CC:

Director, Office of Inspection and Enforcement (30 copies)

Director, Office of Management Information and Program Control (3 copies)

W-

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e OPS~G Public Service Electric and Gas Company 80 Park Plaza Newark, N.J. 07101 Phone 201/430-7000 Mr. Boyce H. Grier Director of USNRC May 22, 1981 Off ice of Inspection and Enforcement Region 1 631 Park Avenue King of Prussia, Pennsylvania 19406

Dear Mr. Grier:

LICENSE NO. DPR-75 DOCKET NO. 50-311 REPORTABLE OCCURRENCE 81-ll/03L Pursuant to the requirements of Salem Generating Station Unit No. 2 Technical Specifications,_ Section 6.9.1, we are submitting Licensee Event Report for Reportable Occurrence 81-ll/03L.

This report is required within thirty (30) days of the occurrence.

~

Sincerely yours,

  1. 4Ukj 1--

R. A. Uderitz General Manager -

Nuclear Production CC:

Director, Office of Inspection and Enforcement (30 copies)

Director, Office of Management Information and Program Control (3 copies)

The Energy People 95-2001 1350Ml 4-BC

Report Number:

81-ll/03L Report Date:

May 22, 1981 Occurrence Date: 4/27/81 Facility:

Salem Generating Station, Unit 2 Public Service Electric & Gas Company Hancocks Bridge, New Jersey 08038 IDENTIFICATION OF OCCURRENCE:

Containment Air Lock Inoperable CONDITIONS PRIOR TO OCCURRENCE:

Mode 3 -

Rx Power 0% - Unit Load O MW DESCRIPTION OF OCCURRENCE:

During a routine entry into the containment, the outer door on the Containment Air Lock, elevation 100', failed to close.

At 0100 hours0.00116 days <br />0.0278 hours <br />1.653439e-4 weeks <br />3.805e-5 months <br /> on April 27, 1981, Action Statement 3.6.1.3.a was entered.

This occurrence constituted operation in a degraded mode in accordance with Technical Specification 6.9.1.9.b.

DESIGNATION OF APPARENT CAUSE OF OCCURRENCE:

Equipment Failure -

The Containment Air Lock Door linkage was worn, causing the door roller bearing to deviate from their proper alignment.

ANALYSIS OF OCCURRENCE:

Technical Specification 3.6.1.3.b requires that each Containment Air Lock shall be operable with both,doors closed except when the Air Lock is being used for normal transit entry and exit through the Containment, then at least one Air Lock Door shall be closed.

CORRECTIVE ACTION

Roller bearings on the outer door were replaced in kind, and the linkage was realigned.

The Containment Air Lock was tested satis-factorily.

Action Statement 3.6.1.3.a was terminated at 0710 hours0.00822 days <br />0.197 hours <br />0.00117 weeks <br />2.70155e-4 months <br /> on April 27, 1981.

FAILURE DATA:

Containment Air Locks Chicago Bridge and Iron Company Bearing Part Numbers CF-1-5 Prepared By ~~~-J~*-J~*-* ~~_s_p_e_y ~~~~....L.~r.,J.~~*::::!:~~~~~'~A~d~&~~k::....._~____,,......-~~~-.-~~~

Manager.- Salem Generating Station SORC Meeting No.

81~39